ML17157B881
| ML17157B881 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 06/03/1992 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17157B882 | List: |
| References | |
| 50-387-90-99, 50-388-90-99, NUDOCS 9207070028 | |
| Download: ML17157B881 (27) | |
See also: IR 05000387/1990099
Text
ENCLOSURE
INITIALSALP REPORT
U. S. NUCLEAR REGULATORY COMMISSION
REGION I
=
. INITIALSYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
REPORT NOS. 50-387/90-99; 50-388/90-99
1
r
PENNSYLVANIAPOWER &LIGHT COMPANY
SUSQUEHANNA STEAM ELECTRIC STATION
UNITS 1 AND 2
ASSESSMENT PERIOD:
December
1, 1990 - April 18, 1992
BOARD MEETING DATE: June 3, 1992
9207070028
92070i
ADOCK 05000387
TABLE
F
I.
INTRODUCTION
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SUh&iARYOF RESULTS..............
II.A
Overview
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II.B
Facility Performance Analysis Summary ..
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PERFORMANCE ANALYSIS.........
III.A Plant Operations
III.B Radiological Controls ..........
III.C Maintenance/Surveillance........
III.D Emergency Preparedness
III.E
Security and Safeguards.........
III.F
Engineering/Technical Support
III.G
Safety Assessment/Quality Verification
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IV.
SUPPORTING DATAAND SUMMARY .....
IV.A Licensee Activities...... ~........
IV.B NRC Inspection and Review Activities...
IV.C
Reactor Scrams and Unplanned Shutdowns
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Attachment
1 - SALP Criteria
I.
INTRODVCTION
The Systematic Assessment of Licensee Performance (SALP) is an integrated NRC staff
effort to collect observations,
data and to periodically evaluate licensee performance on the
basis of this information.
The SALP process is supplemental to normal regulatory processes
used to ensure compliance with NRC rules and regulations.
SALP is intended to be
sufficiently diagnostic to provide a rational basis for allocating NRC resources
and to provide
meaningful feedback to the licensee's
management to improve the quality and safety of plant
operations.
An NRC SALP Board, composed of the staff members listed below, met on June 3, 1992 to
review the collection of performance observations and data, and to assess
the licensee's
performance at the Susquehanna
Steam Electric Station.
This assessment
was conducted in
accordance with the guidance in NRC Manual Chapter 0516, ",Systematic Assessment of
Licensee Performance".
The SALP Board for the Susquehanna
Steam Electric Station assessment
consisted of the
following individuals:
Chairman
Charles W. Hehl, Director, Division of Reactor Projects (DRP)
Members
W. Hodges, Director, Division of Reactor Safety (DRS)
J. Durr, (Acting) Deputy Director, Division of Radiation Safety & Safeguards
(DRSS)
C. Miller, Director, Projects Directorate I-2, NRR
J. White, Chief, Reactor Projects Section 2A
G. Barber, Senior Resident Inspector, Susquehanna
J. Raleigh, Licensing Project Manager, NRR
Other Attendees
E. Wenzinger, Chief, Projects Branch No. 2, DRP
D. Mannai, Resident Inspector, Susquehanna
P. Eapen, Chief, Special Test Programs Section, DRS
W. Pasciak, Chief, Facilities Radiation Protection Section, DRSS
R. Keimig, Chief, Safeguards
Section, DRSS
J. Kottan, Laboratory Specialist, DRSS
J. Noggle, Radiation Specialist, DRSS
C. Gordon,
Sr. Emer Prep Specialist, DRSS
R. Albert, Physical Security Inspector, DRSS
H.
SUMMARYOF RESULTS
II.A
Overview
Overall, both units were operated with a demonstrated high regard for nuclear safety.
The
licensee undertook many initiatives aimed at improving safety.
The new programs were
implemented with good initial results.
Many internal and external assessments
were executed
in a thorough and complete manner.
Both units operated well with high reliability.
Licensee managers,
supervisors,
and workers communicated well among themselves,
and with
the NRC, as issues arose.
The licensee used press releases prudently to keep the media
informed of plant events and public interest items.
Frequent management
meetings between
the licensee and the NRC were viewed as a positive licensee initiative. Licensee
communications were considered a significant strength.
Operations performance remained strong.
Effective management involvement was evident in
day-to-day operations.
Operator staffing, morale, and professionalism were outstanding.
There were few personnel errors'and operators maximized the availability of safety system
equipment.
Procedure use was excellent.
Some weaknesses
were noted in operator skills in
maintaining reactor level and pressure following the Unit '1 scram that resulted in main steam
isolation valve closure.
Similar performance weaknesses
were also noted following a Unit 2
scram and during a requalification program review.
The eventual corrective actions
implemented for these weaknesses
were comprehensive;
however, the tardy response to this
problem contributed to the assignment of a declining trend to this area.
The radiological controls program was effectively administered.
While some deficiencies
existed, the licensee continues to accrue low annual exposures.
Radiological concerns were
identified in ensuring adequate postings and instructions to workers in the drywell, and
effective use of Radiation Work Permits and temporary shielding.
Effluent and
environmental monitoring, transportation and radwaste programs were very effective.
Overall, performance in this area was good.
Strong performance continued in maintenance/surveillance,
security,
and engineering/technical
support areas.
Excellent performance was noted in the Safety Assessment/Quality Verification area.
All
levels of management
were conservatively focused on safe operations and outages.
Deficiency management
was exemplary.
The licensee's extremely effective closeout of
deficiencies resulted in establishing a low backlog of outstanding nonconformances,
engineering discrepancies
and event resolutions.
Improvements were seen in the licensee's
identification and reporting of these deficiencies.
However, concern still exists regarding the
licensee's ability to plan and implement timely corrective actions for some recurring
.problems.
Overall, the licensee emphasized
safety and quality in their conduct of nuclear
activities.
H.B
Facility Performance Analysis Sunnnary
Functional
Area
Rating, Trend
Last Period
Rating, Trend
This Period
Plant Operations
Radiological Controls
Maintenance/Surveillance
Security and Safeguards
1, declining
Engineering/Technical
Support
Safety Assessment/
Quality Verification
Previous Assessment
Period:
Present Assessment
Period:
August 1, 1989 to November 30, 1990
December
1, 1990 to April 18, 1992
III.
PERFORlNANCE ANALYSIS
HI.A Plant Operations
4
The previous SALP rated licensee performance in operations as Category 1. That assessment
concluded that licensee management continued to emphasize
safe and effective operations.
Operator training programs were very good and operational problems were resolved in a
prompt, effective manner.
