ML17199F823

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Insp Repts 50-237/86-15 & 50-249/86-17 on 860519-23. Violation Noted:Failure to Ensure That Drawings Kept Updated & Installation Performed in Accordance W/Drawings
ML17199F823
Person / Time
Site: Dresden  
Issue date: 06/30/1986
From: Bjorgen J, Dunlop A, Eng P, Falevits Z, Hehl C, Key W, Ring M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17199F822 List:
References
50-237-86-15, 50-249-86-17, NUDOCS 8607070263
Download: ML17199F823 (18)


See also: IR 05000237/1986015

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Report Nos. 50-237/86015(DRS); 50-249/B6017(DRS)

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

P. 0. Box 767

Chicago, Illinois 60690

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Morris, Illinois

Inspection Conducted:

May 19 through May 23, 1986

Inspectors:~

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Approved By:

C. W. Hehl, Chief

Operations Branch

Inspection Summary

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Date *

Inspection on Ma} 19 through 23, 1986 (Report Nos. 50-237/86015(DRS);

50-249/86017(DRS )

Areas Inspected: Special team inspection to followup on modification package

problems identified by the Safety Systems Outage Modification Inspection Team

from the Office of Inspection and Enforcement on Unit 3 to determine if

similar problems were present on Unit 2 and, if problems were present, to

determine if they jeopardized the return to operation of Unit 2.

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Results:

The inspection team determined that in the thirteen Unit 2

modification packages inspected about half contained similar problems as had

been identified for Unit 3.

The problems identified were evaluated by the team

to not jeopardize the return to operation of Unit 2.

One violation was

identified in the area of as-built drawings versus as-found electrical

configuration (failure to ensure drawings are kept updated and installation is

performed in accordance with drawings - Paragraph 4) .

2

  • 1.

2.

DETAILS

Persons Contacted

  • N. Kalivianakis, Nuclear Division, Vice President
  • D. Scott, Station Manager
  • J. Brunner, Assistant Superintendent, Technical Services
  • J. Doyle, Quality Control Supervisor
  • D. Farrar, Director of Nuclear Licensing
  • D. Adam, Regulatory Assurance Supervisor
  • R. Flessner, Services Superintendent
  • J. Wujciga, Production Superintendent
  • M. Strait, Station Nuclear Engineering Department
  • J. Achterberg, Technical Staff Supervisor
  • G. Smith, Assistant Technical Staff Supervisor
  • J. Ballard, Zion Quality Control Supervisor
  • J. Wojnarowski, Nuclear Licensing Administration
  • T. Ciesla, Assistant Superintendent, Operations
  • R. Jeisy, Quality Assurance Supervisor
  • Denotes those personnel attending the May 23, 1986, exit interview.

Additional station technical and administrative personnel were also

contacted by the inspectors during the course of the inspection.

Background

From April 21 to May 7, 1986, an inspection team from the NRC's Office of

Inspection and Enforcement performed the second part of a three part Safety

Systems Outage Modifications Inspection (SSOMI) at the Dresden Unit 3 site.

(Note:

The last part of the SSOMI inspection is expected to be completed

July 1986.)

The results of that inspection raised several concerns

regarding the adequacy of modifications performed at the Dresden site,

and the decision was made to perform a Regional followup inspection

beginning May 19, 1986.

The concerns identified during the SSOMI were also

documented in a letter dated May 16, 1986, from James M. Taylor, Director,

Office of Inspection and Enforcement (IE) to Cordell Reed, Vice President,

Commonwealth Edison Company (CECo).

The purpose of the followup inspection

was primarily to determine if problems similar to those identified by the

SSOMI team on Unit 3 were also present on Unit 2.

This information was

necessary because the SSOMI team's inspection was largely focused on Unit 3

and because Unit 2 was operating at power at the time. Additional

objectives of the followup inspection were to determine if any problems

identified presented immediate threat to continued operation of Unit 2 and

to assess CECo corrective actions.

CECo made a presentation to Region III

and IE management personnel at a meeting in Region III offices on May 21,

1986, regarding CEC0

1s assessment of Dresden's modification program

problems and proposed corrective actions. Since CEC0

1s corrective actions

were not finalized by the time of the exit on May 23, 1986, the followup

team did not perform this objective and no further assessment of CEC0

1s

complete corrective actions is contained in this report; however, some

specific corrective actions are addressed with the individual modification

3

3.

packages.

In addition, the followup team expanded the inspection in the

areas of as-built drawings compared to the as-found condition of the plant

and work requests.

