ML17056A149

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SALP Repts 50-220/88-99 & 50-410/88-99 for Mar 1988 - Feb 1989
ML17056A149
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 07/24/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17056A148 List:
References
50-220-88-99-01, 50-220-88-99-1, 50-410-88-99, NUDOCS 8908020385
Download: ML17056A149 (94)


See also: IR 05000220/1988099

Text

ENCLOSURE

1

FINAL SALP

REPORT

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE

INSPECTION

REPORT

NO. 88-99

NIAGARA MOHAWK POWER

CORPORATION

NINE MILE POINT UNITS

1 AND 2

DOCKET NOS. 50-220

and 50-410

ASSESSMENT

PERIOD:

March 1,

1988 to february 28,

1989

BOARD MEETING - April 13,

1989

TABLE OF CONTENTS

I.

INTRODUCTION...............................

~Pa

e

A.

Licensee Activities .....

B.

Direct Inspection

and Review Activities ..............

II.

SUMMARY OF RESULTS ....................

A

Overv>ew

.

~ ......

~

~

~

~

~

~

~

~

0

~

~

~

~

~

~

~

~

B.

Facility Performance

Analysis

Summary ................

C.

Unplanned

Shutdowns,

Plant Trips,

and Forced Outages

.

6

7

III. CRITERIA ........

IV.

PERFORMANCE ANALYSIS

10

A.

Operations

B.

Radiological

and Chemistry Controls

C.'aintenance

and Surveillance

.

D.

Emergency

Preparedness

E..Security

and Safeguards

..

F.

Engineering

and Technical

Support ..

G.

Safety Assessment/guality

Verification

.

10

15

19

25

27

29

32

V.

SUPPORTING

DATA AND SUMMARIES

36

A.

B.

C.

D.

Enforcement Activity

Confirmatory Action Letter ...

Inspection

Hour Summary ............

Licensee

Event Report Causal

Analysi s and

E

Other ............................

Summary ....

36

39

40

41

44

I.

INTRODUCTION

The

Systematic

Assessment

of Licensee

Performance

(SALP)

program is

an

integrated

NRC staff effort to collect the available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

based

upon this

information.

The

SALP program is supplemental

to normal

regulatory pro-

cesses

used to ensure

compliance with NRC rules

and regulations.

The

SALP

program is

intended

to

be sufficiently diagnostic

to provide

a rational

basis for allocating

NRC resources

and to provide meaningful

guidance

to

the licensee's

management

to promote quality and safety of plant construc-

tion and operation.

An

NRC

SALP

Board,

composed

of the staff

members

listed

below,

met

on

April 13,

1989,

to review the collection of performance

observations

and

data

on performance,

and to assess

licensee

performance

in accordance

with

the guidance

in Chapter

NRC-0516,

"Systematic

Assessment

of Licensee

Per-

formance."

A summary of the

guidance

and evaluation criteria is provided

in Section III of this report.

The Board's

findings

and

recommendations

were

forwarded

to

the

NRC

Regional

Administrator

for

approval

and

issuance.

A.

Licensee Activities

Unit

1

The

assessment

period

began

with Unit

1

shut

down

and

defueled.

The

reactor

was shut

down in December

1987

as

a result of

a feedwater

system

induced

transient.

Following the

shutdown,

significant deficiencies

in

the

licensee's

Inservice

Inspection

(ISI)

and

Fire

Protection

Programs

were

identified,

thus

requiring

the

unit to

remain

shut

down

pending

resolution.

Throughout the assessment

period,

the majority of the activities at Unit

1

involved resolution

of the

ISI

and Inservice

Testing

( IST)

Program

con-

cerns,

fire barrier

penetration

concerns,

operator

requalification

and

Emergency

Operating

Procedures

(EOP) training

issues,

and resolution of

additional

specific

issues

outlined

in the

Restart

Action

Plan.

These

issues

are discussed

in further detail

elsewhere

in this assessment.

NRC

Confirmatory Action Letter

(CAL) No.

88-17

was

issued

to

summarize

the

NRC's

overall

concerns

with Unit

1

performance

and

to

formalize

the

licensee's

corrective action commitments prior to Unit

1 restart.

The

CAL was issued

on July 24,

1988

and confirmed three requirements

which

the

licensee

has

committed

to

meet before restart

authorization will be

granted

by the

NRC.

Item one of the

CAL called for Niagara

Mohawk manage-

ment to determine

the root causes

of their problems.

Item two called for

the

licensee

to develop

short-term

and

long-term corrective

actions

to

prevent

recurrence

of these

problems.

To address

these

elements

of the

CAL the licensee

developed

and,provided

to the

NRC

on

December

22, their

Restart

Action Plan

(RAP).

The

RAP was

submitted to the

NRC for review

and approval

and delineates

short-term corrective actions which the licen-

see

must

take

prior

to

Unit

1

restart.

The

NIP

was

made available for review

on site

and

contains

long-term corrective

actions

and additional

programmatic

changes

needed.

At the

end of the

assessment

period.

The

RAP

was still undergoing

NRC review.

The third

item requires

the licensee

to conduct

and document, for NRC staff review,

a self-assessment

of their readiness

to restart Unit 1.

During

the

assessment

period,

major

changes

in

the

licensee's

station

organizational

structure

were

made,

as

well

as

several

key

personnel

changes.

Additionally,

the

new

position

of Executive

Vice

President-

Nuclear

was created

towards

the

end of the assessment

period.

The major-

ity of the other

changes

were at

the site staff

level

and

took

place

throughout the assessment

period.

Unit 2

Early in the

assessment

period,

the licensee

completed

the last

phase of

the Power Asension

Test

Program

and declared

the unit available for com-

mercial

operation

on

March ll, 1988.

The unit operated

at

power until

Ap&l 29,

1988,

when it was

shutdown to support

a three

week planned out-

ag%.

During

power operations

prior to

the

outage,

the unit experienced

two scrams,

one of which was

caused

by personnel

error.

The

three

week

outage

was

completed

and the unit was returned

to power

on

May 22,

1988.

On

May 23,

1988,

a recirculation

pump

seal

leak

caused

a

forced

plant

shutdown.

The

seal

was

repaired

and

the unit

was

returned

to power

on

May 30,

1988.

During

power

operations

through

September

2,

1988,

the

reactor

scrammed

five times.

Two

scrams

were the result of problems with

the

Feedwater

Control

System,

two

were

caused

by deficiencies

in

the

Electrohydraulic Control

(EHC) system,

and personnel

error resulted

in one

additional

scram.

On September

2,

1988,

the licensee

shut the plant

down

due to missed

snubber

surveillance

testing

and

a leak in the cooling coils

of the main generator.

The unit was returned

to power

on September

15,

1988 on single recircula-

tion loop operation

due to binding of the "B" loop recirculation

pump dis-

charge valve.

The unit operated

at power until September

22,

1988,

when

a

reactor

scram resulted

from a loss of Reactor Building Closed

Loop Cooling

due

'to

an

inadequate

plant

impact

assessment

for surveillance

testing.

The unit was returned

to power and operated

at power until the start of a

planned mid-cycle outage which commenced

on October

1,

1988.

The mid-cycle maintenance

and surveillance

outage

was scheduled

to be com-

pleted

by

December

1,

1988.

Outage activities continued

through the

end

of this assessment

period

on

February

28,

1989.

The outage

was

extended

primarily due to containment

isolation- valves failing Appendix J

leakage

testing criteria

and also

due to problems with the

service

water

system

cross-connect

valve

actuation

logic

not

meeting

the

single

failure

criterion.

B.

Direct Ins ection

and Review Activities

Units

1 and

2

An

NRC Senior

Resident

Inspector

was assigned

for the entire

assessment

period.

Previously

assigned

Resident

Inspectors

were

reassigned

and

replaced

in June

and November

1988.

During the

12

month assessment

period,

the

NRC expended

a total of 7756

inspection

hours;

5250

hours at Unit

1

and

2506

hours at Unit 2.

Func-

tional

area distribution

of inspection

hours is documented

at the begin-

ning

of

each

individual

functional

area

and

tabulated

in

Table

2

in

Section

V.C.

During the period,

several

major

NRC team inspections

were conducted,

most

focusing

on Unit

1 as noted below:

During the

month of 'March,

1988,

an inspection of outage activities

at both units was conducted.

The inspection

involved a comprehensive

look at plant maintenance,

modifications

and surveillance at Unit 1,

observation

of a

100% load rejection startup test for Unit 2,

and the

procurement

program

for both

units

with

emphasis

on

purchase

and

dedication of commercial

grade items.

In June,

1988,

an

in-depth

review of the

implementation

and

use of

Emergency

Operating

Procedures

(EOPs)

was

conducted

by

NRC license

examiners

and

by

NRC contractors.

The inspection

focused

mainly

on

Unit

1

EOPs,

but

as

a result of significant deficiencies

identified

'n

Unit

1

EOPs,

the

inspection

was

expanded

to include

Unit 2,

as

well.

For three

weeks in September

and October,

1988,

a Safety

System

Func-

tional Inspection

(SSFI)

was conducted

by

NRC inspectors

and contrac-

tors.

The

inspection

involved

an

in-depth

examination

of the

Core

Spray

System

and

High Pressure

Coolant Injection

(HPCI)

mode of the

feedwater

system.

0

In November,

1988,

a

one

week inspection

was

conducted

to determine

the status

of implementation

of Regulatory

Guide

1.97

"Instrumenta-

tion for Light Water

Cooled

Nuclear

Power Plants to Assess

Plant and

Environmental

Conditions during. and following an Accident", at

both

units.

In

December,

1988,

a

two week Maintenance

Team Inspection

was

con-

ducted at both units

by

NRC inspectors.

The

inspection

focused

on

all

aspects

of maintenance

activities

ranging

from engineering

sup-

port to observation of activities in the field.

In

December,

1988,

a

team

inspection

was

performed

to

examine

the

status of the licensee's

Inservice Inspection (ISI) program at Unit

1

to determine if corrective

actions

were satisfactory

in response

to

previously identified deficiencies.

At the

end of the

assessment

period,

a Special

Team Inspection

(STI)

comprising

NRC personnel

and contractors

was conducted

on site and at

the

corporate

engineering

office.

Overall

focus of the

inspection

was to assess

the effectiveness

of managemert

controls

and oversight

mechanisms

in various

key functional areas.

Various

other

inspections

were

conducted

throughout

the

assessment

period by

NRC resident

inspectors,

Region I and

Headquarters

person-

nel

and

by

NRC contractors.

Most of these

were combined inspections

of a more routine nature

as

opposed

to the comprehensive

team inspec-

tions.

An exception to this was

a special

inspection

by the resident

inspectors

of wiring problems

associated

with the Automatic Oepress-

urization System

(ADS) at Unit 2.

This report is the

NRC's assessment'f

the licensee's

safety

performance

at Nine Mile Point Units

1

and

2 for the period of March 1,

1988 through

February

28,

1989.

The

SALP Board for Nine Mile Point Units

1 & 2:

TITLE

W.

Kane (Chairman)

RE

Capra

R. Conte

J

W. Cook

.

J.

Johnson

W. Johnston

M. Knapp

M. Slosson

E. Wenzinger

Director, Division of Reactor Projects

(DRP)

Director, Project Directorate

No. I-l, NRR

Chief,

Boiling

Water

Reactor

Section,

Division

of

Reactor Safety

(DRS)

Senior

Resident

Inspector,

Nine Mile Point

1

and

2,

ORP

Chief, Projects

Section

2C,

ORP

Deputy Director,

ORS

Director, Division of Radiation Safety

and

Safeguards

(DRSS)

Project Manager,

Nine Mile Point

1 and 2,

NRR

'hief,

Projects

Branch 2,

ORP

Attendees (non-voting)

M.

R.

R.

A.

D.

J.

M.

W.

R.

R.

V.

M.

M.

R.

Banerjee

Barkley

Bellamy

Finkel

Fl orek

Furi a-

Hunemiller

Lancaster

Laura.

Loesch.

McCree.

