ML17157C044
| ML17157C044 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 10/21/1992 |
| From: | Jason White NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17157C042 | List: |
| References | |
| 50-387-92-22, 50-388-92-22, NUDOCS 9210270109 | |
| Download: ML17157C044 (53) | |
See also: IR 05000387/1992022
Text
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UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION I
Inspection
Report Nos.
50-387/92-22; 50-388/92-22
License Nos.
Licensee:
Pennsylvania Power and Light Company
2 North Ninth Street
Allentown,. Pennsylvania
18101
Facility Name:
Inspection At:
Susquehanna
Steam Electric Station
Salem Township, Pennsylvania
Inspection
Conducted:
August 18, 1992 - September 28, 1992
Inspectors:
G. S. Barber, Senior Resident Inspector, SSES
D. J. Mannai, Resident Jnspec r~ES
B. C. Westreich, R
or En
ee
Approved By:
ng
- J.
te, Chief
R
ctor Projects Section No. 2A,
Date
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during day and backshift hours of station activities including: plant operations; radiation
protection; surveillance and maintenance;
and safety assessment/quality
verification. Three
violations were identified.
One violation involved removal of insulation from safety related
equipment without a documented procedure which is a violation of Technical Specification 6.8.1.
Section 4.4.2 pertains.
Two violations concerning a design change to the Control
Structure Chilled Water System occurred.
One violation concerned failure to perform post
maintenance testing in accordance with PP&L's procedure AD-QA-482. The other violation
concerned
the failure to complete a required 10 CFR 50.59 safety evaluation for a change to
the facility. Subsequently,
the licensee returned the system to the original configuration
(without the orifice) and verified that proper flow was achieved.
Section 7.2.1 pertains.
Findings and conclusions are summarized in the Executive Summary.
Details are provided in
the full inspection report.
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'721027010'P
921022
ADOCK 05000387
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EXECUTIVESUMMARY
Susquehanna
Inspection Reports
50-387/92-22; 50-388/92-22
August 14, 1992
- September 28, 1992
Operations (30702, 71707, 71710)
During the period, a trip of the Unit 1 "B" Reactor Recirculation Pump Occurred.
A
momentary power spike of 108% occurred on the Average Power Range Monitor (APRM)
indications during the first few seconds of the transient.
The licensee determined
a Peak
Core.Thermal Power of 100.2 percent.
The licensee methodology utilized GETARS
simulated thermal power points to determine peak power during transients since APRM
indication overpredicts thermal power increase during overpower events.
During overpower
events neutron flux leads reactor heat flux because of the inherent six second delay in
transferring heat to the coolant.
The inspector determined the licensee's methodology to be
sound.
Section 2.2.1 pertains,
One engineered
safety feature actuation occurred during the period.
A loss of shutdown
cooling occurred when the outboard isolation valve went closed.
Shutdown cooling was
promptly restored.
The licensee did not determine the cause.
Section 1.3 pertains.
Maintenance/Surveillance
(61726, 62703)
During the period, on a routine tour, the inspector identified that insulation was removed
from High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC)
systems with Unit 2 operating at power without a prescribed procedure or operations
authorization.
As a result, equipment in these area was exposed to elevated temperatures.
.Because there was no procedure,
the potential effects of these temperatures
were unanalyzed.
The inspector determined that this uncontrolled maintenance activity on safety related
equipment was a weakness.
This is an apparent violation of Technical Specification 6.8.1.
Section 4.4 pertains.
During the period, the licensee identified potential problems with Resistance Temperature
Detectors (RTDs) used to determine suppression pool temperature.
Five of the fifteen RTDs
exhibited unacceptable drift during in-situ testing during the Unit 1 Refueling Outage in the
Spring of 1992.
The licensee believed moisture entrainment may have caused excessive
buildup of voltage to ground, at the sensing element, resulting in the observed drifting. The
licensee is evaluating reportability per 10 CFR 21.
During the period, the "A" Emergency Switchgear Room Cooling (ESRC) system was
declared inoperable due to inadequate cooling water flow from.the "A" Control Structure
(CS) Chilled Water System.
At the time, the "B" Control Structure Chilled Water System
was out-of-service to install a flow orifice which had been previously installed in the "A"
system.
The "B" train was restored to service prior to exceeding the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> Limiting
Condition for Operation (LCO). A design change was performed to install an orifice in a
location that previously had one. The original orifice was removed by a previous design
change.
The new orifice was being installed to allow system flow measurement.
The design change to install the new orifice was performed as resolution of a Noncon-
formance Report (NCR).
This design change altered -system design flow rate.
The orifice
was installed on the "A" CS Chilled Water on August 2 and the system was returned to an
operable status without performing post-maintenance
testing to check system flow rate.
Subsequent
testing revealed flow rates slightly less than the specified design flow. The
licensee failed to perform post-maintenance
testing and a safety evaluation to support the
design change.
Failure to perform the post-maintenance/modification
testing was a procedural violation of
AD-QA-482, Post Maintenance/Modification Test Program.
Failure to perform the safety
evaluation was a violation of 10 CFR 50.59.
Section 7.2.1 pertains.
The licensee discovered that 20 Unit 1 and one Unit 2 solenoid operated valves were rebuilt
using an improper 0-ring lubricant.
Petroleum Jelly was used instead of the preferred Dow
Corning (DC)-55, lubricant.
The performance history for the affected valves showed no
lubricant induced failures, and that all of the suspect valves (except for one) had been rebuilt
since March 1992.
The excepted valve, rebuilt in.early 1984, has been stroked quarterly
with no anomalies.
The licensee is confident the valves willcontinue to operate until they
are all replaced by the next refueling outage in September
1993.
The inspector found the
licensee's actions prompt and comprehensive.
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TABLEOF CONTENTS
EXECUTIVESUMMARY............ ~............... ~...........
