ML17174A744

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Safety Insp Repts 50-237/91-10 & 50-249/91-09 on 910402-0516.Noncited Violations Noted.Major Areas Inspected: Licensee Action on Previously Identified Items,Lers, Operational Safety,Monthly Maint & ESF Walkdown
ML17174A744
Person / Time
Site: Dresden  
Issue date: 06/05/1991
From: Burgess B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17174A745 List:
References
50-237-91-10, 50-249-91-09, 50-249-91-9, NUDOCS 9106120057
Download: ML17174A744 (11)


See also: IR 05000237/1991010

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Repo~t Nos.

50-237/91-0lO(DRP); 50-249/91009(DRP)

Docket Nos.

50-237; 50-249

License Nos.

DPR-19; DPR-25

Licensee:

Commonwea 1th Edi son Company

Opus West II I

1400 Opus Place

  • Downers Grove, IL

60515

Facility Naine:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Conducted: April 2 through May 16, 1991

Inspectors:

D.

Hills

Approved

M.

Peck

R. Lerch

S. Burgess

R. Zuffa, Site Resident Engineer

Illinois Department of Nuclear Safety

By~~ef

Projects Section 18

Inspection Summary

Date 1

'

Ins ection from A ril 2 throu

(Re ort Nos. 50-237/91010(DRP);

50-249 91009 DRP

Areas Inspected: Routine unannounced safety inspection by the resident

inspectors, regional inspectors and an Illinois Department of Nuclear Safety

inspector of licensee action on previously identified items; licensee event

. reports; operational safety;- monthly maintenance; monthly surveillance;

engirieered*safety features walkdown; training effectiveness; events; safety

assessment and quality verification; and systematic evaluation program items

and report review.

Results:* Two non-cited violations were identified.

One involved the use of

non- licensed operators to perform direct reactivity_ changes (parag.raph 4.e)

and the other involved the control of design input assumptions to the diesel

generator service water calculation (pa~agraph 2).

Two unresolved items w~re

identified, one involved the calibration requirements of primary and secondary

containment tsolation damper fail-safe pressure switches (paragraph 7), the

other dealt with reactor. shroud head bolts not fully tightened (paragraph 9) .

9106120057 910605

PDR

ADOCK 05000010

Q

PDR

Plant Operations

This 'area. remains under close scrutiny due ~o the negative trend in operationa 1

practices as delineated in recent inspection reports and as illustrated by

the utilization of non-licensed operators to perform direct reactivity

changes. However, identification of the Unit 2 power/flo~ anomaly and the

quick reaction during the reactor recirculation pump run-up/over power

event indicated good operator response to off normal conditions.

Maintenance/Surveillance

This area remained on a declining trend in regard to wor~ practices. This was

exhibited by the failur~*to properly install -the Unit 2 reactor steam separator

assembly.

Radiological Protection

~erformanc~ in this area remained good.

No problem~ were noted during the

inspection.

Emergency Preparedness

This SALP functional area was not addressed in this inspection period.*

Security

Performance in this area remained good.

No problems were noted during the

inspection.

Safety Assessment and Quality Verification

Performance in this area continued to improve.

This was evident by the

coo~dination and review of NRC concerns identified at the Quad Cities

facility.

Engineering and Technical Support *

This area remains under close scrutiny due to the mixed trend delineated in past

  • reports. This was evident by the utilization of non-conservative assumptions

utilized in the diesel .generator cooling water calculations *

2

.

.

1.

