ML17158B997
| ML17158B997 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 03/14/1997 |
| From: | Pasciak W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Byram R PENNSYLVANIA POWER & LIGHT CO. |
| Shared Package | |
| ML17158B998 | List: |
| References | |
| NUDOCS 9703200086 | |
| Download: ML17158B997 (51) | |
See also: IR 05000387/1997001
Text
CATEGORY 2
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
I
t
CESSION NBR:9703200086
DOC.DATE: 97/03/14
NOTARIZED: NO
IL:50-387 Susquehanna
Steam Electric Station, Unit 1, Pennsylva
50-388
Susquehanna
Steam Electric Station, Unit 2, Pennsylva
AUTH.NAME
AUTHOR AFFILIATION
PASCIAK,W.J.
Region
1 (Post
820201)
RECIP.NAME
RECIPIENT AFFILIATION
BYRAM,R.G.
Power
& Light Co.
SUBJECT:
Forwards
insp repts
50-387/97-01
6 50-388/97-01
on
970114-0224
s notice of violation.Violations either
identified by
NRC or resulted in degradation
of safety-
related
components.
DISTRIBUTION CODE:
IEOIT
COPIES
RECEIVED:LTR I
ENCL Q
SIZE: 3
TITLE: General
(50 Dkt)-Insp Rept/Notice of Violation Response
NOTES:
DOCKET
05000387
05000388
05000387
E
A
P
9'C
RECIPIENT
ID CODE/NAME
PD1-2
INTERNAL: ACRS
AE
LE CE
NR
B
NRR/DRPM/PERH
OE DIR
RGN1
FILE
01
EXTERNAL
LITCO BRYCE P J
H
NRC
NOTES:
COPIES
LTTR ENCL
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RECIPIENT
ID CODE/NAME
POSLUSNY,C
AEOD/SPD/RAB
DEDRO
NRR/DISP/PIPB
NRR/DRPM/PECB
NUDOCS-ABSTRACT
OGC/HDS2
NOAC
NUDOCS FULLTEXT
COPIES
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D
C
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION
LISTS'R
REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL
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ON EXTENSION 415-2083
FULL TEXT CONVERSION REQUIRED
TOTAL NUMBER OF COPIES
REQUIRED:
LTTR
21
ENCL
21
March 14, 1997
Mr. Robert G. Byram
Senior Vice President
- Nuclear
Power 5 Light Company
2 North Ninth Street
Allentown, Pennsylvania
18101
SUBJECT:
NRC INTEGRATED INSPECTION REPORT 50-387/97-01, 50-388/97-01
AND
Dear Mr. Byram:
This refers to the inspections conducted
between January
14, 1997 and February 24,
1997, at the Susquehanna
Steam Electric Station.
The inspections covered routine
activities by the resident inspectors
and announced
inspections
by Region
I specialist
inspectors for radiological effluent control and emergency
preparedness.
The enclosed
report presents
the results of these inspections.
Overall, your conduct of operations
at the Susquehanna
facility during this period was
characterized
by safe operation and conservative
decision making.
The NRC specialist
inspections found that PP5L continues to maintain a very good radioactive liquid and
gaseous
effluent control program, and a good emergency preparedness
program.
However, based on the results of this inspection the NRC has also determined that three
violations of NRC requirements
occurred.
These violations are cited in the enclosed
Notice
of Violation (Notice) and the circumstances
surrounding them are described
in detail in the
subject inspection report.
One violation involves the failure of operators to respond
in
accordance
with procedures
when an accumulation of hydrogen gas occurred in the offgas
recombiner system.
The second violation concerns the design of the bypass indication
system.
The NRC determined that it does not meet a requirement referenced
by 10 CFR 50.55a.
The third violation involves two examples where corrective action in the
maintenance
area was not effective.
These violations are of concern because
they were
~
either identified by the NRC or resulted in the degradation of safety related components.
You are required to respond to this letter and should follow the instructions specified in the
enclosed
Notice when preparing your response.
In your response,
we request that you
discuss the extent to which the bypass indication system installed at Susquehanna
differs
from guidance of Regulatory Guide 1.47 and the system's design specification.
The NRC
will use your response,
in part, to determine whether further enforcement action is
necessary
to ensure compliance with regulatory requirements.
9703200086
970314
ADQCK 05000387
8
llllllll9lllltllilllIIIIIII',IIIIIlllllllllll
Mr. Robert G. Byram
2
In accordance
with 10 CFR 2.790 of the NRC's "Rules of Practice,"
a copy of this letter,
its enclosures,
and your response
will be placed in the,NRC Public Document Room (PDR).
Sincerely,
ORIGINAL SIGNED BY:
Walter J. Pasciak, Chief
Reactor Projects Branch No. 4
Division of Reactor Projects
Docket Nos.:
50-387;50-388
License Nos:
Enclosures:
1. " Inspection Report 50-387/97-01, 50-388/97-01
2.
cc w/encl:
G. T. Jones,
Vice President
- Nuclear Operations
G. Kuczynski, Plant Manager
J. M. Kenny, Supervisor,
Nuclear Licensing
G. D. Miller, Manager - Nuclear Engineering
R. R. Wehry, Nuclear Licensing
M. M. Urioste, Nuclear Services Manager, General Electric
C. D. Lopes, Manager
- Nuclear Security
W. Burchill, Manager, Nuclear Safety Assessment
H. D. Woodeshick, Special Office of the President
J. C. Tilton, III, Allegheny Electric Cooperative,
Inc.
Commonwealth of Pennsylvania
Mr. Robert G. Byram
Dlstnbutlon w/encl:
Region
I Docket Room (with concurrences)
Nuclear Safety Information Center '(NSIC)
D. Barss, NRR (Emergency Plan IRs)
K. Gallagher,
D. Screnci, PAO (1) SALP (23)
NRC Resident Inspector
J. Wiggins, DRS
R. Ragland,
DRS File
PUBLIC
Distribution w/encl: (t/ia E-Mail)
W. Dean, OEDO
C. Poslusny,
Project Manager,
J. Stolz, PDI-2, NRR
Inspection Program Branch, NRR (IPAS)
R. Correia, NRR
D. Taylor, NRR
DOCUMENT NAME: g:ttbranch4<9701.sus
To receive a copy of this document. In
ate ln the boxr
C
~ Copy without attachment/enclosure
'E i Copy with attachment/enclosure
N
No copy
OFFICE
NAME
DATE
RI:DRP
I'Pasciak;
3/t
97
OFFICIAL RECORD COPY
Power and Light Company (PPSL)
Susquehanna
Unit 1 and Unit 2
Docket Nos. 50-387, 50-388
During an NRC inspection conducted
from January
14, 1997, through February 24, 1997,
three violations of NRC requirements
were identified.
In accordance
with the "General
Statement of Policy and Procedures
for NRC Enforcement Actions," NUREG-1600, the
violations are listed below:
Technical Specification (TS) 6.8.1 requires that written procedures
shall be
established
and implemented for applicable procedures
recommended
in Appendix
'A'f Regulatory Guide 1.33, Revision 2, February 1978.
Appendix 'A', item 5, requires procedures
for abnormal, offnormal, and alarm
conditions.
Item 5 further states that procedures
for annunciators
should contain
the immediate action that is to occur automatically and the immediate operator
action.
Alarm response
procedure AR-231-001 for the "Unit 2 Recomb Discharge H2 Conc
Hi - Hi" annunciator lists the automatic action for a 2% hydrogen concentration
as
an Offgas System Isolation.
Further, AR-231-001 Operator action 2.2.1 requires
operators to ensure automatic actions occur.
Contrary to the above, on December
19, 1996, operators failed to ensure the
automatic actions occurred after the "Unit 2 Recomb Discharge H2 Conc Hi - Hi"
alarmed and after a grab sample show a hydrogen concentration of 8%.
Specifically, the offgas system did not automatically isolate and operators
did not
take immediate manual action to isolate it.
This is a Severity Level IV violation (Supplement
1).
10 CFR Part 50, Section 50.55a, "Codes and Standards,"
requires that protection
systems meet the requirements
of the Institute of Electrical and Electronic Engineers
(IEEE) "Criteria for Nuclear Power Plant protection systems," Std 279-1971.
IEEE 279, Section 4.13, requires that, if the protective action of some part of the
protection system has been bypassed,
or deliberately rendered inoperative for any
purpose, this fact shall be continuously indicated in the control room.
Regulatory Guide (RG) 1.47, May 1973, describes
an acceptable
method of
complying with the requirements of IEEE Std 279.
RG 1.47 states that an
acceptable
system will automatically indicate at the system level the bypass or
deliberately induced inoperability of the protection system.
Contrary to the above, since initial operation, the bypass indication system
(BIS) at
Susquehanna
has not provided the continuous control room indication required by
IEEE 279, and 10 CFR 50.55a, when a portion of the residual heat removal system
is bypassed.
The BIS does not automatic'ally indicate at the system level when an
RHR pump is rendered
inoperable by a trip circuit that is enabled when the pump's
suction valve is not full open.
As a result, the RHR system is inoperable during
9703200093
9703i4
ADOCK 05000387
G
quarterly RHR suction valve testing and no automatic indication of this condition is
provided at the system level.
This is a Severity Level IV violation (Supplement
1).
10 CFR 50, Appendix B, Criterion XVI, requires that licensees establish measures to
assure that conditions adverse to quality such as failures, malfunctions,
deficiencies,.defective
material and equipment and nonconformances
are promptly
identified and corrected.
Contrary to the above, two examples were identified where the licensee failed to
control maintenance
activities such that conditions adverse to quality were created
and not promptly identified and corrected.
In 1991, the licensee failed to implement adequate
corrective actions in
response
to a vendor letter that identified a deficiency on the contact
surfaces of the 'E'mergency diesel generator bridge transfer switch.
As a
result of the licensee's failure to implement corrective actions to preclude
the condition identified by the vendor, the transfer switch failed to perform
its function on December 10, 1997, during an 'E'mergency diesel
surveillance test.
2.
In December 1996, the licensee's corrective actions in response
to the failed
'E'iesel generator transfer switch included the development of a trouble
shooting plan.
As a result of inadequate
control and review of the trouble
shooting plan, a failure was induced in safety related equipment and the
'E'mergency
diesel generator failed a second surveillance test.
This is a Severity Level IV violation (Supplement
1).
Pursuant to the provisions of 10 CFR 2.201, Pennsylvania
Power and Light Company is
hereby required to submit a written statement
or explanation to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington,
D.C. 20555 with a
copy to the Regional Administrator, Region I, and a copy to the NRC Resident Inspector at
the facility that is the subject of this Notice, within 30 days of the date of the letter
transmitting this Notice of Violation (Notice).
This reply should be clearly marked as a
"Reply to a Notice of Violation" and should include for each violation:
(1) the reason for
the violation, or, if contested,
the basis for disputing the violation, (2) the corrective steps
that have been taken and the results achieved,
(3) the corrective steps that will be taken
to avoid further violations, and (4) the date when full compliance will be achieved.
Your
response
may reference or include previous docketed correspondence,
if the
correspondence
adequately addresses
the required response.
If an adequate
reply is not
received within the time specified in this Notice, an "order or a Demand for Information may
be issued as to why the license should not be modified, suspended,
or revoked, or why
such other action as may be proper should not be taken.
Where good cause
is shown,
consideration will be given to extending the response time.
Because
your response
will be placed in the NRC Public Document Room (PDR), to the
extent possible, it should not include any personal privacy, proprietary, or safeguards
information so that it can be placed in the PDR without redaction.
If personal privacy or
proprietary information is necessary
to provide an acceptable
response,
then please provide
a bracketed copy of your response
that identifies the information that should be protected
and a redacted copy of your response that deletes such information.