The remainder of this report describes the findings of

the followup inspection team.

Modification Packa9~~

The followup inspection team reviewed portions of thirteen (13)

modification packages for Unit 2 which had been performed on Unit 3.

The results of the examination of each package are detailed in the

following paragraphs.

a.

Modification Packa9es_~1~:~:84:~1-~~d MJ2-~:84:28

These modifications consisted of replacing the pilot solenoid valves

(S0-2-1601-50A and S0-2-1601-508, respectively) for the torus to

reactor building vacuum breaker valves (A0-2-1601-20A and

A0-2-1601-208) with Environmentally Qualified (EQ) solenoids.

The specific problems with these two packages noted on Unit 3

by the SSOMI team which were communicated to the followup team

were:

(1)

The air actuator lines to the vacuum breaker valves were

installed per the modification drawing, but the drawing was in

error. This resulted in the lines being reversed from their

correct configuration.

(2)

The solenoid valves had been installed horizontally instead

of vertically.

(3)

The operational tests did not require valve stroke time tests

as required by Section XI of the ASME Code.

Stroke time

acceptance criteria were changed by the modification.

(4)

Splices (Raychem) on the solenoid valve leads were made

improperly.

(5)

Anti-rotation stops of wrong material were welded on the

valves.

(6)

The operational test was inadequate in that it would not have

verified the fail position on loss of air.

The SSOMI team also noted that the licensee's Quality Control (QC)

representative had signed for correctness for items (1) and (2).

The SSOMI team had verified via photograph that the Unit 2 air

actuator lines were installed correctly (i.e., not in accordance with

the instructions); however, no field change or other vehicle was used

to document the correct method on Unit 2 so that it could be

translated into the Unit 3 modification package.

4

For item (1), the followup team with the assistance of the Senior and

Resident Inspectors physically verified that the Unit 2 air actuator

lines to the vacuum breaker valves were installed correctly.

The

modification drawing for the Unit 2 modification was still in error,

however.

For item (2), the solenoid valves were observed to be installed with

the coil horizontal in Unit 2, the same as was observed for Unit 3.

This problem was judged to not be technically significant in that

the modification package for Unit 2 contained additional information

from the valve manufacturer, ASCO, which stated, "This valve is

designed to perform properly when mounted in any position.

11

An

additional memo from Bechtel indicated, "Coils vertical and upright

or no more than 90° to any side of vertical and upright would

present no problem,

11 and "If vertical and downward, problems

relating to moisture and dirt can be expected to be more severe.~

While this information indicates the solenoid valve coils do not

have to be vertical, both Unit 2 and Unit 3 modification packages

contained operator or QC signatures stating,

11Solenoid mounted with

the coil upright and vertical.

11

The valves were observed to be

physically mounted such that the valve shaft was vertical while the

coil was horizontal. While the installation does not represent a

problem for valve operation, it supports the SSOMI concern as to

whether the personnel involved in the valve installation,

including QC, adequately understood the modification instructions

or the operation of the valves .

For item (3), the Unit 2 packages were found to be satisfactory in

that they contained a stroke time test.

The Unit 2 valves were

found to stroke in 2 seconds which is considered satisfactory.

For item (4), the Unit 2 splices on the solenoid valve leads had

already been redone by the time the followup team arrived onsite.

Discussions with the Assistant Technical Staff Supervisor indicated

that the Unit 2 splices were in the same condition as those of

Unit 3; however, CECo does not believe they were improper.

The

followup team did not attempt to pass judgement on the correctness

of the splices since this issue was known to be in dispute from the

SSOMI team inspection.

The followup team merely confirmed that the

same condition had existed on Unit 2 and was now corrected.

For item (5), the followup team did not examine the anti-rotation

stops and has no conclusion on this item.

For item (6), the followup team did not uncover conclusive evidence

that the operational test was or was not incorrect with respect to

fail position.

The test instructions were vague in that personnel

were instructed to

11 loosen air connection" and

11close supply valve

11

without specifying exactly which connection or valve.

There are

more than one connection and valve such that it is possible to

perform the test correctly or incorrectly depending on which

locations are chosen.

The data in the test merely consists of

11yes

11

and a signature indicating successful performance.

The followup

5

team did not interview the individuals who actually performed the

test and hence no definitive conclusion was reached.

Licensee

personnel indicated that they believe the operational test as

written could have caught the incorrect air actuator installation

for Unit 3.

(Note:

The test had not yet been performed on Unit 3.)