Operations was a significant licensee strength.
Overall, operations performance continued to be strong during the current period.
Unit
availability and capacity factors reached record setting levels.
Operators were attentive to
their duties and effectively controlled planned evolutions.
Procedures were effectively used.
Corporate management provided effective oversight and was heavily involved in operational
decision making.
Operator morale was excellent.
Twelve hour shift rotations continued during the current assessment
period.
This shift
schedule has significantly reduced the need for unplanned overtime.
As evidenced by
minimal personnel errors, the switch to 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts has not adversely affected operator
performance.
Shift turnover was conducted promptly and efficiently. Operators
communicated well and system status was kept up-to-date.
Operator staffing was excellent.
Allcontrol room activities, including access control, were performed in a professional
manner.
The day-to-day performance of control room personnel was excellent.
Safety system availability received significant management attention.
Operations and plant
scheduling ensured that work planning efforts minimized emergency core cooling system
(ECCS) out-of-service time during maintenance periods.
The licensee successfully
maximized safety system availability.
There was one scram on Unit 1 and two scrams on Unit 2 during the SALP period (see
Section IV.D). None of the scrams was attributable to operator error. Operator performance
during all three scrams was sufficient to maintain the safety of the plant.
Emergency
Operating Procedures were used in all cases to bring the plant to a safe, stable state.
Some
weaknesses
were noted in operator skills needed to control reactor level and pressure during
two of the three scrams.
On January
18, 1992, a worker was mildly burned and contaminated to low levels when he
began grinding on an open-ended pipe that normally supplies the common unit offgas
hydrogen recombiner.
A leaky valve allowed the slow buildup of hydrogen which ignited
when grinding began.
The licensee's failure to recognize high offgas pressure alarms as a
symptom of an earlier hydrogen ignition, and the premature closeout of a work authorization
package which resulted in incomplete repair to a leaking maintenance boundary valve were
causal factors to this event.
The event also indicated that the licensee's implementation of
corrective actions from their early industry experience review program was not effective,
their response to the situation was extremely prompt and effective. A sixteen person team
was on-site within four hours of the initial event.
This Event Review Team (ERT) promptly
identified root causes,
causal factors, and proposed comprehensive corrective actions.
The
actions were completed in a timely manner and effectively addressed
the earlier deficiencies
which contributed to this situation.
In general, operator performance on. license examinations was very good.
Two NRC
requalifiication examinations and one initial examination involving 37 individuals were given
in the assessment
period.
The pass rate on the initial examination and the first set of
requalifiication examinations was 100%.
The pass rate on the second set of requalification
examinations was only 75%, and one of three crews did not demonstrate satisfactory
performance.
During these examinations,
weaknesses
were also observed in the
operators'bility
to manually control reactor pressure vessel (RPV) level and pressure.
These
weaknesses
were similar to those observed during the first set of requalification examinations
and during 2 of the 3 actual scrams.
Although the licensee has scheduled additional simulator
training in 1992 to improve this skills weakness,
the slowness in addressing this issue was of
concern to the NRC.
The licensed operator requalification program was determined to be satisfactory for both
requalifiication program evaluations.
However, a programmatic weakness was identified in
the evaluation techniques
used by the facility training staff during dynamic simulator
evaluations for the second program evaluation.
Once the licensee fully understood the
weaknesses,
a strong corrective action plan was developed and implemented.
The licensee did a thorough, comprehensive job during this period in resolving numerous
discrepancies identified by the NRC in an inspection (in the previous period) of the
Emergency Operating Procedures
(EOPs).
The EOP program controls are now effective for
developing and maintaining procedures of high quality.
The process for tracking EOP open
items was well organized and has ensured that identified problems were resolved.
In general,
the EOPs were found to be technically adequate,
though some deviations from the BWR
Owners Group Emergency Procedure Guidelines and the licensee's methodology for
determining area radiation action levels remain to be reviewed by the NRC.
/
The site fire protection program, including procedures and training, was maintained in
accordance with industry standards.
Fire protection equipment was in good operating
condition and combustible materials were identified and stored properly.
The licensee has
made excellent progress resolving previous concerns with fire barrier penetration seals.
The
licensee's corrective actions have fully addressed
these concertos and demonstrated
a strong
commitment to effective fire barrier penetration sealing.
In fact, the average number of fire
zones requiring hourly fire watches in 1990 has decreased
from about 190 per month to about
40 per month.
The average number of these fire zones remained low at about 42 per month
in 1991 and has dropped to about 26 per month, thus far, in 1992.
The reduction in affected
fire zones reflected excellent progress toward recovering from previous weaknesses
in the fire
protection program.
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Plant housekeeping
was excellent.
Plant spaces were well kept.
Debris and unnecessary
clutter were not allowed to accumulate.
The licensee implemented a new administrative
procedure to improve control of transient tools and equipment.'he program described by
the procedure was very thorou'gh and detailed.
Spot checks during initial implementation
. indicated some compliance problems.
However, increased management attention has resulted
in significantly better and more consistent implementation of the procedure, resulting in
significantly better control of transient tools and equipment.
The plant painting and labeling program was a continuing success.
The licensee has
dedicated significant resources to both programs.
Painting and labeling of both unit's turbine
decks are complete and have improved the aesthetic appearance.
Similarly,
based on
discussions with plant personnel, attitudes have been positively influenced by the upgraded
appearance of the Unit'1 Radiological Control Access (RCA) point.
In summary, the licensee continues to operate both Susquehanna
units with an outstanding
regard for operational safety.
Management involvement continued to be strongly evident in
day to day operations.
Operational problems were conservatively resolved.
The operator
requalification program was generally strong, though some weaknesses
were noted.
Operator
control of reactor pressure and level during scrams reflected some inexperience with these
types of events.
Skills training is underway to improve operator responses.
Operator
staffing, morale and professionalism were outstanding.
Overall, strong, conservative plant
operations was a licensee strength.
Performance Rating:
,Board Comment:
1, Declining
An early requalification program evaluation and 2 of 3
scrams showed weaknesses
in operator skills for post
scram reactor level and pressure control. This
performance issue was the basis for the assignment of a
declining trend in this area. The additional training to
cope with this weakness while adequate,
was not
conducted in a timely manner.
III.B Radiological Controls
The radiological controls program was assessed
as Category 2.during the previous SALP
period.
Strengths included the development of various inter-departmental interface positions,
the separation of the chemistry function from the radiation protection group, and strong
management
response to radiological events.
The internal and external exposure controls
programs, including ALARAefforts, were of good quality and effectively implemented.