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SUMMARYOF OPERATIONS ...
1.1
Inspection Activities......
1.2
Susquehanna
Unit 1 Summary
1.3
Susquehanna
Unit 2 Summary
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OPERATIONS
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2.1
Inspection Activities.................
2.2
Inspection Findings and Review of Events....
2.2.1
Unit 1 Reactor Recirculation Pump Trip
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RADIOLOGICALCONTROLS
3.1
Inspection Activities
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3.2
Inspection Findings
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MAINTENANCE/SURVEILLANCE
4.1
Maintenance and Surveillance Inspection Activity
4.2
Maintenance Observations
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Surveillance Observations......... ~..........
4.4
Inspection Findings
4.4.1
Uncontrolled Safety System Insulation Removal ..
4.4.2
Suppression Pool Resistance Temperature Detector
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egradation
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EMERGENCY PREPAREDNESS......,...
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Inspection Activity...... ~........
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Inspection Findings
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6.
SECURITY
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Inspection Activity.....,.......
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Inspection Findings
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Table of Contents (Continued)
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ENGINEERING/TECHNICALSUPPORT................
7..1
Inspection Activity........,..........,........
7.2
Inspection Findings
7.2.1
Emergency Switchgear Room Cooler Event
7.2.2
Improper Lubricant Used on Solenoid Operated Valves (SOV)
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8.
SAFETY ASSESSMENT/QUALITYVERIFICATION
8.1
Licensee Event Reports (LER)
8.1.1
Licensee Event Reports...........=.'.
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MANAGEMENTAND EXIT MEETINGS
9.1
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Inspections Conducted By Region Based Inspectors
9.3
Management Meeting - Federal Field Exercise 3 (FFE-3)
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Details
1.
SUMMARYOF OPERATIONS
1.1
Inspection Activities
The purpose of this inspection was to assess
licensee activities at Susquehanna
Steam Electric
Station (SSES) as they related to reactor safety and worker radiation protection.
Within each
inspection area, the inspectors documented
the specific purpose of the area under review, the
scope of inspection activities and findings, along with appropriate conclusions.
This
assessment
is based on actual observation of licensee activities, interviews with licensee
personnel,
measurement of radiation levels, independent calculation, and selective review of
applicable documents.
Abbreviations are used throughout the text.
Attachment
1 provides a listing of these
abbreviations.
1.2
Susquehanna
Unit 1 Summary
At the start of the inspection period, Unit 1 was at full power.
On August 20, the Unit 1
"B" Recirculation pump tripped from full power resulting in a reduction to 47% power.
Investigation of the pump trip revealed that lube oil pump problems caused
an increase in
recirculating pump speed and an apparent increase in indicated reactor power to 108%.
Subsequent problems with lube oil resulted in a Reactor Recirculation pump tripping.
Section
2.2 pertains.
Following evaluation of the recirculation pump trip event, at 5:00 a.m., August 21, reactor
power was increased to full power.
At 12:46 p.m., August 21, the "C" Circulating Water
Pump tripped on overcurrent on the "A" phase, causing a recirculation system runback.
The
result was a decrease
to 68% power.
Following evaluation, power was returned to 100%,
with three of four circulating water pumps in service.
On September 5, reactor power was reduced to 68% to repair a loose conduit on the 11 main
turbine control valve.
Upon completion of repairs on September 6, power was returned to
100% and remained at or near full power until the end of the period.
Other significant events which occurred during the period include:
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Both Emergency Switchgear Room Coolers were declared inoperable on August 18 requiring
entry into a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> LCO. The "B" cooler was out of service for maintenance when the "A"
cooler was declared inoperable due to insufficient flow. The "B" cooler was returned to
service prior to exceeding the LCO,
Investigation by the licensee indicated that modifications
to the "A" loop were performed contrary to the licensee's modification process,
and without
the required post-modification system test.
Section 7..2 pertains.
2
In response to NRC Bulletin 92-01 Supplement
1, the licensee declared all remaining
Thermo-Lag installations inoperable on August 31.
The licensee implemented compensatory
measures.
1.3
Susquehanna
Unit 2 Summary
Unit 2 entered the period in coastdown at 96.4% power.
On September 6, at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br />,
reactor power was reduced to 60% for the remainder of the cycle to stay within the license
fuel design window. The fifth refueling outage was commenced on September
12, when the
main generator was taken off-line at 5:30 a.m..
The mode switch was placed in Hot
Shutdown, entering Condition 3, at 7:28 p.m. on September
12 and in Cold Shutdown,
entering Condition 4, at 10:25 p.m. on September
13.
The refueling mode, Condition 5, was
entered on September
15 at 12:05 a.m..
Core offload was complete at 9:10 p.m. on
September 26.
Significant events which occurred during the period include:
At 1:46 p.m., September 26, an ESF actuation occurred when the Shutdown Cooling
(SDC) outboard isolation valve went closed and the "B" RHR pump being used for
SDC tripped.
Licensee review of the computer history and NSSSS isolation
indications revealed no abnormal conditions.
The procedure for loss of SDC was
implemented and all fuel movement was stopped.
Though an investigation was
performed, a-cause could not be determined.
Subsequently,
the NSSSS logic was
reset, the isolation valve opened,
and SDC restored.
The licensee continued to
investigate at the end of the inspection period.
On September
10, insulation was removed from HPCI and RCIC piping in preparation
for outage work. This resulted in elevated equipment room temperatures.
The work
was performed without review by Unit Coordination, and without evaluation by
system engineering to determine the impact on equipment qualification and
operability.
This work was performed without authorization from any responsible
department.
Subsequent
analysis determined that EQ limits were not exceeded.
Section 4.4 pertains.
2.
OPERATIONS
2.1
Inspection Activities
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The inspectors verified that the facility was operated safely and in conformance with
regulatory requirements.