If you request
withholding of such material, you ~mus
specifically identify the portions of your response
that you seek to have withheld and provide in detail the bases for your claim of withhold-
ing (e.g., explain why the disclosure of information will create an unwarranted
invasion of
personal privacy or provide the information required by 10 CFR 2.790(b) to support a
request for withholding confidential commercial or financial information).
If safeguards
information is necessary
to provide an acceptable
response,
please provide the level of
protection described
in 10 CFR 73.21.
Dated at King of Prussia,
this 14th day of March 1997
f
~pQ RKQy
Wp0
g.
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
475 ALLENDALEROAD
KING OF PRUSSIA, PENNSYLVANIA19406 1415
Marek 14, 1997
Mr. Robert G. Byram
Senior Vice President
- Nuclear
Power
Ei Light Company
2 North Ninth Street
Allentown, Pennsylvania
18101
SUBJECT:
NRC INTEGRATED INSPECTION REPORT 50-387/97-01, 50-388/97-01
AND
Dear Mr. Byram:
This refers to the inspections conducted
between January
14, 1997 and February 24,
1997, at the Susquehanna
Steam Electric Station.
The inspections
covered routine
'activities by the resident inspectors
and announced
inspections
by Region
I specialist
inspectors for radiological effluent control and emergency preparedness.
The enclosed
report presents
the results of these inspections.
Overall, your conduct of operations
at the Susquehanna
facility during this period was
characterized
by safe operation and conservative
decision making.
The NRC specialist
inspections found that PPhL continues to maintain a very good radioactive liquid and
gaseous
effluent control program, and a good emergency
preparedness
program.
However, based
on the results of this inspection the NRC has also determined that three
,violations of NRC requirements
occurred.
These violations are cited in the enclosed
Notice
of Violation (Notice) and the circumstances
surrounding them are described
in detail in the
subject inspection report.
One violation involves the failure of operators to respond
in
accordance
with procedures
when an accumulation of hydrogen gas occurred in the offgas
recombiner system.
The second violation concerns the design of the bypass indication
system.
The NRC determined that it does not meet a requirement referenced
by 10 CFR 50.55a.
The third violation involves two examples
w'here corrective action in the
maintenance
area was not effective.
These violations are of concern because
they were
either identified by the NRC or resulted in the degradation of safety related components.
You are required to respond to this letter and should follow the instructions specified in the
enclosed
Notice when preparing your response.
In your response,
we request that you
discuss the extent to which the bypass indication system installed at Susquehanna
differs
from guidance of Regulatory Guide 1,47 and the system's design specification.
The NRC
will use your response,
in part, to determine whether further enforcement
action is-
necessary
to ensure compliance with regulatory requirements.
Mr. Robert G. Byram
2
In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice,"
a copy of this letter,
its enclosures,
and your response
will be placed in the NRC Public Document Room (PDR).
Sincerely,
Walter J.
asciak, Chief
Reactor Projects Branch No. 4
Division of Reactor Projects
Docket Nos.:
50-387;50-388
License Nos:
Enclosures:
1
~ Inspection Report 50-387/97-01, 50-388/97-01
2.
cc w/encl:
G. T. Jones,
Vice President
- Nuclear Operations
G. Kuczynski, Plant Manager
J. M. Kenny, Supervisor, Nuclear Licensing
G. D. Miller,'anager - Nuclear Engineering
R. R. Wehry, Nuclear Licensing
M. M. Urioste, Nuclear Services Manager, General Electric
C. D. Lopes, Manager - Nuclear Security
W. Burchill, Manager, Nuclear Safety Assessment
H. D. Woodeshick, Special Office of the President
J. C. Tilton, III, Allegheny Electric Cooperative, Inc.
Commonwealth of Pennsylvania
Docket Nos. 50-387, 50-388
Power and Light Company (PPRL)
Susquehanna,
Unit
1 and Unit
2'uring
an'NRC inspection conducted
from January
14, 1997, through February 24, 1997,
three violations of NRC requirements
were identified.
In accordance
with the "General
Statement of Policy and Procedures
for NRC Enforcement Actions," NUREG-1600, the
violations are listed below:
'echnical
Specification (TS) 6.8
~ 1 requires that written procedures
shall be
established "and implemented for applicable procedures
recommended
in Appendix
'A'f Regulatory Guide 1.33, Revision 2, February 1978.
Appendix 'A', item 5, requires procedures
for abnormal, offnormal, and alarm
conditions.
Item 5 further states that procedures
for annunciators
should contain
the immediate action that is to occur automaticatly and the immediate operator
action.
Alarm response
procedure AR-231-001 for the "Unit 2 Recomb Discharge H2 Conc
Hi - Hi" annunciator lists the automatic action for a 2% hydrogen concentration
as
an Offgas System Isolation.
Further, AR-231-001 Operator action 2.2.1 requires
operators to ensure automatic actions occur.
Contrary to the above, on December
19, 1996, operators failed to ensure the
automatic actions occurred after the "Unit 2 Recomb Discharge H2,Conc Hi - Hi"
alarmed and after a grab sample show a hydrogen concentration
of 8%.
Specifically, the offgas system did not automatically isolate and operators
did not
take immediate manual action to isolate it.
This is a Severity Level IV violation (Supplement
1).
10 CFR Part 50, Section 50.55a, "Codes and Standards,"
requires that protection
systems meet the'requirements
of the Institute of Electrical and Electronic Engineers
(IEEE) "Criteria for Nuclear Power Plant protection systems," Std 279-1971.
IEEE 279, Section 4.13, requires that, if the protective action of some "part of the
protection system has been bypassed,
or deliberately rendered inoperative for any
purpose, this fact shall be continuously indicated in the'control room.
Regulatory Guide (RG) 1.47, May 1973, describes
an acceptable, method of
complying with the requirements of IEEE Std 279.
RG 1.47 states that an
acceptable
system will automatically indicate at the system level the bypass, or
deliberately induced inoperability of the protection system.
Contrary to the, above, since initial operation, the bypass indication system (BIS) 'at
Susquehanna
has not provided the continuous control room indication required by
IEEE 279, and 10 CFR 50.55a, when a portion of the residual heat removal system
is bypassed.
The BIS does not automatically indicate at the system level when an
RHR pump is rendered
by a trip circuit that is enabled when the pump's
suction valve is not full open.
As a result, the RHR system is inoperable during
2
quarterly RHR suction valve testing and no automatic indication of this condition is
provided at the system level.
This is a Severity Level IV violation (Supplement
1).
10 CFR 50, Appendix 8, Criterion XVI, requires that licensees establish measures
to
assure that conditions adverse to quality such as failures, malfunctions,
deficiencies, defective material and equipment and nonconformances
are promptly
identified and corrected.
Contrary to the above, two examples were identified where the licensee failed to"
control maintenance
activities such that conditions adveise
to" quality were created
and not promptly identified and corrected.
1.
In 1991, the licensee failed to implement adequate
corrective actions in
response
to a vendor letter that identified a deficiency on the contact
surfaces of the 'E'mergency diesel generator bridge transfer switch.
As a
result of the licensee's failure to'implement corrective actions to pr'eclude
the condition identified by the vendor, the transfer switch failed to perform
its function on December 10, 1997, during an 'E'mergency diesel
surveillance test.
In December 1996, the licensee's corrective actions in response to the failed
'E'iesel generator transfer switch included the development of a trouble
shooting plan.
As a result of inadequate
control and review of the trouble
shooting plan, a failure was induced in safety related equipment and the
'E'mergency
diesel generator failed a second'surveillance
test.
This is a Severity Level IV violation (Supplement
1).
Pursuant to the provisions of 10 CFR 2.201, Pennsylvania
Power and Light Company is
hereby required to submit a written statement or explanation to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555 with a
copy to the Regional Administrator, Region I, and a copy to the NRC Resident Inspector at
the facility that is the subject of this Notice, within 30 days of the date of the letter
transmitting this Notice of Violation (Notice). This reply should be clearly marked as a
"Reply to a Notice of Violation" and should include for each violation:
(1) the reason for
the violation, or, if contested,
the basis for disputing the violation, (2) the corrective steps
that have been taken and the results achieved,
(3) the corrective steps that will be taken
to avoid further violations, and (4) the date when full compliance will be achieved.
Your
response
may reference or include previous docketed correspondence,
if the
correspondence
adequately addresses
the required response.
If an adequate
reply is not
received within the time specified in this Notice, an order or a Demand for Information may
be issued as to why the license should not be modified, suspended,
or revoked, or why
such other action as may=be proper should not be taken.
Where good cause
is shown,
consideration will be given to extending the response
time.
0
Because your response
will be placed in the NRC Public Document Room (PDR), to the
extent possibl'e, it should not include any personal privacy, proprietary, or safeguards
information so that it can be placed in the PDR without redaction.
If personal privacy or
proprietary information is necessary
to provide an acceptable
response,
then please provide
a bracketed copy of your response that identifies the information that should be protected
and a redacted
copy of your response that deletes such information.
If you request
withholding of such material, you ~mus
specifically identify the, portions of your response
that you seek to have withheld and provide in detail the bases for your claim of withhold-
ing (e.g., explain why the disclosure of information will create an unwarranted
invasion of
personal privacy or provide the information required by 10 CFR 2.790(b) to support
a
request for withholding confidential commercial or financial information).
If safeguards
information is necessary
to provide an acceptable
response,
please provide the level of
protection described
in 10 CFR 73.21.
Dated at King of Prussia,
this 14th day of March 1997
U. S. NUCLEAR REGULATORY COMMISSION
REGION
I
Docket Nos:
License Nos:
50-387, 50-388
Report No.
50-387/97-01, 50-388/97-01
Licensee:
Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
19101
Facility:
Susquehanna
Steam Electric Station
Location:
P.O. Box 35
Berwick, PA 18603-0035
Dates:
January
14, 1997 through February 24, 1997
Inspectors:
K. Jenison,
Senior Resident Inspector
B. McDermott, Resident Inspector
L. Eckert, Radiation Specialist
J. Jang,
Sr. Radiation Specialist
J. Lusher, Emergency Preparedness
Specialist
Approved by:
Walter J. Pasciak, Chief
Projects Branch 4
Division of Reactor Projects
9703200099
9703i4
ADOCK 05000387
6
EXECUTIVE SUMMARY
Susquehanna
Steam Electric Station, Units
1 5 2
NRC Inspection Report 50-387/97-0'I, 50-388/97-01
This integrated inspection included aspects of licensee, operations,
engineering,
maintenance,
and plant support.
The report covers
a 6-week period of resident inspection;
in addition, it includes the results of announced
inspections by Region
I specialist
inspectors for radiological effluent control and emergency preparedness.
~Oerations
\\
An accumulation of hydrogen gas in excess of the Technical Specification (TS)
concentration limit occurred in the Unit 2 main condenser offgas system.
The
system did not automatically isolate as designed,
prior to reaching this level, due to
the use of jumpers in the high hydrogen isolation circuit. Operators did not
manually initiate a system isolation when a TS required alternate sample showed
the hydrogen concentration to be 400% of the automatic system's setpoint.
The
operators'ailure
to implement the actions of the high hydrogen alarm response
procedure
in response to multiple indications of a high concentration
is cited as a
violation.
A Unit 2 RHR pump failed to start when a limit switch on it's suction valve did not
operate properly.
As a result of the switch failure, the 'D'HR pump was
inoperable with the reactor in Condition
1 for greater than the 7 days and 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />
allowed by Technical Specifications.
PPSL has implemented appropriate corrective
actions.