The
effluent monitoring and control program was effective.
Weaknesses
were noted in
management control of contractors that led to an unplanned exposure and in the sampling
methods used to classify radioactive waste.
Radiation Protection
In the current SALP period, a well-defined and staffed radiation protection (RP) organization
was maintained.
Management effectiveness of this organization was enhanced by transferring
radioactive waste (radwaste) functions to a newly formed Effluents Management Section.
The RP organization was effectively augmented during the outages with properly trained and
qualified contracted personnel.
The licensee maintained sufficient supervisory attention to
contracted personnel during these periods.
The radiation protection organization staffing level
remained stable.
Emergency radiological response'to
the victim of a hydrogen burn in a
contaminated area was prompt and effective, and demonstrated
effective contingency
planning.
The licensee continued to accrue low annual exposures through an effective
ALARAprogram.
The licensee's overall training and qualification program for radiation
protection personnel and radiation workers was found to be of good quality.
Notwithstanding the above, in some cases,
the application of radiological controls in the work
place was deficient despite the existence of excellent procedures
and a well defined program.
For example, during the Unit 1 outage, several radiological postings in the drywell were
found devoid of radiation information and several workers demonstrated insufficient
knowledge of the actual radiological conditions in the area.
Such lack of knowledge was
largely attributable to lack of sufficient radiological information provided to workers.
Also,
although Radiation Work Permits (RWPs) were well written, they did not always adequately
convey information to the worker.
Further, the temporary shielding program, while well-
established and supported with sufficient resources,
lacked criteria and guidance to assure the
effective use and optimization of temporary shielding.
Consequently,
shielding of many
sources in the drywell was found to be insufficient to assure that personnel exposures were
maintained As Low As Reasonably Achievable.
Additionally, management
has not yet resolved a long-standing potential airborne
contamination concern as a result of positive containment pressure causing air flow out of the
drywell during maintenance periods.
Several strengths were identified in the radiological control program implementation in the
workplace.
For example, the licensee has implemented good external and internal exposure
control programs.
Personnel exposure data are tabulated, evaluated,
and published at least
daily, providing good controls over accumulation of personnel exposure.
Overall monitoring
of airborne radioactivity was good.
Radiation protection personnel training, qualification,
and ability to use radiation detection instruments appeared very good.
Audits of the radiation protection program continued to be of good quality.
Various audit
perspectives
were obtained from such diverse groups as the corporate radiation protection
group, the station quality control department,
and outside industry experts.
The audits were
performance-based
and reflected good management involvement with the radiation protection
program.
A high degree of corporate and station management involvement in ALARAgoals was
"
evident.
The ALARAgroup was involved early in station outage planning activities and had
complete access to all scheduled work packages.
Emergent work received appropriate
ALARAreviews.
Exposure goals were developed for individual departments
and jobs, and
were considered challenging and'easonable.
The recurring repair of reactor water clean-up
(RWCU) pump seals in both units has accounted for a large percentage of the maintenance
personnel exposure for the last two years.
Due to ALARAconsiderations, in part, the pumps
are scheduled to be replaced with seal-less pumps in 1992.
While some deficiencies existed,
as previously discussed,
the licensee continues to accrue low annual exposures.
Effluent Monitoring and Control and Environmental Monitoring
The licensee continues to implement a very effective radioactive liquid and gaseous effluent
controls program.
The air cleaning systems were tested and well maintained.
Excellent
calibration techniques were implemented for the gaseous
and liquid effluent radiation
monitors.
The radiological environmental monitoring program (REMP) was effectively implemented.
The instrumentation and equipment of the meteorological monitoring program were operable,
calibrated and well maintained. The licensee implemented an effective QA/QC program to
assure the quality of the REMP sample analysis.
An NRC review of the licensee's
Personnel Dosimetry Processing
revealed a strong
commitment to quality.
The licensee demonstrated
a good understanding of the technical
issues regarding thermoluminescent dosimeter (TLD) quality assurance/quality
control, TLD
calibrations, and methods for dose assessment.
Quality Assurance (QA) audits were thorough and of good technical depth and assessed
the
programmatic performance of all three programs.
Procedures
were detailed and well written
to effectively implement these programs.
The licensee implemented an effective program for
measuring radioactivity concentrations in process and effluent samples.
Transportation and Solid Radwaste
NRC review of QA audits.and surveillances of the solid radioactive waste and transportation
program found them to be of excellent scope and technical depth.
The quality assurance
program in the solid radwaste and transportation area was good with only isolated indications
of weaknesses
that were promptly resolved.
For example, initial QA involvement with the
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spent fuel pool clean-out project was marginal,
However, following NRC identification, QA
participation improved to an acceptable level during the project.
Another problem involved
the station practice of releasing waste oil based on effluent Lower Limitof Detection (LLD)
versus environmental LLD levels.
The licensee promptly stopped this practice following
NRC identification, and revised their procedures accordingly.
The staffing and training in the newly organized Effluents Management Section were
considered excellent.
Management response to industry issues was good.
For example, as a
result of a vendor communication, the licensee determined that'a certain resin (Marlex
CL200K) used to manufacture high integrity containers (HICs) was substandard.
In response
to this concern, a nonconformance report was generated,
and the licensee successfully
identified and dispositioned
10 HICs made from this resin.
The licensee's review of this
concern was complete, thorough, and comprehensive.
Overall this functional area appeared
to be managed very well.
Summary
Formal audits of the radiological controls area were of excellent quality.
Radiological
controls were strong relative to internal and external exposure tracking and control programs,
and supervisory oversight and staffing.
However, the implementation of the program in the
drywell during outages exhibited weaknesses
relative to radiological control postings,
effectiveness of RWP's, and resolution of a problem involving positive containment pressure.
The effluent monitoring and control, environmental monitoring, transportation and radwaste
programs were well implemented and maintained.
Response to an event involving a
potentially contaminated burn victim was very effective.
The licensee's overall training
program for permanent and contractor radiation protection personnel was well done.
Performance Rating:
Board Comment:
None
III.C Maintenance/Surveillance
During the previous SALP, the Maintenance/Surveillance
functional area was rated Category
1.
The maintenance and surveillance programs were scheduled,
planned, and implemented in
an effective manner.
A strong management commitment to both programs was evident.
Personnel errors and procedural deficiencies in the maintenance area were minor weaknesses.
Surveillance activities were generally performed well.
During the current period, the maintenance program continued to be effectively implemented.
Management involvement with plant maintenance activities was excellent throughout the
period.