Pennsylvania Power and Light (PP&L) Company management
control was evaluated by direct observation of activities, tours of the facility, interviews and
discussions with personnel,
independent verification of safety system status and Limiting
Conditions for Operation, and review of facility records.
These inspection activities were
conducted in accordance with NRC inspection procedure 71707.
The inspectors performed 36.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> of deep backshift inspections during the period.
These
deep backshift inspections covered licensee activities between 10:00 p.m. and 6:00 a.m. on
weekdays,
and weekends and holidays.
2.2
Inspection Findings and Review of Events
2.2.1
Unit 1 Reactor Recirculation Pump Trip
On August 20, the Unit 1 "B" Reactor Recirculation Pump tripped when the reactor
recirculation pump motor generator (MG) set tripped, following a trip of the "B" 2 lube oil
pump.
The "B" 1 lube oil pump automatically started as designed.
The operators promptly
performed the actions of off-normal procedure ON-164-002, Loss of Reactor Recirculation
Flow.
CRAM rods (pre-defined high reactivity control rods) were inserted following the
recirculation pump trip to reduce power.
Additional rods were inserted to reduce power
below the 80% rod line.
The licensee verified proper core power and flow were achieved for
the condition. 'The licensee was unable to restart the "B" 2 lube oil pump, but since the "B"
1 lube oil pump was already running, the "B" reactor recirculation pump was successfully
restarted.
Following, the licensee performed a transient review and determined no thermal
limits were exceeded.
A review of the General Electric Transient Analysis Recording System (GETARS) Data
indicated that average power range monitor (APRM) indication momentarily increased from
95 to 108% power during the first few seconds of the transient.
Control room operators did
not 'observe any Local Power Range Monitor (LPRM) upscale lights on the full core display.
The licensee determined that peak core thermal power (heatflux) did not exceed 100.2%.
The inspector questioned the licensee on how a peak core thermal power of 100.2% was
determined.
The licensee described an off-normal procedure for reactor power greater than
100% (3293 MWth). The procedure requires the shift technical adviser (STA) to determine
peak core thermal power using GETARS ifit is suspected
that reactor thermal power
exceeded
102% (3358 MWth) of rated thermal power.
Since APRMs indicated 108% the
STA implemented the procedure.
The licensee determined peak thermal power during transients using simulated thermal power.
The simulated thermal power is obtained by using APRM neutron flux signals through a
filtering network with a six second time constant which is representative of fuel
characteristics.
During power increase events neutron flux leads reactor heat flux because of
the fuel time constant.
Thus APRM neutron flux overpredicts thermal power during power
increase events.
This methodology is supported in General Electric Service Information
Letter (GL SIL) No. 158.
This calculation determined that thermal power peaked at 100.2%.
The inspector determined that the licensee's methodology used to ensure compliance with
licensed thermal power appeared
sound.
The inspector observed that the procedure should
contain the steps to determine peak core thermal power rather than simply reference
documents which contain the methodology.
The licensee agreed to a procedure change to
explicitly describe the methodology for determining peak core thermal power in the off-
normal procedure.
The inspector had no further questions.
3.
RADIOLOGICALCONTROLS
3.1
Inspection Activities
PP&L's compliance with the radiological protection program was verified on a periodic basis.
These inspection activities were conducted in accordance with NRC inspection procedure
71707.
3.2
Inspection Findings
Observations of radiological controls during maintenance activities and plant tours indicated
that workers generally obeyed postings and Radiation Work Permit requirements.
No
inadequacies
were noted.
4.
4.1
Maintenance and Surveillance Inspection Activity
On a sampling basis, the inspector observed and/or reviewed selected surveillance and
maintenance activities to ensure that specific programmatic elements described below were
being met.
Details of this review are documented in the following sections.
4.2
Maintenance Observations
The inspector observed and/or reviewed selected maintenance activities to determine that the
work was conducted in accordance with approved procedures,
regulatory guides, Technical
Specifications,
and industry codes or standards.
The following items were considered,
as
applicable, during this review: Limiting Conditions for Operation were met while
components or systems were removed from service; required administrative approvals were
obtained prior to initiating the work; activities were accomplished using approved procedures
and quality control hold points were established where required; functional testing was
performed prior to declaring the involved component(s)
operable; activities were
accomplished by qualified personnel; radiological controls were implemented; fire protection
controls were=implemented;
and the equipment was verified to be properly returned to
service.
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These observations and/or reviews included:
WA 23026, Installation of Vent Tubing on the "A" Emergency Diesel Generator
Injector Drains, dated August 20.
WA 20068, Control Structure Chiller Oil Leak Repair, dated August 22.
WA 13829, Residual Heat Removal PSV Replacement Setpoint Test, dated September
9.
WA 26265, Primary Containment Accident Range Pressure Transmitter internal
wiring inspection, dated September 9.
4.3
Surveillance Observations
The inspector observed and/or reviewed the following surveillance tests to determine that the
following criteria, ifapplicable to the specific test, were met:
the test conformed to
Technical Specification requirements; administrative approvals and tagouts were obtained
before initiating the surveillance; testing was accomplished by qualified personnel in
accordance with an approved procedure;
test instrumentation was calibrated; Limiting
Conditions for Operations were met; test data was accurate and complete; removal and
restoration of the affected components was properly accomplished;
test results met Technical
Specification and procedural requirements;
deficiencies noted were reviewed and
appropriately resolved; and the surveillance was completed at the required frequency.
These observations and/or reviews included:
SO-156-001, Weekly Exercising Control Rods for Operability, dated August 22.
SO-149-002, Residual Heat Removal (RHR) System Quarterly Flow Surveillance,
dated August 27.
SI-255-302, Eighteen Month Calibration of Control Rod SCRAM Accumulator Leak
Detectors, dated September
14.
4.4
Inspection Findings
The inspector reviewed the listed maintenance
and surveillance activities.
