ML17158A499

From kanterella
Jump to navigation Jump to search
Insp Repts 50-387/94-16 & 50-388/94-17 on 940719-0905. Violations Noted.Major Areas Inspected:Plant Operations; Maint & Surveillance;Engineering & Plant Support
ML17158A499
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 09/27/1994
From: Jason White
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17158A497 List:
References
50-387-94-16, 50-388-94-17, NUDOCS 9410050062
Download: ML17158A499 (14)


See also: IR 05000387/1994016

Text

Inspection

Report Nos.

License

Nos.

Licensee:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

50-387/94-16;

50-388/94-17

NPF-14;

NPF-22

Pennsylvania

Power

and Light Company

2 North Ninth Street

Allentown, Pennsylvania

18101

Facility Name:

Susquehanna

Steam Electric Station

Inspection At:

Inspection

Conducted:

Salem Township,

Pennsylvania

July 19,

1994

September

5,

1994

Inspectors:

Approved By:

D. J. Mannai,

cting Seni

esident

Inspector,

SSES

t/zv/>>

e,

C

>e

Reactor Projects

Section

No. 2A,

ate

Scope:

Resident

Inspector safety inspections

were performed in the areas of

plant operations;

maintenance

and surveillance;

engineering;

and plant

support.

Initiatives selected for inspection

were fire protection,

Nuclear

System Engineering

System

Review meeting,

and

Emergency Diesel

Generator

maintenance.

Findings:

Performance

during this inspection period is summarized

in the

Executive

Summary.

Details are provided in the full inspection report.

Violations:

Fire doors were blocked

open without the required administrative

approval.

The failure to establish

continuous fire watches for degraded fire

protection

systems

were identified as apparent violations.

One non-cited

violation was identified during Licensee

Event Report

(LER) review.

It

concerned

the inadequate

establishment

of alternate

sample for an inoperable

turbine building sampler

(LER 94-005-00).

Unresolved

Items:

One unresolved

item regarding the inadvertent

High Pressure

Coolant Injection (HPCI) system

steam supply isolation was identified.

9410050062

940927

PDR

ADOCK 05000387

8

PDR

EXECUTIVE SUMMARY

Operations

Susquehanna

Inspection

Reports

50-387/94-16;

50-388/94-17

July 19,

1994

September

5,

1994

During the period,

a lightning strike rendered

the Simplex fire protection

system inoperable

on two occasions.

Consequently, fire detection

and

suppression

capabilities

were impacted in safety-related

areas of the reactor

building, control structure

and

common plant areas of both units.

Following

the first event,

Technical Specification requirements

were not met when

continuous fire watches

were not implemented within one hour.

Although

several

actions

were taken in response

to the event,

actions to establish

continuous fire watches

was not implemented for several

hours.

Inadequate

communications

were

a significant contributor.

Following the second

event,

the plant staff rigorously pursued

compliance with Technical Specifications.

A Notice of Violation is being issued

as

a result of the occurrence

and the

performance

weaknesses it represents.

Section 2.2 pertains.

Maintenance/Surveillance

During restoration

from the five year overhaul of the 'B'mergency Diesel

Generator,

the water was discovered

in the 'B'DG lube oil system.

Maintenance

personnel

determined

the source of water was

a leak internal to

the turbocharger.

The refurbished turbocharger

was installed

as part of the

five year overhaul.

The licensee

is working with the vendor to determine the

root cause.

The licensee

is rigorously pursuing root cause.

The inspector

will evaluate licensee resolution of the turbocharger

leak during ongoing

inspection activities.

Section 3. 1.1 pertains.

During the inspection period, the high pressure

coolant injection (HPCI)

system

became

inoperable

when the

HPCI system outboard

steam supply isolation

valve unexpectedly

stroked closed

when Instrumentation

and Control

(IEC)

technicians

performed

a residual

heat

removal

(RHR) equipment

area

differential temperature

high channel calibration

and connected

a multimeter

to the wrong terminals.

This human error caused

the valve closure.