Management was involved daily to schedule, coordinate and adjust work activities
for planned and corrective maintenance.
I&CForemen provided increased supervisory
oversight of field activities, spending approximately fiftypercent of their time in the field.
Electrical and mechanical maintenance foremen also spent increased time in the field. The
licensee has corrected the majority of the previously identified weaknesses
and deficiencies in
10
their maintenance'program.
However, some minor deficiencies still exist in the maintenance
procedures,
and the self-assessment
processes for mechanical and electrical maintenance are
not well established.
The maintenance staff was well trained and the turnover rate was low. The training program
was effective and qualification elements were well defined.
The level of experience of
maintenance personnel was high.
This strength contributed significantly to the maintenance
program as evidenced by relatively few performance errors.
Maintenance program performance was very effective as evidenced by high capacity factors
and excellent individual system availability being maintained throughout the period.
However, some weaknesses
were noted.
Control of maintenance activities on the off-gas
recombiner was weak.
Premature closeout of a previous work authorization package to repair
.
a leaking boundary valve and maintenance work documents not containing adequate
instructions relative to purging and monitoring for hydrogen were primary contributors to the
hydrogen recombiner event.
Additionally, early in the period, an unplanned ESF actuation
occurred during the performance of a maintenance activity due to personnel error.
Specifically, a Loss of Shutdown Cooling occurred during replacement of a pressure switch in
the Residual Heat Removal (RHR) pressure permissive circuitry. The cause of the event was
due to an I&Cwork planner not referencing proper electrical drawings when developing the
instructions for pressure switch replacement.
Notwithstanding these isolated deficiencies, the
overall performance of maintenance
was excellent.
During the assessment
period, a Unit 2 refueling outage was completed and a Unit 1
refueling outage was in progress at the end of the period.
Station maintenance and outage
organizations performed well in scheduling, coordinating, and accomplishing work.
Overall,
plant and system performance following the Unit 2 outage was good.
The licensee
aggressively pursued and resolved two unusual problems during the Unit 2 refueling outage.
Unidentified material was found in the reactor vessel and excessive leakage from a control
rod drive occurred during mechanism changeout.
Both problems were handled in a planned
and systematic manner and successfully resolved.
I
Several maintenance program initiatives matured during the assessment
period.
The licensee
continued tracking equipment availability and performance history to trend and assess
maintenance effectiveness.
Maintenance was prioritized according to probabilistic risk
- assessment
and reliability. The maintenance organization interacted well with operations in
the planning, scheduling, authorization and performance of maintenance activities.
The
licensee increased efforts in the use of predictive maintenance.
A supervisor, assistant
foreman, and several mechanics were assigned full time to this area.
The predictive
maintenance program was effective as demonstrated by the identification of combustible gas
in the Unit 2 "C" phase main transformer oil and bearing problems with two Unit 1 turbine.
building fans prior to component failure. The licensee's initiative in the use of predictive
maintenance
was considered
a strength.
11
The surveillance program was effective and well-managed as evidenced by no inadvertent
automatic scrams and few errors.
Scheduling and coordination were strengths of the
program.
Effective interaction with operations during performance of surveillance activities
was a significant contributor to program success.
During the assessment
period, there were no automatic scrams attributable to surveillance
activities.
Surveillance program performance was highly effective.
However, some
personnel errors and procedural deficiencies were identified. For example, an unplanned
reactor water cleanup isolation occurred due to personnel communication error when a
thermocouple calibrator was connected to the wrong test block.
Procedural deficiencies
affecting both units included:
(1) failure to include 18 manual containment isolation valves
associated with each unit in the monthly containment integrity surveillance inspection
procedures;
and, (2) failure to include a required 10 millisecond (msec) trip sensor response
time in the applicable surveillance inspection procedures relative to Turbine Stop Valve
(TSV) and Main Steam Isolation Valve (MSIV) response time verification,
These licensee
'dentified
deficiencies were promptly corrected.
Notwithstanding isolated deficiencies, the
overall conduct of the surveillance program was excellent.
The in-service inspection (ISI) program was effectively implemented.
Personnel responsible
for performing nondestructive examinations in the plant were properly qualified.
In-service
test (IST) results were well organized, trended, and thoroughly reviewed; however, the
licensee did not include check valves in the containment instrument gas (CIG) system in the
IST program as required.
The program for testing and surveillance of motor-operated valves
(MOVs) was thorough, well managed,
and on schedule.
Summary
In summary, the Susquehanna
maintenance and surveillance programs continued to be a
licensee strength. Some isolated minor weaknesses
were noted in both programs involving
personnel errors and procedural deficiencies.
Management was effectively involved and
strongly committed to the maintenance and surveillance programs.
Overall, performance was
outstanding.
Performance Rating:
Board Comment:
None
12
Analysis
During the last SALP period, this area improved to a Category
1 rating.
Strengths included
effective response to an Alert caused by a loss of shutdown cooling, development of Position
Specific Procedures
(PSPs), effective use of PSPs during the annual exercise, excellent
Emergency Response Facility (ERF) readiness,
ample and stable staffing, and effective
training.
Slow Media Operations Center (MOC) information dissemination was noted as a
weakness.
During the current SALP period, one Unusual Event occurred. It involved a localized
hydrogen ignition in the offgas hydrogen recombiner system and the consequent transport of a
contaminated, injured individual off-site. Timely and effective licensee response
was evident
in prompt evaluation and declaration of the Unusual Event.
MOC activation was notably
prompt.
Accurate and complete information was provided to the state, local officials, and the
public.
During the October 16, 1991, annual emergency exercise, the licensee demonstrated
excellent
on-site analysis and response capability, provided timely classifications and notifications,
appropriately prioritized tasks, exhibited a strong emphasis on personnel safety, established
effective communications between ERFs, provided excellent and frequent media briefings,
effectively tracked the progress of in-plant repair teams, developed Protective Action-
Recommendations
(PARs), and effectively interfaced with the Commonwealth of
and Luzerne and Columbia counties.
The February 19, 1992 annual emergency exercise was characterized by excellent on-site
event analysis and response,
timely notifications, and appropriately determined PARs.
Overall; the licensee demonstrated effective performance.
However, for much of the
exercise, interim Emergency Operations Facility (EOF) management
was in charge, of the off-
site response.
Because of the consequent additional workload, the Interim Recovery Manager
was overloaded.
It was not until the corporate based Recovery Manager assumed
his position
(about three hours into the exercise) that sufficient staffing was available to effectively
manage the activities in the EOF.