DETAILS

Persons Contacted

Commonwealth Edison Company

  • E. Eenigenburg, Station Manager_

-*L. Gerner, Technical Superintendent

J. Kotowski, .Production Superintendent

E. Mantel, Setvices Director

  • D~ Van Pelt, Assistant Superintendent - Maintenance

J. Achterberg, Assistant Superintendent - Work Planning

  • G. Smith, Assistant Superintendent-Operations *
  • K. Peterman, Regulatory Assurance Supervisor

M. Korchynsky, Operating Engineer

B. Zank, Operating Engineer

J. Williams, Operating Engineer

R. Stobert, Operating Engineer

T. Mohr, Operating Engineer

M*. Strait, Technical Staff Supervisor

L.* Johnson, Q.C. Supefvisor

J. Mayer, Station Security Administrator

D. Morey, Chemistry Services Supervisor

D. Saccomando, Health Physics Services Supervisor

K. Kociuba, Qua 1 ity Assurance Superintendent

  • D. Lowenstein, Regulatory Assurance Analyst

.

  • R. Ra.dtke, Compliance Engineering, NuClear Licensing
  • R. Wahlen, Technical Staff
  • R. Janecek, Sr. Participant - Offsite Review
  • K. Yaks, ONS Administrator
  • B. Viehl, Nuclear Enginee~ing Department, Supervisor
  • Denotes those attending the exit interview conducted on May 16, 1991.

The inspectors also talked with and interviewed several additional

- licensee employees, including members of the technical and engineering

staffs, reactor and auxiliary operators, shift engineers and foremen,

electrical, mechanical and instrument maintenance personnel, and contract

security personrie 1.

2.

Previously Identified Inspection Items (92701 and 92702)

(Closed) Unresolved Item (50-237/91003-02):

The licensee ha~ resporid~d

to NRC concerns regarding the appropriateness of design input

-

parameters/assumptions uti*lized in the Stone and Webster Diesel Generator

Cooling Water (DGCW) Requirements Calculation (18662-M(CI)-10 .

  • .

Re~ision 0).

Examples of assumption discrepancies included:

1100 gpm design Diesel Generator (D/G) water jacket side flow was

assumed.

This input was non-conservative and inconsistent with the

1080 gpm value required by the vendor manual reference.

3

The calculation assumed 2500 Kw for the continuous D/G output rating

and *2750 Kw for the two hour overload condition. This input was

.

non-conservative and inconsistent with the Final Safety Analysis

Report (FSAR) ratings of 2600 Kw for continiJousoutput and 2860 Kw

for the ove~load condition.

The assumed design cooling manifold temperature alarm location used

. in the calculation was not consistent with plant drawing M517.

The

calculation incorrectly positioned the alarm on the heat exchanger

inlet while the drawing indicated the alarm te~perature switch to be

on the outlet.

The calculation was revised following NRC identification of the .

discrepancies.

The revised calculation resulted in an increase. of the*

minimum flow requirement .from 830 gpm to 840 gpm.

When compared to the

850 gpm available flow established during testing, the use of *corrected

input assumptions reduced 'the analytical flow margin 50%.

To correct the

programmatic deficiencies of inadequate review of design deficiencies, the

licensee issued Engineering and to~struction (ENC)-QE-81, Revision 0, "Rev1ew

of Assumptions and Judgements For Architect Engineered Supplied Design

Evaluations".

ENC-QE-81 was to ensure the applicable regulatory

requirements were addressed for design evaluations and an adequate review

.of associated assumptions was performed.

Failure to adequately control

design input assumptions used by contract architect/engineers is

considered a violation of {50-237/91010-0l{DRP)) 10 CFR 50, Appendix B,

Criterion III, "Design Control".

However, as this was considered to be

-an isolated occurrence of minimum safety significance, and the

appropriate corrective actions were completed, a Notice of Violation is

not being issued 'in accordance with 10 CFR -2, Appendix C, Section V~A.

  • The inspector has no furthei concerns in this area.

{Open)

Open Item (50-237/89019-04):

Verify installation of river level

indication and alarm in the control room for Systematic Evaluation

Program (SEP) Topic II-3.B.l/4.1~4. This item is to remain open until

the mo~ification has been completed .. Current expected completion date is

  • September 1991.

Orie non-cited violation and no deviations were identified in this. area.

3.

Licensee Event Reports Followup (90712 and 92700)

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to determine

that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence had

been accomplished in accordance with Technical Specifications.

a.