This item

will remain unresolved

pending

NRC review of PP&L's completed investigation,

including root cause of the event

and corrective actions.

Section 3.2.1

pertains.

Engineering/Technical

Support

The inspector

attended

the Nuclear System Engineering

(NSE) weekly system

review meeting for the Standby

Gas Treatment

System

(SGTS).

The system

engineer

presented

the system review information in a clear

and effective

manner.

Nuclear Engineering

management

was actively involved.

The inspector

considered

the system review meeting

a strength of the engineering

organization.

Plant Support

During the period, the inspector identified,

on two separate

occasions,

that

a

fire door was blocked

open without the required administrative

approvals.

The

inspector also noted that there were several

licensee identified and

documented

examples of blocked

open fire doors without required administrative

approvals

since January

1994.

The instances

indicate weaknesses

in the

implementation of the fire protection

program

and corrective action process.

The recurring nature of this problem appears

to indicate

a lack of sensitivity

to the safety function of fire doors.

A Notice of Violation was issued

as

a

result of these repetitive occurrences

'and the associated

programmatic

weaknesses

they represent relative to plant safety.

Section 5.3 pertains.

Safety Assessment/Assurance

of guality

The inspector reviewed two Licensee

Event Reports

(LERs) during the period.

One non-cited violation was identified regarding

a condition prohibited by

Technical Specifications

involving inoperable turbine building sampling

system.

Section

6. 1 pertains.

TABLE OF CONTENTS

EXECUTIVE SUMMARY............................

ii

1.

SUMMARY OF FACILITY ACTIVITIES ..................

1

2.

PLANT OPERATIONS (71707,

92901,

93702,

40500)

2.1

Plant Operations

Review

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

2.2

Simplex Fire Protection

System Failures

.

1

1

~

~

2

3.

MAINTENANCE AND SURVEILLANCE (62703,

61726,

92902,

40500)

3. 1

Maintenance

Observations

3. 1. 1 'B'mergency

Diesel

Generator

Turbocharger

Problem

3.2

Surveillance Observations

.

.

.

.

.

3.2.1

HPCI Isolation Caused

by Human Error

3

3

4

5

5

4.

ENGINEERING (71707,

37551,

92903,

40500) .............

5

4.1

Nuclear System Engineering

System

Review Meeting

.

.

.

.

.

.

5

5.

PLANT SUPPORT

.

5. 1

Radiological

and Chemistry Controls

502

Secur ity

0

~

~

~

~

~

~

~

~

~

~

~

~

5.3

Fire Door Blocked Open

~

~

~

6

~

~

~

6

~

~

6

~

~

~

6

6.

SAFETY ASSESSMENT/OUALITY VERIFICATION (40500,

90700,

90712,

92700)

7

6.1

Licensee

Event Reports

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

7

7.

MANAGEMENT AND EXIT MEETINGS

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

8

7.1

Resident Exit and Periodic Meetings

.

.

.

.

.

.

.

.

.

.

.

.

.

8

7.2

Other

NRC Activities

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

8

Detail s

l.

SUNSLRY OF FACILITY ACTIVITIES

Susquehanna

Unit

1 Summary

Throughout the inspection period Unit

1 operated

at essentially

100X of rated

thermal

power with the exception of minor power reductions for surveillance

testing

and reduced electrical

demand

due to cool weathe'r.

On August 2,

a

lightning strike caused

a failure of the Simplex Fire Protection

system.

Section 2.2 pertains.

On August 9,

a one hour emergency notification was

made

to the

NRC when all offsite emergency notification sirens

were inoperable

due

to telephone line problems.

The sirens

were inoperable

from 2:05 p.m. until

6:16 p.m.

Manual actuation of the sirens

was possible

by 2:35 p.m.

The

system

was restored

and successfully tested

by 6:16 p.m.

The

NRC will

evaluate

the licensee's

corrective actions

as part of a future inspection.

On August 18, another lightning strike rendered

the Simplex Fire Protection

system inoperable.

Section 2.2 pertains.