The followup team believes this to be probable in that the test

would not have worked; therefore, an investigation into the cause

may have uncovered the incorrect installation. However, since the

drawing was in error and the installation was correct per the

drawing, the team believes there is an equal likelihood that the

error would not have been recognized and that another fix, such as

reversing electrical leads, would have been incorrectly attempted.

b.

Modification Packages Ml2-2-84-49 and Ml2-2-84-50

These modifications consisted of replacing the Low Pressure Coolant

Injection (LPCI) room cooler motors with EQ motors.

The specific

problems with these two packages noted on Unit 3 by the SSOMI team

which were communicated to the followup team were:

(1)

Questionable method and integrity of Raychem splices,

specifically braiding penetrating the heat shrink to an

indeterminate depth.

(2)

Failure to repair all damaged braiding on motor lead

insulation .

(3)

Questionable seismic analysis for LPCI room coolers and

motors.

(4)

One Unit 3 room cooler fan belt was not installed and the

other was loose.

The followup team reviewed the modification packages noted above

for Unit 2 and the related package for Unit 3.

Due to licensee

manpower constraints resulting from the Environmental Qualification

inspection which was being conducted during the same time period,

the inspectors were only able to view the Unit 2 LPCI room cooler

motor installation. The followup team inspectors noted that the fan

belts were properly installed for Unit 2.

Review of the modification

packages revealed that with the exception of the damaged leads on

Unit 3 equipment, package content was virtually identical.

For item (1), the integrity of the Raychem splices were found to be

similar on Unit 2 to those on Unit 3.

For item (2), the modification on Unit 2 did not have damaged

braiding on motor lead insulation associated with it; consequently,

there was no

11failure to repair

11 on Unit 2.

Subsequent physical

inspection of the coolers found damaged braiding/insulation on one

of the motor leads for the east LPCI room cooler.

The licensee

initiated a work request to repair the damaged leads.

6

For item (3), the Unit 2 installation was identical to that on

Unit 3.

With regard to the seismic adequacy, the inspectors noted

that the motor was rigidly attached to the cooler; however, the

room cooler itself was not rigid and could be swayed by hand.

The

licensee subsequently provided a copy of the seismic evaluation

performed by Westinghouse of this installation. The evaluation has

been forwarded to the SSOMI team for further analysis.

The inspectors also observed that although the modification packages

for Unit 2 were signed as being complete with respect to work and

microfiched, the Quality Assurance approval of the Final

Documentation Checklist was missing.

This item is considered an

example of lack of adequate quality control of the modification

packages as previously identified by the SSOMI team.

c.

Modification packages Ml2-2-85-50; M12-2/3-85-31

These modifications consisted of installing pressure gauges on each

of the Diesel Generator Cooling Water (DGCW) Pump suction lines for

Inservice Testing purposes. Modification packages for Unit 2 and

the swing diesel had been signed off as being complete with regards

to both work and documentation.

The concern raised by the SSOMI team for Unit 3 was that the

modification package specified an isolation valve rated at 2000 psig.

Field inspection revealed that a 150 psig valve was actually

ins ta 11 ed.

Region III inspectors reviewed the modification packages for

Unit 2, Unit 3 and the

11-swing

11 or Unit 2/3 DGCW pump suction lines

and noted that when first authored, all three packages specified use

of a 2000 psig valve.

Prior to installation of the pressure gauge in

Unit 2, however, a pen and ink change was made changing the valve to

150 psig.

Field inspection revealed that 150 psig valves were

installed in all three locations. Consequently, the concern raised

by the SSOMI team is applicable to the Unit 3 and swing DGCW pump

suction lines only.

The licensee stated that a Deviation Report

describing the error was being routed and upon completion of the

approval process would be inserted into the modification package.

In addition, during review and comparison of the three modification

packages, the inspectors noted the following:

(1)

For Unit 2, the modification checklist required valve identifi-

cation tags to be hung and the ISI Coordinator to be notified of

the modification.

The signatures verifying both these tasks

were missing.

(2)

The fabrication sketch of the pressure ~auge installation for

Unit 2 identified two items as Part #2 {pipe) and required

Part #2 to be safety-related. The material certification cards

attached to the modification package only note one item.

Further

investigation revealed that the Part #2 was not used for both

7

(3)

applications, but a reducer was substituted in the field.

However, no changes were made to the modification package to

authorize or document the change made in the field.

A Quality Assurance (QA) holdpoint was required for the fitup

and alignment associated with one of the welds on the swing

diesel installation.