NRC review of the event determined the failure was beyond reasonable
licensee control and, as such, the failure to meet TS is being treated as a non-cited
violation, consistent with section VI.A. of the NRC Enforcement Policy.
PPS.L identified that operators made a reactor mode switch change, placing Unit
1
in Condition 2 (Startup), when the limiting conditions for operation of TS 3.5.1
were not met.
PP&L determined that human performance was the root cause of
the event and implemented corrective actions focused on procedural enhancements
and training.
This violation of TS 3.0.4 is being treated
as a licensee identified non-
cited violation.
Maintenance
Problems with the material condition and reliability of the condensate
transfer
system and the Unit 1 reactor core isolation cooling (RCIC) system steam line drain
pot have not been resolved by PPSL, despite their recurrence over the last year.
PPSL's failure to maintain a reliable condensate
transfer system necessitates
entry
into off normal procedures for loss of emergency core cooling system
(ECCS) keep-
fillpressure
and unplanned starts of certain ECCS pumps.
The failure to resolve the
reactor core isolation cooling (RCIC) drain pot problem has the potential to cause
additional steam leaks and RCIC system unavailability.
The failure to properly perform maintenance
activities on the 'B', 'C'nd 'E'.
resulted in degradation of their generators'lip
ring
assemblies.
Although operability of the diesel generators was not challenged, the
potential existed for common cause degradation
due to inadequate
performance of
maintenance.
The failure to properly perform this maintenance,
in accordance with
procedures,
constitutes
a violation of minor consequence
and is being treated as a
non-cited violation consistent'with Section IV of the NRC Enforcement Policy.
The Susquehanna
Unit 1 and Unit 2 switchyards are considered to be within the
scope of the maintenance
rule program and are being monitored by PPSL on the
plant level.
The inspector found that PPKL was meeting the maintenance
rule
requirements with regard to monitoring of the switchyards.
~ncnineerinq
Nuclear System Engineering provided a through revision of an operability
determination for a degraded power supply impacting low pressure coolant injection
valves.
Although the initial operability determination made by operators on a
backshift was upheld, the initial justification for the degraded condition did not have
a technical basis and relied entirely on meeting
a Technical Specification
surveillance requirement.
~
On December 10 and on December 21, 1996, the 'E'mergency diesel generator
(DG) failed a functional test.
The cause of'the first failure was a high resistance
contact on the DG bridge transfer switch which was not maintained as
recommended
by the manufacturer.
The second test failure was caused by two
damaged
gate firing circuits.
The gate firing circuits were damaged during
inadequate troubleshooting
and testing activities performed by the licensee.
0
The initial Nuclear System Engineering
(NSE) operability determination following the
first failure was determined to be weak, but the NSE activities following the second
failure were determined to be very strong and aggressive.
Causal factors for the
failures included inadequate
control of vendor recommendation
for preventive
maintenance
and vendor manual documentation,
and inadequate
control of pre-
exercising equipment that may mask weaknesses
that would affect TS surveillance
testing activities.
A violation was issued for inadequate corrective actions in
response to the vendor's notification and previous like conditions, and the
licensee's troubleshooting
and testing activities following the first failure.
Plant Su
ort
~
Oversight of the Radiological Effluent Technical Specifications program was good.
Corrective actions for audit findings were considered to be appropriate; the effluent
radiation monitoring system calibration program was well maintained; and
maintenance
and surveillance of air cleaning and ventilation systems were very
good.
The Offsite Dose Calculation Manual and Annual Radioactive Effluent
Release
Report were well-detailed.
The licensee continues to maintain a good emergency preparedness
program.
The
emergency response
plan and implementing procedures were current and effectively
implemented.
The emergency facilities, equipment, instruments and supplies were
found to be maintained in a state of readiness.
All required inventories were
completed.
A sampling of emergency response
organization personnel training
records and the records pertaining to on-shift dose assessment
indicated that
training and qualifications were current.
A review of quality assurance
reports
found that quality assurance
audits were thorough and that they satisfied NRC
requirements.
TABLE OF CONTENTS
I. Operations
"01
02
Conduct of Operations
01.1
Offgas System Recombiner Hydrogen Accumulation
Operational Status of Facilities and Equipment
. ~.....
~
.
02.1
Unit 2 'D'HR Pump Start Failure
08
Miscellaneous Operations Issues
08.1
Mode Change Requirement Not Met ....
08.2
Review of Licensee Event Reports
04
Operator Knowledge and Performance
04.1
Operator Response
to Operational Occurrences
~
~
~
~
0
~
~
0
~
~
~
0
1
1
1
3
3
5
5
5
5
6
II. Maintenance
M1
M2
III. Engineering
Conduct of Maintenance.........
M1.1
Planned Maintenance Activity Review ~.................
M1.2
Surveillance Test ActivitySample Reviews
Maintenance
and Material Condition of Facilities and Equipment
M2.1
Material Condition of Plant Equipment and Systems
~
~
. ~....
Maintenance Staff Knowledge and Performance
M4.1
Review of Emergent Maintenance
- 'E'iesel Generator
Preventive Maintenance
Maintenance Organization and Administration
M6.1
Verification of Maintenance
Rule Requirements
.
8
8
8
9
10
10
11
11
12
12
14
E2
E8
Engineering Support of Facilities and Equipment
E2.1
Operability Determination For RHR Swing-bus MG Set
E2.2
Engineering Support of Diesel Generator Maintenance
E2.3
Bypass Indication System (BIS) Design.....
Miscellaneous Engineering Issues.....
E8.1
Review of FSAR Commitments
14
14
15
18
19
19
IV. Plant Support .....
R1
R2
R3
R6
R7
R8
Radiation Protection and Chemistry Controls (RP&C)
R1.1
Implementation of Radioactive Liquid and Gaseous
Effluent
Control Programs ...
Status of RP&C Facilities and Equipment
.
R2.1
Calibration of Effluent/Process
Radiation Monitoring Systems
(RMS)
R2.2
Calibration of Area Radiation Monitoring Systems (ARMS)
R2.3
Air Cleaning Systems
RP&C Procedures
and Documentation
RP&C Organization and Administration ...
Quality Assurance
(QA) in RP&C Activities
Miscellaneous
RP&C Issues.....';........................
R8.1
Review of FSAR Commitments
19
19
19
.20
20
21
22
23
23
24
25
25
v
TABLE OF CONTENTS (Continued)
P1
P2
P3
P5
P6
P7
P8
Conduct of Emergency Preparedness
(EP) Activities
Status of EP Facilities, Equipment, and Resources
EP Procedures
and Documentation .....
Staff Training and Qualification in EP
EP Organization and Administration
Quality Assurance
Miscellaneous
EP Issues
P8.1
Review of FSAR Commitments
25
26
26
~...'. '8
29
29
30
30
V. Management
Meetings ............
X1
Exit Meeting Summary
30
30
Re ort Deta'ils
Summar
of Plant Status
Unit
1 began this inspection period at 100 percent power.
On January 24, a traffic
accident near the plant caused
a loss of the Emergency Notification system, however
commercial phone I:.,es were still available.
Subsequently
PPSL discovered that the call
back portion of the Tele Notification System for emergency responders
was not functional
and made
a
1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> NRC notification as required by 10 CFR 50.72.
On February 1, PPRL
made an a telephone notification to the NRC after a Unit
controller failed, causing
a reactor power increase to 103.5% of the rated core thermal
power limit. Operators reduced power to less than 100% within approximately 65
seconds of the failure.
Planned power reductions were made during this inspection period
in support of control rod stroke testing, control rod pattern adjustment,
and routine turbine
valve testing.
Unit 2 began this inspection period at 100 percent power with all control rods fully
withdrawn.
Power reductions were made during this period in support of repairs for a
main condenser tube leak and control rod hydraulic control unit maintenance.
On February
15, Unit 2 was at 95% power when a damper for the 'B" emergency switchgear room
cooling train failed.
On February 16, the 'A'mergency switchgear room cooling fan
failed.
The loss of both trains of emergency switchgear room cooling was reported to the
NRC on February 16, as required by 10 CFR 50.72.
I. 0 erations
01
Conduct of
Operations'1.1
Off as S stem Recombiner
H dro en Accumulation
a.
Ins ection Sco
e 71707
On December 19, 1996, hydrogen gas accumulated
in the off gas recombiner
system after problems occurred during a swap of the recombiner train serving the
Unit 2 main condenser.
The inspector observed the response
of control room
operators to this event and subsequent
meetings held to evaluate the occurrence.
b.
Observations
and Findin s
At 7:45 a.m., operators
began to swap alignment of the Unit 2 main condenser
from the Unit 2 offgas train to the common offgas train in accordance with
procedure OP-222-001.
In accordance with procedures,
the automatic Hi - Hi
'Topical headings such as 01, MB, etc., are used in accordance with the NRC standardized
reactor inspection report outline.
Individual reports are not expected to address
all outline
topics.
hydrogen isolation signals for both the Unit 2 and common offgas trains were
manually bypassed.
'
At 8:15 a.m.,
a chemistry grab sample was taken from the Unit 2 offgas
recombiner train as required by TS Action Statement 3.3.7.11 when the automatic
isolation circuit is inoperable.
The grab sample contained
a hydrogen concentration
of 0.24%.
At 10:00 a.m., two automatic valves for the Unit 2 offgas train failed to close as
expected when operators attempted to isolate the Unit 2 offgas train.
Consequently,
the Unit 2 train was not completely isolated.
Operators placed the
transfer evolution on hold pending an investigation of the valves that failed to close
by maintenance
personnel.
At 12:18 p.m., Chemistry informed the control room that an offgas sample showed
an 8% hydrogen concentration.
Based on this sample, operators began
preparations to manually close valves for the Unit 2 recombiner lines in order to
complete the isolation of the Unit 2 train.
At 12:45 p.m., chemistry personnel informed the control room that a confirmatory
sample indicated
a 9% hydrogen concentration.
Operations management
was
informed and preparations
were made to back out the recombiner transfer
procedure
and place the Unit 2 recombiner train back in service.
The inspector discussed
the offgas system alignment and the results of the
chemistry samples with Operations management.
Specifically, the inspector
questioned
whether the offgas system procedures
required operators to manually
initiate a system isolation since the automatic system isolation setpoint had been
exceeded.
At 1:08 p.m. operators manually initiated an offgas system isolation in accordance
with AR-231-001 based on confirmation of a hydrogen concentration greater than
the hi-hi hydrogen setpoint of 2%.
TS 3.12.2.6 requires the hydrogen concentration
in the main condenser offgas
system to be limited to less than or equal to 4% by volume. With the
concentration of hydrogen greater than 4%, the concentration must be restored to
below the limit within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.
During this event, the hydrogen concentration
in
the offgas system exceeded
the 4% hydrogen limit of .TS 3.11.2.6 for less, than 5
hours.
However, operators failed to recognize entry into this limiting condition for
operation.
Based on review of this event, the inspector determined the following:
~
Operators did not implement the actions of AR-231-001 when the first.grab
sample showed the hydrogen concentration
at 400% of the automatic
isolation setpoint I2% hydrogen).
Operators failed to recognize entry into the TS limiting conditions for
operation (LCO) when the hydrogen concentration
exceeded
4%.
A manual bypass of the offgas system's automatic high hydrogen isolation
signal is routinely made to inhibit spurious isolations from moisture in the
system during transfer activities.
The inspector determined that although
this activity is not precluded by TS, the use of alternate grab samples during
a routine evolution is not a conservative method to compensate
for a design
problem.
The operational practice of bypassing the automatic isolations and history of
hydrogen detection system problems led to a general understanding that the
hydrogen indication in the control room was unreliable during recombiner
transfer evolutions.