Pasciak

Shanbaky

Temps'roject

Engineer,

Projects

Section

2C,

DRP

Reactor Engineer,

Projects

Section

2C,

DRP

Chief,

FRSS Branch,

DRSS

Senior Reactor Engineer,

DRS

Senior Operations

Engineer,

DRS

Radiation Specialist,

DRSS

Project Engineer,

NRR

Physical Security Inspector,

DRS

Resident

Inspector,

Nine

Mile Point

1

and

2,

DRP

Radiation Specialist,

DRSS

Project Engineer,

NRR

Chief,

ERPS,

DRSS

Chief,

FRPS,

DRSS

Resident

Inspector,

Nine

Mile Point

1

and

2,

DRP

SUMMARY OF RESULTS

A.

Overview

Overall

licensee

performance

during this assessment

period

has

not

shown

significant

improvement.

Even

though

the

functional

areas

of Security

Safeguards

and

Emergency

Preparedness

continue

to

be

rated

highly,

the

regainder

of the functional

areas

have

shown

marginal, if any,

improve-

ment, or have declined.

In the area of Unit

1 Operations,

early in the asse"sment

period the poor

performance

by licensed operators

as reflected

in their understanding

and

ability to implement the

new Emergency Operating

Procedures

indicated both

poor training and

a complacency with respect

to the adequacy of the train-

ing received.

Evidence of a strained

relationship

between

the Operations

and Training Departments

also

was acknowledged

during the previous assess-

ment period.

Actions

taken

during this

assessment

period to

remedy

the

situation were not successful.

This lack of effective

change

in operator

attitudes

toward training

and

the ineffective station

management initia-

tives to deal

with this situation

continue

to

be significant concerns

to

the

NRC.

In the areas

of Unit 2 Operations,

and Maintenance

and Surveillance,

the

high rate of personnel

errors

by both the

licensed

and

unlicensed

staff

and

maintenance

and

testing

personnel

continued

during this

assessment

period.

Station

and

corporate

management

efforts

to

reduce

or minimize

the frequent

safety

system

challenges

and plant transients

have

not

been

effective.

Likewise,

the direct support

to the

station

provided

by the

Engineering

Department staff has

been

inconsistent

and

not reflective of

an

overall

goal

to

improve

performance

and

enhance

long

term

station

reliability and safety.

This appears

to

be reflective of low performance

expectations

in that it is a newly licensed facility.

Corporate

and sta-

tion

management

should

assure

that

the current level of performance

for

Unit 2 is not acceptable

in light of the large

number

of unplanned trips

'and shutdowns.

The

NRC acknowledges

the licensee's

commitment to

a comprehensive

Nuclear

Improvement

Program

which

addresses

the

root

causes

and

provides

the

essential

elements

to effect overall

performance

improvements.

The

NRC

also acknowledges

the licensee's

recent

management

changes

made to provide

the

necessary

leadership

to the Nuclear Division to ensure

a thorough

and

successful

implementation

of this

Program.

These

changes

are

viewed

as

significant,

however,

because

they were

made late in the assessment

period

their effectiveness

has not been reflected in this assessment.

B.

Facilit

Performance

Anal sis

Summar

Last Period Dates

Unit

1

11/1/86 - 2/29/88

Unit 2

2/1/87

2/29/88

Present Period'ates

Unit

1

3/1/88

- 2/28/89

Unit 2

3/1/88

- 2/28/89

Functional

Category

Last

Area

Period

Category Thi s

Trend

Period

Trend

1.

Operations

1.

Unit

1

2.

Unit 2

2.

Radiological Controls

and Chemistry

3.

Maintenance

and

Surveillance

4.

Emergency

Preparedness

5.

Security and Safeguards

2

3

2

~ .....

improving

3

2 ...... declining

2

(2/2)

6.

Engineering

and

Technical

Support

7.

Safety Assessment/

Quality Verification

3 .....

improving

8.

Licensing

2 ..... declining

N/A

9.

Training and gualification

Effectiveness

N/A

10.

Assurance

of guality

N/A

N/A Indicates that the category

was not rated this period.

" .... This functional area

was not assessed

C.

Un lanned

Shutdowns

Plant Tri

s and Forced

Outa es

1.

Unit

1

Date/Event

6/25/88

Automatic Scram

2.

Until: 2

Power

Level

0%

Descri tion

Reactor

scram signal

due to lower than

normal voltage

on

protective bus.

Cause

Lightning

Strike,

See

LER

88-15

Functional

Area

N/A

Date/Event

Power

Level

Oescri tion

Cause

Functional

Area

3/13/88

Automatic Scram

43%

Low reactor water

level, due to failed

pressure

transmitter

and poor design.

Equipment Failure

ENG/TS

and Design

Deficiency,

See

LER 88-14

3/21/88

Automatic Scram

97.5%

Loop calibration

on

feedwater flow

transmitters

Personnel

error,

Inadequate

Plant

Assessment,

See

LER

88-17

MAINT/SU RV

and

OPS

5/23/88

Forced

Shutdown

6/2/88

Automatic Scram

50/

25.5%

Recirculation

pump seal

leak

High reactor

vessel

water level, failure

of feedwater control

valve feedback

linkage

Personnel

Error, due to

improper

installation

Equipment

Failure,

due to

design error,

See

LER 88-19

MAINT

ENG/TS

(SHUTDOWNS CONTINUED)

Date/Event

Power

Level

Descri tion

Cause

Functional

Area

6/22/88

Automatic Scram

98%

Low reactor water

level, feedwater

level control valve

ramp closed

Manufacturing

SAFETY/EQUAL

design

deficiency,

See

LER 88-25

6/28/88

Automatic Scram

7/11/88

Manual Scram

8/6/88

Automatic Scram

9%

45%

53%

APRM Upscale trip

during start-up

EHC oil leak

Loss of

EHC system

pressure

due to

piping failure caused

by excessive

vibration

Personnel

error, not

controlling

steam

loads

properly,

See

LER

88-26

Personnel

error

(Fitting

not properly

torqued),

See

LER

88-28

Design

deficiency,

due to inadequate

support,

See

LER

88-39

OPS

MAINT

ENG/TS

9/2/88

Forced

Outage

100%

Generator stator

cooling water leak

Missed snubber

testing

Equi pment Fai lure

N/A

Personnel

error,

ENG/TS

See

LER 88-40

9/22/88

Manual Scram

12/1/88

Automatic Scram while

shutdown

98%

0%

Loss of service

water

ARI system actuation

during survei1 lance

testing

Personnel

error,

inadequate

assessment

of

plant impact

Design

deficiency

See

LER

88-66

OPS

ENG/TS

III. CRITERIA

Licensee

performance

is assessed

in selected

functional

areas,

depending

on whether the facility is under construction

or operational.

Functional

areas

normally

represent

areas

significant

to

nuclear

safety

and

the

environment.

Some functional

areas

may not

be assessed

because

of little

or

no licensee

activities or lack of meaningful

observations.

Special

areas

may be

added to highlight significant observations.

The following evaluation criteria were used,

as applicable,

to assess

each

functional area:

1.

2.

6.

7.

Assurance of quality, including management

involvement and control.

Approach to the resolution of technical

issues

from a safety

stand-

point.

Responsiveness

to

NRC initiatives.

Enforcement history.

Operational

and construction

events

(including response

to, analyses

of, reporting of, and corrective actions for).

Staffing (including management).

Effectiveness

of training and qualification programs.

On'he

basi s'f

the

NRC

assessment,

each

functional

area

evaluated

i s

rated

according to three

performance

categories.

The definitions of these

performance

categories

are

as follows:

~Cate or l.

Licensee

management

attention

and

involvement

are

readily

evident

and

place

emphasis

on

superior

performance

of nuclear

safety

or

safeguards

activities,

with

the

resulting

performance

substantially

exceeding

regulatory

requirements.

Licensee

resources

are

ample

and ef-

fectively used

so that

a high level of plant

and

personnel

performance

is

being achieved.

Reduced

NRC attention

may be appropriate.

~Cate or

2.

Licensee

management

attention

to and

involvement in the per-

formance of nuclear safety or safeguards

activities

are

good.

The licen-

see

has attained

a level of performance

above that needed

to meet regula-

tory requirements.

Licensee

resources

are

adequate

and

reasonably

allo-

cated

so that good plant and personnel

performance is being achieved.

NRC

attention

may be maintained at normal levels.

~Cate or

3.

Licensee

management

attention

to or involvement

in the per-

formance

of nuclear

safety

or

safeguards

activities

are

not sufficient.

The licensee's

performance

does

not significantly

exceed

that

needed

to

meet

minimum regulatory

requirements.

Licensee

resources

appear

to

be

strained or not effectively used.

NRC attention

should

be increased

above

normal levels.

10

The

SALP Board

may assess

a functional area to compare

the licensee's

per-

formance during the last quarter of the

assessment

period to that during

the entire

period

inorder to determine

the

recent

trend.

The trend if

used, is defined as:

~lm rovin

Licensee

performance

was determined

to

be

improving near

the

close of the assessment

period.

~geclinin

Licensee

performance

was determined

to

be declining

near

the

close of the assessment

period.

A trend is assigned

only when, in the opinion of the

SALP Board, the trend

is significant

enough

to

be considered

indicative of

a likely change

in

the

performance

category

in the

near future.

For example,

a classifica-

tion of "Category 2,

Improving" indicates

the clear potential

for "Cate-

gory 1" performance

in the next

SALP period.

It

should

be

noted

that

Category

3

performance,

the

lowest

category,

represents

acceptable,

although

minimally adequate,

safety

performance.

If at any time the

NRC concluded that

a licensee

was not achieving

an ade-

quate

level of safety

performance, it would then

be incumbent

upon

NRC to

take

prompt

appropriate

actions

in

the

interest

of public

health

and

sa'fety.

Such

matters

would

be dealt with independently

from,

and

on

a

more urgent

schedule

than,

the

SALP process.

It should

also

be noted that the industry continues

to be subject to ris-

ing performance

expectations.

NRC expects

licensees

to use industry-wide

and plant-specific

operating

experience

actively in order to effect per-

formance

improvement.

Thus,

a

licensee's

safety

performance

would

be

expected

to

show

improvement

over the years

in order to maintain consis-

tent

SALP ratings.

IV.

PERFORMANCE ANALYSIS

A.

~0erati one

1.

~Anal sis

(2274 hours0.0263 days <br />0.632 hours <br />0.00376 weeks <br />8.65257e-4 months <br />,

29.3%)

Unit

1

(1464 hours0.0169 days <br />0.407 hours <br />0.00242 weeks <br />5.57052e-4 months <br />,

18.9%)

4

In

the

last

assessment

period,

performance

in this

area

showed little

improvement

and was rated Category

2.

Contributing to that rating was

the

noted

complacency

of operators

with respect

to overall station quality of

operations.

During the last assessment

the

NRC staff identified the

need

for corporate

and

station

management

to provide positive

incentives

to

revitalize, motivate

and better integrate

the Operations

staff with other

departments.

11

During this

assessment

period,

the unit remained

shut

down

and defueled,

thereby

prohibiting

assessment

of operators'erformance

for

at-power

operations.

However,

observations

of Operations

staff

support

of major

maintenance,

modification

and testing activities (including defueling

of

the vessel)

indicated technical

competence

and

a

good level of knowledge

of systems

operation

during the

plant

shut

down.

This

was particularly

evident

during

the

Safety

System

Functional

Inspection

conducted

in

September

1988 in the operators'upport

provided to the inspection

team.

Personnel

errors

by Unit

1 operators

were

infrequent

and

isolated

this

assessment

period.

Efforts by management

to better integrate

the Operations staff with other

departments

have

been

made during this assessment

period.

These efforts

included; initiation of the Operators

Training

Program Advisory Committee

.(OTPAC)

and

interface

meetings

between

the

Operations

and

the Training

departments;

assignment

of

oversight

responsibility

for

the

Licensed

Operator

Requalification

Training

Program

to the

Operations

Superinten-

dent; rotational

assignments

of Reactor

Operator s

(RO)

and Senior

Reactor

Operators

(SRO)

to

the Training

Department;

and

special

assignments

of

licensed

operators

to the

Maintenance

and

Engineering

staff,

as

needed

during

outages.

