ML17157A627
| ML17157A627 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 03/19/1991 |
| From: | Jason White NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17157A626 | List: |
| References | |
| 50-387-90-26, 50-388-90-26, NUDOCS 9103290049 | |
| Download: ML17157A627 (36) | |
See also: IR 05000387/1990026
Text
U. S. NUCLEAR REGULATORY COMMISSION
REGION I
Inspection
50-387/90-26; 50-388/90-26
Report Nos.
License Nos.
Licensee:
Pennsylvania Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
18101
Facility Name:
Inspection At:
Susquehanna
Steam Electric Station
Salem Township, Pennsylvania
Inspection
Conducted:
December 30, 1990 - February
11, 1991
Inspectors:
G. S. Barber, Senior Resident Inspector, SSES
J. R. Stair, Resident Inspector, SSES
H. J. Kapl n, S
io
Reac
ngineer, DRS
Approved By:
J
~
ite, Chief
eactor Projects Section No. 2A,
Division of Reactor Projects
ate
Ins ection Summar:
~d:R
i
i
p
i
d ai hfll ig
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p
radiological controls, maintenance/surveillance
testing, emergency preparedness,
security,
engineering/technical
support, safety assessment/quality
verification, and Licensee Event
Reports, and Significant Operating Occurrence Reports.
Results:
During this inspection period, the inspectors found that the licensee's activities were
directed toward nuclear and radiation safety.
One violation was identified.
The violation
involved failure to maintain activities as specified by the Procedure 80-QA-300, Conduct of
Operations, relative to implementing Technical Specification 3.6.3 as it pertains to inoperable
See Section 2.2.2 for details.
An Executive Summary is included and provides an overview of specific inspection findings.
T
qg03P90049'><~pg~
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ADQCK 05~ pg~
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TABLE OF CONTENTS
EXECUTIVESUMMARY......
SUMMARYOF OPERATIONS ~...
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1.1
Inspection Activities........
1.2
Susquehanna
Unit 1 Summary
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1.3
Susquehanna
Unit 2 Summary ..
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OPERATIONS
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2.1
Inspection Activities................. ~..........
2.2
Inspection Findings and Review ofEvents...............
2.2.1
Loss of Shutdown Cooling - Unit 2
2.2.2
Inoperable Inboard Main Steam Isolation Valves - Unit 1
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RADIOLOGICALCONTROLS
3.1
Inspection Activities..................
3.2
Inspection Findings
3.2.1
Review of Licensee Posting Practices
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MAINTENANCE/SURVEILLANCE.........................
4.1
Maintenance and Surveillance Inspection Activity
4.2
Maintenance Observations
4.2.1
Use of Unapproved Sealing Material on Secondary Containment
Boundary Removable Walls
4.3
Surveillance Observations........
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EMERGENCY PREPAREDNESS................
5.1
Inspection Activity....................
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Inspection Findings
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SECURITY
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6.1
Inspection Activity............. ~..... ~..............
6.2
Inspection Findings
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ENGINEERING/TECHNICALSUPPORT......................
7.1
Inspection Activity.................... ~...........
7.2
Inspection Findings
7.2.1
RHR Pump Cooler Failure - Metallurgical Report Review
7.2.2
Deficiency 'Reduction Program - Incorrect Assumption Made For
250 VDC
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Table of Contents (Continued)
8.
SAFETY ASSESSME NT/QUALITYVERIFICATION
8.1
Licensee Event Reports (LER), Significant Operating Occurrence
Report
8.1.1
Licensee Event Reports..........................
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9.
MANAGEMENTAND EXIT MEETINGS .......................
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Routine Resident Exit and Periodic Meetings....... ~..........
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EXECUTIVESUMMARY
Susquehanna
Steam Electric Station
Inspection Reports
50-387/90-26; 50-388/90-26
4
December 30, 1990
- February
11, 1991
operations (71707, 92701, 92720)
A loss of Shutdown Cooling in Unit 2 occurred on January
8 which caused reactor
temperature to increase from 108 to 135 degrees F.
The cause was attributed to the failure of
an I&C work planner to reference all applicable drawings when preparing the work
instruction.
On January
15, the inboard Main Steam Isolation Valves (MSIVs) were declared inoperable
due to low Containment Instrument Gas (CIG) pressure.
Plant operators failed to recognize
the applicability of TS 3.6.3 for the condition; and the applicable surveillance procedure
failed to reference the pertinent Limiting Condition For Operation.
This matter was
identified as a violation of TS 6.8.1 for failure to maintain activities in accordance with the
procedure 80-QA-300, Conduct of Operations (NV4 387/90-26-01).
Radiolo ical Controls (71707)
Individual workers and Health Physics personnel implemented radiological protection
program requirements.
Periodic inspector observation noted no inadequacies
in the licensee's
implementation of the radiological protection program.
Licensee posting practices relative to 10 CFR 19.12 were reviewed.
The licensee also
performed a review of posting practices and noted that posting responsibilities were not
clearly delineated nor was the procedure adequate for the scope of the activities.
The
licensee has implemented specific procedure enhancements
and procurement activities to
improve postings.
Maintenance/Surveillance
(61726, 62703)
The licensee exercised good control of maintenance
and surveillance activities.
No scrams
were attributable to maintenance or surveillance activities.
However, improper performance
of a Unit 2 work activity led to a shutdown cooling isolation.
1
The inspector noticed a change in the sealing material used for the temporary walls for the
Unit 1 Reactor Building during a routine tour and questioned
the use of unapproved
material
111
for this application in the plant.