NRC Region
I has requested
a review of the SSES TS for the offgas system
automatic high hydrogen isolation by the Office of Nuclear Reactor Regulation.
Specifically, the review was requested to determine the adequacy of:
1) the
current TS requirements for alternate grab samples,
2) the SSES practice of
bypassing automatic system isolations signals during transfer of recombiners,
and
3) the applicability of the standard Improved Technical Specifications to the SSES
design.
c.
Conclusions
Hydrogen gas accumulated
in the Unit 2 offgas recombiner train, reaching
a
concentration greater than Technical Specification limits and the system did not
automatically isolate, as designed,
prior to reaching this concentration
because
operators bypassed
the isolation circuit. Operators did not manually initiate a
system isolation after both an alarm and an alternate grab sample showed
a
hydrogen concentration
in excess of the automatic isolation setpoint.
The operators'ailure
to manually initiate an offgas system isolation as required by
the alarm response
procedure for high hydrogen concentration
is cited as a
violation.
(VIO 388/97-01-01)
02
Operational Status of Facilities and Equipment
02.1
Unit 2 'D'HR Pum
Start Failure
a.
Ins ection Sco
e 92700
The inspector conducted
an on site review of the subject plant condition in order to
verify that PP&L had met the reporting requirements of 10 CFR 50.73, that PP&L
had taken or planned appropriate corrective actions, and that continued operation of
the facility is being conducted
in accordance with Technical Specifications and
other regulatory requirements.
Observations
and Findin s
On November 21, 1996, the 'D'HR pump automatically tripped when operators
attempted to start it for suppression
pool cooling.
A protective circuit for the pump
was found energized
and would have prevented
a start of the pump in either the
shutdown cooling or low pressure coolant injection (LPCI) modes.
PP5L's investigation determined that Rotor ¹3 of the 'D'HR pump's suction valve
motor actuator (F004D) did not operate consistently with the rotors used for valve
control.
Contacts on Rotor ¹3 continued to show the valve was not full open after
its companion rotors had reached their full open alignment, cutting off power to
open the valve.
This sequence
difference caused the 'D'HR pump trip relay
E11A-K22B to remain energized,
enabling the pump's protective trip.
PPSL determined that Rotor ¹3 of the actuator for valve F004D had been in this
condition since November 14, 1996, when the valve was last operated for a routine
surveillance.
Based on the control room log entries, the inspector determined that
the 'D'HR pump was inoperable for greater than 7 days and 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />.
Action b.1, allows 7 days for restoration of a single inoperable
RHR pump:
If the 7
day period is. exceeded,
Action b.1 further requires that the unit be in hot shutdown
within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />,
Operators were not aware of the. failure and therefore no action
was taken.
PPSL's initial response
to this event was to verify the proper condition of all other
Unit 1 and Unit 2 RHR pump trip relays.
Based on a recommendation
from NSE,
operators cycled valve F004D and the pump's protective relay deenergized.
Additional strokes of F004D in an attempt to repeat the original failure were not
successful.
The root cause was later determined to be a minor variances (0.135
seconds)
in the drop out time of Rotor ¹3 relative to Rotor ¹1.
As an interim
action, temporary procedure changes
were implemented to require verification that
the RHR pump trip relays are deenergized
following routine RHR valve surveillances
and system alignments.
Long term corrective actions consist of enhancements
to
maintenance
procedures for valve actuator limit switches and rework of all the RHR
pump suction valve actuator switches.
The inspector concluded that PPSL's failure to place the unit in hot shutdown after
7 days and approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> was a violation of the TS requirements.
However, the safety significance of this violation was minor due to the fact that all
'ther ECCS sub-systems
were operable during this time and the operability of the
'B'HR pump maintained 100% functional capability in the affected LPCI sub-
system.
Corrective actions for this event were reviewed and found to be good.
'his violation resulted from an equipment failure that was not avoidable by
reasonable
licensee quality assurance
measures
or management
controls, and
therefore is not being cited, consistent with section VI.A. of the NRC Enforcement
Policy,
c.
Conclusions
A Unit 2 'D'HR pump failed to start when a limit switch on it's suction valve did
not operate properly.
As a result, the 'D'HR pump was inoperable with the
reactor in Condition
1 for greater than the 7 days and 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> allowed by
Technical Specifications.
The licensee implemented appropriate corrective actions
and NRC review of the event determined the failure was beyond reasonable
licensee
control.
This issue is being treated as a non cited violation, consistent with section
VI.A. of the NRC Enforcement Policy.
04
Operator Knowledge and Performance
04.1
0 erator Res
onse to 0 erational Occurrences
Control room operators were observed during performance of their on-shift
responsibilities throughout the inspection period.
The inspectors verified that
appropriate alarm response
procedures
were implemented and that the required
actions were completed.
The following activities were observed
and the inspector
determined that operators responded
well to these occurrences.
ON-158-001
Loss of Reactor Protection System,
February 19, 1997
OP-257-004
AR-106
HVAC Reactor Building Fan Damper Trouble, February 24, 1997
0
08
Miscellaneous Operations Issues
08.1
Mode Chan
e Re uirement Not Met
a.
Ins ection Sco
e 92700
As on site follow up of this event, the inspector verified that the reporting
requirements of 10 CFR 50.73 had been met, that appropriate corrective action had
been taken, and that continued operation of the facility was conducted in
accordance with Technical Specifications and other regulatory requirements.
b.
Observations
and Findin
s
During the restart of SSES Unit
1 on October 19, 1996, following it's 8th refueling
outage, operators repositioned the reactor mode switch to "Startup," changing the
reactor's operating mode from "Cold Shutdown" (Condition 4) to "Startup"-
(Condition 2). TS 3.5.1 requires two operable
LPCI subsystems
in Condition 2, and
at the time operators changed the mode switch position, the 'B'oop of LPCI had
not been made operable.
Making a reactor mode change to Condition 2 when an
applicable LCO is not met constitutes
a violation of Technical Specification 3.0.4.
The error was identified by the Unit Supervisor (US), who then directed operators to
align the 'B'PCl.subsystem.
The alignment was completed and the subsystem
was declared operable 44 minutes after the mode switch had been placed in
"Startup."
PPSL attributes the event to human error.
While in Condition 4, the US determined
that an LCO was not required for the RHR-pumps during the process of aligning it
for the standby LPCI mode.
However, the US later failed to recognize that the RHR
realignment was not complete when he authorized the mode change.
In the LER,
PPRL reported that the US lost focus on the requirement of TS 3.0.4.
In response to this event, PPSL counseled the US, reviewed the event with all
operations personnel,
and implemented procedural enhancements
to the operating
procedure which controls the."Startup" mode change.
Actions to prevent
recurrence described
in the LER include a review of this event with operations
personnel during Training Cycle 96-6, and an evaluation to determine if
modifications that would allow faster transition from shutdown cooling to the LPCI
mode would be cost beneficial.
The inspector reviewed changes
PPRL made to procedure GO-100-002 in response
to this event.
The procedure now provides steps to alert the US that LPCI must be
restored and the LCO must be cleared, prior to making the mode change.
The
inspector also reviewed the lesson plan for Manager of Operations Agenda
discussion for training cycle 96-6.
As with the procedures,
this training focused on
a US responsibility to maintain an overall view of plant conditions, evolutions in
progress,
and the goals to be achieved.
As discussed,
making a reactor mode change to Condition 2 when an applicable
LCO is not met constitutes
a violation of TS 3.0.4.
This licensee-identified
and
corrected violation is being treated as a non-cited violation, consistent with Section
VII.B.1 of the NRC Enforcement policy.
Conclusions
PPS.L identified that operators made
a reactor mode change,
placing Unit
1 in
Condition 2 (Startup), when the limiting conditions for operation of Technical Specification (TS) 3.5.1 were not met.
PP8cL determined that human performance
was the root cause of the event and implemented corrective actions focused on
procedural enhancements
and training.
This violation of TS 3.0.4 is being treated
as a licensee identified non-cited violation.
08.2
Review of Licensee Event Re orts
lns ection Sco
e 90712
The inspector reviewed Licensee Event Reports (LERs) submitted to the NRC to
verify that the details of the event were clearly reported, including the accuracy of
description of the cause
and adequacy of corrective action.
The inspector
determined whether further information was required from the licensee, whether
generic implications were involved, and whether the event warranted onsite
followup. The following LERs were reviewed during this inspection period.
b.
Observations
and Findin s
Closed
LER 50-387 96-008: Alternate Continuous Gaseous
Effluent Sampling
On August 2, 1996, Unit 1 was in Condition 3, when the 'A'ngineered Safeguard
System (ESS) bus was inadvertently deenergized
during maintenance
work
(reference
LER 50-387/96-007).
Loss of the 'A'SS bus caused
a loss of the
normal effluent sample flow from the Unit 1 turbine building and reactor building
vents.
TS 3.3.7.11-1 Action 112, states that effluent releases
via this pathway
may continue for up to 30 days provided samples
are continuously collected with
auxiliary sampling equipment.
PP5L determined that the alternate sampling was
not implemented in a timely manner because
personnel failed to question the
effects of alarms that indicate a loss of vent flow, and placed priority on restoration
of the 'A'SS bus.
The failure to follow procedures
is a violation of NRC requirements.
This licensee
identified and corrected violation is being treated as a non-cited violation, consistent
with section VII.B.1 of the NRC Enforcement Policy.
H
Closed
LER 50-387 96-014:
Completion of Technical Specification Required
Shutdown
On October 19, 1996, with Unit
1 starting up, the acoustic monitor for the 'L'ain
steam safety/relief valve (SRV) began to indicate the SRV was open when alternate
control room indications showed that it was closed.
The acoustic monitor was
declared inoperable in accordance with TS 3.3.7.5.
Since it was not expected that
the monitor could be repaired without a drywell entry, the unit was shutdown in
accordance
with TS 3.3.7.5, action 80b.
This issue was previously reviewed in NRC Inspection Report 96-11, section 02.2.
Closed
LER 50-388 96-009:
Unit 2 'O'HR Pump Start Failure.
The event is discussed
in section 02.1 of this report and the LER is therefore
closed.
Closed
LER 50-387/96-013:
Mode Change Requirement Not Met
The event is discussed
in section 08.1 of this report and the LER is therefore
closed.
c.
Conclusions
The events reported by PPhL in the Licensee Event Reports
(LER) reviewed during
this period were appropriately reported and provided an accurate description of their
causes
and corrective actions.
The inspector determined that for the LERs
discussed
in brief, the corrective actions were reasonable,
that no generic
implications were involved, and,that these events require no additional onsite
followup. Two of the LERs listed were reviewed in greater detail as discussed
in
sections 02.1 and 08.1 of this report.
II. IVlain enance
IVI1
Conduct of IVlaintenance
M1.1
Planned Main enance
Activi
Review
a.
Ins ection Sco
e 62707
A variety of maintenance
activities were reviewed on'he basis of their complexity,
safety (or risk) significance, or other considerations.
A sample of work permits,
equipment tagouts, procedures,
drawings, and vendor technical manuals associated
with these maintenance
activities were reviewed as part of the inspection.
Through
observation of the maintenance
activities and interviewing maintenance
personnel,
the inspector sought to verify that the activities were performed in accordance
with
procedures
and regulatory requirements,
that personnel
were appropriately trained
and qualified, and that appropriate radiological controls were followed.
b.
Observa ions and Findin s
The following maintenance
activities were reviewed through direct observation
and/or review of the completed work packages:
WA S70402
Unit
1 Battery Charger 1D633 Corrective Maintenance,
February 14, 1997.