While several

of these

efforts

have

not

been

in place

long

enough

to provide

evaluative

results,

the

OTPAC

was

viewed

as

a

. positive step to resolve

longstanding

problems

and

has

been generally well

received

by the operators.

One area

requiring continued

management

attention

was the matter of oper-

ators'ttitude

towards

continued

training

as

demonstrated

by their

behavior

during training

sessions.

Specific

instances

of

abusive

and

disruptive behavior

by licensed

individuals during requalification train-

ing were noted by the

NRC,

as well as

NHPC management.

There continued

to

be

resistance

by

some

operators

towards

integration

with the training

department.

In addition,

station

management's

efforts to

improve

oper a-

tors'ttitude

and

performance

were ineffective.

This concern

was iden-

tified in the previous

SALP

and continues

to

be

a significant concern

to

the

NRC.

During this

assessment

period,

the

NRC identified that Unit

1 operators

were

not

attending

the

requalification

classes

as

required.

Senior

management

was

not

ensuring

that all requalification

requirements

were

completed prior to submitting

licensed

operator

renewal

applications.

A

review of the

Licensed

Operator Requalification Training Program revealed

that

39 licensed

operators

had not completed

the required training prior

to the

end of the

annual

requalification period.

In addition, deficien-

cies

were

noted

in

the facility senior

management

involvement

in

the

requalification program,

in that the operator

renewal

license applications

contained

inaccurate

" information

concerning

the

completion

of

the

12

requalification

program requirements.

These deficiencies

led to the issu-

ance of Confirmatory Action Letter

(CAL) 88-13

which identified actions

that were to

be taken to correct the deficiencies.

Subsequent

inspection

showed that the licensee

had completed

the

immediate

actions

necessary

to

comply with CAL 88-13.

During the inspection of the Unit 1 Emergency Operating

Procedures

(EOPs),

the

NRC observed

that

the

more

experienced

operators

were

not

able

to

adequately

use

the

EOPs.

The operations

crew observed

could not properly

implement the

EOPs

and lacked

an understanding

of the basis for the

EOPs.

Specific

EOP training deficiencies

included:

a fundamental

understanding

of the

EOPs,

the understanding

of the accident mitigation strategies,

the

ability to implement

the

EOPs,

poor team work and communications,

and the

recognition of emergency

system status

and degraded

plant conditions.

The

inspection

determined

that the

EOPs

were generally well written

and use-

able.

The lack of operator familiarity of the

EOPs

was

due to inadequate

training

during

requalification

and

the

lack of operations

management

involvement in assuring

the training

was effective.

It was

subsequently

identified that licensed

operators

had

expressed

concerns

to station

man-

agement

about the quality and quantity of training

on the

new

EOPs.

How-

ever,

neither the operators

or station

management

pursued

these

concerns

to appropriate

resolution until it became

a regulatory concern.

In

summary,

the

Unit

1

Operations

concerns

raised

during

the

previous

assessment,

with respect

to opera'or

complacency

and the strained

rela-

ti5nship with the Training Department,

were not adequately

addressed

this

assessment

period

and continue to

be of major concern to the

NRC.

Opera-

tors'ttitude

have

not significantly

changed

and

station

management's

efforts

have

been

unsuccessful

in dealing with these

concerns.

However,

it is noted that

subsequent

to the

end of this assessment

period discip-

linary action

was

taken

against

certain

individuals

in the

Operations

Department indicating that certain patterns of behavior

would no longer be

tolerated.

Unit 2

(810 hours0.00938 days <br />0.225 hours <br />0.00134 weeks <br />3.08205e-4 months <br />,

10.4%)

This

area

was

rated

Category

2 (Improving) in the

previous

assessment.

During that asessment

period,

the licensee

had

progressed

through initial

criticality and

the majority of Test Condition

6 of the

Power Ascension

Testing Program.

Minor weaknesses

were noted in the control

room environ-

ment,

the control of operator

aids,

the lack of familiarity of operators

with emergency

equipment location, the lack of emergency

diesel

generator

operating

logs

and the lack of an efficient method of tracking the oper-

ating time on special filter trains for the

purpose

of meeting Technical

Specifications

sampling

requirements.

A

more

significant

weakness

was

'(

13

identified in the

area of operator attention to detail

as demonstrated

by

numerous

personnel

errors

and procedural

compliance violations.

Improve-

ment was

noted

in the

area of operations

management

oversight of day-to-

day activities,

communications

and

responsiveness

to identified concerns.

In addition,

Operations

Department

support

of the

Power

Ascension

Test

Program

was both enthusiastic

and professional.

Operator

conduct of test-

ing

was

cautious

and

response

to

testing

anomalies

was

prompt

and

conservative.

Personnel

errors

continued

to occur at

a high rate during this assessment

period.

The majority of these errors were caused

by inattention to detail

or failure to follow procedures.

An inadequate

plant

impact assessment

for the performance of a loop calibration

on

a feedwater

flow transmitter

resulted

in the 3/21/88

scram.

Improper operator

control of steam

loads

during start-up

resulted

in the 6/28/88 reactor

scram.

Improper

assess-

ment of the

impact of cycling of a service water alternate

cooling outlet

valve

on

a spent

fuel

pool cooling heat

exchanger

resulted

in

a

loss of

Reactor Building Closed

Loop Cooling water

and

a manual scram

on 9/22/88.

Several

personnel

error s were

made during the work release

process,

which

resulted

in inadvertent

Engineered

Safety Features

actuations,

a spill of

1000 gallons of acid,

and

a temporary

loss of shutdown

cooling.

Although

these

personnel

errors

relevant

to the work release

process

resulted

in

events

of relatively minor safety significance,

the potential

effects

of

these

types of er> ors could result in more serious

problems.

Other miscellaneous

personnel

errors

occurred

during this assessment

per-

iod.

For example,

during the

performance

of

a monthly surveillance test,

an operator

performed

a switch line-up incorrectly which resulted

in a

Low

Pressure

Coolant Injection to the reactor

vessel.

Another error occurred

while securing

from an

Emergency. Diesel Generator

(EDG) surveillance test.

An operator inadvertently

opened

the offsite

power

breaker

instead

of the

EDG output breaker.

This broad

spectrum of personnel

errors exemplifies the lack of attention

to detail

and failure to follow procedures.

As

noted

i.n

the

previous

assessment

period

and

as 'discussed

above,

numerous

personnel

errors

con-

tinue to

be

experienced

by the

licensee.

Corrective

actions,

to date,

have

not

been

effective

in reducing

the

number of errors.

This lack of

effective corrective

action

to

reverse

this

trend

indicates

inadequate

management

response

to

an identified concern

and inadequate

assessment

of

the

root

causes.

More significantly,

these

continuing

personnel

errors

represent

station

and

corporate

management's

low

expectations

and

acceptance

of the present

level of employee

performance.

14

Other observations

of control

room activities indicate that the operators

are

experienced,

knowledgeable

and alert

to

off-normal

indications

or

potential

problems.

An example of this

was the performance

of Automatic

Depressurization

System

(ADS) testing

during this assessment

period.

The

control

room operators

and

technicians

conducting

the test

identified

a

significant

system wiring error that effectively disabled

the Division I

ADS and which had gone undetected

since initial fuel load.

Control

room formality was

observed

to be satisfactory;

however, there is

a large

number

(approximately

50-60)

of lit annunciators

in the control

room that exist during

normal

plant operations

and

which

could

mask

a

potential

problem.

This also reflects

an environment that accepts

a

low

standard.

The licensee

does

have

a

program to reduce

the

number of nor-

mally lit annunciators,

but progress

to date

has

been

slow.

More emphasis

should

be

placed

on . this

item

by

station

and

Engineering

Department

management.

Evidence exists

to demonstrate

that Operations

management

has

become

more

involved

and aggressive

in improving the operations

staff training,

pro-

fessional

development,

and

working environment.

Examples

include:

min-

imization

of overtime;

successful

negotiation

for five additional

SRO

positions;

approval

of

an

SRO

inter-departmental

rotation

policy for

career

development;

increased

training for non-licensed

operators,

includ-

ing simulator training;

and the development

of an improved equipment mark-

upmnstruction

for the Operations

Department.

An

example

of the

Opera-

tions staff

being

proactive

involves

the

implementation

of

BMR

Owners'roup

recommendations

for actions

to take

when experiencing

power

osci 1-

lations

subsequent

to

a recirculation

pump trip.

Procedures

were revised

and operators

trained well in advance

of the

NRC Bulletin being

issued.

The

concern

identified

at

Unit

1

regarding

operators'nability

to

understand

and

adequately

use

the

Emergency

Operating

Procedures

(EOPs)

did not exist at Unit 2 when

the Unit 2 operators

were

subjected

to the

same

type of scenarios.

The major difference

was

determined

to

be that

the Unit 2 operators

were

accustomed

to the

EOPs

as part of their initial

license

training

and

conduct

more

frequent

training

on

EOPs

in

the

Requalification Training Program.

In

summary,

the Unit 2 Operations

Department

is staffed with experienced

and competent

personnel;

however, closer attention to detail

by operations

staff

and

licensed

operators

is

needed

to

stem

the

numerous

personnel

errors.

More importantly, station

and

corporate

management's

performance

expectations

were

too

low and

have resulted

in complacency

as exemplified

by

the

overall

poor

performance

trend

during

this

assessment

period.

15

2.

Performance

Ratin

Category:

Unit

1 - 3

Unit 2 - 3

3.

Board Recommendations:

NRC:

Licensee:

Restart

Panel

continue to monitor licensee

performance

and assist

in directing

NRC inspection efforts at

NMP.

Unit

1 -

(See

note below)

Unit 2 Raise

performance

expectations

of the Unit 2

Operations

Department

and

closely

monitor

progress.

Develop

and

implement

a detailed

and timely

plan

to

reduce

the

number of lit annuncia-

tors

on the main control panel.

Note:

. No specific

recommendations

have

been

made for this or any

. other

functional

area, if it is addressed

in the licensee

corrective

actions

documented

in the

Restart

Action

Plan

and Nuclear

Improvement

Program

which have

encompassed

the

major areas

of concern to the

NRC.

B.

Radiolo ical

and Chemistr

Controls

(513 hours0.00594 days <br />0.143 hours <br />8.482143e-4 weeks <br />1.951965e-4 months <br />,

6.6%)

1.

~Anal sis:

The combined

Radiological

Control

Programs

at Nine Mile Point Unit

1 and

Unit 2 were rated

as Category

2 (Declining) during the previous

assessment

period.

Program

weaknesses

identified last

period

indicated

a

need

to

improve supervisory oversight of ongoing work activities; personnel

atten-

tion to detail;

the corrective

action

program

to

ensure

personnel

are

adhering

to

good

radiological

control

practices

and

procedure

require-

ments;

contamination control; ongoing job ALARA reviews

and non-radiolog-

ical water chemistry.

During this

assessment

period,

region-based

inspectors

performed

seven

routine

inspections.

Radiological

controls

were

also

examined

during

a

Maintenance

Team Inspection.

The resident

inspectors

reviewed this area

on

an on-going basis.

16

Radiation Protection

The radiation

protection

program is

common

to both units

and is imple- .

mented

through

two

separate

radiation

protection

groups

reporting

to

a

common

manager

.

During this assessment

period,

the

licensee

implemented

several

personnel

and organizational

changes,

the

most significant being

the

replacement

of the Unit

1

Radiation

Protection

Supervisor

and

the

creation of a dedicated

Site

ALARA Coordinator.

NRC

observations

late this

assessment

period

indicated

that first line

supervisory

oversight

of ongoing

work activities

has

improved

with the

addition of several

new Chief Technicians.