On August 26, while pe}forming

residual

heat

removal

(RHR) equipment

area high differential temperature

channel calibrations,

technicians

connected

a multimeter across

incorrect

terminals causing the high pressure

coolant injection (HPCI) system

steam

supply outboard isolation valve to close.

The licensee

made the required four

hour

NRC notification per

10 CFR 50.72.

Section 3.2.1 pertains.

On September

1 and again

on September

2, reactor

power was reduced to 80X to investigate

and repair

a suspect vibration probe

on the 'A'eactor feed

pump turbine

(RFPT).

Susquehanna

Unit 2 Summary

Unit 2 operated

at full power throughout the inspection period with the

exception of one planned

downpower

and minor power reductions for surveillance

testing

and reduced electrical

demand

caused

by cool weather.

The planned

downpower to 40X was for condenser

maintenance,

reactor recirculation motor

generator

set '2B'aintenance,

single loop testing

and

a control rod sequence

exchange.

2.

PLANT OPERATIONS (71707,

92901,

93702,

40500)

2.1

Plant Operations

Review

The inspectors

observed

the conduct of plant operations

and independently

verified that the licensee

operated

the plant safely

and according to station

procedures

and regulatory requirements.

The inspectors

conducted regular

tours of the following plant areas:

~

Control

Room

~

Control Structure

~

~

Unit

1 and

2 Reactor

Buildings

~

~

Unit

1 and

2 Turbine Buildings

~

Engineered

Safeguards

Service Water

Emergency Diesel Generator

Bays

Protected

Area Perimeter

Security Facilities

Pump House

Control

room indications

and instrumentation

were independently

observed

by

NRC inspectors

to verify plant conditions were in compliance with station

operating procedures

and Technical Specifications.

Alarms received in the

control

room were reviewed

and discussed

with operators;

and operators

were

found cognizant of control board

and plant conditions.

Control

room and shift

manning were in accordance

with Technical Specification requirements.

During plant tours,

logs

and records

were reviewed to ensure

compliance with

station procedures,

to determine if entries

were correctly made,

and to verify

correct communication of equipment status.

These records

included various

operating logs, turnover sheets,

blocking permits,

and bypass logs.

The

inspector observed plant housekeeping

controls including control

and storage

of flammable material

and other potential safety hazards.

Inspections

were performed

on backshifts during July 19,

22, 26, 27,

1994

and

August 5,

18,

20 and 22,

1994.

Deep backshift inspections

were conducted

on

July 20-21,

1994 (10:00 p.m. - I:00 a.m.),

August 27 (ll:45 a.m. - 7:45 p.m.),

and August 28 (10:15 a.m. - 4:15 p.m.)

2.2

Simplex Fire Protection

System Failures

On August

2 at 9:31 p.m.,

a lightning strike rendered

the Simplex fire

protection

system inoperable.

As a result, fire suppression

and detection

capabilities

were impacted in safety-related

areas of both units

and

common

areas.

The licensee

entered

Technical Specification

(TS) Limiting Condition

for Operation

(LCO) Action Statements

for TS 3.3.7.9, 3.7.6.2,

and 3.7.7.

Significant Operating Occurrence

Report

(SOOR)94-545 documented

the event.

Subsequent

to declaring the Simplex fire protection

system inoperable,

the

licensee

began to implement compensatory

measures

per TS requirements,

which'equired

the establishment

of continuous fire watches within one hour.

The

site fire protection

system engineer

and

I8C technicians

were called in to

support problem resolution.

Shift supervision notified operations

and station

management

that continuous fire watches

could not be established

in the one

hour required

by Technical Specifications.

Roving fire watches

were

implemented while the list of affected fire zones requiring continuous fire

watches

was being prepared

in parallel with troubleshooting to restore

the

Simplex panel to an operable status.

At shift turnover time the next day,

approximately

10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> after the simplex fire panel

was declared

inoperable,

the inspector discovered that the continuous fire watches

required

by TS were

not established.

Contrary to management

expectations,

operations failed to

vigorously implement the required continuous fire watches.