Accordingly, the licensee is reviewing their use of
consumable materials for various safety-related applications.
F >ur LERs were reviewed during the period concerning missed surveillances
as a result of
dissimilar causes.
The inspector plans to continue monitoring this area for potential program
weaknesses.
Emer enc
Pre aredness
issues emerged during the reporting period.
~ecurit
(71707)
Routine observation of protected area access
and egress control showed good control by the
licensee.
En ineerin /Technical Su
ort (37700, 71707, 92720)
Metallurgical Reports covering the RHR Pump Motor Cooler Failures were reviewed.
These
reports concluded that the primary cause of the failure was under deposit corrosion with some
contribution from microbiological induced corrosion.
A Licensee Event Report (LER) was written to document a concern identified in 1989
regarding the ability of the 250 VDC batteries to meet their four-hour minimum load
requirements.
This LER was written as a result of reviewing old issues for reportability
under the new reporting criteria established by the licensee.
This issue was not reported at
the time it was identified since compensatory
measures
were promptly implemented.
afet
Assessment/As
urance f
ualit
(90712, 92700, 92701, 92720)
A total of 14 LERs were reviewed during the period, 5 of which were followed up in this
report.
A total of 61 Significant Operating Occurrence Reports were reviewed during the period, 3 of
which were followed up in this report.
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1.
SUlVMARYOF OPERATIONS
1.1
Inspection Activities
~Detail
The purpose of this inspection was to assess
licensee activities at Susquehanna
Steam Electric
Station (SSES) as they related to reactor safety and worker radiation protection.
Within each
inspection area, the inspectors documented
the specific purpose of the area under review, the
scope of inspection activities and findings, along with appropriate conclusions.
This
assessment
is based on actual observation of licensee activities, interviews with licensee
personnel,
measurement of radiation levels, independent calculation, and selective review of
applicable documents.
Abbreviations are used throughout the text.
Attachment
1 provides a
listing of these abbreviations.
1.2
Susquehanna
Unit 1 Summary
Unit 1 operated at or near full power until experiencing an extraction steamline isolation on
February 4.
A manual power runback to 80 percent was performed pending repairs to a level
control valve on the drain line to the 3C feedwater heater.
Full power was restored on
February 6 and was maintained throughout the remainder of the period.
Scheduled power
reductions were also conducted during the period for control rod pattern adjustments,
surveillance testing, and maintenance.
No ESF actuations or scrams occurred during the
period.
1.3
Susquehanna
Unit 2 Sumniary
Unit 2 operated at full power prior to January 5, when the unit was shutdown to replace an
0-ring on the "B" reactor recirculation pump motor.
Other problems corrected while
shutdown were two suppression pool-to-drywell vacuum breakers which failed to reseat
following functional testing, and a failed main generator current transformer.
Full power was
restored on January
12 following repairs and was maintained throughout the rest of the-
period.
Scheduled power reductions were conducted during the period for control rod pattern
adjustments,
surveillance testing, and maintenance.
One ESF actuation and no scrams
occurred during the period.
A shutdown cooling system isolation occurred on January 8.
See Section 2.2.1 for details.
2.
OPERATIONS
2.1
Inspection Activities
The inspectors verified that the facility was operated safely and in conformance with
regulatory requirements.
Pennsylvania Power and Light (PP&L) Company management
control was evaluated by direct observation of activities, tours of the facility, interviews and
discussions with personnel,
independent verification of safety system status and Limiting
2
Conditions for Operation, and review of facility records.
These inspection activities were
conducted in accordance with NRC inspection procedures 71707, 92701, and 92720.
The inspectors performed
15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> of deep backshift inspection during this reporting period.
2.2
Inspection Findings and Review of Events
2.2.1
Loss of Shutdown Cooling - Unit 2
A loss of shutdown cooling (SDC) occurred at 9:44 a.m., January 8, due to the opening of a
states link in the RHR Low Pressure permissive circuitry. The licensee was installing a new
switch (B31-N018A) in the RHR pressure permissive circuitry when the isolation occurred.
To de-energize the circuit, a states link (a connector that the work instructions described
as
providing 'power between terminal points FF-1 and FF-2 as shown on GE Elementary Dwg.
No Ml-B21-101 Sheet
10) was opened.
However, opening of this states link also
deenergized
the K39 and K33A relays; which, in turn, caused RHR suction valves
(F-008 and F-009) to close.
During the transient, from 9:44 a.m. to 1,0:50 a.m., reactor
water temperature rose from 108 to 135 degrees F.
The licensee throughly examined the cause for this event, prior to resetting the isolation
signal, to ensure that no additional problems would result.
The isolation was reset, SDC
restored,
and the heatup was terminated.
The licensee formed an Event Review Team (ERT) ~
The NRC was notified per 10 CFR 50.72.
The ERT reviewed the event and determined that the cause was due to an I&C work planner
not referencing the proper drawings when he developed the instructions for the pressure
switch replacement.
The work instructions involved jumper installation and opening states
links within a wiring panel.
The jumper installation was necessary
to prevent the RHR
isolation by maintaining the circuit energized when the links were opened.
However, the
work planner improperly based the work instructions solely on GE Elementary Dwg. No.
M1-B21-101, an elementary drawing that did not describe all of the details within the wiring
panel
~ The ERT determined that the use of the elementary drawing was improper to use as a
sole reference for planning the work. The ERT concluded that the work planner failed to
review the applicable wiring connection lists and diagrams that were pertinent to this work;
and consequently failed to identify the proper jumper connections on the work description.
As a result, the jumpers were not installed on the proper contacts.