The signature block for the hold point

is dated October 19, 1985, two months prior to work initiation

and states,

11 N/A per phone call.

11

Discussions with the licensee

personnel involved could not clarify the reason for .or the

disposition of the holdpoint; however, the licensee believes

this to be an incorrect recording of the date in that the work

was performed on December 19, 1985.

The above 3 items are considered further examples of a lack of

adequate quality control of the modification packages as previously

identified by the SSOMI team.

d.

Modification Packa9e M12-2-84-9

This modification consisted of modifying the control circuit to the

core spray inboard isolation valves to prevent hammering on a

continuous close signal.

The problem noted on Unit 3 by the SSOMI

team and communicated to the followup team was that the Raychem

splices did not meet the minimum bend radius requirements.

The

inspectors examined core spray inboard isolation valve MOV 2-1402-25A

and found that the splices were not bent in excess of the minimum

bend radius as was observed in Unit 3.

The wiring in the valve was

bent to some degree and the outer jacket was cracked; however, the

inner insulation appeared to be intact.

e.

Modification Package M12-2-83-29

This modification consisted of a change to LPCI suction valves

M03-1501-5A, B, C, and D to ensure closure upon ECCS actuation.

The

problem with this package noted on Unit 3 by the SSOMI team and

communicated to the followup team was incorrect installation of the

Raychem splices. This problem was not found by the followup team to

be present on Unit 2 in that this modification had not yet been

performed on Unit 2.

Modification Package M12-2-83-30

This modification consisted of modifying the Core Spray (CS) suction

valves M03-1402-3A and 38 control circuitry to allow closure upon

ECCS actuation.

The problem with this package noted on Unit 3 by the

SSOMI team which was communicated to the followup team was an

incorrect cable termination on both motor control centers (MCC).

This problem was not found by the followup team to be present on

Unit 2 in that this modification had not yet been performed on Unit 2 .

8

g.

Modifi ca ti on PackE_ge M12-2-84-14

This modification consisted of installing 4-way valves, flanges and

gauges to allow end tank removal on the Containment Cooling Service

Water (CCSW) piping to the pump vault coolers.

The specific problems

with this package noted on Unit 3 by the SSOMI team which were

communicated to the followup team were:

(1)

The mechanic installed the 4-way valve in a manner not in

accordance with the procedure, and initiated a Field Change

Request (FCR) after installation.

(2)

150 psig flanges were installed instead of the 300 psig flanges

required by the drawing.

(3)

Sheet gasket material was used rather than the flexitallic

gaskets required by the specification.

The followup team reviewed the repair program for this modification

which was developed by Sargent and Lundy (S&L) outlining the

requirements for the modification including:

installation of new

piping, fittings, valves and supports; welding and inspections;

retesting of lines; and documentation.

The following documentation

was reviewed:

welding procedure specifications and qualification

records, welder qualification records, inspection and examination

reports, examination procedures and personnel qualifications,

complete station traveler, and certificates of conformance

for all piping, fittings, structural steel, filler metal, valve

body and all other material.

Regarding items (1) and (2), the

inspector's review determined that on Unit 2 the modification had

been performed in accordance with both the drawings and the repair

program including the use of both 150 psig and 300 psig flanges.

However, use of some of the 150 psig flanges in 300 psig locations

was not correct per the drawings and conf'irms the findings from the

SSOMI team also exist on Unit 2.

Regarding item (3), however, the

inspector's review confirmed that sheet gasket material had been

used on Unit 2 also, instead of the required flexitallic gaskets.

During the above review, the inspectors also noted an apparent

additional problem with material traceability. Dresden Station uses

red tags to identify items stored in the warehouse and for material

traceability to the CMTRs.

Review of S&L drawing no. M-487, Revision

A, noted that twelve - 300 psig CCSW flanges were required per pump

unit and four - 150 psig CCSW flanges per unit at the 4-way valves.

Upon examination of the red tags for materials withdrawn from the

warehouse, 24 tags for the 150 psig flanges and one tag for the 300

psig flanges were found.

There appeared to be no traceability for

eleven of the 300 psig flanges. Further discussion with licensee

personnel revealed that the personnel performing the modification in

the field found seven - 300 psig flanges already installed and in

adequate condition so they were reused.

One new 300 psig flange was

used; thus, producing one new red tag. This explanation shows that

150 psig flanges were used in some of the 300 psig locations and no

9

h.

changes were made to the modification package to document what was

actually done.