The review noted
that work was properly released before its commencement;
that systems and components
were'roperly
tested before being returned to service and that surveillance and maintenance
activities were conducted properly by qualified personnel.
Where questionable
issues arose,
the inspector verified that the licensee took the appropriate action before system/component
operability was declared.
Except as noted below, the inspectors had no further questions on
the listed activities.
4.4.1
Uncontrolled Safety System Insulation Removal
On September 9, during a tour of the Unit 2 emergency core cooling pump rooms, the
inspector noted elevated Reactor Core Isolation Cooling (RCIC) and High Pressure Coolant
'njection (HPCI) system room temperatures.
Unit 2 was at 60% power at the time.
The inspector discovered that insulation was being removed from steam piping in preparation
for the upcoming outage starting September
12.
Maintenance personnel had removed and
were removing insulation from HPCI and RCIC steam piping, valve and pumps.
The inspector contacted the system engineer to assess
the licensee's evaluation of the
connection between insulation removal and increased area temperatures.
The system engineer
was not aw'are of any insulation removal from steam piping and other components.
In response to the inspector's questioning, the licensee later determined that insulation was
being removed from safety related equipment by an uncontrolled station work practice that
allowed removal without review or approval by either plant scheduling (unit coordination) or
operations.
The licensee subsequently
documented this undesirable work practice in
Significant Operating Occurrence Report (SOOR) 2-92-087.
Further, no engineering evaluation was requested or performed by systems engineering to
assess
the impact of premature insulation removal on equipment qualifications or system
operability.
To address the potential safety concerns,
the work group reinstalled all removed installation.
The HPCI and RCIC.room coolers were operated to reduce room temperatures.
The licensee
determined that since room temperatures
did not exceed the environmental qualification (EQ)
limit and since the duration of the elevated temperatures
was short, equipment operability was
not affected.
Maxiinum HPCI room temperature reached was 105'F and RCIC room
temperature reached was 114'F.
The HPCI EQ limit was 112'F, while the RCIC EQ limit
was 123'F.
The inspector noted that the work performed was accomplished without the use of an
approved procedure nor was it controlled in accordance with either NDAP-QA-306,
System/Equipment
Release, or AD-QA-502, Work Authorization System.
The inspector
determined that the conduct of maintenance activities that removed insulation required by
design from safety related equipment without an approved procedure or instruction was a
weakness.
Technical 6.8.1 requires that safety related activities be performed in accordance
with approved procedures.
This lack of control of maintenance activities was of particular
concern.
The inspector concluded that the actual safety significance was minimal since
temperatures did not exceed the EQ limit. However, the potential was significant as
uncontrolled maintenance
was performed on safety related equipment. This was a violation of
TS 6.8.1 which requires that instructions or procedures be established for work on safety
related equipment.
(VIO 50-388/92-22-01).
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4.4.2
Suppression Pool Resistance Temperature Detector (RTD) Degradation
On August 25, the licensee informed the inspector of a potential problem with resistance
temperature detectors (RTDs) used for suppression pool temperature.
Five of the fifteen
RTDs exhibited unacceptable drifting during in-situ testing performed during the Spring
1992, Unit 1 refueling outage.
This potentially nonconforming condition was documented in
Nonconformance report (NCR)92-058 on March 19.
This NCR was forwarded for a
reportability evaluation on May 1.
The licensee believed the problem may have been related
to moisture entrainment in the RTD which results in an excessive build-up of voltage to-
ground within the circuitry. This voltage buildup resulted in the observed drifting.
The RTDs are manufactured by Hy-Cal Engineering of El Monte, California. The licensee
believes only one lot is affected, and involves a new design containing an additional layer of
insulation on the RTDs (Model No. RTS-4096-B-A-100-C-290-3-12-XI-M3).
The licensee's
initial testing identified the degradation.
Subsequent
testing by the vendor has shown less of
a voltage buildup to-ground.
The licensee and vendor are considering the collective impact
of their respective testing.
The licensee is also evaluating reportability per 10 CFR 21.
The inspector questioned the licensee on the differences between their results and those of the
vendor.
The licensee stated that entrained moisture within the RTD disassociates
the
magnesium oxide coating and forms an electrolytic cell which acts as an internal battery.
'he removal of the RTD from service allows this effect to dissipate with time.
Thus, the
testing results seen by the vendor and by the licensee are explainably different. After further
discussion the licensee agreed to informally report this nonconforming condition.
The
licensee documented their conclusions in an August 26 submittal (PLA-3842) to the NRC,
and initiated actions to report the event in accordance with 10 CFR 21.
The inspector had no
further questions.
5.
5.1
Inspection Activity
The inspector reviewed licensee event notifications and reporting requirements for events that
could have required entry into the emergency plan.
5.2
Inspection Findings
No events were identified that required emergency plan entry.
No significant observations
were identified.
6.
SECURITY
6.1
Inspection Activity
PP&L's implementation of the physical security program was verified on a periodic basis,
including the adequacy of staffing, entry control, alarm stations, and physical boundaries.
These inspection activities were conducted in accordance with NRC inspection procedure
71707.
6.2
Inspection Findings
The inspector reviewed access and egress controls throughout the period.
No significant
observations were noted.
7.
ENGINEERING/TECHNICALSUPPORT
7.1
Inspection Activity
The inspector periodically reviewed engineering and technical support activities during this
inspection period.
The on-site Nuclear Systems Engineering (NSE) organization, along with
Nuclear Technology (NPE) in Allentown, provided engineering resolution for problems
during the inspection period.
NSE generally addressed
the short term resolution of problems
and scheduled modifications and design changes, by the Nuclear Modifications organization
as appropriate, to provide long term problem correction.
The inspector verified that problem
resolutions were thorough and directed at preventing recurrences.
In addition, the inspector
reviewed short term actions to ensure that they provided reasonable
assurance
that safe
operation could be maintained.