Accordingly, when the
links were opened, the isolation logic was actuated,
and the RHR valves closed.
As a result of this event, the licensee is developing an Instrumentation & Controls planners
guide.
This guide willprovide direction for planning of I&C maintenance
functions
including utilization of all applicable drawings and references during the planning process.
Training on this document will be performed for appropriate personnel.
In addition, the
physical wiring arrangement in the subject panel willbe modified to improve field
wiring/internal wiring interface and to improve logic circuit testability.
The estimated
3
completion date for the planners guide preparation and applicable training is September
1,
1991.
The inspector reviewed the ERT findings and proposed corrective actions and noted that the
conclusion and corrective measures
appeared
to adequatly address this event.
2.2.2
Inoperable Inboard Main Steam Isolation Valves - Unit 1
The Containment Instrument Gas (CIG) System supplies a local MSIV accumulator that,
along with springs, ensures rapid closure of the Main Steam Isolation Valves during accident
conditions.
Accordingly, MSIV closure time is dependent on the air pressure in the
While the pre-1989 FSAR listed "springs alone" as an acceptable closing
method, NCR 89-0064 questioned
the ability of the inboard MSIVs to close during a design
basis accident (DBA) with springs alone.
After detailed analysis, the licensee concluded that
both springs and air are necessary
to meet the design closure times for a DBA, i.e., greater
than 3 but less than 5 seconds.
As a result, the licensee modified the inboard MSIV
operability statement in the applicable Shift Surveillance Operating Log Procedure SO-100-
006 to require that CIG pressure be maintained at 85 psig or greater to ensure these closure
times.
At 8:40 a.m., January
15, an operator on rounds noted that Unit 1 CIG pressure
had dropped
to 80 psig.
The operator reported the low pressure to the control room.
Consequently,
the
inboard MSIVs were declared inoperable,
and TS LCO 3.4.7.a. was entered since procedure
SO-100-006 referenced this TS as being applicable.
TS LCO 3.4.7.a requires restoration of
the affected MSIVs to operability, or isolation of the affected steam lines within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />; or
otherwise, plant shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Accordingly, action was taken by IAC
to adjust the malfunctioning Pressure Control Valve (PCV-16241) to achieve control pressure
in the normal band.
Following successful adjustment,
the system was returned to an operable
status.
CIG pressure was restored,
and TS LCO 3.4.7.a.
was exited at 3:15 p.m.
The
licensee continues to monitor CIG pressure to verify that pressure remains above 85 psig.
During this evolution, the outboard MSIVs remained operable since these valves were not
affected by the malfunctioning of PCV-16241.
The cause of the event appears
to be due to a combination of factors:
1) low flow through the
valve hampers its ability to control pressure in a tight band; 2) very fine particles on the
valve disc and seat are believed to hamper totally free, uninhibited valve movement; and 3)
the control band for the valve is at the extreme low end of its design.
The licensee took
immediate corrective action to adjust the PCV within the control band and has taken
additional action to increase flow through the system to improve PCV response.
In addition,
system filters were inspected for unusual debris or dessicant breakdown.
No unusual
indications were noted.
The inspector reviewed the licensee's actions and specifically questioned
the licensee on the
applicability of TS LCO 3.6.3, "Primary Containment Isolation Valves," since the MSIVs
0
affected are listed in Table 3.6.3.1.
The licensee reviewed the TS and determined that it was
applicable.
The inspector noted that TS 3.6.3.a. requires remedial action within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,
whereas TS 3.4.7.a. allowed 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
Specifically, TS 3.6.3.a. requires isolating the '
affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> (as opposed to the 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> permitted by TS 3.4.7.a) or be
in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and cold shutdown within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The inspector noted that while neither TS was actually violated in this particular instance, it
was fortuitous, and not by design, that the licensee did not exceed the LCO for TS 3.6.3.
The inspector identified, that TS 6.8.1 required the licensee to establish, implement, and
maintain written procedures'affecting
safety-related activities; and that Procedure 80-QA-300,
"Conduct of Operations," Section 6.2, Formal Directions, required the licensee to maintain
plant operations within the boundaries specified by Technical Specifications and License
Conditions.
Accordingly, the failure to maintain plant operations
as specified by Procedure
80-QA-300, "Conduct of Operations," due to the plant operators'ailure
to implement the TS 3.6.3.a relative to their determination that the inboard MSIVs were inoperable constitutes
a
violation of TS 6.8.1. (NV5 50-387/90-26-01)
The licensee has subsequently
submitted PCAF 1-91-0028 to add TS LCO 3.6.3.a to Shift
Surveillance Operating Log Procedure,
SO-100-006.
3.
RADIOLOGICALCONTROLS
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3.1
Inspection Activities
PP8.L's compliance with the radiological protection program was verified on a periodic basis.
These inspection activities were conducted in accordance with NRC inspection procedure
71707.
3.2
Inspection F<indings
Observations of radiological controls during maintenance activities and plant tours indicated
that workers generally obeyed postings and Radiation Work Permit requirements.
No
inadequacies
were noted.
3.2.1
Review of Licensee Posting Practices
The inspector reviewed posting practices relative to 10 CFR 19. 12 to assess
the licensee's
method for posting information pertaining to violations, civil penalties,
and orders that were
related to radiological working conditions.
Postings must be made within two days of receipt
and they must be made in areas in which the affected activities take place.
In addition, they
must remain posted for 5 days or until corrective action is complete, whichever is longer.
The licensee previously identified some problems with postings.
SOOR 1-90-306
documented
missing postings in the control structure access
area that were removed for a
remodeling effort.