WA S72516
'B'iesel Generator Slip Ring Brush Investigation,
February 5, 1997
~
WA S72517
'C'iesel Generator Slip Ring Brush Investigation,
February 6, 1997.
WA V70291
High Pressure
Coolant Injection (this WA is associated
with
CR 96-2240)
WA S70254
WA S79015
High Pressure
Coolant Injection
Destructive Examination of ThermoLag Material
WA V70300
Safety Parameter
Display System-Uninterruptible
Power
Supply
c.
Conclusions
In general, the work activities were adequately controlled and observed portions
were performed in accordance with station procedures.
In some cases, it was not
apparent to the inspector that work groups were using procedures
as discussed
in
NDAP-QA-500, Conduct of Maintenance.
The licensee's followup for problems
identified with the diesel generator slip rings is discussed
in section M2 of this
report.
M1.2, Surveillance Test Activit Sam
le Reviews
'a.
Ins ection Sco
e 61726
The inspectors observed portions of selected surveillance tests involving different
technical disciplines for safety-significant systems.
b.
Observations
and Findin s
Through observation and review of records, the inspectors verified that the test
activities were properly released for performance, that the test instrumentation was
within its current calibration cycle, and that it was being performed by qualified
personnel
in accordance
with approved test procedures.
The inspectors
also
verified that the tests conform to TS requirements
and that applicable LCOs were
taken.
The following activities were reviewed=during this period:
SO-024-001
'A'iesel Generator Monthly Surveillance, February 3, 1997
SO-259-002
Quarterly Suppression
Chamber Vacuum Breaker Test,
February 14, 1997
Sl-280-308
18 Month Calibration of RWCU, MSIV, PCIS, Secondary Containment
Isolation Reactor Vessel Water Levels, February 21, 1997
c.
Conclusions
The routine surveillance activities observed during this inspection period were
adequately performed.
10'aintenance
and Material Condition of Facilities and Equipment
Material Condition of Plant
E ui ment and S stems
Ins ection Sco
e 62707
During routine observations
of plant operations the general condition of
equipment'as
examined to determine the effectiveness of licensee controls for identification
and resolution of maintenance
related problems.
Observations
and Findin s
The non-safety related condensate
transfer system (CTS) is shared
by both SSES
units and provides the keep-fill system for the emergency
core cooling
systems'ECCS)
discharge
piping full. The CTS is designed to keep the systems'ischarge
piping full to preclude water hammer transients that could prevent the ECCS
systems from providing their intended safety function.
Since January
1996, the
CTS has experienced
seven'functional
failures that have caused
some ECCS
subsystems
to loose keep-fill pressure.
During these events the ECCS
subsystems'ere
either declared inoperable or operators started the ECCS pumps to prevent
voids in their discharge
piping when. the keep-fill pressure
decreased
to
approximately 50 psig. Although PP5L determined that none of the 1996 failures
were repeat maintenance
preventable functional failures, the events resulted in
entries into off-normal operating procedures,
ECCS equipment,
and
unnecessary
starts of ECCS equipment.
In one case,
a human error led to loss of
the Unit 1 'B'oop of RHR and the 'B'oop of core spray, placing the unit in TS 3.0.3.
One 1997 failure is still under review by PP5L as a possible repeat
maintenance
preventable
functional failure.
Based on review of these events, the
inspector determined that PPSL is not maintaining the CTS such that it will provide
the minor, but continuous inflow into the discharge
lines to make up for leakage
across the ECCS pump discharge
check valves as described
in the FSAR.
The Unit
1 reactor core isolation cooling (RCIC) system steam line drain pot has not
worked properly since June 1995.
To compensate
for the non-functional steam line
drain pot, a manual bypass valve was opened
by operators
in accordance
with
alarm response
procedures
and recommendations-from
Nuclear System Engineering.
Following the unit's restart from the Fall 1996 refueling outage,
a steam leak
developed
as a direct result of the drain pot bypass valve being continually open
(Reference
NRC Inspection Report 96-11)
~ Although the licensee has made several
attempts to solve the drain pot problem, these maintenance
activities have not been
successful.
The inspector determined that PPRL has not been effective in
correcting this long standing problem with the potential create additional steam
piping leaks and render the RCIC system inoperable.
Conclusions
The material condition and reliability of the condensate
transfer system and the
reactor core isolation cooling system steam line drain pot have not been corrected
11
by PP5L, despite continued problems over the last year.
PPSL's failure to maintain
a reliable condensate
transfer system continues to necessitate
entry into off normal
procedures for loss of ECCS keep-fill pressure
and unplanned starts of certain ECCS
pumps.
The failure to correct the RCIC drain pot has the potential to cause
additional steam leaks and RCIC system unavailability.
M4
IVlaintenance Staff Knowledge and Performance
M4.1
Review of Emer ent Maintenance
- 'E'iesel Generator Preventive Maintenance
a.
Inspection Scope (62707)
On January
17, 1997, during inspection of the partially disassembled 'E'iesel
generator, the inspector found that one of generator's
stationary brushes was not
in contact with its respective collector ring.
In response to the inspector's
observation, the licensee initiated a condition report (CR 97-0096) to documented
the problem.
The inspector reviewed PPSL's operability determination,
maintenance
procedures,
and subsequent
investigations related to this observation.
b.
Observations
and Findin s
Each generator has two slip rings and eight brushes connecting the field wiring to
the rotating assembly.
The four brushes for each slip ring are each held in contact
with the ring by a spring arm.
A retaining clip is used to keep the brush from
moving completely out of its holder, but does not normally contact the brush.
Based on interviews with electrical maintenance
personnel,
the inspector
determined that the problem with one 'E'G brush had been recognized during a
maintenance
run earlier that week.
Licensee personnel stated that the condition
would be corrected during the routine maintenance
surveillance SM-024-E01,
"Diesel Generator 'E'8 Month Inspection."
The inspector noted that the 'E'G
was not considered operable between the time the maintenance
personnel identified
the problem and the maintenance
surveillance.
The inspector discussed the generator brush binding with an electrical group
supervisor and subsequently
he initiated a CR to evaluate the degraded condition.
The inspector noted that it was not clear how the retainer clip became misaligned,
what the operability impact was, and whether the problem existed on the other
CR 97-0096 documented
the brush problem and provided an operability
determination.
However, the operability determination did not address the potential
for, or effects of,.a loss of brush contact during extended operation.
A subsequent
revision of the operability determination included additional inspections by NE
personnel, contacts with the voltage regulator manufacturer and another Cooper
Bessemer owner who experienced
similar problems, and an assessment
of the
potential for common mode failure.
12
Additional inspection by PP&L under WA S72516 and S72517 found that the
'B'nd
'C'iesels each had one brush retainer clip misaligned to the point where it
impacted the free movement of the brush.
PPS,L determined the restricted
movement of one brush on each of the two generators'would
not impact
operability.
However, the loss of multiple brushes for a single collector ring has the
potential to cause
a loss of generator field, depending
on the number of remaining
brushes
and their condition.
The brush binding was caused
by misalignment of its retaining clip.
Based on the
as-found condition, the retaining clip rotated clockwise with the torquing of its
fastener.
The inspector reviewed SM-024-E01, Revision 6, "Diesel Generator
'E'8
Month Inspection" and MT-GE-002, Revision 12, "Brush, Commutator And Slip
'ing
Inspection And Maintenance."
SM-024-E01, steps 6.18.1 and 6.18.1, require
checks to ensure the brushes
are properly positioned.
MT-GE-002, step 8.4.1 also
contains
a step to ensure freedom of movement of the brush in its holder.
Based
on review of the procedures
and the as-found condition, the inspector determine
that the root cause of the problem was inadequate
work performance
and
oversight.
The inspector determined that the licensee's failure to adequately perform checks of
the generator brushes constitutes
a violation of minor significance and is being
treated as a non-cited violation consistent with Section IV of the NRC Enforcement
Policy.
Conclusions
The failure to properly perform maintenance
activities on.the 'E', 'B'nd
'C'mergency
diesel generators
resulted in degradation of their generators'lip
ring
assemblies.
Although the operability was not challenged prior to identification, the
potential existed for common cause degradation
due to inadequate
performance of
maintenance.
The failure to properly perform safety related maintenance
activity in
accordance with established
procedures constitutes
a violation of minor
consequence
and is being treated as a non-cited violation consistent with Section
IV of the NRC Enforcement Policy.
IVl6
Maintenance Organization and Administration
M6.1
Verification of Maintenance
Rule Re uirements - Switch ards
a.
Ins ection Sco
e
6270'7
During review of emergent maintenance
on the 500 kV switchyard air system, the
inspector sought to verify that the basic requirements of the maintenance
rule have
been satisfied with regard to the SSES switchyards.
b.
Observations
and Findin s
13
The 500 kV switchyard air system is comprised of a single air manifold which
supplies air pressure to maintain the switchyard breakers
in their closed position.
Check valves for individual breakers
are relied upon to sustain the required air
pressure
at individual breakers short duration air supply problems.
On January 23, a leak developed
on the air manifold, causing an alarm at both
SSES and the Power Dispatcher office. A temporary fix was implemented,
however on January 24 the problem resurfaced.
While permanent repairs were
being effected on January 25, the air supply to 5 of the 6 breakers in the
switchyard had to be isolated from their air supply.
During this time, the
breakers'heck
valves were relied upon to maintain the air pressure
and consequently their
positions.
The inspector reviewed PPRL's actions in response to this incident
because
both the air leak, and actions necessary to repair it, had the potential to
cause
a load reject for SSES Unit 2.
In accordance with the PPSL maintenance
rule implementing procedures,
GDS-18,
"System Scoping for Maintenance
Rule Applicability," and GDC-14, "Determining
'Levels of Monitoring Required foI Structures, Systems,
and Components Within The
Scope of 10 CFR 50.65," the switchyards are classified as non-risk significant
systems
and are monitored using plant level performance criteria.
These criteria
are:
Unplanned Capability Loss Factor - 0%
Unplanned Scrams while Critical over last 12 months - 0
No repetitive Maintenance Preventable
Functional Failures
The inspector found that PPS.L system engineers
are performing quarterly system
reviews for the switchyard system as required by NDAP-QA-0501.
However, the
inspector noted that the problems that occurred on January 23 are not counted for
maintenance
rule purposes
since the switchyards are monitored on the plant level.
PPS,L does address
this type of failure under the corrective action process
due to
the potential for such
a problem to cause
a plant transient.
Conclusions
The Susquehanna
Unit
1 and Unit 2 switchyards are considered to be within the
scope of the licensee's maintenance
rule program and are being monitored on the
plant level.
The inspector found that PPRL was meeting the maintenance
rule
requirements with regard to monitoring of the switchyards.
14
III. En ineerin
E2
Engineering Support of Facilities and Equipment
.E2.1
0 erabilit
Determination For RHR Swin -bus MG Set
a.
Ins ection Sco
e 37551
On February 10, 1997, PPSL initiated CR 97-0225 after discovering that the Unit
2, Division II RHR swing-bus motor generator
(MG) set voltage was reading low.
During routine rounds, an NPO found that the MG set output voltage was reading
460 Vac vice the expected 480 Vac. The inspector reviewed the licensee's actions
in response to this discovery and the support provided by Nuclear Systems
Engineering
(NE).
b.
Observations
and Findin s
The Division II RHR swing-bus MG set provides the normal power supply for valves
that must'ep'osition for proper Division II (the 'B'HR loop) LPCI injection.
Specifically it supplies power to the RHR injection'.valve, the RHR minimum flow
valve, the reactor recirculation pump discharge valve and the recirculation pump
discharge bypass, valve.
The operability determination for CR 97-0225 is based on an assessment
of TS 3.8.3 which requires-the preferred power source,
a preferred power source M/G
set, alternate power source,
and automatic transfer switch.