7.2
Inspection Findings
7.2.1
Emergency Switchgear Room Cooler Event
On August 18, with Unit 1 at 100% power and Unit 2 at 96% power, the "A" Emergency
Switchgear Room Cooling (ESRC) System was declared inoperable due to inadequate flow
through the "A" Control Structure Chilled Water System.
At the time "B" Control Structure
Chilled Water was out-of-service to install a flow orifice which had previously been installed
in the "A" Control Structure Chilled Water System.
As a result, both trains of ESRC were
inoperable which required the licensee to enter a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> LCO. The "B" train was returned
to service prior to exceeding the LCO. With both systems unavailable, this condition could
have prevented the fulfillmentof the affected rooms safety functions for systems needed to
safely shutdown the reactor and maintain it in a safe shutdown condition.
The licensee made
the required NRC notification per 10 CFR 50.72.
The licensee performed an investigation of the, event and determined the following sequence
of events:
~
In July 1991, Operations requested
that Engineering investigate the need to maintain
locked valves in the Control Structure Chilled Water System.
Operations was
interested in reducing the number of locked valves required to be maintained.
To
assist in accomplishing this, Engineering decided to check system flow to verify the
last flow balance.
When attempting to measure flow in the ESRC system, the licensee
discovered that a flow orifice was not installed as indicated on the system drawings.
In August 1991, PP&L determined that a design change initiated in June 1982 by
Bechtel, to remove the orifice had not been fully incorporated into all drawings.
The
design change, Startup Field Request (SFR) 2923, had been issued because
calculations showed the design flow rate of 49 GPM could not be maintained with the
orifice installed,
This explained why the orifice was shown on the system drawing,
but not installed in the system,
In September
1991, the licensee determined that in order to measure system flow, the
orifice should be reinstalled.
Flow measurements
were 34 gpm for the "A" ESRC
and 28.5 gpm for the "B" ESRC.
New calculations were performed which showed
that the system required 29 gpm to perform its cooling function.
Engineering changed
the design flow rate for the Control Structure Chilled Water to the Emergency
Switchgear Room Cooling Coil accordingly.
In November 1991, a Nonconformance Report (NCR) was issued to document the
drawing discrepancies.
The NCR resolution instructed changing all drawings to
reflect that a new orifice was to be installed.
The work was to be controlled by three
work authorizations (WAs): one for fabrication, one for installation, and one for post
installation fiow testing.
The completion of all three Work Authorizations was not
required prior to returning the system to service.
On August 2, 1992 the'newly fabricated orifice was installed in the "A" Control
Structure Chiller System and the system was declared operable.
A post modification
flow test was not performed.
On'ugust 12, 1992 the "B" Control Structure Chiller was taken out of service for
maintenance.
On August 18, the WA for installing the "B" orifice was brought to Unit Coordination
and the lack of a specified retest was questioned.
The system engineer also noted that
the retest WA was not directly tied to the installation WA or operability of the system,
and realized that the retest had not been performed on the "A" Control Structure
Chilled Water system.
Unit coordination and system engineering deemed it necessary
to immediately obtain the flow data for the "A" subtrain.
The flow test subsequently
0
(
0
10
performed measured flow rate at 25.8 gpm.
The required flowrate was 29 gpm.
Consequently,
the "B" Control Structure Chilled Water System was returned to.-service
immediately after the discovery.
The LCO when both systems are inoperable is 12
hours.
Subsequently,
when investigating the low system flow, the orifice was removed from the "A"
system and was determined to be installed backwards.
This was indicative of an installation
error.
Final resolution of the investigation determined that the orifices should remain
removed and all documentation changed to reflect this condition.
No data was taken to
determine the flow of the system with the orifice in the correct orientation.
A minor
modification request was processed for future consideration.
The inspector's reviewed the Event Review Team (ERT) report and LER 92-013-00 and
identified the following:
~
The licensee identified that a Design Change Package (DCP) was required for
modification work instead of the NCR which was used.
Use of the DCP would have
required a 10 CFR 50.59 evaluation and increased
management control and
supervisory oversight of the performance of the modification and retest.
The use of
the NCR as -the controlling document was improper.
No retest was performed on the system prior to declaring it operable.
The licensee
investigation identified that retest requirements are not addressed
adequately on NCRs,
The NCR was reviewed by the system engineer and his supervisor, the compliance
organization, and Quality Control prior to work being performed.
It was not
identified during the review and concurrence process that the more formal DCP
process should have been used for work that involved modification to a safety related
system.
Previous licensee calculations have shown that the Emergency Switchgear would have
continued to perform its safety functions for at least 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> without the ESRC
operable, and with the likelihood of continued operation of up to 100 days.
The actual safety significance of this event was minimized since the system was only slightly
below required flow rates for a short period of time.
Licensee analysis indicated the
emergency switchgear would have continued to operate for an extended period of time with
no cooling.
However, the extent to which levels of protection and procedural controls were
bypassed
to allow this event to occur indicated a significant weakness in management control.
and oversight.
The design change was not recognized
as a modification, and thus, was not reviewed in
detail.
As a result, a required post maintenance/modification
retest was not specified or
completed in accordance with AD-QA-482, Post Maintenance/Modification Test Program.
11
After orifice installation, the system was improperly declared operable on August 2, 1992 and
returned to service without the required retest.
Subsequent post-installation testing identified
that the flow rates were slightly below acceptable levels on August 18, 1992.
This is an apparent violation of AD-QA-482, Post Maintenance/Modification Test Program,
which requires that post maintenance/modification
testing be performed after maintenance or
modifications and prior to returning a safety system to an operable status.
This procedure
provides the controls and appropriate levels of review to ensure that adequate post
modification testing is performed.
(VIO 50-387/92-22-02)
Additionally, during performance of this modification, the licensee failed to perform the '-
required 10 CFR 50.59 evaluation for making changes to the facility as described in the
safety analysis report.