(Closed) LER 237/91001:

Partial Group I Isolation Due to Shorting

of 18 Main Steam Isolation Valve (MSIV) Position Indicating Light

Socket.

b.

(Closed) LER 237/91003:

Omission of Liquid Radwaste Discharge

Composite Analysis Due to Management Deficiency. -

c.

(Closed) LER 237/91006:

Unplanned Primary Containment Group V *

4

'

i

.*

Isolation Due to Unknown Causes.

d.

(Closed) LER 237/91007:

Violation of Core Thermal Power Limits Due

to Unplanned 28 ReaC:tor Recirculation Pump Speed<Increase.

In additi~n,.the inspecto~ reviewed the licensee's Deviatio~ re~orts

(DVRs) generated during the inspection period. This was done in an

effort to monitor the conditions related to plant or pers.onnel

  • performance, potential trends, etc.

DVRs were also reviewed for

initiation and disposition as required by .the applicable procedures and

the Quality Assurance (QA) manua 1.

No violations or deviations were identified.

4.

Operational Safety Verification (71707)

The inspectors daily and randomly verified during back shift and on

weekends, that the facility was being operated in conformance with the

licenses and regulatory requirements and that the licensee's management

control system was effectively carrying out its responsibilities for safe

operation. This was done on a sampling basis through routine direct

observation of activities and equipment, tours~ interviews and

discussions with licensee personne 1, verification of safety system status

and limiting conditions for operation action requirem~nts (LCOs),

corrective action, and review of facility_retords.

On a sampling basis the inspectors daily verified proper control room

staffing and access~ operator behavior, a~d coordination of p1ant

activities with ongoing control room operations; verified operator

adherence with the latest revisions of procedures fo~ ongoing activities;

verified operation as required by Technical Specifications (TS);

including compliance with LCO~, with.emphasis on engineer~d.safety

features (ESF) and ESF electrical alignment and valve positions; .

monitored instrumentation recorder trace channels for abnormalities;

.verified status of variou~ lit annunciators fo~ operator understanding,

off-normal condition, and corrective actions being taken; examined

nuclear instrumentation and other protection channels for proper

operability; reviewed radiation and stack monitors for abnorma*l

conditions; verified that onsite and offsite power was avajlable as

required; observed the frequency of plant/control room visits by the

station manager, superintendents, assistant superintendents, and othe~

managers; *and observed the Safety Parameter Display System for


~o~p=e=rao-i-1 *

During tours of accessible areas of the plant, the inspectors made note

of general plant/equipment conditions, including control of -activities in

progress (maintenance/surveillance), observation of shift turnovers,

general safety items, etc. The specific areas observed were:

a.

Engineered Safety Features (ESF) Systems

. Accessible portions of ESF systems and components were inspected to

verify:

valv~ position for proper flow path_; proper alignment of

5

b.

power supply breakers or fuses {if visible) for proper actuation on

an initiating signal; proper removal of power from components if

required by TS or FSAR; and the operability of support systems

essential to system actuation or performance through observation of

instrumentation and/or proper valve alignment.

The inspectors also *

visually inspected components for leakage, proper lubrication,

cooling water supply, etc.

Radiation Protection Controls

The inspectors verified that workers were following health physics

procedures for dosimetry, protective clothing, frisking, posting*,

etc.i and randomly examined radiation protection instrumentation 'for

use, operability, and calibration.

c.

Securit.y .

Each week during routine activities ortours, the inspector

monitored the li~ensee's security program to ensure that observed

actions were being implemented according to their approved security

plan.

The inspector noted that persons within the protected area

  • displayed proper photo-identification badges and those individuals

requiring escorts were properly escorted~ The inspector also

verified that checked vital areas were locked and alarmed *

d.

Housekeeping and Plant Cleanliness.

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection, protection of safety-related

equipment from intrusion of foreign matter and general protection of .

equipment from hazards.

e.