The inspector

expressed

concern to the licensee that actions to establish

continuous fire

watches

had ceased.

Following management

involvement, the shift began

rigorously establishing

the required continuous fire watches to comply with

Technical Specifications.

At 11:00 a.m.

on August 3, the licensee

began to

post the continuous fire watches.

Subsequently,

the simplex system

was

restored at ll:45 a.m.

The licensee initiated a comprehensive

review of the event.

Four previous

Simplex system failures were identified since

1988.

After these resulted in

failure to comply with Technical Specification requirements.

Two were due to

lightning strikes.

The last reportable

event

was

on August 13,

1993 when the

-Simplex panel

was lost due to a lightning strike.

Prior to permanent corrective a'ctions

being impl'emented for the August 2,

1994

event,

another lightning strike rendered

the system inoperable

on August 18,

1994 at 7:00 a.m.

The plant staff aggressively

pursued

implementation of

compensatory

measures.

A draft response

procedure

being developed following

the August 2,

1994 event

improved implementation of compensatory

measures.

On August 29, the licensee

established

a formal Event Review Team

(ERT) to

broadly review the Simplex failure events

and to determine

comprehensive

corrective actions to prevent recurrence.

The Event Review Team investigation

was not fully completed at the end of the report period.

The team did,

however, determine initial root causes.

They were:

1) inadequate

corrective

actions

and actions to prevent recurrence for previous events,

2) inadequate

communications

between shift supervision

and plant management,

and 3)

miscommunications

between shift supervision

and the site fire protection

engineer.

The inspector determined that actions to comply with Technical Specifications

were not rigorously pursued to completion

by the operating shift.

When plant

management

became fully aware that the required continuous fire watches

were

not yet established,

plant staff was directed to aggressively

pursue

resolution of the issue.

The inspector

noted that the licensee's

response

procedures

for loss of the Simplex system were not detailed

enough to

implement numerous

continuous fire watches in a timely manner,

given the

magnitude of the simplex fire protection system failure.

This was contrary to

licensee

management

expectations for the corrective actions associated

with

the August

1993 event.

Notwithstanding response

procedure

inadequacies,

the

failure of the operating shift to establish

any continuous fire watches

was

a

significant weakness.

Actual safety significance of the events

was low since

roving fire watches

were established,

and, if needed,

suppression

systems

affected

by this event could be manually initiated.

The formation of an

ERT

and their initial conclusions

were considered

a strength.

Although system modifications were implemented to harden the system in 1990,

lightning strikes continue to affect system operability.

The inspector

was

concerned,

given the failure history, that compensatory

measures

were not

effectively proceduralized

to allow a timely determination of affected fire

zones

and, thus, timely implementation of fire watches.

The ineffective

communications that occurred during the operating shift's response

to the

event

was also

a contributor.

The plant staff's failure to implement

continuous fire watches

required

by TS is an apparent violation

(VIO 50-387/94-16-01

Common).

3.

MAINTENANCE AND SURVEILLANCE (62703,

61726,

92902,

40500)

3. 1

Naintenance

Observations

The inspector

observed

and/or reviewed selected

maintenance activities to

determine that the work was conducted

in accordance

with approved procedures,

regulatory guides,

Technical Specifications,

and industry codes or standards.

The following items were considered,

as applicable,

during this review:

Limiting Conditions for Operation were met while components

or systems

were

unremoved

from service;

required administrative approvals

were obtained prior to

initiating the work; activities were accomplished

using approved

procedures

and quality control hold points were established

where required; functional

testing

was performed prior to declaring the involved component(s)

operable;

activities were accomplished

by qualified personnel;

radiological controls

were implemented; fire protection controls were implemented;

and the equipment

was verified to be properly returned to service.

Maintenance

observations

and/or reviews included:

WA 43131,

Support

CRD Pump '2A'epair,

dated July 20,

1994.

WA 43030,

Fuel Line Component

Replacement

on the 'B'mergency

Diesel

Generator,

dated July 26.

WA 43356,

Remove

Resin

Heel

From 'C'ondensate

Deminer alizer, dated

August 17.