This is an apparent violation of 10 CFR 50.59 which requires that a
safety evaluation be performed whenever there is a change to plant design. (VIO 50-387/92-
22-03)
7.2.2
Improper Lubricant Used on Solenoid Operated Valves (SOV)
I
Circle Seal (a valve manufacturer who supplies several solenoid valves in use at the
Susquehanna
units) was contacted by the licensee on September 2 to discuss the use of
petroleum jelly as an 0-ring lubricant.
This initial contact arose out of the licensee's review
of NRC Generic Letter (GL) 91-15 which endorsed NUREG 1275, Operating Experience
Report Feedback- SOV Problems.
This GL identified the potential effects of using improper
lubricant (such as lubricants containing hydro-carbons) on certain materials used for 0-rings
in solenoid operated valves.
The licensee identified that petroleum jelly was being used as an 0-ring lubricant for
rebuilding certain safety-related SOVs.
On September 9, nonconformance report (NCR) 92-
204 identified that the vendor manual (IOM 239) for safety related Circle Seal SOVs required
the use of petroleum jelly as an 0-ring lubricant,
IOM 239 required that petroleum jelly be
used sparingly on 0-rings when assembling the Circle Seal SOV valve bodies (SV31S-9101-
3, -4).
Electric Power Research Institute (EPRI) report NP-7414 (Pgs. 56 and 57) identified that
petroleum based lubricants (hydrocarbon based materials) should not be used with certain 0-
ring materials because
they cause swelling, softness and deterioration.
This report
documented this degradation in 0-ring materials, such as, ethylene propylene elastomers
(EPR and EPDM).
The licensee determined that, as many as, twenty valves in Unit 1 and one valve in Unit 2
may have been rebuilt with petroleum jelly applied to the 0-rings.
Consequently,
the
licensee was required to perform an operability assessment.
12
In the preliminary operability assessment,
the licensee determined that there were no
identifiable consistent trends, nor any noticeable increase in the frequency of failures, to
indicate that the use of the petroleum jelly had any deleterious effect.
The lubricant was not
required to ensure proper functioning of the valves, but was to be used as an aid for
reassembly.
This lubricant was used to ensure that flexible components would not be
distorted during re-assembly,
and would be properly seated in their respective groove or
holding restraints and be unstressed
when in their fully assembled configuration.
Based on
this assessment,
the licensee concluded that the affected SOVs were operable,
The inspector
noted the low the failure frequency as a sufficient basis for the licensee's preliminary
assessment.
Thus, their preliminary operability evaluation was acceptable.
The licensee completed their final operability assessment
on September
15. All 21 affected
valves were reviewed.
The licensee conducted a search for all available information related
to SOV failures and degradations.
Eight LERs, 50 SOORs, 25 NCRs, and all SOV related
failure WAs were reviewed.
At the conclusion of this review the licensee confirmed that no
failures had occurred at Susquehanna
as a result of improper 0-ring lubrication.
For the
subject valves, no failures have been detected which were traceable to this cause.
Allbut one
of the SOVs had been rebuilt since March 1992.
The remaining valve (rebuilt in March
1984) was stroked quarterly and has operated successfully.
The licensee plans to replace all
affected valves within the next several months.
The last three valves to be replaced are inside
containment and serve only a test function for the wetwell to drywell vacuum breakers.
They
willbe replaced during the Fall 1993 outage.
Allaffected valves are expected to be replaced
by the end of the outage.
The inspector reviewed the licensee's actions and found them to be thorough and
comprehensive.
Their SOV replacement schedule appears consistent with each valves safety
significance.
The inspector had no further questions.
0
13
8.
SAFETY ASSESSMENT/QUALITYVERIFICATION
8.1
Licensee Event Reports (LER)
8.1.1
Licensee Event Reports.
The inspector reviewed LERs submitted to the NRC office to verify that details of the event
were clearly reported, including the accuracy of the description of the cause and the adequacy
of corrective action.
The inspector determined whether further information was required
from the licensee, whether generic implications were involved, and whether the event
warranted onsite followup. The following LER was reviewed:
gott i
92-013-00
Emergency Switchgear Room Cooling Inoperable - Could Prevent Fulfillment
of a safety function.
On August 18, 1992 with both units at full power, the
"A" Emergency Switchgear Room Cooling (ESRC) was declared inoperable
due to Low Cooling Water Flow.
Section 7.2 pertains.
9.
MANAGEMENTAND EXIT MEETINGS
9.1
Resident Exit and Periodic Meetings
The inspector discussed
the findings of this inspection with station management
throughout
and at the conclusion of the inspection period.
Based on NRC Region I review of this report
and discussions held with licensee representatives,
it was determined that this report does not
contain information subject to 10 CFR 2.790 restrictions.
9e2
Inspections Conducted By Region Based Inspectors
~Da e
~Sub'eet
9/21-9/25/92
Outage HP
~ln pettin
~Re
rt No
92-23
~Re ~rtin;
~ln pe~et r
J.'oggle
14
9.3
Management Meeting - Federal Field Exercise 3 (FFE-3)
On September
18, a Management Meeting was held between PP&L and the NRC to discuss
Federal Field Exercise 3 (FFE-3).
The licensee discussed their objectives, their
understanding of the overall Federal objectives and the NRC objectives for FFE-3.
also presented their expectations of the exercise.
Attachment 2 lists the meeting attendees.
Attachment 3 is a copy of the PP&L management
presentation.