Reactivity Control By Non-Licensed Individuals

The licensee identified the inappropriate practice of utilizing non-

licensed operators to perform local manual operation of the reactor

recirculation (RR) pump scoop tube positioner. The change in the

position of the scoop tube resulted in a direct change of reactor

reactivity. This evolution was performed on the 2A RR pump by a

. non-licensed operator on June 29 and 30, 1990~ The problem was

attributed to a failure of the corporate 11censing organization to

identify local scoop tube manipulations as a direct reactivity

control during the review of the Title 10, Code of Federal

Regulations, Part 55, March 1987 revision.

To correct the

deficiency, Dresden Operating Procedure {DOP) 202-12, "Recirculation

Pump Motor Generator Set Scoop Tube Operation", was revised to.

restrict local RR pumpscoop tube manipulation only by licensed *

operators.

The practice was in violation {50-237/91010-02(DRP)) of

10 CFR 50.54(i) and 10 CFR 55.13, which requires the licensee to not

permit manipulation of the controls of the facility by anyone who is

not a licensed operator or licensed operator trainee.

However, as

this violation was considered*an isolated occurrence and

corresponded to the criteria for the exercise of discretion

delineated in 10 CFR 2, Appendix C, S~ction V.G.1, a Notice of

Violation is not being issued.

The inspectors considered licensee

identification of this issue to represent good coordination and

  • review of NRC concer.ns at the Quad Cities facility.

The inspectqrs also monitored various records, including tagouts,

jumpers, shiftly logs and surveillance, daily orders, maintenance items,

various chemistry and radiological sampling and analysis, third party

review results, overtime records, QA and/or Quality Control (QC) audit

results, and_postings required per 10 CFR 19.11.

One non~cited violation and no deviations were identified in this area.

5.

Monthly Maintenance Observation (62703)

Station maintenance activities affecting the safety-related systems and

components listed below were observed/reviewed to ascertain that they

were conducted in accordance with approved procedures, regulatory guides,

and industry codes or standards and in conformance with Technical

Specifications.

The following items were considered during this review:

the Limiting

Conditions for Operation were met while components or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; _functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by

qualified personnel; parts and materials used were properly certified;

radiological and, fire prevention controls were implemented.

Wo~k

requests were reviewed to determine status of outstanding jobs and to

assure that priority is assigned to safety-related equipment maintenance

which may affect system performance.

The inspectors-monitored the licensee's work in progress and verified

that it was being performed in accordance with proper procedures, and

approved work packages, that applicable drawing updates *were made and/or

planned, and that operator training was conducted in a reasonable period

  • of time.

The following maintenance activities were observed and reviewed.:

Unit 2

2C Electromatic Relief Valve Repla~ement

Control Rod Drive Overhauls

Unit 3

30 Condensate Booster Pump Motor Overhaul

Turbine Building Sample Panel Hangers & Tube Installation

No violations or deviations were identified in this area.

7

...

6~

Monthly Surveillance Observation (61726) *

The inspectors observed surveillance testing required by Technical

Specifications during the inspection period and. verified that testing was

performed in accordance with adequate procedures, ~hat test

instrumentation was calibrated; that LCOs Were met, that removal and

restoration of the affected components were accompli~hed, that results

conformed with .Technical Specifi*cations and procedure requirements and

were reviewed by personnel*other than the individual directing the test,

and. that any* deficiencies identif.ied during the testing were properly

reviewed and resolved by appropriate management personnel.

Th_e

in~pectors witnessed port"ions of the following test activities:

Unit 2

~

High Pressure Coolant Injection (HPCI) System Cold Fast Start Testing

Rod Worth Minimizer Checkout

Post-LOCA Containment. -H2/02 Monitor Calibration

Unit 3

ReactQt Wide~Range Pressure Instrumentation Calibration

LPCI System Flow Instrumentation Calibration

No violations or deviations were identified in this area *

7.