The licensee
determined that there was no impact on operability since the surveillance
requirements for TS 3.8.3 do not specify a minimum voltage,'he TS only requires
that the load groups be energized.
In review of CR 97-0225, the inspector found that PPRL's initial operability
determination was based on the RHR swing-bus motor generator set having power
available and did not address whether 'the degraded voltage output would affect
operability of downstream components.
This issue was immediately discussed with
the Shift Supervisor and subsequently,
Nuclear System Engineering personnel.
According to the guidance in Generic Letter 91-18, when it is not clear that a
system can perform as described
in its current licensing bases,
performance of the
TS surveillance alone may not verify operability.
The inspectors determined that
the initial operability evaluation did not address whether the system could perform
as required by licensing basis.
0
On February 11, the licensee completed
a supplemental operability determination to
address the minimum voltage necessary for operability of the subject motor
operated valves.
The supplemental'evaluation
gave appropriate consideration to the
capability and design basis requirements of the valves for the'degraded
voltage
condition.
PPSL determined that the connected equipment will meet its design
basis and operate
as expected down to 90% of equipment rated voltage (460 Vac).
15
The inspector determined that although the supplemental operability determination
provided a sound technical position, the initial operability determination by the
operations shift and shift technical advisor did not.
C.
Conclusions
Nuclear System Engineering provided a through revision of an operability
determination for a degraded power supply impacting low pressure
coolant injection
valves.
Although the initial determination made by operators on a backshift was
upheld, the initial determination did not provide any technical justification and relied
on meeting the verbatim requirements of Technical Specifications.
E2.2
En ineerin
Su
ort of Diesel Generator Maintenance
a.
Ins ection Sco
e 62707
On December 10 and 21, 1996, the 'E'G failed surveillance SO-024-014,
Monthly Functional Test.
The inspector reviewed the SSES engineering activities in
response
to the failures, licensee's activities to resolve the. root cause of the DG
failures, evaluated the licensee's,corrective
action, and performed an-independent
limited root cause evaluation of the failures.
b.
Observations
and Findin
s
At 8:30 a.m. on December 10, 1996, approximately 20 seconds after the 'E'G
began surveillance SO-024-014, Monthly Functional Test, a generator loss of field
alarm annunciated.
The alarm was followed by a master trip lock out relay.
The
inspector reviewed the associated
work authorizations,
the SSES trouble shooting
plan dated December 10, CR 96-2198 and the SSES 'E'G operability
determination associated with this failure.
Subsequent
to the December 10.failure
and the initial corrective actions by the licensee, testing activities were performed.
These activities were followed by a second surveillance failure on December 21,
1996.
The inspector further reviewed the licensee's corrective actions through
February 24, 1997 involved with the second diesel failure.
The following WAs were reviewed/evaluated
by the inspector:
WA A63686, Work Activity
WA Z62350, Status Activityfor 'E'G Availability
WA S61863, Investigate and Troubleshoot
WA S61896, Investigate and Troubleshoot
The inspector determined that the 'E'G was not credited as the power source for
any SSES class
1E system during either of the test failures, and the test'failures
had no effect on the TS operability requirements of either unit.
It was further
determined that each of the other four diesels (A through D) was properly aligned in
the control room throughout the tests and'was available to perform its intended TS
function.
16
Even though the failures did not have an immediate impact on the operability of
either unit, several safety significant issues were identified by the inspector during
the 'event reviews.
The licensee was not able to identify a specific cause of the December 10,
failure, immediately following the failure. The failure was similar to one that
occurred on August 8, 1993, and described in Significant Operations
Occurrence
Report (SOOR)93-194 and a third one described
in SOOR 1-92-
293.
The operability determination that was written following the December
10, 1996, failure did not fully explain the cause of the failure, and did not
fully explain why successful completion of a surveillance test following the
December 10 failure supported the position that the equipment was
The inspector concluded that the operability determination was
not complete.
2
~
SSES Operations management
came to a similar conclusion following their
review of the operability determination and requested
additional testing and
evaluation of the 'E'G.
The inspector determined that the actions taken by
Operations management
were aggressive,
technically based and very
conservative.
The testing that was performed on the 'E'G following the first failure was
not well controlled, was not approved by the manufacturer,
was not
described in the DG vendor manual (IOM-79), and did not rec'eive
a rigorous
formal engineering safety evaluation.
Following the second 'E'G
surveillance test failure, the licensee and a vendor representative
concluded
that the trouble shooting and maintenance
activities conducted following the
first failure caused the failure of two gate firing circuits, which resulted in
the second
DG surveillance test failure.
In addition, it was concluded that
the testing outlined in TP-024-149, Diesel Surveillance did not adequately
test the components affected by the trouble shooting activities.
The inspector determined that the licensee failed to adequately control DG
maintenance
and testing activities during the execution of the trouble
shooting plan following the first failure. Very aggressive
and comprehensive
corrective actions were undertaken
by the licensee following the second
test failure. These actions included a return to service component testing
matrix prepared with the help of vendor representatives.
10 CFR 50 Appendix B states that measures
shall be established to assure that
conditions adverse to quality such as failures, malfunctions, deficiencies, defective
material and equipment and nonconformances
are promptly identified and
corrected.
Contrary to the above,
The licensee failed to implement adequate
corrective actions in response
to a
1991 vendor letter that identified a deficiency on the contact surfaces of the
17
'E'mergency diesel generator bridge transfer switch.
As a result of the
licensee's failure to implement corrective actions to preclude the condition
identified by the vendor, the transfer switch failed to perform its function on
December 10, 1997, during an 'E'mergency diesel surveillance test.
The licensee's corrective actions in response to the failed 'E'iesel generator
transfer switch included the development of a trouble shooting plan dated
December 10, 1996, that was associated
with CR 96-2198.
The trouble
shooting activities conducted under the plan were not adequately
implemented, controlled, nor reviewed in that the activities resulted in the
failure of additional equipment and a second 'E'mergency diesel generator
surveillance test failure.
These two issues are considered examples of inadequate
corrective action and are
being cited as a violation.
(VIO 50-387/97-01-02I
The licensee performed an extensive root cause
and engineering evaluation of the
two failures and identified the following two additional contributing factors in
addition to a number of issues of lessor importance.
Each of the licensee identified
issues is associated with a condition report with.required corrective action and
management
review milestones.
The cause of the first failure was a failure of an DG bridge transfer switch to
make an effective contact upon receiving a start signal.
This susceptibility
was identified by the vendor in 1991 and communicated to the licensee by
letter.
The licensee included the letter in the vendor manual but did not
include the maintenance
recommendations
of the vendor in the 'E'G
preventive maintenance
program nor did it perform an engineering evaluation
determining that the preventive maintenance
recommendations
of the vendor
were not necessary.
Normal surveillance activity of the 'E'G included an allowance for
manipulating the bridge transfer switch prior to the performance of the
surveillance.
This switch manipulation masked the lack of the vendor
recommended
preventive maintenance
by mechanically removing an oxide
coating on the transfer switch contacts.
Conclusions
On December 10 and 21, 1996, the 'E'G failed surveillance SO-024-014,
Monthly Functional Test.
The cause of the first failure was a high resistance
contact on the DG bridge transfer switch which was not maintained as
recommended
by the manufacturer.
The second test failure was caused by two
damaged
gate firing circuits.
The gate firing circuits were damaged
during
inadequate
troubleshooting
and testing ac'tivities performed by the licensee.
The
initial SSES engineering operability determination following the first failure was
determined to be weak, but the SSES engineering activities following the second
failure were determined to be very strong and aggressive.
Additional causal factors
18
include the control of vendor recommendation for preventive maintenance
and
vendor manual documentation,
and the control of pre-exercising equipment that,
may mask weaknesses
that would affect TS surveillance testing activities.
A
violation was issued for inadequate
corrective actions to the vendors notification
and previous like conditions, and the licensee's troubleshooting
and testing
activities following the first failure.
E2.3
B
ass Indication S stem
BIS Desi
n
a.
Ins ection Sco
e 37551
As follow up to the Unit 2 RHR pump start failure discussed
in section 02.1, the
inspector reviewed the alarm circuitry that provides indication of the RHR pump's
proper standby alignment.
b.
Observations
and Findin s
During discussions with NE personnel the inspector learned that the bypass
indication system
(BIS) annunciator for the RHR pump is energized when the
pump's suction valve is fully closed.
In contrast, the RHR pump trip signal occurs
when the valve in not full open.
The Institute of Electrical and Electronic Engineers
(IEEE) "Criteria for Nuclear Power
Plant Protection Systems," Standard 279-1971, requires that when the protective
action of some part of a system has been bypassed,
this fact shall be continuously
indicated in the control room.
Regulatory Guide 1.47 provides additional guidance,
and requires that the indication of a bypass condition should be at the system level,
whether or not it is also at the component or channel level.
The inspector determined that the BIS alarm does not, in all cases,
indicate when
the automatic start of the RHR pump is inhibited by the suction valve interlock.
10 CFR Part 50, Section 50.55a, "Codes and Standards,"
requires the SSES design
to meet IEEE 279 standard
and failure to meet this requirement is a violation.
(VIO 97-01-03)
Based on this finding, the inspector questioned whether the licensee's design basis
review project in response to the October 9, 1996, NRC request for information
under 50.54(f) had previously identified this discrepancy.
Conclusion
The NRC has identified that the bypass indication system
(BIS) does not alarm
when a protective trip is active for individual residual heat removal pumps.
NRC
regulations require that when a system is bypassed,
that it shall be continuously
alarmed at the system level in the control room.
The failure to provide an alarm for
this bypass
is a violation of 10 CFR 50.55a, "Codes and Standards."
19
E8
Miscellaneous Engineering Issues (92902)
E8.1
Review of FSAR Commitments
A recent discovery of a licensee operating their facility in a manner contrary to the
Updated Final Safety Analysis Report (UFSAR) description highlighted the need for
a special focused review that compares plant practices, procedures
and/or
parameters
to the UFSAR description.
While performing the inspections discussed
in Section 08.2 this report, the inspectors reviewed the applicable portions of the
UFSAR that related to the areas inspected.
The inspector determined that the
Bypass Indication System for the RHR system does not meet the FSAR Section.
3.13 commitment to Regulatory Guide 1.47, May 19, 1973.
Section 08.2 of this
inspection report contains addition information on this issue.
IV. Plant Support
R1
Radiation Protection and Chemistry Controls (RP5C)
R1.1
Im lementation of'Radioactive
Li uid and Gaseous
Effluent Control Pro rams
a.
Ins ection Sco
e 84750-01
The inspection consisted of:
(1) tour radioactive liquid and gaseous
effluent
pathways and its process facilities, (2) review of radioactive, liquid and gaseous
effluent release permits, (3) review of Condition Reports compiled by the
Operations,
and (4) review of unplanned or unmonitored release pathways.
b.'bservations
and Findin s
Radioactive liquid effluents from the site were released into the cooling tower
blowdown line for dilution prior to reaching the Susquehanna
river.
blowdown line flow rates varied depending on the river flow rate which was a
minimum of about 5,000 gpm during radioactive liquid releases.
Radioactive
gaseous
effluents from the site were released through five rooftop vents on the
reactor building.
Radioactive gaseous
effluents (i.e., noble gases,
particulates,
and
radioiodines) were monitored at each vent.
The inspectors toured'the above release pathways and selected radioactive liquid
and gas process facilities and equipment; including
(1) radioactive liquid and
gaseous
effluent radiation monitoring system (RMS), (2) air cleaning systems,
and
(3) the control room.