However,

the licensee

failed

to identify, over

an

extended

period of time,

a situation

where

perman-

ently installed ladders

allowed unauthorized

access

to the Radwaste

Sample

Tank Room,

an

area controlled

as

a

Locked High Radiation

Area.

In addi-

tion, the Radiation

Protection

Manager

and the Supervisor of Radiological

Support

had infrequently entered

the Reactor

Buildings indicating

a

con-

tinuing need for additional

management

oversight.

An

adequately

defined

personnel

training

and qualifications

program

is

maintained

and implemented.

For contract

health

physics

technicians,

the

licensee

verifies

experience,

administers

a

screening

exam

to evaluate

technical

background

and

provides

additional

site

specific

training

as

necessary.

The

program

to

maintain

-radiation

protection

personnel

cujaizant of new procedures

and

procedure

changes,

a

weakness

identified

in the previous

assessment

period, is adequate.

The appropriate

personnel

wer e trained

on the requi red procedures

in

a timely manner

and

procedure

adherence

has

improved.

The licensee's

ALARA program

management

has

shown

improvement during the

current assessment

period.

The use of detailed

isometric

diagrams

of the

drywell

helped

reduce

exposures

associated

with locating individual

com-

ponents.

In addition,

improvements

were realized

by the

use of

a

mockup

at Unit

2 in planning corrective

maintenance

on

the recirculation

loop

isolation valve

In response

to

NRC

concerns,

the

site

ALARA program

responsibilities

were transferred

from the Respiratory Protection Coordi-

nator to

a dedicated

Site

ALARA Coordinator.

To strengthen

and

upgrade

the site

ALARA program,

a consultant is currently assessing

the program's

effectiveness

and

recommending

improvements.

Improvements

included

changes

to the Radiation

Exposure

Monitoring System

(REMS),

the addition

of

hold

points

on

jobs

not initially requiring

an

ALARA review,

and

methods

to

reduce

the

person-rem

exposures

associated

with miscellaneous

RWP's.

In addition,

to

improve

corporate

oversight

of

the

program,

a

Health Physicist

from the site

organization

was transferred

to the cor-

porate staff to coordinate

ALARA improvements.

17

Licensee

exposure for 1988 totaled approximately

804 person-rem for Unit

1

(outage year)

and

85 person-rem

for the startup year at Unit 2.

Although

above

the industry's

annual

BWR average

of approximately

500

person-rem,

the

extended

outage

at Unit

1

and significant ISI rework contributed to

the higher exposures.

Licensee

performance

during 1988 was adequate

given

the additional

work scope

and high inplant source

term and

showed improve-

ment during the

second half of the

SALP period.

Goals for 1989

have

been

set aggressively

at

509 person-rem

for Unit

1 and

128 person-rem for Unit

2 (its first full operating year).

Unit

1 continues to suffer from a high

inplant

source

term.

Chemical

decontamination

efforts originally planned

for 1988

have

been

delayed

and is currently

under

consideration

for the

1990

refueling

outage.

These

delays

are

contributing to the

continued

high person-rem

exposures

at Unit l.

Adequate

internal

exposure

controls

and contamination

controls

were pro-

vided for ongoing

work.

Licensee

corrective

actions

and

assurance

of

quality

were

generally

adequate

although

occasional

weaknesses

were

exhibited.

For example,

a review this period of corrective actions

asso-

ciated with a workers ingestion of a hot particle indicated

an aggressive

approach

to both the worker's concerns

and the technical

evaluation of the

existence

of a. discrete particle

and its characteristics.

In contrast,

the

licensee

incorporated

a

new type of respiratory protection

equipment into

the emergency kits without first establishing

and

implementing

the

neces-

sary procedures.

The

licensee

took actions

to

improve

intra-departmental

coordination of

work activities.

A Work Control Center

was established

at Unit

1 for the

processing

of all

work requests

and

a

dedicated

Health

Physics

Planner

provides

a single interface with the Radiation

Protection

(RP) department

in the

processing

of required

Radiation

Work Permits

and

pre-job

ALARA

reviews.

In addition,

two

RP liaisons

were assigned

to the Unit

1 Mainten-

ance department

to coordinate on-the-job support of work activities.

These

licensee

initiatives

have

improved

the

coordination

of work activities

with the

RP group during the Unit

1 extended

outage.

Radioactive Effluent Controls

The program for Unit

1 was evaluated

in the

areas

of instrument calibra-

tion, release

permits,

the Off-Site Dose Calculation

Manual

and the

semi-

annual

effluent

reports,

and

found to

be effectively

implemented.

The

program for Unit 2 has

shown

improvement

from the last

assessment

period.

As identified in the

previous

SALP, operability of the

Gaseous

Effluent

Monitoring System

(GEMS)

has

been

a continuing

problem at Unit 2.

Fur-

ther, alternate

methods for gaseous

effluent monitoring when the

GEMS was

inoperable

had

been lacking.

The licensee

has taken action to improve the

18

operability of the

GEMS and

has

developed

and

implemented

procedures

for

alternate

monitoring

methods

when

the

GEMS

is

inoperable.

During

the

assessment

period there

were

no unplanned effluent releases,

and

planned

releases

were at levels

normal for a Boiling Water Reactor site.

Radiolo ical Environmental Monitorin

Pro

ram

The

licensee

has

contracted

with

a

vendor

laboratory

to

perform

the

analysis

of environmental

samples

required for the Radiological

Environ-

mental Monitoring Program

(REMP).

The licensee's

environmental

dosimetry

program results

show

good

agreement

with both the State of

New York and

NRC environmental

dosimeters.

Audits in this

area

of both

the

vendor

laboratory

and

the

REMP were

found to

be thorough,

with all

recommenda-

tions addressed

in a timely manner.

~Trans ortation

The transportation

program is conducted

by a site Materials Shipping group

which has

shown significant improvement

since the hiring of a group super-

visor during the

second half of the

SALP period.

Filling of this position

has

led to additional

management

review of shipments

prior to leaving the

site,

which reduces

the

chances

of errors while shipping.

There

were

no

ma'jor problems

noted during this period.

The licensee

is in the

process

of implementing

the=use of a computer code for the purposes

of determining

traRsportation

and

waste

classification

which will further

enhance

this

program by reducing calcu2ational

errors.

Solid Radioactive

Waste

Each unit at the site continues

to maintain its

own

program for the pro-

cessing

and

packaging

of radwaste.

Although

these

two programs utilize

separate

vendors

and processes,

each

has continued to improve its program.

Continued

developments

by both units in the

area of waste solidification

will 'further

enhance

these

programs.

Audits

by

the

licensee's

quality

assurance

department

were thorough,

with all recommendations

addressed

in

a timely manner.

During this assessment

period

the licensee

could not account for several

small,

non-irradiated,

local

power

range

monitor fission

chambers.

The

licensee

identified that this

small

amount

of special

nuclear

material

was missing

as

a result of an annual audit,

and believes that the fission

chambers

were disposed

of with radioactive

waste.

The discovery

of the

missing

material

is

commended;

however,

the

loss

is reflective

of

a

previously ineffective special

nuclear material control program.

19

Overall

Summar

The

licensee

made

several

enhancements

to

address

previously identified

weaknesses

and

the overall

program

has

shown

steady

improvement

over the

SALP period.

Observations

indicate that

although

supervisory

oversight

of ongoing work has

improved,

RP

management

oversight is weak.

In addi-

tion, significant licensee initiatives which began

late in the

assessment

period

are

expected

to

improve accountability

and oversight

of ongoing

work.

2.

Performance

Ratin

Category:

2

3.

Board Recommendations:

NRC:

None

Licensee:

Place

more emphasis

on Unit

1 decontamination

C.

Maintenance

and Surveillance

(2639 hours0.0305 days <br />0.733 hours <br />0.00436 weeks <br />0.001 months <br />,

34%)

l.'Anal sis

Dumng

the

previous

assessment

period,

the

maintenance

and surveillance

alas

were evaluated 'separately

and

each

area

was rated

Category

2.

For

this assessment

both functional areas

have

been

combined

and

one category

rating is assigned.

During this assessment

period

the licensee

transferred

the responsibility

for the Instrumentation

and Controls (IEC) organization

from the Technical

Superintendent

to

the

Maintenance

Superintendent

as

part

of

a station

reorganization.

The Unit

1

and

Unit

2

Maintenance

Superintendents

and

Unit Supervisors

presently

have

a

dual

reporting'esponsibility

to the

Site

Superintendent

of

Maintenance

and

the

Station

Superintendents

of

Units

1 and 2.

Maintenance

Unit

1 and

2

During the last

assessment,

improvement

in first line supervisory

over-

sight and higher visibility and interaction of senior

maintenance

manage-

ment

in the field were

noted.

Root

cause

evaluations

and attention

to

detail

in maintenance

implementation

were

noted

as

weaknesses,

but were

showing signs of improvement.

20

Improved

management

involvement in housekeeping,

selective observation of

work in progress

and interface

and

feedback

meetings with craft personnel

indicated

management's

contribution to

an overall effectively implemented

maintenance

program

this

assessment

period.

Maintenance

Department

management

benefits

from

experienced

and

knowledgeable

personnel

who

provide continuity by their long term involvement

and

low turnover rate.

Contractor

maintenance

work

was

effectively controlled;

however,

weak-

nesses

existed in the

type of checklist

used for the surveillance

of the

contractors.

A system for maintenance

trending

and performing root cause

analysis

has

been

established

with both

corporate

and

site

personnel

trained

in the analysis

techniques.

The Nuclear Engineering Organization

has

established

a central

program

to evaluate

the effectiveness

of the

maintenance

program.

In addition to

a

sound corrective

and preventive

maintenance

program

the

licensee

has initiated

the

increased

use

of predictive

and

diagnostic

techniques.

A rotating

equipment

vibration analysis

program

and

use of

infrared thermography

techniques

are

among

the

new techniques

being

used.

An additional initiative developed

is the functional work control program.

Work is

being

planned,

prioritized

and

scheduled

in

accordance

with

directives.

Backlog monitoring

has

been

established

through

the

use of

ma'intenance

performance

indicators

and the work tracking system.

De~ite

these

initiatives,

weaknesses

in procedural

adequacy

and compli-

anCe

were

observed

this assessment

period.

The written periodic mainten-

ance

program did not appear

to include all vendor recommendations

and

some

of the periodic

maintenance

activities

were

being

performed without the

benefit of written guidance.

A review of Unit

1 waste

surge tank

pump

and

diesel fire pump

and Unit 2 emergency

diesel

generator

maintenance

indi-

cates

procedures

were either

not being complied with or were poorly writ-

ten.

Some

maintenance

personnel

appeared

to

be insufficiently trained to

properly

implement

these

procedures

or

change

them if necessary.

The

maintenance

personnel

continuing training

program

was

also

found to

be

lacking

and

inconsistently

implemented.

Concerns

regarding

procedural

compliance

were brought to the licensee's

attention early in the assess-

ment period

and periodically thereafter.

However,

the

licensee

did not

take prompt and effective action to reverse this trend.

Another

weakness

that

continues

to exist is in the area

of followup and

correction of previously identified problems.

An example

was poor follow-

up

on the maintenance

self-assessment

performed

in 1987.

A licensee

audit

identified that

no

program or responsible

organization

was

made

account-

able

for

reviewing

maintenance

self-assessment

item

resolutions

and

recommending corrective actions.

21

In contrast

to the weaknesses

addressed

above,

the repair of the recircu-

lation loop isolation valve at Unit 2 was

an example of a well planned

and

executed

maintenance activity.

The licensee

utilized

a

mock-up to ensure

proficiency

during

the

actual

maintenance

and

to fine

tune

the

work

instructions.

No significant problems

were encountered

physically or pro-

cedurally.

During the last assessment,

problems in the area of repetitive

equipment failure due to

inadequate

root

cause

determination

were

docu-

mented,

In this

assessment

period,

no

problems

of this

nature

were

observed.

During this

assessment

period

several

deficiencies

were noted with house-

keeping,

in particular with the material

condition of the

HPCI/FW, shut-

down cooling and core spray

systems at Unit 1.