The licensee has undertaken a study to determine the best
long-term means of resolving this staffing issue.
Subsequent to the end of this SALP period,
the licensee developed an interim corrective action plan of training site managers
as Recovery
Managers.
That plan was temporarily interrupted in order to pursue other possible interim
and long-term corrective actions,
However, training of TSC Emergency Directors on EOF
related response activities was completed.
The interim action plan willbe implemented upon
additional training and procedural revisions and is scheduled for completion in September,
1992.
13
NRC review noted that the October 1991 exercise scenario was challenging and provided a
good environment for self-assessment.
NRC review also noted that the February 1992-
exercise scenario was carefully tailored by the licensee to challenge the Emergency'Response
Organization (ERO) in aspects not clearly demonstrated during previous exercises and
program reviews, and that this self-challenging aspect was instrumental in revealing whether
suspect areas were problems.
Such critical self-examination'y the licensee was considered a
major strength.
Administration of the drill and exercise program was excellent.
Six station drills were
conducted in 1991 in addition to other, smaller scale drills required by the emergency plan.
Rotation of players for drills and exercises was notable.
Though ERO members -were
required to participate in drills and exercises at least once every four years to maintain
certification, the licensee established
a goal of ERO member participation once every two
years.
During this period, that goal was met by key ERO members.
Station and corporate management effectively maintained emergency response qualifications,
reviewed and approved the emergency plan and procedure changes,
participated in drills and
exercises,
and interfaced with state and local agencies.
EP training quality was excellent.
AllERO positions had sufficient numbers (3 to 5) of
trained and qualified personnel.
Classroom training was conducted throughout the year and
was well-defined.
Lesson plans were properly controlled, accurate and well detailed.
An
initiative to change from classroom-based
to performance-based
training was in progress.
Performance during the emergency exercises demonstrated
that emergency response facilities,
equipment, and supplies were very well maintained.
Emergency response procedures were
generally well-maintained, but there were weaknesses
in PSP provisions for turn-over of
functions from the Technical Support Center (TSC) to the EOF.
Administrative procedures
were well-stated.
The licensee's
1991 audit was appropriate in scope and content, and combined the Technical
Specification audit with the 10 CFR 50.54 (t) review.
Off-site interface results were
provided to state and county officials. Audit reports received wide management distribution.
To provide better visibilityand tracking of EP items, Nuclear Emergency Planning (NEP)
was in the process of transitioning to the station commitment tracking system.
NRC review
concluded that this transition was a good initiative.
EP program administration was effective.
The EP program was effectively administered by
the Supervisor, Nuclear Emergency Planning.
EP staffing was stable and had a good
discipline mix. The licensee met regularly with state and local officials to assure
coordination of emergency preparedness
activities.
14
Su~mary
In summary, the licensee has implemented an effective EP program.
Management was
effectively involved.
Response to actual events was appropriate and timely. The quality of
the drill and exercise program, the audits and reviews, and the depth of the ERO were
considered strengths.
A need for more timely full staffing of the EOF was evident, as was a
need for more specific provisions for turn-over of functions from the TSC to the EOF.
Performance Rating:
Board Comment:
None
III.E Security and Safeguards
, During the previous assessment
period the licensee's performance was rated as Category
1.
That rating was based on implementation of a highly effective and performance-oriented
security program.
Management attention and support were evident in all aspects of the
program.
Resources
were allocated to ensure necessary program upgrades and staffing, an
aggressive audit program, and an effective training program.
During this, period, the licensee continued to sustain a superior level of performance.
Upgrades and enhancements
to security systems and equipment were continued and included
the installation of state-of-the-art intrusion detection equipment on portions of the protected
area perimeter and new security computer software to provide more rapid and varied data
processing,
diagnostics and programming ease.
The upgrade of the perimeter intrusion
detection system is an ongoing project and is scheduled to be completed during the next
assessment
period.
The expenditure of resources for these capital improvements was
indicative of management's
continuing commitment to maintain an effective security program.
The security staff maintained effective communications with other station departments
and
met daily with maintenance to review security maintenance requirements and to discuss
potential interface problems.
The licensee continued effective implementation of the Fitness
for Duty (FFD) Program.
The station-supplied corrective and preventive maintenance
support for security equipment was very aggressive and resulted in excellent on-line
availability for security equipment, thus reducing the need for compensatory
measures
and
attendant overtime.
This support further reflected management's
commitment to an effective
prograIll.
Security supervisors were well trained.
These qualified security professionals closely
monitored the program and ensured that it was carried out effectively and in compliance with
NRC regulations,
as evidenced by an excellent enforcement history.
The supervisory staff
was actively supported by a very knowledgeable and effective corporate staff in making
program plan changes,
self-assessment,
upgrades,
and enhancements.
Corporate and station
15
security personnel continued to actively participate in groups engaged in nuclear plant security
matters and also maintained excellent rapport and liaison with Commonwealth and local law
enforcement agencies.
Security force staffing was consistent with program needs as
evidenced by the minimal use of overtime.
The security officers demonstrated
a very
professional demeanor and a thorough and comprehensive knowledge of their duties, the
station and its systems.
This resulted in a very positive attitude toward the program by other
station staff.
The turnover rate in the security force remained very low. The continuing-
strong demonstration of these attributes reflected the licensee's resolve to implement an
effective and high quality program.
The training and requalifiication program was well developed and administered by full time,-
highly qualified instructors.
Lesson plans were kept current and accurately reflected the
commitments in the licensee's program plans.
Facilities were provided within the owner-
controlled area for personnel training and firearms requalifiication.
They were well-equipped,
well-maintained, and made good use of instructional aids.
The training program was very
effective as evidenced by a minimum number of personnel errors.
Excellent technical
training continued, as well as training in non-security related areas such as supervisory skills
and station systems.
The training program contributed-very positively to the overall success
of the security program.
Audits of the security program conducted by the licensee's Quality Assurance Group were
found to be comprehensive
and thorough.
Findings from audits and surveillances were
directed toward improving the effectiveness of the program as opposed to being compliance-
oriented.
Corrective actions were prompt and thorough with aggressive follow-up to ensure
implementation.
The aggressive audit and surveillance program further enhanced
the quality
of the security program.
The licensee's event reporting procedures were clear, consistent with the NRC's reporting
requirements,
and well understood by the supervisory staff.
There was one event requiring a
prompt report during the period. It involved a computer failure.
Corrective actions were
prompt and appropriate.
Loggable events were appropriately tracked and, where required,
corrective action was initiated to preclude adverse trends.
The licensee submitted four security program plan changes during this period.