ESF Walkdown (71710)

A review of the reactor building ventilation isolation damper

.

surveillance procedure, Dresden Technical Surveillance (DTS) 1600-29,

Revision 01; plant drawings M-269, Revision H; M-529, Revision K; M~25,

  • Revision BN; and M-356, Revision AU, indicated several discrepancies *.

Plant drawings M-269 and M-529 identified the reactor building

ventilation isolation dampers, including the fail-safe closure mechanism

and the air reservoir accumulator, as safety~related. However, plant

drawings M-25 and M-356, associated with containment ventilation

isolation dampers, excluded the air reservoir from the safety-related

boundary. *In addition, the safety-related pressure switches associated

with the isolation d~mper fail-safe closure mechanism did not appear to

be incorporated into the station calibration program.

Some of the

similar pressure switches on the primary containment isolation dampers

also did not appear td be periodically calibrated. This issue is

considered an unresolved item (237/91010-03(D~P)) pending further

review of the calibration requirements for the pressure switches.

No violatioris or deviations w~re identified in this area.

8. * Training Effectiveness (41400, 41701)

The effectiveness of training programs for licensed and non-licensed

personnel was reviewed by the inspectors during the witnessing of the

licensee's performance of routine surveillance, maintenance, and

8

operational activities and during the review of *the licensee's response

to ~vents Which occurred during.the inspection period. Personnel -appeared

to be knowl~d_geable of the tasks being performed.

No viol~tions or deviations were identified. '

.

9.

Events (93702)

On April 11, 1991, Dresden Unit 2 exceeded 102% of rated core thermal

power for approximately 5 seconds .. The transient occurred due to ~

malfunctioning deviation meter during resetting of the 28 reactor

recirculation (RR) pump motor-generator (M/G) set scoop tube lockout.*

.

The magnitude of the over power event was limited by the prompt action of

the reactor operator who locked-out the scoop tube at the back panel.

On

April 15, 1991~ a se~ond Unit 2 reactor.overpowe~ event occurred as a

result *of a level transient following the startup of the standby reactor

feedwater pump (RFP).

Reactor power exceeded 102 percent for a 20 second

duration with a 105 percent peak core thermal power.

The second event

occurred while the RR pump scoop tube was locked out for repair.of the

flow controller deviatfon meter. *The standby RFP was started following a

seal failure on one of the two operating pumps;

Lifting of the Shroud Head and Steam S~parator Assembly

On March 22 ~ 1991, Dresden Unit 2 experie*nced an unexpected anomaly in

electrical output as cooling water flow through the reactor core was

  • * i ncrea.sed.

As coolant flow through the reactor core increased from 72 to

75 million pounds per hour, the plant's electrical output increased by 2

megawatts instead of the anticipated 30 megawatt increase. Also, reactor

co.olant temperature in the annulus region increased about 2 degrees

Fahrenheit at the same time the core flow/electrical output anomaly

occurred.

Because the power/flow anomalies were similar to a Vermont

Yankee event associated with the steam separator lifting from the seat on

the core shroud in the reactor, the licensee commenced a Unit 2 shutdown

on March 24, 1991, to inspect the reactor internals.

An investigation

'team comprised of CECo ~orporate and plant individuals was formed to

review this ev~nt, along with other recent maintenance-related problems

during the Unit 2 refuel outage.

On March 27, 1991, regional NRC

specialists arrived on site. to review the event and licensee actions.

On March 27, 1991, the steam dryer was removed to facilitate inspection

of the shroud head bolts. With assistance from General Electric Company

(GE), a detailed inspecti9n plan was initiated and* implemented, with

emphasis placed on verifying if the shroud head bolts were latched and

tightened. Troubleshooting and corrective .action was performed under

WR 000524.