This item appears to be similar to item (1) of the

SSOMI team's problems and is considered a further example of lack of

adequate quality control of the modification packages as previously

identified by the SSOMI team.

Mod if i cat i_g.D_ Packa_ge M12-2-83-40

This modification consisted of replacing reactor water level

instrumentation and modifying the instrument racks for new EQ

transmitters.

The problems with this package noted on Unit 3 by the

SSOMI team which were communicated to the followup team were incorrect

Raychem splices and separation less than 6 inches as required by

drawing.

The followup team did not find problems with Raychem splices

on Unit 2 in that different types of splices were used for the Unit 2

modification.

The followup team was unable to examine the separation

issue during the week of inspection.

i.

Modification Packa_ge M12-2-83-57

This modification consisted of installing shear lugs on the Main Steam

lines to prevent the restraints from slipping down the pipe.

The

SSOMI team did not communicate any problems with this package on

Unit 3 to the followup team.

The followup team examined this

package for Unit 2 and did not find any discrepancies with the

Unit 2 package, either.

j.

Modification PackE_9~_M12-2~§4-~

This modification consisted of replacing/rewiring various HGA-11

relays due to potential difficulty in meeting seismic requirements.

The specific problems with this package noted on Unit 3 by the SSOMI

team which were communicated to the followup team were:

(1) A lead was terminated to an incorrect terminal point and then

jumpered to the correct point.

An additional modification

would remove the jumper.

(2)

Drawings contained incorrect information.

(3)

Construction test contained steps where either A or B was

to be performed.

Both A and B were signed indicating

performance.

The followup team reviewed both the Unit 3 and Unit 2 packages in

order to better understand the Unit 3 problems and determine if they

were present on Unit 2.

With regard to item (1), the inspectors noted that while the manner

in which the lead and jumper were connected was not strictly in

accordance with the letter of the package description, it would

10

electrically accomplish the same function.

A note on drawings

12E-2758L and 12E-3758L stated that when modification M12-2(3)-82-27

(the additional modification described in item (1) earlier) was

performed, the jumper was to be removed and the lead terminated

at the correct terminal point.

The modification packages for

M12-2(3)-82-27 were not in a condition to be performed at the time

of the inspection and, therefore, the inspector could not determine

if the package would specifically describe the correct electrical

installation.

With regard to item (2), following the 1icensee's drawings and

drawing control system was found to be extremely difficult. The

licensee utilizes four categories of drawings:

As-built drawings,

Construction drawings, Completed Hold File drawings and Critical

drawings.

To determine physical configuration in the fie1d, a

combination of the first three types of drawings was often

required.

Even Critical drawings, which the licensee described

as being correct field drawings, appeared to have discrepancies.

Further discussion of drawings versus configuration in the field

is contained in Paragraph 4 of this report.

Paragraph 5 of this

report discusses the inspection team's examination of work requests

which was motivated by the drawing concerns.

With regard to item (3), the followup team found that Unit 2 did

not have this problem in that the Unit 2 construction test did not

contain either/or steps described in item (1) .

The inspectors also encountered an additional concern as a result of

modification M12-2-84-8.

When leads were lifted or landed on a

relay or terminal board which already contained other leads at the

same point, the only circuits that were checked for continuity were

the newly landed leads. Other leads that had been installed at the

same time were not checked to see if they remained properly landed

even though they may have been disturbed by the new actions. This

practice produces the potential of other systems, not specifically

involved in the modification, not getting adequately tested to

ensure proper operation.

Upon field inspection of electrical

cabinets, the inspectors noticed loose leads which were not

terminated and which were not taped over or otherwise marked as

spares.

This observation, without tracing back the specific wires,

does not necessarily reflect a problem.

However, it tends to give

credence to the concern over a need to verify other leads not

specifically involved in the subject modification remaining properly

terminated.

The licensee agreed to review this area for possible

corrective action.

The inspection attempted to verify the ability of surveillance tests

to adequately test the features of a system following performance of

a modification with the drawing difficulties described in Paragraph 4

present.

The followup team was unable to complete this effort in

the week spent onsite, but this issue is expected to be pursued in

the second part of the SSOMI team effort.

11

No new violations or deviations were identified in this area; however,

several of the issues identified in the preceeding paragraphs were

previously identified by the SSOMI team and may be considered violations

pending the completion of the SSOMI effort.

4.

Modification and As-Built Plant Configuration Review

a.