The revisions
were technically sound and demonstrated
a thorough knowledge and understanding of NRC
requirements
and security objectives, not only by station staff but also by corporate staff who
are responsible for this activity.
16,
Summary
In summary, the licensee continued to maintain a very effective, high quality and
performance-oriented
program.
Management attention and support were clearly evident in all
aspects of the program implementation and resources were appropriately allocated to continue
system and equipment upgrades.
In addition, a well-trained, professional staff was retained
and performance-based
audits and self-assessments
were conducted to monitor program
implementation.
These efforts reflected the licensee's commitment to a high quality and
effective security program.
Performance Rating:
Board Comments:
None
III.F Engineering/Technical Support
In the previous SALP report, Engineering and Technical Support was rated as Category 2.
Sound technical resolution of safety significant issues, plant support, an aggressive self
assessment
program in the electrical distribution area, an effective modification process,
and a
highly qualified staff were noted as positive attributes.
However, the SALP noted
weaknesses
in addressing
causal factors and the implementation of timely corrective actions
for recurring electrical bus trips due to poor design of electrical insulators, emergency diesel
generator crankcase overpressurizations,
and reactor water cleanup system pump seal failures.
The timeliness of dispositioning of engineering discrepancies
was also cited as a weakness.
During the period, the engineering and technical support organizations were reorganized to
address
these weaknesses
and to provide better support to the plant. At the end of the period,
the licensee was making good progress in resolving outstanding engineering discrepancies.
During the current SALP period, the engineering organization underwent an additional
organizational change.
As a consequence of the Organizational Effectiveness Review (OER),
the licensee re-aligned the classical engineering disciplines into Modifications, Technology,
Fuels, and Systems Engineering to provide increased focus and a unified approach for
engineering support.
Systems Engineering now reports to the engineering manager instead of
the plant superintendent.
The Modifications and Nuclear Technology organizations were
formed to recognize the diversity of roles that each performs.
Modifications focuses on the
development of design changes, while Nuclear Technology works to resolve long-term plant
and system problems.
The new organization was implemented in November 1991 and was
viewed as a positive licensee initiative. However, because of long lead times of many
engineering issues,
the effectiveness of the new organization has yet to be fully demonstrated.
17
During this period, the licensee's efforts to provide timely closeout of plant deficiencies
continued to be a high priority for the engineering organization.
The licensee's deficiency
management
strategy effectively lowered the thresholds for operability and reportability
reviews.
As a result, licensee event reports were developed for two previously identified
design weaknesses.
The first involved reactor building ventilation system performance during
an accident, and the second involved the capabilities of the 250v DC batteries to meet the
four-hour rating.
The licensee's evaluation and recent reporting of these, and other
conditions that were reevaluated and determined to be outside the design basis, were
excellent.
Corporate engineering support to the site has been very good.
Nuclear Technology
performed thorough and comprehensive evaluations of such issues as the potential pressure
locking of residual heat removal (RHR) and core spray (CS) injection valves, electrical design
deficiencies, and elevated drywell (DW) temperatures
that resulted from a loss of drywell
cooling.
The final evaluations of these issues were found to be complete, comprehensive,
'nd
of excellent quality.
One weakness
was noted in the otherwise strong performance in this
area.
This involved an incomplete initial evaluation of a drywell (DW) temperature excursion
following the loss of drywell cooling.
The licensee's initial evaluation did not consider all
the potential effects of elevated temperatures
on system, structures, and components in the
drywell. This appeared to be primarily due to a lack of effective guidance for the initiation
of detailed engineering evaluations.
The Nuclear Engineering Department design change packages continue to be 'thorough and
technically sound.
The high quality of the modification packages is evident by the small
number of changes made to the modification packages during installation.
The design and
installation kickoffmeetings are useful efforts to enhance cooperation between the Nuclear
Plant Engineering and the responsible station groups.
The system engineers are involved in
the design and installation kickoffmeetings, and provide effective overview for the
installation and closeout of,plant modifications.
The motor-operated valve (MOV) program was'horough,
'well managed,
and on schedule.
Personnel responsible for the development and implementation of the motor-operated valve
program were knowledgeable of the applicable technical and regulatory aspects of MOV
reliability determination.
Design basis reviews and motor-operated valve switch settings
calculations were thorough and technically sound.
A significant effort has been made in
conjunction with industry groups regarding motor-operated valve diagnostic test equipment,
and testing of grease for motor-operated valves under the NRC Generic Letter 89-10 MOV
program.
The engineering organization has demonstrated
an excellent safety perspective by continually
reassessing
the basis of the original design for adequacy.
The licensee has been proactive in
implementing their design basis reconstitution and has aggressively resolved discrepancies
identified by the process.
This design basis reconstitution initiative is a significant licensee
strength.
18
Systems Engineering provided effective and visible support in resolving day-to-day
engineering problems.
The licensee increased the number of system engineers by combining
the plant technical staff and the resident engineering staff. The resultant organization reduced
, the maximum number of systems assigned to an engineer from six to two. This allowed the
system engineers to develop the necessary
system expertise to effectively address day-to-day
issues.
System Engineering resolution of certain recurring deficiencies has been occasionally
ineffective or untimely. For example, spurious Electrical Protection Assembly (EPA) breaker
tripping has been a problem since 1982, but little progress has been made in establishing a
permanent solution.
Past reliability problems included inadvertent tripping of EPA breakers
due to large motor starts, poor breaker design, and high ambient temperature surrounding the
EPA logic cards.
Although the licensee has been historically slow to resolve this problem,
management
has initiated action to improve or replace the affected equipment.
In summary, the licensee has made excellent progress in reducing the number of outstanding
engineering deficiencies,
Actions in response to the OER provide increased efficiency and
focus in the engineering organization.
The new organization is effectively involved with the
understanding
and assessment of the design basis.
Systems Engineering was strengthened
significantly by the OER, and continues to resolve day-to-day problems in an effective
manner.
However, certain long-standing and recurrent problems, such as EPA breakers,
continue to require management attention to assure an-effective and timely resolution.
The
engineering organization has changed significantly during this assessment
period.
These
changes have resulted in improved focus'in many areas, while in other areas, the new
organization remains untested.
Performance Rating:
Board Comment:
None
HI.G Safety Assessment/Quality Verification
During the previous assessment
period, this area was rated Category 1.
Licensee staff was of
high caliber and capable of resolving complex technical issues.
Licensee management
emphasized
thorough self-assessment
and organizational effectiveness.
The licensee's
use of
PRA in evaluating the relative risk of various engineering and,operational deficiencies was a
noteworthy strength.
