ML17054B789

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Forwards Safety Insp Rept 50-220/85-09 on 850501-0630 & Notice of Violation
ML17054B789
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 07/23/1985
From: Collins S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Hooten B
NIAGARA MOHAWK POWER CORP.
Shared Package
ML17054B790 List:
References
NUDOCS 8508070763
Download: ML17054B789 (4)


See also: IR 05000220/1985009

Text

e

JUL 2 3 1985

Docket

No. 50-220

Niagara

Mohawk Power Corporation

ATTN:

Mr. B.

G.

Hooten

Executive Director

Nuclear Operations

300 Erie Boulevard

Syracuse,

New York

13202

Gentlemen:

Subject:

Inspection

50-220

8 -09

This refers to the routine,

safety inspection

conducted

by Mr. S.

Hudson of

this office on May

1 to June

30,

1985 at Nine Mile Point Nuclear Station, Unit

1 of activities authorized

by

NRC License

No.

DPR-63

and to the discussions

of

our findings held by Mr. Hudson with Mr. T.

Roman of your staff at the conclusion

of the inspection.

e

Areas

examined during this inspection

are described

in the

NRC Region I

Inspection

Report which is enclosed with this letter.

Within these

areas,

the

inspection consisted

of selective

examinations

of procedures,

and representa-

tive records,

interviews with personnel,

and observations

by the inspector.

Based

on the results of this inspection, it appears

that one of your activities

was not conducted

in full compliance with NRC requirements,

as set forth in the

Notice of Violation, enclosed

herewith

as Appendix A.

This violation has

been

categorized

by severity level in accordance

with the revised

NRC Enforcement

Policy (10 CFR 2, Appendix C) published

in the Federal

Register Notice (49 FR 8583) dated

March 8,

1984.

You are required to respond to this letter

and in

preparing your response,

you should follow the instructions

in Appendix A.

This violation apparently resulted

from the lack of adequate

controls

over

mechanical

jumpers.

The vent paths

on each of the control rod drive withdraw

lines were connected

together with tygon tubing (a mechanical

jumper) for use

as

a flush path during the

1982-1983 recirculation piping replacement

outage.

This condition remained until June

1985.

while no loss of a safety function

occurred, this event demonstrates

the potential for future events

which degrade

safety.

In your response,

you should address

the administrative controls you

intend to implement to prevent recurrence.

The responses

directed

by this letter and the accompanying

Notice are not

subject to the clearance

procedures

of the Office of Management

and Budget as

required

by the Paperwork Reduction Act of 1980,

PL 96-511.

e

OFFICIAL RECORD

COPY IR 9 MILE1 85-09 - 0001.0.0

07/17/85

'..: 8508070763

850723

PDR

ADOCK 05000220

8

PDR

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Niagara

Hohawk Power

- Corporation

)gi g g 1985

Your cooperation

in this matter is appreciated.

Sincerely,

Original Signed Bye

I

Samuel J. Collins, Chief

Projects

Branch

No.

2

Division of Reactor Projects

Enclosures:

1.

Appendix A, Notice of Violation

2.

NRC Region I Inspection

Report

Number 50-220/85-09

cc w/encls:

T.

Lempges,

Vice President,

Nuclear Generation

T. Perkins,

General

Superintendent,

Nuclear

Generation

T.

Roman, Station Superintendent

J. Aldrich, Supervisor,

Operations

W. Drews, Technical

Superintendent

Troy B. Conner, Jr.,

Esquire

John

W. Keib, Esquire

Department of Public Service,

State of New York

Public Document

Room (PDR)

Local Public Document

Room (LPDR)

Nuclear Safety Information Center

(NSIC)

NRC Resident

Inspector

State of New York

bcc w/encls:

Region I Docket

Room (with concurrences)

Senior Operations Officer (w/o encls)

Section Chief,

DRP

DRP

udson/mjd

7/)7/85

RI: DRP

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Vitl85

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7/+85

OFFICIAL RECORD

COPY IR 9 MILE1 85"09

0002.0.0

07/17/85

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