In addition,

the

237 foot

elevation of Unit I reactor building including the entrance

to the drywell

and

the

CRD hydraulic

control

units

area

were

in

poor

condition

and

inhibited routine tours by plant personnel.

Typically the remote

areas

of

the plants

and the high work areas

have

been of concern;

however,

overall

improvements

in housekeeping

were

observed

during this assessment

period.

For

example,

the

condenser

bay

and

refueling

floor

areas

were

much

improved.

Increased

management

and

station

employee

attention

to this

area

was evident.

Su'rveillance - Unit I

Dumng

the

previous

assessment

period,

the

Technical

Specification

sur-

"vetllance testing

program

was

determined

to

have

been effectively imple-

mented

with only minor

problems

identified.

However,

numerous

problems

identified in the Inservice Inspection

( ISI) Program demonstrated

the

need

to strengthen

corporate

and station

management

oversight of the

program.

During this

assessment

period,

missed

surveillance tests

and surveillance

related

problems

remained at

a low level.

Licensee corrective actions for

the

known ISI problems

resulted

in the identification of more ISI Program

deficiencies.

Additionally, 'problems

were identified by the

licensee

in

the

Inservice

Testing

(IST) Program this assessment

period.

Problems

in

the ISI and

IST Programs

are attributed to past

management

ineffectiveness

in the oversight of these

programs.

Followup

NRC inspections

early in the

assessment

period identified addi-

tional

ISI

weaknesses

in

the

area

of

licensee

overview of contractor

activities

involving thickness

measurements

of piping

systems

and

the

torus

shell.

Additionally,

the

licensee's

own Quality

Assurance

(QA)

Department

issued

a Stop Work Order

on contractor's

ISI activities because

of the

poor quality of examination

documentation

and result

evaluation.

This action,

although

indicative

of

good

QA oversight,

indicates

weak

oversight

by the

Engineering staff

who were responsible

for revising

and

implementing the ISI Program

and associated

corrective actions.

22

Throughout the assessment

period,

licensee

management

devoted considerable

resources

to resolve

the

issues

related

to ISI

on Unit

1.

NRC reviews

near

the

end of the

assessment

period

determined

that

the licensee

had

established

satisfactory

control

systems

and

a

new organization

staffed

with appropriately qualified individuals to effectively implement the

new

ISI Program.

The

Unit I Safety

System

Functional

Inspection

(SSFI)

team

found

some

examples

where

the

surveillance

testing

data

collection,

results

review

and acceptance

criteria

would not adequately

support

system

operability

decisions.

This weakness

appeared

to be

a direct result of poorly defined

system

design

requirements.

A

subsequent

team

inspection

identified

examples

of poor procedural

compliance

and adequacy.

Frequently performed

surveillance

tests

were not followed step-by-step

and

in

some

instances

the

attached

checklists

were

used

without

reference

to

the

written

procedure.

Surveillance - Unit 2

During

the

previous

assessment

period,

several

surveillance

tests

were

missed

because

of inattention to detail

and insufficient supervisory over-

sight.

In'ddition,

numerous

unanticipated

events

occurred

during

the

performance

of

surveillance

testing.

These

events

were

generally

the

result of test procedure

inadequacies

or personnel

errors.

The implemen-

taVon of the Surveillance

Testing

Program

was found to be adequate

during

tlTh initial phase

of power operations;

however,

closer

management

atten-

tion was needed.

During this assessment

period,

the licensee'

failure to perform required

surveillance

tests

was

again

a

concern.

Examples

of

missed

tests

in-

cluded:

failure to record

surveillance

data

during reactor

cooldown sub-

sequent

to

a reactor

scram

due

to operator

error; failure to perform

a

surveillance

test

on

a

primary containment

penetration

due to personnel

error;

missed

snubber

surveillance

tests

due

to

an

inadequate

list of

snubbers;

and

missed

Average

Power

Range Monitor surveillance

due to pro-

gr'ammatic deficiencies.

As in the previous

assessment

period,

this

high

number of missed

surveillance

tests

indicates

inattention

to detail

and

insufficient supervisory

oversight.

The

missed

surveillance

tests

were

spread

between

the

different

station

departments

and

the

Engineering

staff.

The unit again

experienced

many unanticipated

events

during the perform-

ance

of surveillance

testing

during this

assessment

period.

The pre-

ponderance

of

these

events

was

caused

by

procedural

inadequacies

or

personnel

error.

23

Examples

of events

caused

by procedural

problems

include

an inadvertent

actuation

of the

standby

liquid control

system

(SLS)

discharge

valves

during

SLS surveillance

testing

and

a temporary

loss of shutdown

cooling

during

leak

detection

surveillance

testings

These

test

procedure

inadequacies

were not considered

to be

a significant problem, but indicate

technical

procedural

development

could be improved.

Examples of events

caused

by personnel

errors include

a high pressure

core

spray

(HPCS)

system initiation during

surveillance

testing

when

an

IKC

technician failed to follow the procedure

by measuring

resistance

across

an

open contact

vice measuring

voltage

as specified in the procedure,

and

a reactor

scram which resulted

from an

inadequate

plant

impact

assessment

before

performing loop calibrations

on feedwater

flow transmitters.

These

procedural

problems

and personnel

errors collectively indicate poor station

management

oversight,

especially

since

the

same

concerns

were identified

during the last assessment

period.

Corrective actions

to address

these

concerns

include the development of a

more

formalized

tracking

system,

the

implementation

of

an

Engineering

Department

control

program

for Technical

Specification

equipment surveil-

lance lists,

and

(subsequent

to

the

end of the

assessment

period)

the

clarification of,

and training

on,

the

procedural

compliance policy and

re'quirements

documented

in Station General

Order 89-03.

NRC-review of the Unit 2 ISI Program iden;ified that, staffing was adequate

and

personne'1

were

experienced

and

knowledgeable.

Examination

data

were

well documented,

licensee

reviews

were

thorough

and professionally

done.

The disposition

of results

was technically justified and

the closeout

of

findings

was

based

on

sound

engineering

analysis.

Implementation

of the

Unit 2 ISI Program

was considered

good.

The

Power

Ascension

Testing

Program

(PATP)

was

completed

during

the

assessment

period.

The results

indicated that

the testing

occurred with-

out major .exceptions

and

was consistent with the good quality of the

PATP

as discussed

in the previous

assessment.

The minor exceptions

were

ade-

quately

analyzed

and

resolved.

The

program

was

closed

with

no

major

technical

problems.

Fire Protection

Units I and

2

During

the

previous

assessment

period

frequent

and

recurring

personnel

errors

were

noted

in the

implementation

of the

station

Fire Protection

Program

with

an

improving

trend

at

the

conclusion

of

the

assessment

period.

This trend did not continue

throughout this assessment

period as

similar personnel

errors

occurred.

In addition,

the

licensee

identified

a

significant

breakdown

in their

Technical

Specification

fire barrier

24

penetrations

surveillance

program

which led to the discovery of a multi-

tude

of improperly

designed

and/or

installed fire barrier

penetration

seals

at Unit 1.

Further, this Unit

1 penetration

surveillance

problem,

was

identified

to

the

licensee

in

1985

as

the result of

a contractor

audit;

however,

comprehensive

corrective

action

was not taken until this

assessment

period.

Although personnel

errors

have persisted

and

management

followup of pre-

viously identified concerns

was

inadequate,

the

licensee's

Fire Protec-

tion/Prevention

Program for both units

was

observed

to

be generally

ade-

quate.

The deficiencies

identified during this assessment

period

by the

licensee

and

NRC

inspectors,

and

inspector's

review of the

licensee's

corrective

actions

indicated that the

Fire Protection/Prevention

Program

requires

improved overall day-to-day coordination

and management

guidance.

Overall

Summar

The licensee

has

implemented

an effective maintenance

program.

The mate-

rial condition of the plant,

the

experience

and

knowledge of onsite

per-

sonnel,

the controls

for

+he performance

of maintenance,

the interaction

between

Maintenance

and Operations staffs,

and

the documentation

of main-

tenance activities

were considered

adequate.

However,

corporate

and sta-

tion

management

attention

is required

to

address

improved

oversight

of

performance,

effectiveness

and timeliness

of corrective actions,

and ade-

quicy and compliance with maintenance

procedures.

The surveillance

program at Unit

1 is adequate.

The ISI program which was

considered

poor at the beginning of the

assessment

period

shows signifi-

cant

improvement,

thus

demonstrating

that

the

licensee's

management

is

capable of ensuring correction of identified problems

once their attention

is focused

on it.

This

same

focus

by management

needs

to

be

applied

to

ensure

the

IST program is properly implemented

and that surveillance pro-

cedures

are adequate

and adhered to by station

employees.

Implementation of the Unit 2 surveillance testing experienced

various pro-

cedural

and personnel

deficiencies during this assessment

period.

Follow-

up of technical

testing

problems

has

generally

been

good.

The

licensee

has

implemented

more stringent control

in the surveillance

testing

area,

effectiveness

of which

has

not

been fully determined.

In

summary,

per-

formance in the surveillance

area

was minimally acceptable.

Overall,

performance

in the fire protection

area

has declined

over this

assessement

period.

25

2.

Performance

Ratin

Category:

3

3.

Board Recommendations:

NRC:

None

Licensee:

None

D.

Emer

enc

Pre aredness

(224 hours0.00259 days <br />0.0622 hours <br />3.703704e-4 weeks <br />8.5232e-5 months <br />,

2.9%)

'1.

A~nal sis

During the previous

assessment

period,

licensee

performance

in this area

was rated

Category

1.

This assessment

was

based

upon

good exercise

per-

formance

and the licensee's

own initiatives in routine emergency

prepared-

ness activities.

During the current

assessment

period,

one partial-participation

emergency

exercise

was

observed,

a routine safety

inspection

was

conducted,

and

a

special

Emergt.ncy

. Response

Facility

(ERF)

Appraisal

was

conducted

to

verify licensee

implementation of NUREG-0737,

Supplement

1 orders.

In-"%he partial-participation

exercise

held

on August 2,

1988,

the primary

.

objective of the scenario

was to test the interface

between

the licensee's

Emergency

Plan

and

Security

Contingency

Plan.

The licensee's

execution

and participation

demonstrated

thorough

response

and

a strong

commitment

to emergency

preparedness.

The

NRC team found that personnel

demonstrated

complete

knowledge

of procedures

under

emergency

conditions,

interfaced

well with the security force,

and

implemented

the

emergency

plan effic-

iently.

Analysis and classification of events

were timely and

command

and

control

exhibited

by

managers

of each

emergency

response

facility were

effective.

No significant deficiencies

were

identified

and

only minor

facility and

performance

weaknesses

were

noted.

The

licensee

concurred

with

the

NRC-identified

findings

and

initiated

appropriate

corrective

action.

In

conjunction

with

the

annual

exercise,

the

ERF Appraisal

was

also

performed.

Results of the appraisal

identified certain

programmatic

areas

which were either

incomplete

or in need of increased

licensee

attention.

Of primary concern

was the licensee's

dose

assessment

model.

The

NRC team

found that

improvements

were

needed

in all aspects

of the

dose

assessment

program

including

undefined

isotopic

distributions

and

release

rates

associated

with all Unit 2

FSAR accidents

and post-accident

sample results

not

properly

incorporated

into

dose

calculations.

Other

identified

26

deficiencies

were found in the storage

capacity of the Unit I Plant

Computer

System to report pre-event

and post-event

plant data,

and

Emer

gency Operations Facility habitability.

In response

to

NRC initiative

the licensee

addressed

all appraisal

findings and committed to resol

ng

each

item to the next scheduled refueling outage.

Following the

appraisal,

on September

25,

1988,

a separate

concern

was identifi

with

Technical

Support Center habitability when dampers within the

TS

ventilation system failed.

This problem was not corrected

unt

the

end

of the period.

'

During the routine safety inspection

conducted

in February

1989, all

major areas

of the licensee's

emergency

preparedness

pro

am including

program changes,

emergency

equipment,

organization

and

anagement

control,

training,

program audits

and follow-up of open items

re reviewed.