Weaknesses
were noted in resolving certain safety significant concerns,
especially postulated conditions outside the plants design basis.. In addition, in the early part
of the last SALP, the licensee allowed the backlog of open Significant Operating Occurrence
Reports (SOORs); Non Conformance Reports (NCRs) and Engineering Discrepancy Reports
(EDRs) to grow significantly. However, later in the period a backlog reduction program was
h
19
begun.
Good progress was made throughout the period in reducing the backlog.
The
licensee instituted a policy that required the closeout of all backlog items by the end of each
refueling outage.
During the current SALP period, licensee performance in this area continued to be strong.
Corporate management
continued to show a strong on-site presence and remained actively
involved with decision-making.
The integrated planning effort to ensure that all operational
and outage activities were scheduled to minimize safety impact continued as a licensee
strength.
Operational and outage safety were top priority when planning and conducting
operational evolutions, maintenance and surveillance activities.
The plant scheduling group
played an important role in ensuring that planned activities were conducted to result in a net
safety benefit.
The licensee's planning activities were conducted in a safety conscious
manner.
The licensee continues to incorporate Probabilistic Risk Assessment
(PRA) findings and
insights when planning these various types of activities.'mprovements
made to the operating
p'rocedures and training, accident management
strategies,
and the prioritization of preventive
and corrective maintenance activities are frequently the result of the individual plant
evaluation (IPE) methodologies being applied to the respective programs.
Furthermore, the
licensee.has
continued to be an industry leader in assessing
and planning for the risks nuclear
- facilities are subjected to while in shutdown conditions.
The licensee completed and fully implemented their Organizational Effectiveness Review
(OER) during this assessment
period.
The goal of the OER was to solicit and implement
grass roots level comments on how to make the organization more effective.
The new
organization increases the Nuclear Department's
span of control, while reducing the layers of
management
between the workers and senior management.
The OER dissolved certain
historical alignments and shifted the organization to be more responsive to plant needs.
The
OER was viewed as a positive licensee initiative.
The licensee continued to use the nuclear safety assessment
group (NSAG) effectively.
During the assessment
period, NSAG conducted thorough evaluations of plant operations,
maintenance and outage safety, and remained involved with performing self-assessments
of
previous plant performance to ensure safety significant issues were being properly addressed.
These NSAG activities have provided a significant contribution to the assurance of safety at
Susquehanna.
The licensee's staff was generally well-prepared and technicaHy correct when discussing
emerging safety issues and open licensing actions with NRC staff. In general, the licensee is
proactive and plans its licensing activity to ensure that delays in processing licensing actions
are minimized, and that timely NRC reviews are facilitated.
There have been isolated
instances where responses
to licensing submittal commitments and requests for additional
information (RAIs) have been less than timely.
20
The licensee did not recognize the extent and significance of the operator performance
weaknesses
related to reactor level and pressure control identified during the first
requalification program evaluation and in a previous reactor scram event.
Therefore, they did,
not correct the weaknesses prior to the second requalifiicatio'n program evaluation.
Following
.
the second licensed operator requalifiication program evaluation, the licensee took prompt. and
comprehensive actions to address the operator performance and programmatic weaknesses:
They performed a thorough root cause analysis.
Their proposed corrective actions
appropriately addressed
the identified root causes.
I
The reductio'n of the backlog of identified deficiencies remained a licensee priority. The
licensee made significant progress in reducing the overall number of deficiencies..
When the
licensee began their deficiency reduction in August 1990, there were 277 NCRs and 378
SOORs in the backlog.
Of these, 23 NCRs and 13 SOORs remain as of April 1992.
In
addition, the licensee had identified the remaining deficiencies to be closed out in the Unit 1
Cycle. 6 refueling outage.
They have made excellent progress and their goal continues to be
zero deficiencies at the end of the outage.
The control and management of deficiencies is a
significant licensee strength.
The Susquehanna
Review Committee (SRC) and the Plant Operations Review Committee.
(PORC) continue to perform their respective off-site and on-site safety reviews.
responsibilities in an effective manner.
The SRC utilizes outside contract and utility
personnel, that bring a diverse and unique safety perspective to the committee.
The licensee
also utilized Event Review Teams (ERTs) to perform in-depth reviews of safety-related
events.
The results of their reviews were broad, comprehensive,
and demonstrated
the
licensee's strong commitment to formal root cause analysis techniques.
These investigations
were found to be extremely thorough at the plant and system level, but showed some
weakness in two specific areas.
The first w'eakness involved component level root cause investigation, specifically for high
temperature effects on electronic components.
Accelerated aging was seen in capacitors used
for the main steam line radiation monitors and for logic cards used for the reactor protection
The licensee's root cause analysis did not fully investigate these
component level degradations.
The second root cause investigation weakness involved the
identification of past similar industry events for the january 18, 1992 hydrogen recombiner
event.
The event review team's (ERT) initial review did not consider past industry events as
contributing to the root cause or identify other applicable similar events.
However, this
review did identify weakness in the industry experience revievy program (IERP).
The IERP's
primary focus was on the review process and did not ensure that long-lasting corrective
actions were generated.
The licensee is reevaluating their approach to these two identified
weaknesses.
Except for these two minor weaknesses,
the licensee's
safety review activities
were found to be strong and comprehensive,
with a balanced safety perspective evident.
21
.
Licensee event reports (LERs) and 10 CFR 50.72 Event Notifications (ENs) were well
written with clear descriptions of the subject events.
The root cause analyses presented in the
LERs was adequate,
and recommended corrective actions were'technically correct.
When in-
'epth
engineering analysis and evaluation were required, the problem was referred to
corporate engineering for solution.
These solutions were generally very good.
The licensee has continued their efforts to determine the root cause of the past emergency
diesel generator crankcase explosions at Susquehanna.
The quality and detail of the reports
=produced on this issue were considered to be outstanding.
In general, the documented
information and the presentations
given by the licensee were very informative and well
prepared.
Even though no single root cause for the crankcase explosions was identified, the
licensee performed corrective actions which addressed
all four major causal factors.
Overall,
the actions taken to assure the safe and reliable operation of the emergency diesel generators
are considered
a commendable effort on the part of the licensee.
The licensee was successful at resolving problems that arose on an individual occurrence basis
once they were clearly recognized.
However, there were some observations that indicated
weakness relative to the licensee's ability to recognize potentially significant problems and
effect timely corrective actions.