Visual inspections 6n seven accessible shroud head bolts with

an underwater camera indicated that the bolts were *latched, but not

  • tightened. Subsequently, all 48 bolts were verified latched, but not

tightened. Based on an evaluation performed by GE, the_ loose shroud head

bolts would allow the shroud head and steam separator to lift at high

core flow conditions.* The GE analysis for the Vermont Yankee event

concluded that no significant changes in plant safety margins occurred

during operation with the -separator assembly lifted. The causal factors

for the bolts not being fully tightened is an unresolved item

(249/91009-04(DRP)).

g

10. Safety Assessment and Quality Verification (35502 and 40500)

Dres~en Station Technical Support Engineers partiGipate~ in the-daily

Quad Cities NRC Electrical Distribution Safety Funetional Inspection

(EDSFI) debriefings~ - As a result issues raised at the Quad Cities

facility were also evaluated for applicability at Dresden. This included*

the seismic qualification issue of the D/G fuel oil transfer and air

start systems.

When the seismic analysis for the Dresden fuel* oil

transfer system could not be retrieved, the licensee commissioned a

Seismic Qualified Utility Group walkdown by Stevenson and Associates to

address -system operability concerns. Additionally, licensee. identification

of the inappropriate- use of non-licensed operators to perform reactivity

manipulations, as delineated in paragraph 4.e., resulted from the

coordination of NRC concerns raised at the Quad Cities plant.

-~o vi6lations or deviations were identified in this area.

11. Systematic Eva iuation Program Items (92701)

NUREG 1403,

11Saf.ety Evaluation Report Related to the Full-term Operating

License for Dresden Nuclear Power Station,

11 Table 2.1, identified 22 SEP

Integrated Plant.Safety Assessment Report (IPSAR) topic resolutions to be

confirmed by the NRC Region _III office *. -

The expected completidn date for Item 2 for Topic II-3.b.l/4.l.4 is

detailed as Open Item 50-237/89019-04 in p~ragraph 2 of this report.

In

addition to Item 2, the following four items remain to be verified as

closed by the licensee and confirmed by the NRC:

Item 6 - .Topic VI-4/4.18.6

Item 13 - Topic III-2/2.2.2 (Supp. 1)

Item 14 - Topic III-4.A/4.5.3 and 2.2.2 (Supp. 1)

Item_ 16 - Topic VI-4/4.18.2; Topic VI-6/4.19

Each of these items were in some stage of verification review by the

licensee.

No violations or deviations were identified.

12.

Report Review (90173)

During the inspectiori period, the inspector reviewed the licensee's_

Monthly Operating Report for February 1991.

The inspector confirmed that

the information provided met the requirements of Technical Specification -6.6.A.3 and Regulatory Guide 1.16. The inspector also reviewed the

Dresden Nuclear Power Station Monthly Plant Status Report for March 1991._

No violations or deviations were_ identified .

10

13.

Violations For Which A "Notice of Violation" Will Not Be Issued

The NRC uses the Notice of Violation as a standard method for formalizing

the existence of a violation of a _legally binding requirement.

However,

because the NRC wants to encourage and support licensee's initiatives for

self-identificatiori and correctioh* of problems, the NRC will not generally

issue a Notice of .Violation for a violation that meets the requirements

set forth in 10 CFR 2, Appendix C,Section V.A.

Violations of regulatory

  • requirements fdentified during the inspection for whi~h a Notice of

Violation will not be issued are discussed in paragraphs 2 and 4;e.

14. Unresolved Items

15.

Unresolved items are m~tters about which more info~mation is required

in order to ascertain whether they are *acceptable items, items of

Tionco~pliance, or deviations.

The two unresolved items disclosed

during this inspection are discussed in paragraphs 7 and 9.

Exit Interview

The inspectors met with licensee representatives (denoted in paragraph ,1)

during the inspection period and at the conclusion of the inspection

period on May 16, 1991.

The inspectors summarized the scope and results

of the inspection and di~cussed the likely content of this inspection

report.

The licensee acknowledged the information a~d did not indicate

that any of the information disclosed during the inspection could be

considered proprietary in nature.

  • *

11