Licensee investigation found that there were four reasons why the event
0
cumented missing postings in the control structure access
area that were removed for a
remodeling effort.
Licensee investigation found that there were four reasons why the event
occurred:
1) clear accountability for posting, auditing, and updating of these
requirements were not specified in NDI-QA-3.3.4, the licensee's procedure which describes
posting requirements; 2) the locations of all posting areas was not procedurally identified; 3)
routine reviews of the condition and content of the material posted is not performed; and 4)
postings are performed by several groups on site which leads to inconsistent posting practices.
The licensee took prompt action to correct the immediate posting deficiencies by replacing the
removed postings, auditing postings to ensure the proper material was in place, and providing
direction on removing out-of-date information. In addition, as long-term corrective action,
NDI-QA-3.3.4 is being revised to specify the Docket Control Center Supervisor as the
individual who is solely responsible for updating and ensuring adequate postings.
A new
procedure checklist will be used as the basis for future audits.
The licensee is also in the
process of procuring dedicated bulletin boards for postings.
Long-term actions are scheduled
to be completed on or before March 31, 1991.
Some of the new bulletin boards were in
place at the end of the inspection period.
The inspector reviewed licensee actions for their self-identified posting problems and noted
that they were thorough and their schedule appeared
to be timely. A spot check of existing
postings showed that they were adequate.
However, the postings in the Unit
1 Access Area
were cluttered and portions of the postings were covered.
This was corrected by the licensee.
In addition, the inspector questioned
the licensee on postings made at the corporate office.
The licensee informed the inspector that postings at the corporate offices are made on the
corporate communications bulletin boards and are controlled by Licensing.
At the time of
this review, there were no outstanding violations, civil penalties, or orders involving.
radiological work practices that required posting by the licensee at the corporate office.
The
inspector had no further questions.
4.
MAINTENANCE/SURVEILLANCE
4.1
Maintenance and Surveillance Inspection Activity
On a sampling basis, the inspector observed and/or reviewed selected surveillance and
maintenance activities to ensure that specific programmatic elements described below were
being met.
Details of this review are documented in Sections 4.2 and 4.3.
4.2
Maintenance Observations
The inspector observed and/or reviewed selected maintenance activities to determine that the
work was conducted in accordance with approved procedures,
regulatory guides, Technical
Specifications, and industry codes or standards.
The following items were considered,
as
applicable, during this review: Limiting Conditions for Operation were met while
components or systems were removed from service; required administrative approvals were
obtained prior to initiating the work; activities were accomplished
using approved procedures
and quality control hold points were established
where required; functional testing was
performed prior to declaring the involved component(s)
operable; activities were
.t
accomplished by qualified personnel; radiological controls were implemented; fire protection
controls were implemented; and equipment was returned to service in accordance with the
licensee's procedures.
These observations and/or reviews included:
evaluation of differential and discharge pressures for the "A" Containment Radiation
Monitor Sample Pump per WA S16089 on January 24;
investigation of Transverse Incore Probe problems per WA 16099 on January 24;
eighteen month inspection on the "E" Emergency Diesel Generator per WA A-04597
on January 25;
inspection/replacement of Cylinder Liners as Required to Support Diesel Generator
(DG) Work per WA S05015 on January 25;
annual preventive maintenance
on the "A" Containment Instrument Gas compressor
per WA P05044 on February
1; and,
installation of relays and wiring to support the "C" DG Fuel Oil Tank Low Level
Switch Upgrade per WA C00675 on February 7.
No unacceptable
conditions were identified.
4.2.1
Use of Unapproved Sealing Material on Secondary Containment Boundary
Removable Walls
During a tour of the Unit 1 reactor building, the inspector noted that the licensee had
replaced the caulking type sealing material used on the removable walls of the Unit
1 reactor
building with an expandable
foam type material.
Per applicable drawings and design
specifications,
a neoprene gasket provides the primary sealing material for the removable
walls.
However, per the drawings, ifair gaps exist around the gasket, an approved sealing
material such as Dow Corning 790 caulking may be used for additional sealing.
The licensee
was therefore asked to provide a copy of the replacement item equivalency evaluation (RIEE)
or a safety evaluation which properly evaluated the material and determined it was acceptable
for use.
The licensee was not able to find documentation which provided the requested
information and consequently
generated
a Nonconformance Report (NCR) to document the
condition and disposition the nonconformance.
The inspector reviewed the NCR and noted that an NPE evaluation stated that the expandable
foam (HILTICB120 Filler Foam) now "in-use" was unacceptable
due to its inferior
adhesion,
tensile strength, and flame resistance characteristics.
The maintenance group
disagreed with the evaluation and stated that they considered
the foam acceptable for use
since the neoprene gasket provides secondary containment boundary integrity, and the sealing
material, although used for additional protection, is not required.
Based on the NCR, the
inspector noted that the licensee must determine whether the material is acceptable for use
and take action in accordance with that determination.
Since the licensee verified that the neoprene 'gasket was in place on the removable walls, the
inspector noted that secondary containment integrity was not in question.
However, the
concern remained regarding the licensee's
apparent failure to perform a proper evaluation
prior to substituting another material for the specified sealant.
Work documents provided by
the licensee demonstrated
that review was performed and authorization obtained prior to
substituting the sealing material.
However, it was apparent that the review failed to
adequately consider the drawing specification calling for DOW Corning 790 caulking.
The use of the Susquehanna
Approved Materials (SAM) list in authorizing the substitution of
material on safety-related applications is not appropriate without a proper evaluation.