No

significant deficiencies

were found regarding

the

r grammatic

changes

or

walkthroughs (training) of key emergency

respon

p

sonnel with the

excepti on of licensed

operator

knowledge of th

ope

tion and capability

of the

Tone Alert System.

Minor concerns

wer

d tified with the

licensee's

recent revisions to and distribu

the

Emergency

Plans

and

Implementing Procedures,

personnel

used t

gn

ct independent

program

reviews,

and information provided in gen

al

ployee training.

Coordination of onsite

and offsite

em

preparedness

activities are

administered

by the

Emergency

Coordi

from the site.

The training

department

is responsible

for inst

of most emergency

response

personnel

and scenario

develoment

reparation

is provided through

~coatract

support.

During. the r

nt

eorganization

of the Nuclear

Services Division, two additio

1-time equivalent staff members

were authorized for the

emer

r eparedness

program.

In addition,

the

Emergency

Coordinator

p

n has

been

upgraded to

a manager

level

with direct access

to the

r, Nuclear Services.

Such changes

are

an

indication of strong

pro

upport from upper-level

corporate staff.

Each calendar quarter

icensee

coordinates

with the State of New York

and other power rea

censees

within the State

concerning offsite

emergency

prepare

s

ssues.

The

EP staff also maintains

membership

on the

Oswego

Co

arming Committee

and is currently assisting

the

State

and local

a

rities in the development of procedures

for meteoro-

logical forecas

ng.

During an accident, this process

would ensure that

inputs into th

dose

assessment

model

are identical at each jurisdictional

level.

Promp

notification ( siren)

system capability was degraded

on

several

occ

ions during the period and the licensee notified

NRC

immediatel

after identification of these

problems.

26 A

deficiencies

were

found

in

the

storage

capacity

of the

Unit I Plant

Computer

System to report pre-event

and post-event

plant data,

and

Emer-

gency

Operations

Facility habitability.

In

response

to

NRC initiatives

the

licensee

addressed

all appraisal

findings

and committed to resolving

each

item

to

the

next

scheduled

refueling

outage.

Following

the

appraisal,

on

September

25,

1988,

a separate

concern

was identified with

Technical

Support Center habitability when dampers within the

TSC ventila-

tion system failed.

This problem

was not corrected

until the

end of the

period.

During the routine safety inspection

conducted

in February

1989, all major

areas

of the licensee's

emergency

preparedness

program including program

changes,

emergency

equipment,

organization

and

management

control, train-

ing,

program audits

and follow-up of open

items were reviewed.

No signif-

icant deficiencies

were found regarding

the

programmatic

changes

or walk-

throughs (training) of key emergenc>

response

personnel

with the exception

of licensed operator

knowledge of the operation

and capability of the Tone

Alert System.

Minor concerns

were identified with the licensee's

recent

revisions

to

and distribution

of

the

Emergency

Plans

and

Implementing

Procedures,

personnel

used

to

conduct

independent

program

reviews,

and

information provided in general

employee training.

Co'ordination

of onsite

and offsite emergency

preparedness

activities are

administered

by

the

Emergency

Coordinator

from the site.

The training

department is responsible

for instruction of most

emergency

response

per-

soltnel

and

scenario

develoment

and

preparation

is provided through

con-

tract support.

During the recent

reorganization

of the

Nuclear

Services

Division,

two additional full-time equivalent staff

members

were author-

ized for the

emergency

preparedness

program.

In addition,

the

Emergency

Coordinator

position

has

been

upgraded

to

a

manager 'level with direct

access

to the

Manager,

Nuclear Services.

Such

changes

are

an

indication

of strong

program support

from upper-level

corporate staff.

Each calendar

quarter

the licensee

coordinates

with the State of New York

and other

power

reactor

licensees

within the

State

concerning

offsite

emergency

preparedness

issues.

The

EP staff also maintains

membership

on

the Oswego

County Planning

Committee

and is currently assisting

the State

and

local

authorities

to

assure

meteorological

forecasting

methods

are

consistently applied

and understood for accurate

input to the dose assess-

ment

models.

During

an

accident,

this

process

would ensure

that inputs

into the dose

assessment

model

are identical at each jurisdictional level.

Prompt

notification

( siren)

system

capability

was

degraded

on

several

occasions

during

the

period

and

the

licensee

notified

NRC

immediately

after identification of these

problems.

27

In

summary,

the licensee

has

demonstrated

a positive continued

commitment

to emergency

preparedness.

The relationship

between

the licensee

and off-

site authorities continues to be strong.

Training of all levels of emerg-

ency

response

personnel

was effective

as

evidenced

by exercise

perform-

ance.

Although

items identified during

the

ERF Appraisal

remain

incom-

plete,

responsiveness

to

NRC initiatives has

been timely and

the licensee

has

made progress

in correcting most

NRC concerns.

Management

involvement

is of the level

necessary

to ensure

that the

emergency

preparedness

pro-

gram can

be efficiently implemented.

2.

Performance

Ratin

Category:

1

3.

Board Recommendation:

NRC:

None

Licensee:

None

E.

Securit

and Safe

uards

(137 hours0.00159 days <br />0.0381 hours <br />2.265212e-4 weeks <br />5.21285e-5 months <br />,

1.8:.')

l.'Anal sls:

Du~ng

the

previous

assessment

period,

the

licensee's

performance

was

raYed

as

Category

1.

No regulatory

issues

were

identified

by

either

region-based

or resident

inspectors.

During

the

assessment

period

the

licensee

continued

to

demonstrate

a

thorough understanding

of NRC security objectives

and maintained

an excel-

lent enforcement history.

One

unannounced

routine security inspection

was

performed

by region-based

inspectors.

Routine inspections

by the resident

inspectors

continued throughout the period.

Corporate

management

involvement

and

interest

in

the

security

program

remained

evident during this

assessment

period

by

the

continued

on-site

presence

of the

Security

Manager

who reports directly to the

corporate

Executive Vice President for Nuclear

Generation.

The Security

Manager

and his supervisory staff are well-trained and qual-

ified security professionals

who are

vested with the

necessary

authority

and discretion

to ensure

that the station's

nuclear

security

program is

carried out effectively and in compliance with NRC regulations.

Security management

also continues

to actively participate

in the Region I

Nuclear Security Association

and in other

groups

engaged

in nuclear plant

security matters.

28

The licensee

continued to enhance

the security program during this assess-

ment period.

All search

equipment

in both

access

control portals

was

up'-

graded,

vehicle barriers

and double

fences

are

being erected

at the pro-

tected

area

boundary,

the Unit

1 intrusion detection

system

was

upgraded

and plans

have

been

developed

to upgrade

the Unit 2 instrusion detection

system.

Security

systems

and equipment

are tested

and maintained

by dedi-

cated

instrumentation

and controls

( I&C) and maintenance

groups

(a total

of 22 personnel)

~

These

are indications of the licensee's

commitment

to

maintain

a quality and highly effective program.

To

ensure

a

comprehensive

annual

audit of the

security

program,

the

licensee's

Safety

Review

and Audit Board

used

the

services

of nuclear

security consultants.

The licensee

continued to implement the Commitment

to

Excellence

Program

in security.

The

program

centered

around

three

areas:

1) performance testing of security force members;

2) conducting

an

in-house

regulatory

effectiveness

style

review;

and

3) daily

audits/

surveillances

of security

posts

including at least twenty-percent

inspec-

tions

on

backshifts.

These

are

further

indications

of the

licensee's

commitment to the program.

A review of the licensee's

security event reports

and reporting procedures

found

them to

be consistent

with

NRC regulations

(10 CFR 73.71).

There

were

two security

event

reports

submitted

during

the

assessment

period.

One event

involved the loss of offsite local

law enforcement

communica-

ticms capabilities

and

the other,

the discovery

of drugs

on-site.

The

licensee

took prompt and effective compensatory

and/or corrective

measures

for each event.

Staffing of the proprietory

security

force

continues

to

be

adequate

as

evidenced

by

a limited use of overtime.

The security force training

and

qualifications

program is well-developed

and is administered

by an experi-

enced

staff of five, full-time individuals

(including

the

supervisor).

Facilities for training

and requalification

are available

on site or on

adjacent,

owner-controlled

property.

These facilities are

well-equipped

and

maintained.

Security

contingency

response

drills are

conducted

at

least

once

each

month.

These drills are effectively

used

for training

purposes

and the drill critiques

are

integrated

into the

formal training

program.

The

licensee

instituted

a

procedure

during

this

assessment

period to ensure

the participation of the operations

organization

during

contingency drills if the scenario

could affect plant operation..

During the

assessment

period,

the

licensee

submitted

one revision to the

Physical

Security

Plan

under

the

provisions

of

10 CFR 50.54(p).

This

revision

was

of

high quality,

technically

sound,

and

reflected

well-

developed

policies

and

procedures.

Security

personnel

involved in main-

taining the

program

plans

are very knowledgeable

of

NRC requirements

and

objectives.

29

In summary,

the

licensee

continues

to maintain

a very effective

and per-

formance-oriented

security

program.

Significant

enhancements

to

the

program

continued

during this

assessment

period

which is indicative of

management

attention

to

and

support

for the

program.

The efforts

to

upgrade

the operation

and reliability of systems

and equipment during this

period

are

commendable

and

demonstrate

the

licensee's

commitment

to

maintain

an effective and high quality program.

2.

Performance

Ratin

Category:

I

3.

Board Recommendations:

NRC:

None

Licensee:

None

F.

En ineerin

and Technical

Su

ort (523 hours0.00605 days <br />0.145 hours <br />8.647487e-4 weeks <br />1.990015e-4 months <br />,

6.7%)

l.

~Anal sis

Du'ring

the

previous

assessment

period,

the

licensee's

performance

was

rated Category

2 in this functional area.

Problems

were identified in the

foRowing areas:

insufficient station-to-engineering

department

interface;

in0dequate

involvement of engineering

in the

resolution

of ISI

program

concerns;

and,

inadequate

control over contractors.

In

order

to

improve

station-to-engineering

department

interfaces,

the

Engineering

Department

now includes

a

permanent

site

engineering

group

that

reports directly to

the

Vice President

of Nuclear

Engineering

and

Licensing.

This group was established

during the middle of the

SALP cycle

and is

responsible

for coordinating

and

implementing

engineering

modifi-

cations

and expediting corporate

engineering

support for plant operations.

Greater

engineering

staff participation

in routine

station

meetings

was

evident

and

appears

to

have

a

positive

impact

on

the

assignment

and

accountability for Engineering

Department action items.

One

area of particular

concern

during this

SALP period

was the reverifi-

cation of the first 10 years of the Inservice Inspection (ISI) Program for

Unit 1.

Early in the

SALP period

numerous deficiencies

were identified in

the

program involving many required

inspections

which

had

not

been

per-

formed because

of improper development

and implementation of the ISI Pro-

gram by

a contractor

and insufficient licensee

oversight of that contrac-

tor.

However,

an

NRC team inspection

conducted

near

the

end of the

SALP

period concluded that the licensee

has effectively corrected

deficiencies

previously identified in the ISI Program.

As

a result of increased

man-

agement attention to these deficiencies,

the program is presently

defined,

structured

and

adequately

staffed

with qualified individuals

to effec-

tively implement the

new program.

30

Problems

previously identified regarding

the

adequacy

of the licensee's

control

over

contractors

were

also

noted

during this period.

Specific

problems

noted during this period included:

weaknesses

in the

licensee's

review

of

contractor

procedures

and

inspection

results;

deficiencies

regarding

contractor dedication

of commercial

grade

items for Unit 2

and

oversight of Unit

1 ISI program contractors.

These deficiencies

indicate

poor

engineering

management

oversight

to

assure

adequate

control

of

contractors.

To

enhance

plant

safety

and

provide

better

direct

plant

support,

the

licensee

has established

a priority system

whereby all safety significant

projects

are Priority

1

and other work which affects

safety

systems

are

Priority 2.