The inspectors noted that the effluent control procedures
were detailed, easy to
follow, and Offsite Dose Calculation Manual (ODCM) requirements were
incorporated into the appropriate procedures.
The inspectors also determined that
the liquid and gaseous
discharge permits were complete, and met the Technical
Specification (TS)/ODCM requirements for sampling and analyses
at the frequencies 0
20
and lower limits of detection established
in the TS/ODCM. There were no
unplanned releases
during 1996.
c.
Conclusions
Based on the above observations,
reviews, and discussions,
the inspectors
determined that the licensee established,
implemented,
and maintained effective
radioactive liquid and gaseous
effluent control programs.
R2
Status of RPS.C Facilities and Equipment
R2.1
Calibration of Effluent/Process
Radiation Monitorin
S stems
a.
Ins ection Sco
e 84750-01
The inspectors reviewed the most recent calibration results for the following
selected effluent/process
RMS and its system flow rates for both units.
The
inspectors also reviewed the licensee's
RMS self-assessment
and RMS work orders.
The inspector also reviewed selected)RC
calibration procedures.
Liquid Radwaste Effluent Monitor (Common to both units)
Liquid Radwaste Effluent Line Flow Rate
Cooling Tower Blowdown Flow Rates
Service Water Effluent Monitors
Residual Heat Removal Service Water Radiation Monitors
Main Steam Line Monitors
Standby Gas Treatment Vent Monitors (Common to both units)
Reactor Building Vent Noble Gas Monitors (low, mid., and high ranges)
Reactor Building Vent Noble Gas Monitoring System Flow Rate
Turbine Building Vent Noble Gas Monitors (low, mid., and high ranges)
Turbine Building Vent Noble Gas Monitoring System Flow Rate
Offgas Pre-Treatment
Noble Gas Monitors
b.
Observations
and Findin s
The IRC Department and Chemistry Department had the responsibility of performing
electronic and radiological calibrations, respectively, for the above effluent/process
radiation monitors.
The System Engineer had the responsibility to maintain the
operability for the abo've RMS and upgrade the system,
as necessary.
All
calibration results reviewed were within the licensee's acceptance
criteria.
During
the review of the above RMS radiological calibration efforts, the inspectors
independently verified several calibration results, including linearity tests and
conversion factors.
The comparison results were very good.
During the previous inspection conducted
in July 1995, it was noted that the
.
radiological calibration techniques implemented by the licensee were excellent, such
as energy calibration and five solid sources for the conversion factors and the
21
linearity test (See Inspection Report Nos 50-387/388/95-19 for detail).
No changes
in radiological calibration methodology were noted.
c.
Conclusions
Based on the above review, the inspectors determined that the licensee had
maintained an excellent RMS calibration program.
R2.2
Calibration of Area Radiation Monitorin
S stems
ARMS
a.
Ins ection Sco
e 83750
The inspectors reviewed the most recent calibration results for the following
selected ARMS for both units.
Sectio~ 12.3.4 of FSAR describes many aspect of
the ARMS and the inspectors reviewed selected aspects
including: (1) ARMS
locations, (2) selection criteria for energy dependence,
accuracy, and
reproducibility, (3) calibration method and testability, and (4) alarm set points.
Reactor Building Area High Radiation Monitors (Units
1 &2)
Turbine Building Area High Radiation Monitors (Units
1 &2)
Spent Fuel Pool Area High Radiation Monitors (Units 1&2)
Refueling Floor Area High Radiation'Monitors (Units 1&2)
The following 1&C calibration procedures were reviewed to determine their
adequacy.
0
IC-079-010
Channel Calibration of Area Radiation Monitors
SI-179-305
18 Month Calibration of Spent Fuel Storage Pool Area
Radiation RE-23714 Monitor
SI-279-337
18 Month Calibration of Spent Fuel Storage Pool Area
Radiation RE-13714 Monitor
Observations
and Findin s
The l&C Department had the responsibility to perform electronic and radiological
calibrations for the above ARMS. The expected
dose rates of the radiological
calibration equipment were calculated by radiation protection (RP) personnel.
The
inspectors noted that the above calibration procedures were easy to follow. All
reviewed calibration results were within the licensee's acceptance
criteria.
The inspectors discussed
ARMS locations; selection criteria for energy dependence,
accuracy,
and reproducibility; calibration method and testability; and alarm set
points with representatives
from l&C and RP.
The inspectors noted that the
licensee had good knowledge in the abov'e areas.
The inspectors also discussed
free air calibration methodology described
in "ANSI/ANS-HPSSC-6.8.1-1981,
Location and Design Criteria for Area'Radiation Monitoring Systems for Light Water
Nuclear Reactors."
The licensee stated that they would consider this reference for
potential program enhancements.
0
22
c.
Conclusions
Based on the above reviews and discussions,
the inspectors determined that the
licensee established
and implemented
a good ARMS calibration program.
R2.3
Air Cleanin
S stems
a.
Ins ection Sco
e 84750-01
The inspector reviewed the licensee's:
(1) most recent surveillance test results,
(2) work orders, system performance summaries,
and interviewed system
engineers,
as needed, to determine the implementation of TS requirements for the
following systems.
~
Control Room Emergency Outside Air Supply System
~
The inspectors reviewed the following surveillance test results for the above noted
ventilation systems.
~
~
Visual Inspection,
In-Place HEPA Leak Tests,
In-Place Charcoal Leak Tests,
Air Capacity Tests,
Pressure
Drop Tests, and
Laboratory Tests for the Iodine Collection Efficiencies.
b.
Observations
and Findin
s
The licensee has chosen to assign
a group of individuals within system engineering
to oversee each of the ventilation systems.
As a group of individuals had been
assigned,
the individuals were not solely dedicated to ventilation system oversight.
One of these individuals supervised the other system engineers
assigned to the
station ventilation systems.
Test procedures
provided good guidance.
Surveillance test results of the above
systems were within the licensee's
acceptance
criteria established
by the test
procedures
and TS.
Discussions with the system engineers
and review of
performance summaries indicated that a good level of attention had been placed on
ventilation systems.
Most importantly, the inspectors noted that there had been no
turnover among the ventilation system engineers over the past several years.
Conclusions
Based on the above reviews and discussions,
the inspectors determined that the
above noted ventilation systems were well maintained.
23
R3
RPKC Procedures
and Documentation
a.
Ins ection Sco
e 84570-01
The inspectors reviewed the ODCM implemented at the SSES including:
(1) dose
factors, (2) setpoint calculation methodology,
and (3) bioaccumulation factors for
aquatic sample media.
The inspector reviewed the 1995 Annual Radioactive
Effluent Report to verify the implementation of TS.
b.
Observations
and Findin s
The ODCM provided descriptions of the sampling and analysis programs, which are
established for quantifying radioactive liquid and gaseous
effluent concentrations,
and for calculating projected doses to the public.
All necessary
parameters,
such as
effluent radiation monitor setpoint calculation methodologies,
site-specific dilution
factors, and dose factors, were listed in the ODCM. The licensee adopted other
necessary
parameters
from Regulatory Guide 1.109.
The 1995 Annual Radioactive Effluent Report provided total released radioactivity
for liquid and gaseous
effluents.
The report also contained any changes to the
ODCM as necessary
and meteorological data.
There were no obvious anomalous
measurements,
omissions or trends.
The 1995 projected dose assessment
report
contained maximum individual and population doses resulting from routine
radioactive airborne and liquid effluents.
Doses were well below the regulatory
limits. The inspectors reviewed selected 1996 monthly projected dose assessment
results and noted that there were no trends.
Conclusions
Based on the above review, the inspectors determined that the licensee's
contained sufficient specification,.information,
and instruction to acceptably
implement and maintain the radioactive liquid and gaseous
effluent control
programs.
The licensee met all TS/ODCM reporting requirements.
R6
RPEcC Organization and Administration
a.
Ins ection Sco
e 84570-01
H
The inspector reviewed the organization and administration of the radioactive liquid
and gaseous
effluent control programs and discussed with the licensee changes
made since the last inspection, conducted
in July 1995.
b.
Observations
and Findin s
The chemistry staff had primary responsibility for conducting the radioactive liquid
and gaseous'effluent
control programs.
Operations,
Engineering, Radwaste
Operations,
and Instrumentation and Controls organizations supported the
radiological effluent control programs relative to air cleaning systems, radioactive
0
24
liquid discharges,
and radiation monitoring system calibrations.
The Chemistry
Supervisor remained under operations.
Since the last inspection of this program area, the following organizational changes
were made.
The reactor water cleanup and fuel pool system engineers were reassigned
to system engineering from chemistry.
Chemistry was reassigned
to the Operations Manager.
The Chemistry Department lost one technician and one scientist position.
No degradation of the effluents control program was noted as a result of these
changes.
Conclusions
The RPSC organization assigned oversight of the radioactive effluents control
program was well staffed.
R7
Quality Assurance
(QA) in RPSC Activities
a.
Ins ection Sco
e 84750-01
The inspection consisted of a review of Quality Assurance
(QA) Audit Reports
required by the TS and a review of corrective actions implemented to address
audit
findings.
The inspectors reviewed QA Audit Report Nos.95-033 and 95-114 which
were reports regarding the chemistry and effluents programs, respectively.
The
inspectors also reviewed QA Audit Report No.95-159 which pertained to an audit
of a vendor who supplied chemistry analytical services to the licensee.
The inspectors also reviewed (1) QA policy of the measurement
laboratory; (2)
implementation of the measurement
laboratory quality control (QC) program for
radioactive liquid and gaseous
effluent samples;
and (3) internal memorandum,
Requirements
for Radiological Programs.
b.
Observations
and Findin s
The inspectors noted that individuals with appropriate backgrounds were used to
conduct the audit.
No "technical" issues of regulatory significance were identified
by the licensee audit team.
Licensee corrective actions to audit observations
and
recommendations
were considered to be appropriate.
The inspectors noted that the
frequency by which QA audits was changed from yearly to once per every two
years according to the UFSAR.
The inspectors noted that QC for gamma measurements
were maintained.
Comparisons
of QC samples
(blind, spike, and duplicate) were in good agreement.
25
Conclusion
Based on the above reviews, the inspectors determined that the licensee met the
QA audit requirements
and implemented
a very good QC program for chemistry
measurements.
R8
Miscellaneous
RPRC Issues
R8.1
Review of FSAR Commitments
A recent discovery of a licensee operating their facility in a manner contrary to the
Updated Final Safety Analysis Report (UFSAR) description highlighted the need for
a special focused review that compares plant practices, procedures
and/or
parameters
to the UFSAR descriptions.
While performing the inspections discussed
in this report, the inspectors reviewed
the applicable portio'ns of the UFSAR that related to the areas inspected.
The
inspectors verified that the UFSAR wording was consistent with the observed plant
practices, procedures
and/or parameters.
P1
Conduct of Emergency Preparedness
(EP) Activities
lns ection Sco
e 82701
The inspector reviewed the licensee's action item tracking system and the
emergency planning self-assessment
program to determine the effectiveness
of licensee controls.
Observations
and Findin
s
An action item is initiated by a CR and tracked in the licensee's action item tracking
system.
The inspector reviewed 14 emergency preparedness
items listed in the
action item tracking system that resulted from condition reports, recommendations
from the 1996 audit, and comments from emergency drills. Those items were
appropriately assessed
and were being tracked.
Corrective action completion dates
were assigned
and being met.
The Supervisor, Nuclear Emergency Preparedness
performed self- assessments
using tracking system items to determine whether corrective actions were adequate
and whether enhancements
could be made to the emergency preparedness
program.