The
individual(s) reviewing the SAM list misinterpreted the allowed use of the Hilti foam for this
application.
Since weaknesses
in the process for substitution of materials apparently exist,
and the licensee has agreed to evaluate this matter for improvement.
This item will remain
unresolved pending evaluation of the licensee's review and corrective actions pertaining to the
substitution of materials.
(UNR 50-387/90-26-02)
4.3
Surveillance Observations
The inspector observed and/or reviewed the following surveillance tests to determine that the
following criteria, ifapplicable to the specific test, were met:
the test conformed to
Technical Specification requirements;
administrative approvals and tagouts were obtained
before initiating the surveillance; testing was accomplished by qualified personnel in
accordance with an approved procedure;
test instrumentation was calibrated; Limiting
Conditions for Operation were met; test data was accurate and complete; removal and
restoration of the affected components
was properly accomplished;
test results met Technical
Specification and procedural requirements;
deficiencies noted were reviewed and
appropriately resolved; and the surveillance was completed at the required frequency.
These observations and/or reviews included:
50-250-00, RCIC Quarterly Flow Verification, performed on January 24.
SO-030-003, Quarterly Control Structure Chilled Water Flow Verification, performed
on February 7.
No unacceptable
conditions were identified.
4.3.1
The following LERs reviewed by the inspector are included in this section since they involve
surveillances which were not performed within their respective TS windows.
LER 90-031-
Technical
ecificati n R
uired Area Radiation Surve
Not Perf rmed-
Unit 1
On November 29, 1990, the licensee discovered that a radiation survey of the reactor
building refueling floor was not performed as required by TS 3.3.7.1, Action 71
~ The
licensee performed the required radiation surveys on November 27 and 28, preceeding the
event, but failed to perform the survey. on November 29.
Upon discovery of this condition
on November 30, the required survey was immediately performed.
The surveys were being
performed at 5:30 p.m. each day by second shift personnel,
and the survey was performed on
November 30 at 2:00 a.m., resulting in the required survey being taken approximately eight
and one half hours late.
The radiation surveys were required to compensate for the spent fuel storage pool criticality
monitors which had been removed from service on November 27, 1990.
The criticality
monitors were removed from service, declared inoperable, and TS LCO 3.3.7.1 entered
while an inspection of the reactor water cleanup filter/demineralizer vessels took place.
Since
the inspection of the filter/demineralizers required removal of floor plugs on the refueling
deck, the licensee was concerned that radiation levels in the vicinity of the criticality monitors
would increase resulting in exceeding alarm setpoints.
Alarming of the monitors would
interfere with work being performed since personnel are required to withdraw from the area
upon the sounding of the alarm per 10 CFR 70.24 (a)(3).
Therefore, the justification for
removing the criticality monitors from service was to prevent their alarming and to allow the
performance of the inspections.
The licensee determined that the missed survey was caused by personnel error and procedural
inadequacies
in that the responsibilities and specifications for performing the non-routine
survey was not clearly defined by procedures,
the survey was not designated
as priority work
or scheduled on the health physics (HP) work list, and the means available to remind HP
personnel that the survey was required was not sufficiently obvious.
In this case, the inspector also noted that the need to remove the criticality monitors from
service was not clearly established,
adequate procedural controls were not in place to assure
that compensatory
measures
were accomplished,
and the work for which the criticality
monitors were removed from service was not expedited.
In reviewing the procedural'controls
for removing equipment from service, the inspector noted that guidance had not been
established
to cause evaluation of decisions to remove equipment from service and voluntarily
enter TS LCOs.
Accordingly, the licensee. initiated action to implement such guidance in
.
appropriate procedures
to correct this weakness.
Other corrective action, planned or taken,
0
included revising procedures to: 1) clearly define responsibilities for non-routine survey
performance; 2) better identify the requirements for surveys; 3) improve the process for
communicating information and instructions; and 4) document shift turn-over instructions.
Personnel training relative to this event and the revision of the applicable procedures
is
planned for completion by March 9, 1991.
These corrective actions appear adequate to resolve the problem.
Since the licensee met the
requirements
stated in 10 CFR 2 Appendix C, Sections V.A and V.G.1, this item is
considered
a non-cited violation,
(NON 50-387/90-26-03)
LER
0-009-0
HPCI and R I
team
I
Pre sure Low Re
onse Time Te tin
Not
Performed Within R
uired Time Interval -
nit 2
On September
19, 1990, the licensee discovered that the response time testing for HPCI and
RCIC steam supply low pressure instrumentation was not completed within the required
18
month surveillance interval specified by the TS.
The elapsed time from previous testing was
approximately 30 1/2 months or 8 months beyond the allowable grace period.
The licensee
immediately tested both the HPCI and RCIC instruments following discovery, with
satisfactory results.
The licensee found the cause of this event to be an incorrect determination of channel
redundancy of the affected instrumentation during a review of the elementary diagrams in
1989.
This resulted in procedural revisions which specified testing at a lesser than allowable
frequency.
Corrective actions taken were to correct the testing frequencies specified in the
applicable surveillance procedures
and to assure that no other similar situations existed by
reviewing response time testing procedures for correct testing frequencies.
Inspector review of this event and the licensee's corrective actions found their response
acceptable.
Since the licensee met the requirements
stated in 10 CFR 2 Appendix C, Section
V.A and V.G.1, this item is considered
a non-cited violation.