During the various modification package reviews (primarily

M12-2-84-8), the inspectors noted that considerable difficulty

was experienced when trying to compare the licensee's electrical

design drawings (including those designated as the

11as-built

11

drawings) with the configuration or wiring of electrical components

as found installed in the plant.

Some modifications were found

incorporated into the design drawing but not yet installed in the

field, while others related to the same design drawings had been

partially or completely installed in the field but were not

reflected on the drawings.

The inspectors noted that modifications

to a particular design drawing are not necessarily implemented in

the field in a chronological order.

For example, a modification

issued in 1986 to a particular electrical circuit can be installed

prior to a modification issued in 1980, which impacts the same

circuit on the drawing.

While it is not a specific requirement that

modifications be accomplished in chronological order, the system

which the licensee uses to try and control this situation coupled

with the numbers of modifications implemented over the current plant

lifetime have combined to produce a very confusing situation. It is

extremely difficult, if not impossible, to determine the as-built

condition of Dresden's electrical systems by utilizing only the

design or

11as-built

11 drawings.

This situation may have contributed

to the findings in the remainder of this section.

(1)

For modification package M12-2-84-8~ the modification was

completed on Unit 2 in January 1985 and, therefore, per the

licensee's document control system, the drctwings affected by

M12-2-84-8 should have been listed as "Completed Hold File.

1

-'

The licensee's Records Retention Vault, however, still listed

the modification as incomplete and the drawings were marked

11 For Construction Only.

11

Communications between the

modification group and the Records Retention Vault were

inadequate in that only oral communications between the groups

were required to change the status of the modification.

The

licensee has corrected the specific deficiency in the Records

Retention Vault.

In addition, a change to the Dresden

Administrative Procedures (OAP) will be initiated to require

the modification group to complete a form signifying final

installation approval which is then sent to the records vault

to implement the change to the status of the drawings.

(2)

The inspectors reviewed drawing 12E-2697, Revisions AF through BB,

and compared the drawings to the actual configuration found in

the field.

Revisions AF through BB of drawing 12E-2697 show an

internal conductor connecting terminal EE-10 to device CPT.

This conductor was not found installed in the field.

12

(3)

Revisions AF through BB of drawing 12E-2697 show only one

internal conductor attached to terminal EE-13 (connecting

device HJ-4); however, field inspection found a second field

conductor attached to terminal EE-13.

(4)

Revisions AB through AJ of drawing 12E-2758B show a jumper

between terminal DD-19 and DD-20 on Auxiliary Electric

Equipment Room panel 902-33. This wire was not found installed

in the field.

(5)

The licensee utilizes a system of as-built drawings designated

Critical drawings in the control room which are marked up to

show modifications and changes.

This system has been

established for use by operating and maintenance personnel per

OAP 2-9 for shift decisions, outage management and trouble

shooting.

From a sample of four Critical drawings, drawing

12E-3437A, Revision P, did not reflect the as-built plant

condition in that Revision J had been designated the as-built

drawing.

(6)

As-built Drawing 12E-2758B, Revision AB, for panel 902-33 shows

a jumper between points 7 and 9 of relay 1530-202.

This wire was

not found installed in the field.

The inspectors recognize

these points are spare contacts.

(7)

As-built Drawing 12E-2758B, Revision AB, shows wire FF-71 on both

sides of terminal block DD-21 and wire FF-72 on both sides of

terminal D0-22.

Field inspection indicated that only the

internal sides of DD-21 and 22 are wired.

(8) As-built Drawing 12E-2758B, Revision AB, shows AQ-2 connected

to point DD-54, but field inspection found AH-2 connected to

DD-54.

These items (1) through (8) represent examples of a failure to

assure that changes and modifications to as-built drawings are

properly controlled and implemented, and to assure that the as-built

drawings are kept updated to reflect the condition of the plant.

These items are considered to be a violation of 10 CFR 50, Appendix B,

Criterion VI (237/86015-0l(DRS); 249/86017-0l(DRS)).

This violation

is similar to a previous violation (237/86001-02(DRS);

249/86008-0l(DRS)) and a previous open item (237/86005-0l(DRS);

249/86008-0l(DRS)) issued at Dresden.

b.

In addition to the examples of a violation discussed previously, the

inspectors also noted the following problems while comparing

drawings with field configuration:

(1)

The inspector selected Core Spray - LPCI Containment Cooling

system drawing 12E-2697, Revisions AF through BB, and drawing

12E-2758B, Revisions AB through AJ,for a field inspection to

determine if modifications applicable to these drawings had

13

been properly implemented in the field, and whether the

drawing revisions designated by the licensee as

11 As-Built~

reflect the actual condition of the plant. The inspector also

attempted to determine the method used to identify, control and

update the as-built drawings located in Central File.