An area that has been under review is the licensee's emergency action
level (EAL) classification scheme,
i.e., whether to continue to seek NRC approval
for the Nuclear Management
and Resources
Council, Inc. (NUMARC) National
Environmental Studies Project (NESP)007 EALs or retain and enhance the Criteria
for Preparation
and Evaluation of Radiological Emergency Response
Plans and
Preparedness
in Support of Nuclear Power Plants, NUREG 0654/FEMA-REP-1,
Revision 1, EALs that comprise the current classification scheme.
(This matter is
discussed
further in section P3.)
The licensee also initiated a self- assessment
into
26
why the maintenance
group had performed work and made changes to EP
equipment and facilities without informing the EP group and why emergency plan
procedure changes were not always complete.
The licensee determined that the
problem appeared to be in the ownership of the EP program.
Conclusions
The inspector determined through interviews with emergency personnel
and
review of CRs that the action item tracking system was appropriately used
to identify and track corrective action items.
Additionally, self-assessments
were being performed to evaluate the appropriateness
of corrective actions
for identified items and to identify areas for improvement in.the EP program.
P2
Status of EP Facilities, Equipment, and Resources
a.
Ins ection Sco
e
82701
The inspector conducted
an audit of the licensee's
emergency facilities and
equipment by touring the Control Room, Operations Support Center (OSC),
Technical Support Center (TSC), the Emergency Operations Facility (EOF).
The
inspector reviewed facility equipment inventories and surveillances conducted
during the last quarter of 1996, for completeness
and accuracy.
b.
Observations
and Findin s
The inspector found the emergency facilities to be operationally ready and
emergency equipment as described in the emergency plan.
The inspector noted
that the inventories and surveillances of the facilities and equipment were properly
completed and that any identified discrepancies
were either immediately corrected
or documented,
with work orders written for repair or replacement.
Conclusions
The inspector found that emergency facilities and equipment were as described
in
the emergency plan, survey instruments were within the calibration requirements,
inventories and surveillances were completed,
and the facilities and equipment were
~ in a state of readiness.
P3
EP Procedures
and Documentation
a.
Ins ection Sco
e 82701
1
The inspector reviewed recent emergency response
plan changes to assess
the
impact on the effectiveness of the EP program.
b.
Observations
and Findin s
27
0
The inspector reviewed Revision 25 to the emergency
plan during the inspection.
The changes
made to the emergency plan were: changes
in alarm panel
designation; changes
in staffing of the new organization due to the relocation of the
EOF to the East Mountain Business Center; changes
in management
and facility
titles; corrections of typographical errors, and other minor corrections.
Additionally, the inspector discussed
an unresolved item with the licensee that had
been opened in'1990, during inspection 50-387,388/90-18,
and subsequently
closed based upon the licensee's submittal of NUMARC EALs. The unresolved item
involved a review of the NUREG 0654 EALs to assure that all EALs in use at that
time were clear and unambiguous
(50-387, 388/90-18-01).
When the licensee
decided to convert to the NUMARC NESP007 EAL guidance, the unresolved item
became moot.
The licensee submitted the NUMARC NESP007 EAL scheme to the NRC for
approval in January 1993.
The NRC responded with a request for additional
information in January 1994.
The licensee met with the NRC in June 1994 to
discuss the EALs and resubmitted them for approval in October 1995.'he
NRC
requested
additional information in July 1996.
In response,
the licensee sent a
letter in October 1996 requesting
an extension of time for the response
and another
meeting with the NRC early 1997.
The unresolved item was closed in inspection report 50-387, 388/95-25, because
the licensee had submitted the NUMARC NESP007 EALs to the NRC and the matter
was being tracked as a licensing issue.
During the inspection, the inspector determined that the licensee continued to make
changes to the current (NUREG 0654) EALs to meet the NUREG 0654 EAL
guidance throughout the period.
Identified ambiguities were also reduced through
the 10 CFR 50.54(q) process for emergency plan changes.
However, the licensee
indicated to the inspector that it is uncertain about whether it will continue to seek
NRC approval for the NUMARC NESP007 EALs or update the current EALs.
Conclusions
The inspector concluded that Revision 25 to the plan met 10 CFR 50.54 (q)
requirements
and did not reduce the effectiveness of the emergency plan.
With regard to the NUMARC versus NUREG EAL matter, this will be tracked as an
inspector followup item.
(IFI 50-387, 388/97-01-04)-
~i
28
P5
Staff Training and Qualification in EP
a.
Ins ection Sco
e 82701
The inspector interviewed the Vice President Nuclear Operations, the Plant
Manager, Health Physics Supervisor, Supervisor Nuclear Emergency Planning,
Recovery Managers,
and training personnel to determine the effectiveness of
training.
Additionally, the inspector reviewed EP training records, training
procedures,
lesson plans, emergency plan, and position specific procedures
associated with on-shift dose assessment
to evaluate the licensee's
EP training
program'.
b.
Observations
and Findin s
The inspector interviewed personnel who were qualified members of the emergency
response
organization.
AII of the personnel interviewed indicated that the licensee
conducted integrated mini drills in the TSC and the EOF and found them to be very
effective for training and keeping personnel current in their EP duties and
responsibilities.
Additionally, the inspector reviewed approximately 30% of the
emergency response
organization
(ERO) training records and verified that
, 'qualification and training were in accordance with the training matrix and were
current.
The inspector determined that all on-shift level II health physics tech'nicians were
trained in dose assessment
and protective action recommendations
for providing
suppolt to the shift supervisor prior to the manning and activation of the TSC.
The
technicians performed on-shift dose assessments
using real time meteorological and
source term conditions.
Training does not include performing "what if" calculations
because
those calculations would be performed at the TSC and/or EOF, once they
are activated.
The inspector also reviewed the dose calculator training and dose assessment
and
protective actions lesson plans.
c.
Conclusion
~
The inspector found, through inter'views and the review of training records, that the
ERO, and radiation protection personnel were being adequately trained as required
by the emergency plan, the training was current and that the training program was
being effectively implemented.
The inspector also found that dose calculator
training and dose assessment
and protective action lesson plans were acceptable.
29
p6
EP Organization and Administration
a e
Ins ection Sco
e 82701
The inspector reviewed the licensee's
EP group staffing and management
to
determine what changes
have occurred since the last program inspection
(September,
1994) and if those changes
had any adverse effect on the program.
Observations
and Findin
s
Since the last program inspection (September
1994), the position of
Supervisor, Emergency Preparedness
was refilled, one of the EP staff retired
and the position was eliminated.
During that period of time, the licensee
moved its EOF to a location that is about 23 miles from the plant.
Additionally, the licensee streamlined its ERO by eliminating some of the
administrative positions.
The move and changes to the ERO were approved
by the NRC. A demonstration
drill was performed in July 1996.
Conclusions
The inspector concluded that management
involvement and control of the EP
program was good.
Changes
made since the last program inspection did not appear
to have any adverse effects on the
program.'7
Quality Assurance
Ins ection Sco
e 82701
The inspector reviewed QA audit (10 CFR 50.54(t)) reports of the EP program,
conducted
in 1995 and 1996.
Additionally, the inspector interviewed a director of
an off-site agency to determine the effectiveness of the licensee's off-site interface.
Observations
and Findin s
The inspector reviewed audit reports95-023 and 96-057.
Audit report 95-.
023 contained no items that rose to the level necessitating
a CR, but
included 18 recommendations.
Audit report 96-057 contained three items
requiring a CR and six recommendations.
The three CRs identified the
following deficiencies:
(1) annual preventive maintenance
on the public
notification system was not preformed in 1995 (CR 96-1118); (2) some
emergency procedures
were, not current (CR 96-1132); and (3) three
individuals "on-call" had been removed from the qualification system.
The inspector also compared the reports of the audits and noted negative trends in
the maintenance
of training records (both on and off-site), in maintenance
of
facilities and equipment,
and in emergency plan and position specific procedure
changes.
These negative trends had also been identified by the licensee and
corrective actions were being taken.
30
The inspector interviewed the Director, Luzerne County Emergency Management
Agency, to determine the effectiveness of the licensee's off-site interface.
The
Director indicated that the licensee was very supportive in training county and local
municipality representatives,
and in assisting the county with emergency plan
changes.
The Director also indicated that many of the emergency county personnel
are volunteers and the licensee's extra efforts and time expended for training these
personnel was very much appreciated.
Additionally, the inspector was given a tour
of the Luzerne County Emergency Operations Center and the emergency response
mobil command unit and its associated
emergency equipment.
c.
Conclusion
The inspector concluded that the licensee had conducted audits in accordance with
10 CFR 50.54(t), as required, and that the off-site interface was effective.
PS
Miscellaneous
EP issues
P8.1
Review of FSAR Commitments
A recent discovery of a licensee operating its facility in a manner contrary to the
UFSAR description highlighted the need for a special focused review that compares
plant practices, procedures,
and/or parameters
to the UFSAR description.
Section
13.6 of. the UFSAR refers to the emergency plan.
Since the UFSAR does not
specifically include emergency plan requirements,
the inspector compared
licensee'ctivities
to the emergency
plan.
The inspectors specifically reviewed on shift dose
assessment
capabilities and training.
This is discussed
in Section P5.
No
discrepancies
were noted.
V. Mana ement Meetin
s
X1
Exit Meeting Summary
i
inspectors presented
the Effluent Control Program inspection results to members of the
licensee management
at the conclusion of the inspection on January 17, 1997.
The
licensee acknowledged the findings presented.
The inspectors presented the inspection results to members of licensee management
at the
conclusion of the inspection on February 26, 1997.
The licensee acknowledged the
findings presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary.
No proprietary information was identified.
~Oened
ITEMS OPENED, CLOSED, AND DISCUSSED
50-388/97-01-01
50-387,388/97-01-02
50-387/97-01-03
50-387,388-97-01-04
Closed
VIO
IF I
Operators'ailure to implement actions of high
hydrogen alarm response
procedure
in response to
multiple indications of a high concentration
Adequacy of BIS alarm circuits for the RHR systems
Corrective Action For 'E'G Maintenance
Completion of corrective action for EAL scheme
50-387/96-008
50-387/96-01 3
50-387/96-01 4
50-388/96-009
LER
Alternate Continuous Gaseous
Effluent Sampling
LER
Mode Change Requirement Not Met
LER
Completion of Technical Specification Required
LER
Unit 2 'D'HR Pump Start Failure
f
ARMS
CFR
CR
LCO
LER
NRC
NE
Ol
RPC
Sl
SOOR
TS
LIST OF ACRONYMS USED
Area Radiation Monitoring Systems
. Code of Federal Regulations
/
Condition Report
Condensate
Transfer System
Diesel Generator
Emergency Action Level
Emergency Response
Organization
Heating, Ventilation, and Air Conditioning
Instrumentation and Controls
Limiting Conditions for Operation
Licensee Event Report
Low Pressure
Coolant Injection
Motor Generator
Non-Cited Violation
'otice
of Violation
Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Nuclear Systems
Engineering
Nuclear Management
and Resources
Council, Inc.
National Environmental Studies Project 007 EALs,
Criteria for Preparation
and Evaluation of Radiological Emergency
Response
Plans and Preparedness
in Support of Nuclear Power Plants,
NUREG 0654 FEMA-REP-1, Revision 1, EALs
Off-site D'ose Calculation Manual
Office of Enforcement
Office of Investigations
Operational Support Center
Quality Assurance
Quality Control
Reactor Core Isolation Cooling
Radiation Monitoring System
Radiation Protection
Radiological Protection and Chemistry
Systematic Assessment
of Licensee Performance
International System of Units
Significant Operations Occurrence
Report
Safety/Relief Valve
Susquehanna
Steam Electric Station
Technical Specification
Updated Final Safety Analysis Report
S'