(NON 50-388/90-26-01)
LER
0-010- 0
ondensate Transfer Pum
Dischar e Low Pressure Alarm
ic
urveillance Not
om le ed Within the R
ired Monthl
Time Interval -
nit 2
On October 2, 1990, the licensee discovered that the monthly channel functional test of the
condensate
transfer pump discharge low pressure alarm logic had not been completed within
the required surveillance time interval.
The discovery was made during a review of a print-
out of surveillance tests that had been determined not applicable for existing plant conditions
(out-of-mode)
~
The latest possible date for performing the surveillance was September 27.
Since the test was immediately performed following discovery on October 2, the test
exceeded
the allowable period by 5 days.
The licensee determined the cause of the event to be a scheduling error on the part of
Instrumentation and Controls (I&C) personnel due to insufficient procedural controls.
Station
10
procedures did not require independent review of out-of-mode determinations, which might
have identified the improper placement of this test in the out-of-mode category.
In response,
the licensee reviewed all common surveillance tests under
ISAAC department
responsibility and verified that no other tests were inappropriately placed in the Out-of-Mode
condition.
Corrective actions completed to prevent a recurrence involve changes to ISAAC and
administrative'procedures
which now require a second level of review prior to placing a
surveillance in the out-of-mode category.
The inspector reviewed and discussed
this event with members of the licensee's staff.
Licensee response to the event was found to be appropriate.
Since the licensee met the
requirements
stated in 10 CFR 2 Appendix C, Sections V.A. and V.G.1, this item is
considered
a non-cited violation.
(NON 50-388/90-26-02).
LER 90-012-00 Turbine Overs
eed Testin
Not
om leted Within Re uired Time F llowin
erational Condition Chan
es -
nit 2
On October 28, the licensee determined that they had, on two previous occasions,
not
complied with the TS requirement to perform turbine overspeed
protection testing within 24
hours of entry into Condition 2 (Startup).
The requirement to perform this testing within 24
hours of startup was incorporated into the TS 4.0.3 bases in 1988 as a result of Generic Letter 87-09, but is not stated in TS 4.3.8.2, which mandates turbine overspeed protection
system testing requirements.
The licensee determined that since performance of this test follows placing the turbine in
service at approximately
15 percent power, overspeed
testing could not be performed within
the required 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following entry into Condition 2.
The amendment to TS 4.0.3 bases
did not recognize this testing constraint and imposed the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> time limit. However, the
licensee failed to recognize this new turbine overspeed
testing requirement.
The licensee has temporarily changed their testing method such that the valves are now cycled
in Condition 4 (Cold Shutdown) prior to placing the unit in startup.
However, the licensee
considers this undesirable due to the potential degradation of the turbine valves which are
cycled without steam pressure to mitigate mechnical shock upon closure.
The preferred
method is with the turbine in service.
Accordingly, the licensee plans to submit a TS change
request which would require turbine overspeed protection system testing within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of
placing the turbine in service, thereby reducing the potential for valve degradation.
The inspector reviewed and discussed
this event with appropriate licensee staff.
As a result,
the inspector found the licensee's actions in response to this event acceptable.
However, a
violation of the licensee's TS did occur as a result of the failure to perform this test within
the required 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following entry into Condition 2.
Since the licensee met the
requirements
stated in 10 CFR 2 Appendix C, Section V.A. and V.G.1, this item is
considered
a non-cited violation.
(NON 50-388/90-26-03).
11
Qgnclusion
Although the above LERs all pertain to missed surveillances,
the causal factors are dissimilar.
The inspector, therefore, concluded that enough dissimilarities between these LERs exist such
that non-cited violations were appropriate for each situation.
Specifically:
the causes for
LER 90-031-00 involved poor shift turnover and inadequate procedural guidance concerning
radiation surveys; the cause for LER 90-009-00 involved an error made in previous
determination of the appropriate frequency in which to perform certain HPCI and RCIC
instrument response time testing; the cause for LER 90-010-00 involved an error placing a
surveillance test for the condensate
transfer system logic onto the out-of-mode list; and, the
cause for LER 90-012-00 involved the failure to recognize that an amendment to a TS bases
resulted in a change in the requirements
to perform turbine overspeed
testing.
In each case,
the licens'ee met the requirements of 10 CFR 2 Appendix C, Sections V.A. and V.G.1.
As
part of the routine resident inspection program, the inspectors will continue to monitor this
area to determine ifthere are programatic weaknesses.
5.
5.1
Inspection Activity
The inspector reviewed licensee event notifications and reporting requirements for events that
could have required entry into the emergency plan.
5.2
Inspection Findings
No events were identified that required emergency plan entry. No inadequacies
were
identified.
6.
SECURITY
6.1
Inspection Activity
PPEcL's implementation of the physical security program was verified on a periodic basis,
including the adequacy of staffing, entry control, alarm stations, and physical boundaries.
These inspection activities were conducted in accordance with NRC inspection procedure
71707.
6.2
Inspection Findings
On a periodic basis, the inspector reviewed access
and egress controls throughout the period.
No unacceptable conditions were noted.
0
12
7.
ENGINEERING/TECHNICALSUPPORT
7.1
Inspection Activity
The inspector periodically reviewed engineering and technical support activities during this
inspection period.
The on-site Technical (Tech) section, along with Nuclear Plant
Engineering (NPE) in Allentown, provided engineering resolution for problems during the
inspection period.
The Tech section generally addressed
the short term resolution of
problems while NPE scheduled modifications and design changes,
as appropriate,
to provide
long lasting problem correction. The inspector verified that problem resolutions were
thorough and addressed
at preventing recurrences.
In addition, the inspector reviewed short
term actions to ensure that the licensee's corrective measures
provided reasonable
assurance
that safe operation could be maintained.