Review

of Central File records indicated that the following

modifications and revisions associated with drawing 12E-2697

have already been implemented in the field.

Modification Nos.

M12-2-80-33

M12-2-79-52

Record~evision

DCR-83-55 (M12-2-82-46)

FCR-2386

M12-2-84-16

M12-2-83-40

M12-2-8T-30

Applicable

Drawing Revisions

AJ

AK

AT

AU

AZ

AU

AW/BB

BA

(Note:

80 denotes the year the modification was issued.)

The following modifications have not been implemented in the

field yet, but the design was incorporated into drawing

12E-2697:

Modification Nos.

M12-2/3-80-06

M12-2-80-=36

M12-2-8~-29

Applicable

Drawing Revisions

AG/AL/AS

AM/AN/AP/AR

AV

(2)

The licensee designated Revision AF of drawing 12E-2697 as the

as-built revision.

The inspector attempted to verify the

as-built configuration of Main Control Board panel 902-3 using

the as-built Revision AF and the latest Revision BB of design

drawing 12E-2697.

Due to the perplexity of the existing

drawing control system the inspector had to use 18 different

revisions to drawing 12E-2697, AF through BB, to determine if

field installed components or panel wiring appear on the

drawings.

The inspector could not determine the as-built

configuration of this panel using the existing system.

During

the limited review of this panel the inspector observed the

following discrepancies:

(a)

The white conductor of external cable no. 22839 was

improperly spliced to a green conductor approximately

18 inches away from point EE-76 where it was terminated.

The splice contained a ring-type lug on each conductor

and was held together with a nut and bolt.

Black tape was

wrapped around this splice. This splice was not in

accordance with existing procedures or industry practices.

14

(b)

The metal protective cover over device

11 GHC

11 was observed

to be in contact with the exposed resistor and capacitor

of the printed electronic circuit board mounted inside the

panel.

(3)

The inspector examined a portion of the Auxiliary Electric

Equipment room panel 902-33 as shown on wiring diagram

12E-2758B, Revision AB (as-built) through Revision AJ (latest).

Central File records indicated that the following modifications

and drawing revisions ~o drawing 12E-2758B had been implemented

in the field:

Modification Nos.

M12-2-82-27

M12-2-84-08

M12-2-84-118

Applicable

DrE-~l!!.9 Revisions

AC/AF

AH

AJ

During this inspection the inspector observed the following

discrepancies:

(a)

Conductors terminated to points DD-89 and DD-90 were

observed to be very loose.

(b)

Point DD-84 contained a lug that extruded away from the

terminal point and appeared not be be securely held

underneath the terminating screw.

(c)

The red conductor of cable no. 22646 was found terminated

to point DD-80 in the panel, but was not shown on any of

the design drawing revisions. This conductor was later

determined to be a spare.

(4)

Drawings 12E-3437, Revision S, and 12E-3438, Revision V, showed

portions of the LPCI pump start circuitry, which do not

appear to be functional as shown.

The licensee indicated that

during the drawing revision process these portions should have

been removed from the drawings, but the balloon encircling the

portion of the circuitry to be removed faded with each copy of

the drawing.

Eventually the drawing no longer showed the

circuit was removed.

The licensee had work requests complete or in progress to

correct the items described in previous items (2) through (4);

however, these findings are considered further examples of the

issues identified by the SSOMI team.

One violation was identified in this area.

15

5

Work Requests

During the review of modification M12-2-84-8, the inspectors became

concerned about the licensee's method for updating drawings to reflect

the "as-built" condition of systems in the plant.

The inspectors were

concerned that the licensee would have a significant problem selecting the

appropriate drawing revisions that would accurately reflect the

as-installed condition of plant systems without a detailed system walkdown.

In an attempt to resolve this concern, several

work requests were reviewed to determine which

routinely utilized for maintenance activities.

are identified as follows:

completed safety-related

drawing revisions were

The work requests reviewed

Unit

3

3

2/3

2

2

2

2

Work

Request

42217 &

42218

47867

44726

48239

43469

44028

48180

Date

03/86

10/85

12/85

10/85

04/85

10/85

10/85

Description

Inspect/repair pressure suppression

1 evel trasnmitters for "EQ"

Replacement of ECCS fill pump

motor

Repair cables to the 2/3 diesel

cooling water pump

Maintenance on limitorque operator

for the isolation condenser valve

2-1301-1

Replaced motor & rewired operator

for isolation condenser valve

2-1301-4

Replaced motor on valve 2-1301-4

Rebuilt operator on valve 2-1301-4

Of the eight packages reviewed, only three referred to specific drawings

for the maintenance to be performed.