WA 44057,

Remove/Reinstall

Turbocharger

on the 'B'mergency

Diesel

Generator,

dated August 26.

3.1. 1 'B'mergency Diesel Generator

Turbocharger

Problem

On August 24, during restoration

from a five year overhaul,

water was

discovered

in the 'B'mergency

Diesel

Generator

(EDG) lube oil system while

performing

a jacket water flush.

The licensee

determined

the source of water

was

a leak internal to the turbocharger.

The turbocharger,

which was

refurbished

by the vendor,

was installed

as part of the five year overhaul of

the engine.

The 'B'DG had not yet been run with the refurbished

turbocharger.

SOOR 94-477 documented

the event.

Maintenance

personnel

removed the water from the lube oil system.

The

refurbished turbocharger

has

been

removed

and returned to the vendor for a

failure analysis.

The old turbocharger

has

been reinstalled.

The licensee,

in concert with the vendor, is performing

a root cause investigation of the

failure.

The inspector expressed

concern to licensee

management

regarding the potential

for common

mode failure of the

EDGs pending the final bounding determination

of root cause.

The licensee,

based

on successful

surveillance tests,

system

logs, lube oil analysis

and operator rounds,

concluded

the other

EDGs do not

presently

have water contamination of the lube oil system.

The licensee

is

rigorously pursuing root cause.

The inspector will continue to evaluate

licensee resolution of the turbocharger malfunction as part of the

SOOR

resolution process.

3.2

Surveillance Observations

The inspector

observed

and/or reviewed the following surveillance tests to

determine that the following criteria, if applicable to the specific test,

were met:

the test

conformed to Technical Specification requirements;

administrative

approvals

and tagouts

were obtained before initiating the

surveillance;

testing

was accomplished

by qualified personnel

in accordance

with an approved

procedure;

test instrumentation

was calibrated; 'Limiting

Conditions for Operations

were met; test data

was accurate

and complete;

removal

and restoration of the affected

components

was properly accomplished;

test results

met Technical Specification

and procedural

requirements;

deficiencies

noted were reviewed

and appropriately resolved;

and the

surveillance

was completed at the required frequency.

Surveillance observations

and/or reviews included:

S0-249-002,

quarterly

RHR System

Flow Verification, dated August 18,

1994.

S0-256-001,

Meekly Control

Rod Exercising,

dated August 19.

SI-013-248,

Semi-Annual

Functional Test of Fire Protection Ionization

Detectors

in Fire Zone 026-H Control

Room, dated August 27.

3.2.1

HPCI Isolation Caused

by Human Error

On August 25,

1994, while 15C Technicians

were performing residual

heat

removal

(RHR) system

equipment

area differential temperature

high channel

calibrations,

a multimeter was connected

to the wrong terminals.

This

resulted in the

HPCI system

steam supply outboard isolation valve stroking

closed.

Operators

verified no valid leak or high temperature

condition

existed

and reopened

the valve to restore

the system to an operable status

in

accordance

with the system operating

procedure.

At the conclusion of the inspection period, station personnel

had not

completed their investigation of this event.

This item will remain unresolved

pending

NRC review of PP8L's corrective actions

(URI 50-387/94-16-02).

4.

ENGINEERING (71707,

37551,

92903,

40500)

4. 1

Nuclear System Engineering

System

Review Meeting

The inspector attended

the Nuclear System Engineering

(NSE) System

Review

meeting for the standby

gas treatment

system

(SGTS).

The system engineer

discussed

system, availability, performance,

areas of concern,

material

condition, deficiencies,

modifications

and enhancements.

The system engineer

appeared

very knowledgeable of system performance

and design.

The

presentation

was clear,

concise

and comprehensive.

Engineering

and operations

management

attended

the meeting.

Although usually present,

Maintenance

was

not represented

at this meeting.

The Vice-President - Nuclear Engineering

maintained

a healthy questioning attitude throughout the meeting.

Several

followup actions

were required

as

a result of these questions.