7.2
Inspection Findings
7.2.1
RHR Pump Cooler Failure - Metallurgical Report Review
The inspector reviewed several supplemental
metallurgical reports provided by the licensee
covering their investigation of a leak in the residual heat removal (RHR) pump motor oil
cooler that occurred in May 1990.
(See Inspection Report 50-387/90-10).
These reports
were identified as PLI-64448, PLI-64190 and TML-197-90-002.
The RHR pump motor coolers are fabricated from a single coil of 7/8 inch diameter copper
tubing.
There are 8 coolers (4 per unit).
Emergency Service Water (ESW) flows through
the cooler and is the heat sink for the system.
The ESW system is supplied by a pond with
makeup water coming from the cooling tower blowdown and with additional makeup from
the Susquehanna
River, as needed.
The licensee reviewed the likely failure mechanisms
and concluded that the leakage was
caused by corrosion involving both microbiological induced corrosion (MIC) and under
deposit corrosion.
The inspector also noted that, in addition to examining the failed RHR pump motor cooler,
the licensee examined the remaining seven coolers and two 90-10 copper-nickel RCIC
(reactor core isolation cooling) coolers.
During these additional examinations, similar
corroded conditions as observed in the failed RHR cooler were found, except that no through-
wall leakage had occurred.
Pit depths varied, but in one of the RHR units pit depth was
found to be 35% of the wall, and a pit depth of 60% of the wall was found in one of the
RCIC coolers.
The licensee also noted that during a destructive examination, various internal
deposits had high levels of microbiological activity and contained high levels of sulfate
reducing and acid producing bacteria.
Such indications supported MIC as a major cause of
13
the corrosion.
The corrosive conditions were aggravated by the fact that the ESW was
stagnant between 65 to 75 percent of the time since 1987.
Subsequent
to the event, the licensee replaced all eight RHR coolers with new copper units
and plans to replace the RCIC 90-10 copper-nickel coolers with AL6XN(Ni-Cr-Mo
stainless),
an alloy of superior resistance to MIC. This alloy will also be used to'replace the
tubing in other selected heat exchangers.
In addition, the licensee intends to initiate an 18
month inspection and cleaning program for those components subject to MIC. No
inadequacies
were noted.
7.2.2
Deficiency Reduction Program - Incorrect Assumption Made For 250 VDC
Battery Load Profiles
As part of a comprehensive program to reduce the number and impact of outstanding
deficiencies, the licensee is reviewing all open NCRs, SOORs, and EDRs.
This is being
done as a part of the licensee's overall deficiency reduction program.
In addition to assessing
significance, basis for continued operations,
and the adequacy of schedules for closure of
these deficiencies,
a re-evaluation of the previous reportability determinations
was performed
using current philosophy and NRC guidance.
The licensee's current reporting threshold
emphasizes
the need to evaluate reportability based on the potential adverse consequences
of
these uncorrected deficiencies.
As a result the following item was deemed to meet reporting
thresholds such that had it occurred today, it would have been determined to be reportable
and thus was reported per 10 CFR 50.73.
SOOR 1-89-045 documented
a condition that could have pievented the fulfillmentof the
safety function of the Unit
1 250VDC battery.
This system had no automatic trip features or
procedural controls to ensure the removal of certain non-safety related loads during a station
blackout.
Battery banks ID650 and ID660 are required to provide power to essential loads
during a station blackout.
Overloading these batteries could have prevented the fulfillmentof
the support system safety function for HPCI ~
There was no similar impact on Unit 2 since a
modification was completed in 1982 which installed a non-safety related battery bank for non-
essential loads.
This condition was originally identified on January 26, 1989, but was not reported.
However, based on the new reporting criteria, this postulated single failure event was later
reported via LER 50-387/90-027-00.
At the time this postulated event was identified, the
licensee modified plant procedures ON-104-001, "Unit 1 Response
to Loss of All Offsite
Power," and EO-100-030, "Unit 1 Response
to Station Blackout," to require removing non-
essential loads during a station blackout.
These procedure changes provided reasonable
assurance
that the Unit 1 250 VDC system would perform its safety related support function.
'he inspector reviewed the licensee's actions for this event and noted that the licensee took
prompt compensatory
action to correct the deficiency when it occurred.
The licensee
determined, in 1989, that the event was not reportable since the compensatory
action
ll
C
0
V
14
, corrected the deficiency.
The reporting of this event is due to applying current criteria which
effectively lowered the reporting threshold.
These criteria are a direct result of more
stringent review standards
and have resulted in increased reporting of these types of events.
The inspector had no further questions at this time.
8.1
SAFETY ASSESSMENT/QUALITY VERIFICATION
Licensee Event Reports (LER), Significant Operating Occurrence Report
(SOORs), and Open Item (Ol) Followup (90712, 92700)
8.1.1
Licensee Event Reports
The inspector reviewed LERs submitted to the NRC office to verify that details of the event
were clearly reported, including the accuracy of the description of the cause and the adequacy
of corrective action.
The inspector determined whether further information was required
from the licensee, whether generic implications were involved, and whether the event
warranted onsite followup. The following LERs were reviewed:
Unit
1
90-023-'00
90-024-00
Ninth Fuel Bundle Loaded into Core Before SRM's Verified Operable.
ESF Actuations Due to Opening of 13.8 KV Startup Bus 10 Feeder Breaker.
90-025-00
Spurious Actuation of the RPS While in Cold Shutdown - No Control Rod
Motion Since All Rods Inserted.