All Priority

1 and

2 projects are

on schedule.

Additionally,

the Vice President,

Engineering

and Licensing holds

a weekly staff meeting

to discuss

the status

of each project.

This

system is effective

as evi-

denced

by all priority safety significant projects

being

on

schedule

and

the observation

that there

was

no appreciable

backlog of projects

during

the Unit 2 and ongoing Unit

1 outages.

The

licensee's

Engineering

and

Technical

Support

staff

were

generally

effective

in resolving

engineering

concerns

at

both units

with

notable

improvement

in

design

change

activities.

However,

during this period,

performance

by the Engineering staff was inconsistent

and is

a matter of

concern

to the

NRC

and merits attention

by management.

While a number of

activities

and

specific

projects

for which

the

engineering

staff

had

control

over were

conducted

in

a professional

manner,

weaknesses

in other

areas

were detrimental

to the overall

assessment

of the engineering

sup-

port function.

Examples of both are discussed

below.

The licensee

has

developed

a detailed

commercial

grade dedication

program

to upgrade

equipment to safety-related

status.

This program

was developed

based

upon discovery

by the licensee of weaknesses

in the General Electric

commercial

grade

items

dedication

process

and

the

necessity

to

resolve

potential

electrical

equipment

safety

concerns

prior to Unit

2 initial

licensing,

The

licensee's

program

employs

the

EPRI guidelines

and

the

documented

engineering

evaluations

were

determined

to

be

thorough

and

technically sound.

Several

design

and

replacement

activities

were

performed

well including

the replacement

of the Unit

1 feedwater

check valves,

the Unit 1 Antici-

pated Transient Without Scram

Alternate

Rod Injection modification,

and

the

upgrade

of

the

Unit

1

Mark I

containment

to

meet

the

acceptance

criteria of

NUREG 0661.

The

licensee

addressed

all of the

significant

31

technical

aspects

of the Bulletin 85-03,

"Motor Operated

Valve

Common

Node

Failures During Plant Transients

Due to Improper Switch Settings" at both

.

units.

The

necessary

corrective

actions

were

properly coordinated

with

the maintenance

and operation staffs.

However,

poor

performance

in other

areas

indicates

an inability of the

engineering

department

to consistently deliver quality work.

Examples of

these

inconsistencies

include: the

numerous deficiencies identified in the

implementation

of Regulatory

Guide

1.97 for Unit 1; the failure to report

the

125 Vdc design deficiencies

in a timely manner for Unit 1; the failure

to detect

and

resolve

an

automatic

depressurization

system

(ADS) wiring

error which rendered

one division of ADS inoperable for Unit 2; inadequate

corrective actions to identify all improperly sealed

penetrations

and con-

duits for internal

flooding for Unit 2;

and

the inadequate

resolution of

post-accident

sampling

system divisional

power supply problems at Unit 2.

Slow resolution of design deficiencies

at Unit 2

have

resulted

in plant

transients

and

unnecessary

safety

system

actuations.

Examples

included

the reactor building ventilation problems,

reactor

vessel

instrumentation

common

reference

leg sensitivity concern

and

the

feedwater

control

valve

problems.

A 'Safety

System

Functional

Inspection

(SSFI)

performed

by

an

NRC

team at

Unit

1 concluded that design

information for both the core spray

and HPCI/

FW~ys:ems

was

not

adequately

controlled

or

supported

by sufficiently

detailed

analysis.

This

lack of defined

design

analysis

for the

core

spray

and

HPCI/FW

systems

degraded

the quality of

system

operating

and

surveillance

procedure

guidance.

A specific

concern

was

the Appendix

K

reload analysis.

Inadequate

analyses

led to operation

of the plant out-

side

of

the

design

basis

on

two

separate

occasions'hese

potential

problems

were

known by the licensee

in early

1987,

but were not resolved

until brought to the

licensee's

attention

by the

NRC.

This

was another

example of inadequate

licensee

followup to identified deficiencies.

The licensee

has developed

a comprehensive

training program for individuals

at all levels

in the

Engineering

organization.

The

permanent

training

staff is supplemented

by individuals

from various disciplines

assigned

as

instructors.

If required,

consultants

are

retained for specific courses.

At the end of the

SALP period,

the

NRC identified significant deficiencies

in the implementation

of the licensee's

engineering

training

program.

A

review of the training records

and

licensee

gA audits

revealed

that most

of the

engineers

were

not receiving

adequate

training

according

to the

projects training program.

While the licensee

has

developed

a comprehen-

sive training program,

the

program

has

not

been

effectively

implemented.

32

In

summary,

the

licensee

has

made

limited

progress

in

addressing

engineering

and

technical

support

deficiencies

that

were

identified

during the last

SALP period.

While

some engineering activities exhibited

strong

engineering

control,

numerous

examples

of

poor

performance

of

engineering

activities

were

identified.

These

examples,

collectively,

indicate

poor

control

and

coordination

of

engineering

efforts

and

inadequate

management

oversight

of

the

engineering

function

to

assure

consistency

of

performance

of the

on

and off site

engineering

staff.

Performance

in, this

area

contributed

to

the

issuance

of Confirmatory

Action Letter 88-17

and

continues

to

be

of

concern

to

the

NRC staff.

2.

Performance

Ratin

Category:

3

3.

Board Recommendations:

NRC:

None

Licensee:

None

G.

Sa et

Assessment/

ualit

Verification (1446 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.50203e-4 months <br />,

18.7%)

l.

A~aal sis

This

new

functional

area

assesses

the

effectiveness

of the

licensee's

programs

provided to assure

the safety

and quality of plant operations

and

activities.

It is a compilation of the Licensing

and Assurance

of guality

functional

areas

provided

in the previous

SALP reports,

but also

incor-

porates

relevant

indications

discussed

in all other current

functional

areas.

During the previous

SALP period,

the licensee

was evaluated

as Category

3

in the area of Assurance

of guality and Category 2, declining, in the area

of Licensing.

Performance

in the Assurance

of guality area

was

noted to

be

inconsistent.

Improvements

occurred

in

problem

identification

and

resolution,

effectiveness

of the guality Assurance

organization,

Unit

2

operations,

staff

performance,

and

Technical

Specification

interpreta-

tions.

Weaknesses

were identified

in station

and

corporate

management

oversight

and coordination,

radiological controls,

teamwork

and

communi-

cation,

and

housekeeping.

In the

licensing

area it was

noted

that

the

technical

approach

to,

and resolution for issues

were generally

sound

and

conservative;

however,

on occasions,

the licensee

demonstrated

a lack of

understanding

of regulatory

requirements

and

a

reluctance

to

make inde-

pendent

conservative

decisions

on

issues

involving regulatory

compliance.

33

During this assessment

period the licensee's

performance

in correcting the

SALP identified weaknesses,

in responding to plant events,

and in conduc-

ting other activities

and functions impacting quality and safety assurance

has

been

inconsistent.

However,

at

the

end of the

rating

period,

the

licensee

took significant action to demonstrate

senior

management's

com-

mitment to identify

and

resolve

long-standing

problems

in

the

Nuclear

Division.

In response

to

CAL 88-17,

a

number of assessment

programs

and

corrective

actions

were initiated including the

Restart

Task

Force,

the

Restart

Action

Plan

(RAP),

and

the

Nuclear

Improvement

Program

(NIP).

Particularly noteworthy is that the licensee

established

a

new position of

Executive

Vice President

Nuclear Operations.

The hiring of a senior indi-

vidual

from outside

the

organization

broke

a

long-standing

tradition of

promoting

from within and demonstrated

that senior

management

is serious

about

breaking

down

the

organizational

"culture"

and

correcting

the

leadership

deficiencies

that

have contributed

to

many of the

problems at

Nine Mile Point.

The licensee

has

made

several

additional

organizational

changes

in

an attempt

to strengthen

the organization

including the estab-

lishment of a Regulatory

Compliance

Group.

This group provides

a continu-

ity to the organization

which was

not previously observed.

It has facil-

itated

improvements

in:

1) tracking

and timely resolution

of identified

problems,

concerns

and

commitments;

2) interdepartmental

communications;

3) defined responsibilities

and

accountabi lities;

and

4) consistency

in

operations

and administration

between Units

1 and 2.

The- licensee

has

also

requested

independent

organizations

to assist

them

in evaluating

the

effectiveness

of

the

Nuclear

Organization

and

has

scheduled

a self-evaluation

before restarting Unit 1.

These efforts indi-

cate

that

Niagara

Mohawk is

making

a

concerted

effort to correct

the

leadership

weaknesses

identified in the previous

SALP.

The effectiveness

of the above

changes

is still being evaluated.

Throughout

the

period

the licensee

has

demonstrated

increased

effective-

ness

in problem identification,

both programmatic

and technical.

However,

corrective

actions

in general

have

not

been

properly

implemented

to pre-

vent recurrence.

This is evident for both units and is attributed to the

inability to clearly identify the applicable

root cause

and

the

lack of

defined responsibility

and accountability within the organization.

In contrast,

the licensee's

recent corrective actions with respect

to the

Unit

1 Inservice Inspection

Program deficiencies

represent

a true commit-

ment

to develop

and

maintain

an effective

Inservice

Inspection

Program.

Significant

technical

manpower

resources

have

been

dedicated

to this

effort, increased

management

attention

and control

have

been

observed

and

there is evidence of a heightened sensitivity

by all station

employees

of

the proper implementation of the program.

The licensee's

actions concern-

ing the identification of the

ADS logic circuitry deficiencies,

and ser-

vice water system single failure corrective actions

were also

commendable.

34

The

licensee's

approach

to

the

resolution

of technical

issues

from

a

safety

standpoint

has

not

always

been

timely

and

conservative.

For

example,

the

licensee

has

not

been

effective at

reducing

the

number of

scrams,

Engineered

Safety

Feature

(ESF) actuations,

and

personnel 'errors

experienced

at

Unit

2 following the

completion

of the

Power

Ascension

Testing

Program

early

in

the

rating

period.

This

problem

appears

to

result

from the licensee's

(inappropriate)

willingness to accept

the high

number of events

as

being

normal

and

acceptable

for

a

newly

licensed

facility.

In addition,

the

licensee

has

not

always

been

aggressive

in

pursuing safety issues it did not perceive to be restart

issues

on Unit 1,

such

as

resolution

of

a vital area

question

regarding

the diesel

gener-

ators

and

the development

and

implementation

of

a

long-term

program for

the torus wall thinning issue.

The station Quality Assur ance

(QA) Surveillance

Group is an aggressive

and

thorough

oversite

group.

It is

particularly

flexible

and

active

in

responding

to recognized

independent

oversight

needs.

Corrective actions

resulting

from the

QA Surveillance

Group effort

now

appear

to

reverse

negative

trends prior to the development

of major problems.

This repre-

sents

a measurable

improvement

over previous

assessments.

However,

weak-

nesses

have

been identified in the technical quality of the

QA audits per-

formed

by the

QA Audit Group.

Audits

have

been

noted

to

be

weak

and

shallow despite

past

NRC criticism in

SALPs.

The

licensee

is

aware of

this

and is taking

steps

to strengthen

the

group's

technical

abilities.

Weaknesses

have

also

been identified in the threshold for highlighting QA

id5ntified deficiencies

and significant adverse

trends

to senior

station

and

corporate

management.

Added corporate

management

attention

should

be

given to ensuring that significant findings are properly escalated

so that

prompt and effective action

can

be taken.

One instance

observed

during this assessment

period indicated

a reliance,

by the line organization,

on

the

QA organization

to identify problems.

Corrective

actions

taken

by the Engineering staff to address

Unit I ISI

program deficiencies

were too dependent

upon the

QA staff to ensure

proper

implementation.

This ultimately resulted

in

a

QA Stop Work Order because

of ineffective program implementation.

Increased

Engineering

and contrac-

tor supervisory oversight resulted.

During the

assessment

period,

the Site Operations

Review Committee

(SORC)

and the Safety

Review

and Audit Board

(SRAB)

have

not demonstrated

their

effectiveness

in overviewing station activities.