The inspector

concluded that the weekly System

Review meeting concept

was

an

engineering

strength.

System performance is reviewed with management

and long

term corrective actions

and performance

improvements

are planned for

implementation.

The meeting facilitates direct management

involvement with

system performance

issues.

However, the inspector

observed

action items are

not formally documented.

The licensee is considering the need to document

follow up actions.

The inspector

had

no further questions.

5.

PLANT SUPPORT

(71750,

71707,

92904,

40500)

5.1

Radiological

and Chemistry Controls

During routine tours of both units, the inspectors

observed

the implementation

of selected

portions of PP&L's radiological controls program to ensure:

the

utilization and compliance with radiological work permits

(RWPs); detailed

descriptions of radiological conditions;

and personnel

adherence

to

RWP

requirements.

The inspectors

observed

adequate

access

controls to various

radiologically controlled areas

and

use of personnel

contamination monitors

and frisking methods

upon exit from these

areas.

Posting

and control of

radiation

and high radiation areas,

contaminated

areas

and hot spots,

and

labelling and control of containers

holding radioactive materials

were

verified to be in accordance

with PP&L procedures.

Workers complied with

radiation work permits

and appropriately

used required personnel

monitoring

devices.

Health Physics technician control

and monitoring of these activities

was satisfactory.

Overall, the inspector

observed

an acceptable

level of

performance

and implementation of the radiological controls program.

5.2

Security

Implementation of the physical security plan was routinely observed

in various

plant areas with regard to the following:

protected

area

and vital area

barriers

were well maintained

and not compromised;

isolation zones

were clear;

personnel

and vehicles entering

and packages

being delivered to the protected

area

were properly searched

and access

control

was in accordance

with approved

licensee

procedures;

security access

controls to vital areas

were maintained

and persons

in vital areas

were authorized for entry; security posts

were

adequately

staffed

and equipped,

security personnel

were alert

and

knowledgeable

regarding position requirements,

and written procedures

were

available;

and adequate

illumination was maintained.

Licensee

personnel

were

observed to be properly implementing

and following the physical security plan.

5.3

Fire Door Blocked Open

On July 20 at 2:40 p.m., while conducting

a routine tour, the inspector

discovered fire door 44,

Common Equipment

Room to

CRD

Pump Area, in the

656'levation

of the turbine building, blocked open.

A warning was painted

on the

floor that read

"Do Not Block Fire Door Zone."

The inspector notified the

control

room.

Shift supervision

promptly dispatched

an assistant

unit

supervisor

(AUS) to unblock the door.

A compensatory

hourly firewatch was in

place for

an existing door deficiency.

However, Nuclear Department

Administrative Procedure,

NDAP-(A-0441, Fire Protection

System Status Control,

requires that if a fire protection

system or equipment is removed

from service

or impaired,

a Fire Protection

Systems

Status

Change

(FPSSC)

form, NDAP-gA-

0441-1,

and separate

Equipment

Release

Form (ERF)

be issued.

This is to

ensure

the impairment is controlled

and required compensatory

measures

are

implemented.

This activity was not performed to support blocking open Fire

Door (FD) 44.

The inspector

noted that since January

1,

1994 there were four documented

licensee identified examples of blocked

open fire doors without following

procedural

requirements.

The affected plant locations included Standby Liquid

Control

(SBLC) Penetration

Room

(SOORs94-037

and 94-246),

and Main Steam

Pipe

Tunnel

(SOOR 227).

SOOR 94-154 documented

the

same fire door

44 was blocked

open twice without the required administrative approvals

on March 4 and March

7,

1994.

The inspector also noted there were other examples of fire doors

being blocked

open without necessary

compensatory

measures

or administrative

approvals prior to 1994.

Again on August 23, the inspector identified that

fire door 44 was blocked

open without the necess'ary

administrative

authorization.

Shift supervision

issued

SOOR 94-475 documenting the inspector

identified unauthorized fire door blockage.

Previously,

inspector considered

the licensee identification and documentation

of the previous fire door blockage

problems

a strength.