Several of the packages referred to

"manuals and drawings available in maintenance files under EP number."

The

licensee's procedure for drawing control, OAP 2-3, authorizes maintenance

to be performed with "as-built" drawings from the maintenance department

satellite files.

As noted in Paragraph 4, the licensee's "as-built" drawings may or may not

reflect the actual conditions in the plant. It was also noted that the

five work packages that did not invoke specific drawings were closed

without the drawing(s) number(s)and revision(s) utilized to perform the

work being documented in the package.

The inspector, therefore, was unable

to determine which drawings or revisions were used to perform the work.

16

Based on this uncertainty, the inspector requested the

licensee to remove the connection cover on the Unit 2 isolation

condenser inboard isolation valve 2-1301-1 in order to perform

a detailed wiring inspection. This particular valve had been

internally rewired under work request 48239 in October 1985.

The work request invoked drawings 12E-2674E, Revision T, and

12E-2507A, Revision F, for the wiring details. A review of

these drawings found that drawing 12E-2674E, Revision T,

invokes drawing 12E-2507B for the wiring schematic for the

valve.

It was noted that drawings 12E-2507A and 12E-2507B

provide different wiring schematics for the valve.

During the

actual valve wiring inspection on May 22, 1986, the licensee's

technical staff engineer selected Revision U to drawing

12E-2674E.

The inspector noted that, for the area of interest,

Revisions U and T of the drawing are the same.

The limitorque

wiring for valve 2-1301-1 was found to conform with drawing

12E-2674E.

The wiring at the motor control center 28-1, however, did not

agree with the drawing.

Connection points, although

electrically equivalent, did not match the connection drawing.

During the wiring of valve 2-1301-1, several problems were

noted.

These included:

(a) A leaking torque switch housing gasket that allowed grease

to cover many of the wires.

(b)

The outer shielding on the cables from the power supply

junction box to the operator showed signs of aging.

The

condition of the actual cables could not be evaluated.

(c)

The rotor contacts for the limit switches were severely

corroded.

(d) Three lug connections were damaged with one lead to the

closed torque switch damaged to the extent that it broke

while moving the attached wire during the inspection.

(e)

The insulation on the motor leads was nicked adjacent to

the Raychem splice.

(f) The insulation on one of the leads to the lower rotor

connections was cracked exposing bare wire.

(g)

In motor control center (MCC) 28-1 compartment J-4, two

wires were noted to be spliced with short lengths of

unidentified gray wire such that it was difficult to

confirm the proper wire color code.

Items (a) through (f) above were referred to the environmental

qualification team, which was onsite for evaluation.

The

results of that evaluation will be included in report 237/86013.

Item (g) was pointed out to the electrician foreman for action.

17

  • r

-

.

,._

During the review of work request 47867 for replacement of the

Unit 3 Emergency Core Cooling System (ECCS) keep full pump in

the west corner room, it was noted that a non-safety-related

motor was installed in the safety-related application. Although

the appropriate form, OAP 11-5a, was included in the package, the

acceptance criteria utilized to upgrade the motor application

was not readily apparent in the data. The needed technical

comparison and evaluation of the original installation

specifications versus the part being utilized was not included

in the package.

Pending resolution, this issue will remain an

unresolved item (249/86017-02(DRS)).

No violations or deviations were identified; however, one issue

requires further review and is documented as an unresolved item.

6.

Unresolved Items

7.

Unresolved items are matters about which more information is required

in order to ascertain whether they are acceptable items, violations or

deviations.

An unresolved item disclosed in the inspection is discussed

in Paragraph 5.

Exit Interview

The inspection team met with the licensee representatives denoted in

Paragraph 1 on May 23, 1986, at the conclusion of the inspection.

The

inspectors summarized the scope of the inspection and the findings.

The

licensee acknowledged the statements made by the inspectors with respect

to the unresolved item and the violation denoted in Paragraph 4.a.

The

inspectors also discussed the likely informational context of the

inspection report with regard to documents or processes reviewed by the

inspectors during the inspection.

The licensee did not identify any such

documents/processes as proprietary.

18