Observations

indicated

that these

committees

get

bogged

down

in too

much detail.

Nany of the

presentations

made to these

committees

have

been ill-prepared

and ineffec-

tive.

SRAB consultants

were

observed

to

be

very active

and

provided

excellent

input to the

SRAB meetings

and reviews.

Observations

made of

the Independent

Safety Engineering

Group

(ISEG) indicated that this group

was also

not fully effective.

Members of the

group

were

too far removed

from day-to-day station activities

and their

assessments

appeared

to

be

lost at too low a level in the organization.

35

A review of the

Licensee

Event Reports

(LERs) submitted during the period

indicates that the reports were thorough, detailed,'ell

written and

easy

to understand.

The root cause of the event

was clearly identified in most

cases.

The

LERs presented

the event information in

an organized

pattern

that led to a clear understanding

of the event information.

Significant weaknesses

in the area of reportability were identified during

the Safety

System

Functional

Inspection.

As

an

example,

delayed

correc-

tive actions

for

an

improper

Technical

Specification

Limiting Condition

for Operation

allowed the plant to

be placed

in

an

unanalyzed

condition

and

resulted

in

untimely

reporting.

Additional

corporate

management

attention

is

needed

to

improve

the

prompt

evaluation

and

reporting

of

significant potential

safety issues.

Responses

to bulletins,

generic letters

and multi-plant action

items

such

as'eneric

Letter 83-28,

and

the

ATWS

Rule

(10 CFR 50.62),

have

been

generally timely and complete.

The licensee's

requests

for amendments

and

reliefs

have

been

adequate

and indicate appropriate

planning

and

assign-

ment of priorities.

The quality of the reviews performed

by the licensee

under the

requirements

of 50.59

has

also

improved

over

the last rating

period.

However,

the licensee's

analysis of industry operating

experience

has

been

slow and in some

cases

inadequate.

In summary,

licensee

performance

in the areas

related to Safety Assessment

and-Quality Verification has

been inconsistent.

Strengths

have

been

noted

in the

areas

of:

1) demonstration

by

management

that it

has

begun

to

aggressively

pursue

correction

of identified

leadership

deficiencies;

2) increased

effectiveness

in problem identification; 3) establishment

of

the Regulatory

Compliance

group; 4) an aggressive

and thorough

QA surveil-

lance

group;

and

5) detailed

and

thorough

LERs.

In contrast

weaknesses

have

been

identified

in the

areas

of:

1) defined responsibilities

and

accountability;

2) implemenation of corrective actions;

3) continuing high

event rate at Unit 2 attributable to

a complacent attitude with respect

to

new

plant

operations;

4) aggressiveness

in

pursuing

potential

safety

issues;

5) shallowness

of

QA audits;

and 6) inadequate

review of industry

operating experience.

2.

Performance

Ratin

Category:

3

Improving

3.

Board Recommendation:

NRC:

None

Licensee:

Management

attention

should

be

focused

to ensure

that the

increased

emphasis

on

correcting

deficiencies

at

Unit

1

does

not result

in insufficient attention

to

problems

at

Unit 2.

36-

V.

SUPPORTING

DATA AND SUMMARIES

A. Enforcement Activit

Table 1.1

Unit

1 Enforcement Activities

Violations Versus Functional

Area

~B

~Severit

Level

Functional

Area

No. of Violations in Each Severity Level

V

IV

III

II

I

Total

Plant Operations

Maint/Surv

Eng/Tech Support

Emergency

Preparedness

Security

8

Safeguards

Radiological

Controls

Safety

Assessment

guality

Verification

TOTAL

1

6

0

0

0

7

Note:

There are five apparent violations pending final staff review.

37

Table 1.2

Unit 2 Enforcement Activities

Violations Versus Functional

Area

~B

~Severit

Level

Functional

Area

No. of Violations in Each Severity Level

LI

V

IV

III

II

I

Total

Plant Operations

Maint/Surv

Eng/Tech Support

Emergency

Preparedness

Security

and

Sqfeguards

1

1

1

0'adiological

Control s

Safety

Assessment/guality

Verification

TOTAL

17

1

4

1

0

0

23

Escalated

Enforcement Action

An Enforcement

Conference.

was

held

on July 11,

1988 for Unit

1 to discuss

an apparent

violation of

10CFR50

Appendix

R "Fire Protection

Program for

Nuclear

Power

Facilities

Operating

Prior

to

January

1,

1979".

Two

severity level

IV violations were

issued

on

September

19,

1988 citing the

licensee

against

Appendix

R

and

Appendix

B, "guality Assurance

Criteria

for Nuclear

Power Plants

and

Fuel

Reprocessing

Plants".

An Enforcement

Conference

was held

on February 2,

1989 for Unit 2 to dis-

cuss

a wiring error

in the Automatic Oepressurization

System Oivision I

actuation

logic.

A Notice

of Violation

was

issued

on

Harch

13,

1989

citing

an

aggregate

severity

level III violation with no civil penalty.

38

An Enforcement

Conference

was held

on March 30,

1989 for Unit 1 to discuss

Licensed Operator Requalification Training Program deficiencies identified

early in this

assessment

period.

Potential

violations

from the

Safety

System

Functional

Inspection,

and Inservice Testing deficiencies

and

125

'OC battery

concerns

are

being

included

in this

action.

Enforcement

actions

are pending.

B.

Confirmator

Action Letters

CAL

On

March 28,

1988,

the

NRC issued

CAL 88-13 which documented

the licen-

see's

commitment that Unit

1 would not restart until Operator Requalifica-

tion deficiencies

were corrected.

On July 24,

1988,

the

NRC issued

CAL 88-17 which documented

the licensee's

commitment that Unit

1 will not

be restarted

until

problems

in several

areas

are resolved

and

NRC approval is obtained.

CAL 88-17 superseded

CAL

88"13.

39

C.

Ins ection

Hours

Summar

Unit

1

TABLE 2

Unit 2

Area

Hours

% of Time

Hours

% of Time

Plant Operations

1464

Radiological

Controls

232

27.9

4.4

810

32.3

281

11.2

Maintenance

and

Surveillance

2041

38.9

598

23.9

Emergency

Preparedness

117

Security

and Safeguards

70

Engineering

and Technical

Support

413

2.2

1.3

7.9

107

67

110

4.3

2.7

4.3

Safety Assessment/

equality Verification

913

17.4

533

21.3

TOTALS

5250

100.0

2506

100.0

40

D.

LICENSEE EVENT REPORTS

CAUSAL ANALYSIS

TABLE 3

Cause

Determined

~b

SALP Board

An assessment

has

been

conducted to determine

the root cause of each event from

the perspective

of the

NRC.

The

causes fell into the following categories

and

sub-categories.

Personnel

Errors

~PE

1.

Lack of Knowledge

(LK) - the individual

was not properly trained or

provided with instructions

from supervision.

2.

Inattention

to Detail

( ID) -

the

individual failed to

pay

proper

attention to a task

and was careless.

3.

Poor

Judgement

(PJ) -

the

individual

failed to

make

the

correct

assessment

with the proper

amount of training and attention to facts.

~E'ui ment Malfunction/Failure ~EN/F

1..Random

(R)

isolated

component

problem

not of generic

concern.

2.

Design Deficiency (00) - poor design

was the

cause

of the

malfunc-

tion/failure.

3.

Construction Deficiency (CD) - improper installation during construc-

tion/modification

caused

or

could

have

caused

the

malfunction

failure.

4.

Maintenance

Deficiency

(MD) -

improper

preventive

or

corrective

maintenance.

Procedural

Error ~PROE

The procedure failed to provide adequate

instruction,

was poorly worded or

was not properly reviewed for use.

ineffective Corrective Action ~ICA

Action

was

not

taken

by

management

or the

action

taken

on

a previously

identified

item

was

not timely or did

not

correct

the

root

cause

and

allowed this occurence.

41

TABLE 3 (Cont'd)

LICENSEE EVENT REPORTS

Unit

1 ~Summar

of Cause

Determined

~b

SALP Board

~b

Functional

Areas

CAUSE

OPS

RAD

MAINT/SURV

ENG/TS

EP

SEC

SAFETY/(AV

PE/LK

PE/ID

PE/PJ

EM/F/R

1

EM/F/DD

EM/F/CD

EM/F/MD

PROE

TOTAL

TOTAL

9

0

0

0

24

"Total is greater

than the number of LERs since

some

LERs have

more than

one cause

code assigned.

The licensee

issued

a total of 16

LERs this

assessment

period.

42

TABLE 3 (Cont'd)

LICENSEE EVENT REPORTS

Unit 2 ~Summer

of Cause

Determined

~b

SALF Board

~b

Functional

Areas

CAUSE

OPS

RAD

MAINT/SURV

ENG/TS

EP

PE/LK

2

1

2

PE/ID

4

2

11

SEC

SAFETY/(AV

TOTAL

18

PE/PJ

1

EM/F/R

1

EM/F/DD

EM/F/CD

EM/F/MD

PROE

16

19

3

TOTAL

10

3

35

23

0

0

0

71*

  • Total is greater

than the number of LERs since

some

LERs have

more

than

one cause

code assigned.

The licensee

issued

a total of 65

LERs

this assessment

period.

43

E.

Other

Investi ations

and Alle ations

Summar

An Office of Investigation

(OI) Review was

prompted following a

Region I

inspection of the Unit

1 Licensed

Operator Requalification Training Pro-

gram which identified potential

material

false statements

made

on License

Renewal

Form 398s.

The OI Report concluded that there were

no intentional

material

false

statements

made

by

licensee

management

or

licensed

operators.

During this

assessment

period,

a total of nine allegations

were received

and

reviewed

by the

NRC.

Six allegations

were determined

to be unsubstan-

tiated

and one allegation

was

a valid concern.

The

two remaining allega-

tions were still under review at the end of the assessment

period.

Mana ement Conferences

On April 26,

1988,

the licensee

gave

a presentation

to

NRC Management

on

torus thinning and Inservice Inspection

issues

for Unit 1.

On

May 4,

1988,

a meeting

was

held to discuss

the licensee's

approach

to

is'sues

requiring resolution prior to Unit

1 restart.

On-May 10,

1988,

SALP management

meeting

was conducted on-site.

On. July 25,

1988,

the

Regional Administrator,

Executive Director of Oper-

ations,

and the Associate Director for Projects,

NRR met with the licensee

on-site to discuss

NRC's

concern

over the licensee's

continued

poor per-

formance

and issue Confirmatory Action Letter (CAL) 88-17.

On

August 18,

1988,

the

Regional

Administrator

was

on-site

to

discuss

corrective actions concerning

CAL 88-17 with site

and corporate officials.

On October

18,

1988,

a meeting

was

held in Region I to review progress

in

resolving restart

issues.

On October 21,

1988,

NRC

senior

staff

met with the

licensee

to discuss

restart

issues for Unit 1.

On October 27,

1988,

the licensee

made

a presentation

in Region I concern-

ing the

status

and

scheduling

of Unit

1

Inservice

Inspection

Program.

On

November 25,

1988,

a

management

meeting with the Executive Vice-Presi-

dent

was held concerning

the Restart Action Plan.

44

On

December 6,

1988,

NRC

management

met with the

President

of Niagara

Mohawk to discuss

the Restart Action Plan.

On

December

20,

1988,

the

licensee

gave

a 'presentation

to

NRC staff in

Headquarters

concerning

improvements

made in the Unit

1 Inservice

Testing

Program.

On

December

22,

1988,

the

licensee

presented

the

Restart

Action Plan to

the

NRC for review in a management

meeting in Region I.

On

January

19,

1989,

the

NRC

Restart

Panel

was on-site

to present

the

licensee with comments

on the Restart Action Plan.

On January

31,

1989,

the

licensee

made

a presentation

to the

NRC staff

regarding details concerning

Conformance

with Regulatory

Guide

(RG) 1.97.

On February

21,

1989,

the licensee

made

a

second

presentation

to the

NRC

staff in Headdquarters

concerning

RG 1.97.