90-026-00
Control Structure Ventilation Dampers Could Fail Closed During
LOCA/LOOP. This event was reviewed in NRC Inspection Report No.
50-
387/90-25.
90-027-00
Incorrect Assumption Made For 250 VDC Battery Load Profiles.
This event is
reviewed in Section 7.2.2. of this report.
90-028-00
Postulated Single Failure Could Have Placed the Plant in a Condition Outside
Design Basis.
This event was reviewed in NRC Inspection Report 50-387/90-
15.
90-029-00
"B" Standby Gas Treatment System Unexpected Auto Start.
90-030-00
Entries Into Condition 2 Without Completed Surveillances on Unit 1 and Unit
2.
This event was reviewed in NRC Inspection Report 50-387/90-25.
i
l
1y
15
90-031-00
Technical Specification Required Area Radiation Survey Not Performed.
This
event is reviewed in Section 4.3.1
~ of this report.
+nit 2
90-008-01
Secondary Containment Boundary Poor was Blocked Open.
This report
updates LER 90-008 and provides the results of a radiological evaluation of the
effects of the open door on accident analysis dose estimates.
This event was
initially reviewed in NRC Inspection Report No. 50-388/90-15.
90-009-00
HPCI and RCIC Steam Supply Pressure Low, Response Time Testing Not
Performed Within Required Time Interval.
This event is reviewed in Section
4.3.1. of this report.
90-010-00
Condensate Transfer Pump Discharge Low Pressure Alarm Logic Surveillance
Not Completed Within the Required Monthly Time Interval.
This event is
reviewed in Section 4.3.1. of this report.
90-011-00
RWCU Inboard Containment Isolation Valve Declared Inoperable Due to
Incorrect Torque Switch Setting.
This event was reviewed in NRC Inspection
Report 50-388/90-21.
90-012-00
Surveillances Not Completed Within Allowable Time Following Operational
Condition Changes.
This event is reviewed in Section 4.3.1. of this report.
Except as described in the details of this report, the inspector had no further questions
regarding these matters.
8.1.2. Significant Operating Occurrence Reports
SOORs are provided for problem identification and tracking, short and long term corrective
actions, and reportability evaluations.
The licensee uses SOORs to document and bring to
closure problems identified that may not warrant an LER.
The inspectors reviewed the following SOORs during the period to ascertain whether:
additional followup inspection effort or other NRC response
was warranted; corrective action
discussed in the licensee's report appears appropriate; generic issues are assessed;
and,
prompt notification was made, ifrequired:
~Uni i
33 SOORs, inclusive of 1-90-427 through 1-90-431 and 1-91-001 through 1-91-028.
16
1
iit it 2
30 SOORs, inclusive of 2-90-167 through 2-90-171 and 2-91-001 through 2-91-025.
The following SOORs required inspector followup:
1-91-010
documented
the failure to enter all applicable TS LCOs during a drop in CIG
pressure.
See Section 2.2.2 of this report for details.
2-91-003
documented
the inability to perform surveillances on IRMs and SRMs in
accordance with the unit's TS.
This situation was reviewed in NRC Inspection
Report 50-388/90-25.
2-91-009
documented
an unexpected
isolation of RHR shutdown cooling on January
8.
This event is reviewed in Section 2.2.1. of this report.
Except as described in the details of this report, the inspector had no further questions
regarding these matters.
9.
MANAGEMENTAND EXIT MEETINGS
~
~
~
~
~
~
9.1
Routine Resident Exit and Periodic Meetings
The inspector discussed
the findings of this inspection with station management
throughout
and at the conclusion of the inspection period.
Based on NRC Region I review of this report
and discussions
held with licensee representatives,
it was determined that this report does not
contain information subject to 10 CFR 2.790 restrictions.
7'
Abbreviati n List
ATTACHMENT 1
P
- Administrative Procedure
- Automatic Depressurization
System
ANSI - American Nuclear Standards Institute
- Containment Atmosphere Control
CFR
- Code of Federal Regulations
CIG
- Containment Instrument Gas
- Control Rod Drive
CREOASS - Control Room Emergency Outside Air Supply System
- Diesel Generator
DX
- Direct Expansion
ECCS - Emergency Core Cooling System
- Engineering Discrepancy Report
- Electrical Protection Assembly
ERT
- Event Review Team
- Engineered Safety Features
- Engineering Service Water
- Engineering Work Request
- Fuel Oil.
FSAR - Final Safety Analysis Report
ILRT - Integrated Leak Rate Test
ISAAC
- Instrumentation and Control
JIO
- Justifications for Interim Operation
LCO
- Limiting Condition for Operation
LER
- Licensee Event Report
LLRT - Local Leak Rate Test
- Loss of Coolant Accident
MSIV - Main Steam Isolation Valve
- Non Conformance Report
- Nuclear Department Instruction
NPE
- Nuclear Plant Engineering
- Nuclear Plant Operator
NRC
- Nuclear Regulatory Commission
- Open Item
PC
- Protective Clothing
- Primary Containment Isolation System
PMR
- Plant Modification Request
PORC - Plant Operations Review Committee
- Quality Assurance
RCIC - Reactor Core Isolation Cooling
- Regulatory Guide
- Residual Heat Removal Service Water
SGTS - Standby Gas Treatment System
- Surveillance Procedure,
Instrumentation and Control
- Surveillance Procedure,
Operations
SOOR - Significant Operating Occurrence Report
SPING
- Sample Particulate, Iodine, and Noble Gas
- Source Range Monitor
TS
- Technical Specifications
WA
- Work Authorization
~e