Examples include:
(1) operator skill weakness,
observed
early in the period in an operator requaMcation program review and, later, in actual
perfoimance involving two plant transients,
was not effectively resolved until again observed
during another operator requalification program review in January 1992; (2) operators'ailure
to recognize and fully evaluate an offgas high pressure alarm as a symptom of a probable
hydrogen ignition, two days prior to the January 18,1992 event; (3) and failure to effectively
correct a long-standing and recurring problem involving reactor protective system (RPS)
electrical protective assembly (EPA) breaker tripping events.
With these exceptions,
the
licensee has been effective in establishing and implementing good corrective measures to
resolve problems.
In summary, licensee management
demonstrated
a conservative safety perspective with a high
level of involvement with day-to-day activities and continues to emphasize thorough self-
assessment
and organizational effectiveness.
The OER has lead to increased departmental
effectiveness by emphasizing customer service.
Outstanding deficiencies received an
extraordinary amount of attention, and as a result, are at historically low levels.
Safety
review activities were conducted in an effective manner with few weaknesses
noted.
The
licensee continued to emphasize safety and quality during the conduct of nuclear activities.
Performance Rating:
Board Comment:
None
22
IV.
SUPPORTING DATAAND SUMMARY
IV.A Licensee Activities
During the assessment
period, both Susquehanna
units operated safely and effectively. Plant
availability and capacity factors reached record levels.
Unit 1 experienced one unplanned
shutdown, which was an automatic scram.
Unit 2 experienced three unplanned shutdowns;
an automatic scram, a manual scram and a manual shutdown.
(See Section IV.D - Reactor
Trips and Unplanned Shutdowns).
A refueling outage was completed on Unit 2 and a Unit 1 refueling outage was in progress at
the end of the period.
The Unit 2 fourth refueling outage took place from March 9, 1991
through May 9, 1991 for a total of 61 days.
The Unit 1 sixth refueling outage began on
March 9, 1992 and was in progress at the end of the assessment
period.
Major activities
during both outages included core refueling, main generator rotor disassembly
and inspection,
emergency core cooling system (ECCS) valve work and testing, surveillance testing and
inservice inspections.
IV.B NRC Inspection and Review Activities
During this assessment
period, there were two full-time NRC resident inspectors assigned to
the site.
They performed on-going safety inspections throughout the SALP period.
Several periodic inspections were performed by regional inspectors in the areas of
Maintenance, Emergency Preparedness,
Security, Engineering, and Radiological Controls.
The NRC conducted one inspection during the period involving Motor Operated Valve
Dynamic Performance (GL 89-10).
IV.C Reactor Scrams and Unplanned Shutdowns
Date
Power
Level
Root Cause
%unctional
Area
Event Description:
UNIT 1
1.
07/31/91
100%
Component Failure
N/A
AUTOMATICSCRAM due to a loss of one offsite power source with an existing half scram
condition.
The loss of power to Startup Transformer 10 (T-10) was due to a loss of the
Montour Mountain Line. The resultant undervoltage and underfrequency tripped the "A"
RPS Motor Generator Set.
This sequence completed a full scram logic signal since a half
scram signal had been previously inserted due to a failed power supply to the "B" Main
Steam Line Radiation Monitor.
23
1.
08/06/91
100%
Component Failure
N/A
AUTOMATICSCRAM due to turbine stop valve closure.
A fault in the electro-hydraulic
control system caused the ¹1, ¹3, and ¹4 turbine stop valves to close.
2.
08/21/91
100%
Component Failure
N/A
, MANUALSHUTDOWN to replace a defective main transformer.
The shutdown was based
upon high combustible gases found during analysis of transformer cooling oil.
3.
03/18/92
100%
N/A
Component Failure
MANUALSCRAM due to degraded plant conditions following 2C engineered
safeguards
'ystem
(ESS) bus lockout.
Operators manually scrammed the unit in anticipation of Main
Steam Isolation Valve Closure.
ATTACHIVlENT1
SALP WGTEMA
Licensee performance is assessed
in selected functional areas depending on whether the
facility is in a construction or operational phase.
Functional areas normally represent areas
significant to nuclear safety and the environment.
Some functional areas may not be assessed
because of little or no licensee activities or lack of meaningful observations in that area.
Special areas may be added to highlight significant observations.
The following evaluation criteria were used, as applicable, to assess
each functional area:
1.
Assurance of quality, including management involvement and control;
2.
Approach to resolution of technical issues from a safety standpoint;
3.
Enforcement history;
4.
Operational and construction events (including response to, analyses of, reporting of,
and corrective actions for);
5.
Staffing (including management);
6.
Effectiveness of training and qualification program.
On the basis of the SALP Board assessment,
each functional area evaluated is rated according
to three performance categories.
The definitions of these performance categories are given
below:
Category 1:
Licensee management attention to and involvement in nuclear safety or
safeguards activities resulted in a superior level of performance.
NRC willconsider reduced
levels of inspection effort.
Category 2:
Licensee management attention to and.involvement in nuclear safety or
safeguards activities resulted in a good level of performance.
NRC willconsider maintaining
normal levels of inspection effort.
Category 3: Licensee management attention and involvement in nuclear safety or safeguards
activities resulted in an acceptable level of performance; however, because of the NRC's
concern that a decrease in performance may approach or reach an unacceptable level, NRC
willconsider increased levels of inspection effort.
Category N: Insufficient information exists to support an assessment of licensee
performance.
These cases would include instances in which a rating could not be developed
because of insufficient licensee activity or insufficient NRC inspection.
The SALP Board may assess
a functional area to compare the licensee's performance during a
portion of the assessment
period to that during an entire period in order to determine a
performance trend.
Generally, performance in the latter part of a SALP period is compared
to the performance of the entire period.
Trends in performance from one period to the next
"
may also be noted.
The trend categories used by the SALP Board are as follows:
Improving: Licensee performance was determined to be improving
Dedining:
Licensee performance was determined to be declining and the licensee had not
satisfactorily addressed
this pattern.
A trend is assigned only when, in the opinion of the SALP Board, the trend is significant
enough to be considered indicative of a likely change in the performance category in the near
future.
For example, a classification of "Category 2, Improving" indicates the clear potential
for "Category 1" performance in the next SALP period.
It should be noted that Category 3 performance,
the lowest category, represents
acceptable,
although minimally adequate,
safety performance. Ifat any time the NRC concluded that a
licensee was not achieving an adequate level of safety performance, it would then be
incumbent upon NRC to take prompt appropriate action in the interest of public health and
safety.
Such matters would be dealt with independently from, and on a more urgent schedule
than, the SALP process.