ATTACHMENT 1
A
reviati n Li t
-A
- A
ANSI - A
'SME
- C
CFR
-C
CIG
- C
CREOAS
-D
DX
-D
ECCS -E
- E
-E
- E
ERT
- E
- E
ESW -E
EWR - E
-F
FSAR - F
ILRT - I
- I
JIO
- J
LCO
- L
LER
- L
LLRT - Loc
LOOP - Lo
MSIV - M
NCR -N
- N
NPE
- N
NPO -N
NQA - N
NRC
- N
-0
- 0
PC
-P
- P
PMR -P
dministrative Procedure
utomatic Depressurization
System
merican Nuclear Standards Institute
- American Society of Mechanical Engineers
ontainment Atmosphere Control
ode of Federal Regulations
ontainment Instrument Gas
- Control Rod Drive Mechanism
S - Control Room Emergency Outside AirSupply System
iesel Generator
irect Expansion
mergency Core Cooling System
ngineering Discrepancy Report
mergency Preparedness
lectrical Protection Assembly
vent Review Team
ngineered Safety Features
mergency Service Water
ngineering Work Request
uel Oil
inal Safety Analysis Report
- Heating, Ventilation, and Air Conditioning
ntegrated Leak Rate Test
nstrumentation and Control
ustifications for Interim Operation
imiting Condition for Operation
icensee Event Report
al Leak Rate Test
- Loss of Coolant Accident
ss of Offsite Power
ain Steam Isolation Valve
on Conformance Report
uclear Department Instruction
uclear Plant Engineering
uclear Plant Operator
uclear Quality Assurance
uclear Regulatory Commission
pen Item
ut-of-Service
rotective Clothing
rimary Containment Isolation System
lant Modification Request
,h
b
PORC - Plant Operations Review Committee
PSID
- Pounds Per Square Inch Differential
- Quality Assurance
- Reactor Building
RCIC - Reactor Core Isolation
Cooling'G
- Regulatory Guide
- Residual Heat Removal Service Water
SGTS - Standby Gas Treatment System
- Surveillance Procedure, Instrumentation and Control
- Surveillance Procedure,
Operations
SOOR - Significant Operating Occurrence Report
- Safety Parameter Display System
'PING
- Sample Particulate, Iodine, and Noble Gas
TS
- Technical Specifications
WA
- Work Authorization
1
FEE-3 MANAGEMENTMEETING
July 30, 1992
A%I'ACHMENT2
Nuclear Regulatory Commission (NRC)
Thomas T. Martin, Regional Administrator, Region I
Richard W. Cooper, Director, DRSS
Charles W. Hehl, Director, DRP
, Charles L. Miller, Director, PD1-2, NRR
G. Scott Barber, NRC, Senior Resident Inspector - SSES
David J. Mannai, NRC Resident Inspector - SSES
James J. Raleigh, NRC Project Manager
Brian J. M'Dermott, Reactor Engineer, DRP
Pennsylvania Power & Light Company (PP&L)
Harry W. Keiser,,Senior Vice President - Nuclear
Robert G. Byram, Vice President - Nuclear Operations
Frederick T. Eisenhuth, Senior Engineer, Nuclear Plant Management
ATTACHMENT 3
FFE-3
MEETING WITH
NRC REGIONAL ADMINISTRATOR .
FRIDAY, SEPTEMBER 18,
1992
KING OF PRUSSIA,
I.
INTRODUCTIONS
II.
FF'E-3
OBJECTIVES
III.
EXPECTATIONS
IV.
FFE-3 SPECIFIC
ITEMS
SUMMARY
HAROLD W. KEISER:
SENIOR VICE PRESIDENT - NUCLEAR
ROBERT G.
BYRAM:
VICE PRESIDENT - NUCLEAR
OPERATIONS
FREDERICK T.
EISENHUTH:
FFE-3
PROJECT
MANAGER
FFE-3
OBJECTIVES
A.
PP&L OVERALL OBJECTIVES
B.
FEDERAL OVERALL OBJECTIVES
C.
SPECIFIC
NRC
REGION I OBJECTIVES
D.
PUBLIC UNDERSTANDING AND CONFIDENCE
~
0
0
PP
L OVERALL OBJECTIVES
FOR FFE-
MONSTRATE
BLIC HEAL
FECTIVE
E
ABILITYTO
PROTECT
TH AND WELFARE THROUGH
MERGENCY RESPONSE
II.
INCREASE UNDERSTANDING OF
FEDERAL
ELEMENTS IN FULL-SCALE RESPONSE
III.
ENHANCE FEDERAL/STATE/LOCAL
RELATIONSHIPS
IV.
IMPROVE EMERGENCY .RESPONSE
V.
OVE
IDE
ARE
IMPR
CONF
PREP
PUBLIC KNOWLEDGE OF
AND
NCE IN EMERGENCY
'NESS
MEASURES
FEDERAL OVERALL OBJECTIVES
DEMONSTRATE THE ACTIVATION OF THE FRERP
INCLUDING THE
TRANSITION OF THE FEDERAL RESPONSE
FROM ONE STAGE
TO
ANOTHER.
2.
DEMONSTRATE THE FEDERAL ONSCENE
OPERATIONS
CENTER FUNCTIONS
SUCH AS INFORMATION COLLECTIONS
PROCESSZNGt
AND
DZSSEMINATION.
THE ONSCENE
OPERATIONS
CENTERS
WOULD INCLUDE
THE FEDERAL RADIOLOGICAL MONITORING ASSESSMENT
CENTER
(fRMAC) t
THE DISASTER FIELD OFFICE
(DFO) t
AND THE MEDIA
OPERATIONS
CENTER
(MOC).
DEMONSTRATE THE TIMELY AND ORDERLY
COLLOCATION OF THE FEDERAL RESPONSE
CENTERS
WHERE
APPROPRIATE.
3.
4.
DEMONSTRATE THE EFFECTIVENESS
OF THE INTERFACES
BETWEEN THE
FEDERAL AGENCIES'FFSZTE
AUTHORITIES (STATE AND LOCAL) AND
THE LZCENSEEg
OF COMMUNICATIONS
BETWEEN THESE
GROUPS.