The licensee,

in

response

to earlier events,

had concluded previous corrective actions

were

ineffective.

The licensee

formed

a team to resolve the blocked open fire door

issue.

However, the performance

indicates continuing ineffective corrective

actions for previous events

and lack of sensitivity to the safety function of

fire doors

on the part of station personnel.

The actual safety significance

of the events

was low since roving fire watches

also patrolled the affected

areas

as part of their rounds.

However, fire doors,

which are fire rated

barriers,

function to prevent the spread of fire.

The

NRC and licensee

identified examples of the failure to properly implement fire protection

system status control

as required

by NDAP-gA-0441 is

a significant condition

adverse to quality.

The ineffective corrective act'ions to preclude repetition

of improperly blocked

open fire doors is

a violation of 10 CFR 50 Appendix

B

Criterion XVI.

(VIO 50-387/94-16-03).

6.

SAFETY ASSESSMENT/EQUALITY VERIFICATION (40500,

90700,

90712,

92700)

6.1

Licensee

Event Reports

The inspector

reviewed

LERs submitted to the

NRC office to verify that details

of the event, were clearly reported,

including the accuracy of the description

of the cause

and the adequacy of corrective action.

The inspector determined

whether further information was required

from the licensee,

whether generic

implications were involved,

and whether the event warranted onsite follow up.

The following LERs were reviewed:

Unit

1

94-005-00

Unit

1 Turbine Building Sampler for Particulate,

Iodine,

and

Mobile Gas

(SPING) Alternate Sampling,

Disconnected

On March 8,

1994, it was determined that the alternate

continuous

sampling

required

by Technical Specification 3.3.7. 11 Action 112 for an out-of-service

turbine building SPING was not completed

as required.

Chemistry personnel

discovered

the sample tubing from the

SPING vent to the alternate

pump suction

became disconnected.

TS Action 3.3.7. 11 Action 112, which required continuous

sampling of iodines

and particulates,

was not met from 10:15 a.m. - 1:35 p.m.

on March 8.

Sample results before

and after the event indicated that releases

were less than the lower limit of detection.

The licensee

concluded there

was

no unmonitored release

during the time of suspect

sampling.

Corrective

actions

included clamping the sample tubing.

The inspector

agreed with the licensee's

reportability analysis

and considered

corrective actions

adequate.

This violation will not be subject to

enforcement

action

because

the licensee's effort in identifying and correcting

the violation met the criteria specified in Section VII.B(2) of 10 CFR Part 2,

Appendix C.

94-011-00

Reactor

Water Cleanup

(RWCU) System Isolation on High Differential

Flow

On July 7,

1994, the Unit

1

RWCU system isolated

on high differential flow.

The high differential flow was caused

by leakage

past

a maintenance

boundary

valve.

NRC Inspection

Report 50-387/94-11

documented

the event.

7.

MANAGEMENT AND EXIT MEETINGS (30702)

7.1

Resident Exit and Periodic Meetings

The inspector discussed

the findings of this inspection with PP8L station

" management

throughout the inspection period to discuss

licensee activities

and

areas of concern to the inspectors.

At the conclusion of the reporting

period, the resident

inspector staff conducted

an exit meeting

summarizing the

preliminary findings of this inspection.

Based

on

NRC Region I review of this

report

and discussions

held with licensee representatives, it was determined

that this report does not contain information subject to 10 CFR 2.790

restrictions.

7.2

Other

NRC Activities

On August 8-10,

and 15-16,

1994,

an

NRC Region I Reactor

Engineer

conducted

an

engineering

inspection.

Inspection results will be documented

in NRC

Inspection

Report 50-387/94-17,

50-388/94-18.

On August 8-10,

NRC Region I conducted

an initial license examination.

Examination results

are documented

in NRC Inspection

Report 50-387/94-15,

50-388/94-16.

On August 29-31

and Sept 1-2,

an

NRC Region I Security Inspector performed

a

Safeguards

Inspection.

Results will be documented

in NRC Inspection

Report

50-387/94-18;

50-388/94-19.