DEMONSTRATE THE SUPPORT
OF
FEDERAL RESPONSE
EFFORTS
FOR
STATE AND LOCAL GOVERNMENTS.
5.
6.
DEMONSTRATE THE ADEQUACY OF
FEDERAL AGENCY PROCEDURES,
TRAINING, AND RESOURCES
IN ADDRESSING STATE AND LOCAL NEEDS.
DEMONSTRATE THE EFFECTIVENESS
OF KEEPING THE WHZTE HOUSE
AND
CONGRESS
INFORMED OF THE SITUATZON AND OF
FEDERAL ACTIONS
ZN
SUPPORT
OF THE STATE AND UTILITY ZN AN ONGOING EVENT.
7.
DOCUMENT THE ACCURACYt CONSISTENCY,
AND TIMELINESS OF THE
RELEASE Of PUBLIC INFORMATZON, AND THE COORDINATION OF
SUCH
INFORMATION AMONG THE FEDERAL AGENCIES'FFSITE
AUTHORITIES'ND
LICENSEE
BOTH AT THEIR ONSCENE
AND HEADQUARTERS
LOCATIONS.
8.
e'EMONSTRATE
THE ADEQUACY OF THE FEDERAL INTERAGENCY PLANS
AND PROCEDURES
fOR PERFORMING
FUNCTIONS AT FEDERAL ONSCENE
OPERATIONS
CENTERS.
THESE
FUNCTIONS INCLUDE:
ALERTING AND
UPDATING AGENCIES'ENERATING ZNZTZAL RESPONSE
DECISIONS'ND
TRACKING INITIAL RESPONSE
DECISIONS.
r
DEMONSTRATE AGENCY"DEVELOPED PLANS AND PROCEDURES
THAT
ADDRESS
THE ISSUES
OF
REENTRY,
RETURNS
RELOCATIONS
AND
RECOVERY PROBLEMS,
DEMONSTRATE THE FORMULATION OF VIABLE
SOLUTIONS.
S
10.
DEMONSTRATE THE ADEQUACY OF
PROCEDURES
GROUPS
AND THEIR ABILITYTO-COORDINATE RECOMMENDATIONS WITH
THE LEAD FEDERAL AGENCY ZN SUPPORT
OF
STATE AND LOCAL
DECISIONS.
11.
DEMONSTRATE THE ABILITY OF
THE AMERICAN NUCLEAR ZNSURERS
(ANZ) TO IMPLEMENT THE PRICE"ANDERSON
LEGZSLATZON BY
ADDRESSING FINANCIAL CONCERNS
ASSOCIATED WITH THE EVENT
RESPONSE.
12."
DEMONSTRATE THE REQUEST
AND APPROVAL PROCESS
OF A
PRESIDENTIAL DECLARATION OF
EMERGENCY UNDER THE STAFFORD
ACT.
13.
DEMONSTRATE RESPONSE
CAPABILITY IMPROVEMENTS WHICH RESULTED
FROM LESSONS 'LEARNED IN EARLIER EXERCISES
OR REAL-WORLD-
EVENTS.
SPECIFIC
NRC
REGION I OBJECTIVES
EFFORTS
TO ENSURE
PUBLIC UNDERSTANDI
G AND
0 FIDE
E
~
PUBLIC AFFAIRS WORK GROUP
~
PPLL PUBLIC INFORMATION PLAN
.
~
STATE PUBLIC INFORMATION EFFORTS
PPS L EXPECTATI N
~
PARTICIPATING FEDERAL AGENCY PERSONNEL
ARE FULLY TRAINED AND QUALIFIED FOR
RESPONSE
ROLES
I
~
JOINT FACILITY FUNCTIONS ARE FORMALIZED
AND WELL UNDERSTOOD
BY RESPONDING
PERSONNEL
~
OVERALL FFE-3
PREPARATIONS
MUST ENSURE
SUCCESS
NMENTS,
OCAL GOVER
~
INTERFACES WITH
STATE,
AND UTIL
MATCH PHILOSOPH
REQUIREMENTS
OF
ORGANIZATIONS I
L
ITY ARE TAILORED TO
IES,
STRUCTURES,
AND
THE PARTICULAR
NVOLVED
~
ALL PARTICIPANTS RECEIVE ORIENTATION IN
EXERCISE
PLAY AND OBJECTIVES
EFE-3 SPECIFIC
ITEMS
A.
ROLE
OF
NRC DIRECTOR OF SITE OPERATIONS
B.
SITE
TEAM PARTICIPATION IN PPRL
PRACTICE DRILLS .
DECEMBER
,
1992
JANUARY 26,
1993
C.
ONSITE SCENARIO
~
PPLL WORKING WITH NRC
CONTRACTOR
~
FULL ONSITE
PLAY DAY 1
~
CONTROL CELL DAYS 2,3,4
D.
RECOVERY PHASE
EXPECTATIONS
~
FOCUS
OF PLAY AT DFO AND FRMAC
~
LEVEL OF
FEDERAL PLANNING
E.
FEMA INTERFACE
F.
DOE INTERFACE
lt
FFE-3 SPECIFIC
ITEMS
CONT.
G.
NRC CHAIRMAN/COMMISSIONER INVOLVEMENT
~
.
TABLETOP
~
ACTUAL EXERCISE
H.
FFE-3
CONTROL SYSTEM
I.
POST
EXERCISE
REVIEW
SUMMARY
i
~
A SUCCESSFUL
DEMONSTRATION OF
EMERGENCY
RESPONSE
CAPABILITIES IS ESSENTIAL
~
IMPROVED PLANS AND PROCEDURES
IS AN
EXPECTED BENEFIT
AND ENHANCED
~
RELATIONS WITH PUBLIC MUST BE PRESERVED
~
ALL PARTICIPATING ORGANIZATIONS MUST
WORK TO
ENSURE
SUCCESS