ML16342D466

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Insp Repts 50-275/96-20 & 50-323/96-20 on 960818-0928. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML16342D466
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 10/22/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D465 List:
References
50-275-96-20, 50-323-96-20, NUDOCS 9610290211
Download: ML16342D466 (30)


See also: IR 05000275/1996020

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

50-275, 50-323

License Nos.:

DPR-80, DPR-82

Report No.:

50-275/96-20; 50-323/96-20

Licensee:

Pacific Gas and Electric Company

Facility:

Diablo Canyon Nuclear Power Plant, Units

1 and 2

Location:

7 1/2 miles NW of Avila Beach

Avila Beach, California

Dates:

August 18 through September

28, 1996

Inspectors:

M. Tschiltz, Senior Resident Inspector

S. Boynton, Resident Inspector

D. Corporandy,

Project Inspector

D. Allen, Reactor Inspector,

Region IV

Approved By:

R. Huey, Acting Chief, Project Branch E

Division of Reactor Projects

ATTACHMENT:

Partial List of Persons Contacted

List of Inspection Procedures

Used

List of Items Opened,

Closed, and Discussed

List of Acronyms

96i02902ii 96'l022

PDR

ADQCK 05000275

8

PDR

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Units

1 and 2

NRC Inspection Report 50-275/96-20; 50-323/96-20

~Oeretinne

~

Management

demonstrated

conservative

decision making when both units were

curtailed during periods when wildland fires had the potential to jeopardize two of

the three offsite power distribution lines (Section 01.1).

Investigative and corrective actions to address

deficiencies with the controls

established for the moveable incore detector system keys during containment

entries were not timely or comprehensive

(Section R1.1).

Maintenance

~

Inadequate

work planning and procedures

were identified as significant contributors

to the deformation of spent fuel pool cooling piping during the application of a

freeze seal.

A noncited violation was identified (Section M1.1.1).

Maintenance activities associated

with charging pump relief valve weld replacement

were well coordinated

and properly performed (Section M1.1.2)

Maintenance workers did not replace tripper cams and tripper arm assembly that

had abnormal wear during overhaul of a motor-operated

damper actuator.

Failure to

replace the tripper cams resulted in the inability to place the valve in the manual

mode during subsequent

testing (Section M1.1.3).

~En ineerin

Engineering aggressively resolved equipment concerns associated

with recently

installed 4160V breaker auxiliary switches and with the chemical and volume

control system (CVCS). This was demonstrated

by the accomplishment

of several

design changes

made to improve system reliability and reduce unnecessary

operation of engineered

safety feature equipment (Sections E1.1 and E1.2).

Routine system engineer system walkdowns failed to identify and evaluate

12 CVCS system valves with evidence of packing leakage (Section E1.2).

Plant Su

ort

Procedural requirements for establishing

a fire watch were not met prior to

commencing welding in the turbine building.

A noncited violation was identified

(Section

F1

~ 1) ~

A superseded

revision of a chemistry procedure was utilized when drawing a

primary sample.

The procedure for sampling, which had been revised in April, was

used on a daily basis and was required to be verified to be the latest revision every

I 4

4

-2-

30 days.

Similar problems were noted with "issued-for-use" documents

in NRC

Inspection Report 50-275/96-06; 50-323/96-06.

A violation was identified

(Section R3.1).

There has been

a noted improvement in the general housekeeping

and radiological

work practices observed

in the Fuel Handling Building areas designated

for work on

radioactive components

(Section R8.1).

0

Re ort Details

Summar

of Plant Status

Unit 1 began this inspection period at 100 percent power.

On August 19, the unit was

curtailed to 70 percent power due to a wildland fire that threatened two of the three

500 kV transmission. lines from the plant.

The unit returned to 100 percent power on

August 20. The unit was briefly curtailed to 70 percent power on August 21, when there

was, again,

a perceived threat to the 500 kV lines from the wildland fire. Following the

curtailment, the unit returned to and remained at 100 percent power for the balance of the

inspection period.

Unit 2 began this inspection period in power ascension

at 90 percent power, following a

unit trip on August 10.

Unit 2 returned to full power on August 18.

On August 19, the

unit was curtailed to 70 percent power due to a wildland fire that threatened two of the

three 500 kV transmission

lines from the plant.

The unit returned to 100 percent power on

August 20. The unit was briefly curtailed to 70 percent power on August 21, when there

was, again,

a perceived threat to the 500 kV lines from the wildland fire. Following the

curtailment, the unit returned to and remained at 100 percent power for the balance of the

inspection period.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety-conscious.

Wildland fires that burned in areas in the vicinity of two of the three 500 kV

distribution lines created an increased potential for the loss of these lines.

Based

upon the load carrying capacity of the 500 kV line not threatened

by the fire and

the potential for grid instability, plant management

made the decision to curtail both

units to 70 percent power.

These management

actions were viewed as proactive

since they limited the potential for unplanned

plant transients

and challenges to

plant systems and operators.

02

. Operational Status of Facilities and Equipment

02.1

Effluent and Environmental Radiation Meteorolo ical Monitorin

lns ection Sco

e 71750

Radiation stack monitor recorder traces were reviewed and the operability of the

plant's meteorological indicators was audited for the period from August'2-31,

1996.

-2-

b.

Observations

and Findin

s

Primary meteorological instrumentation for the plant was out of service for the

period reviewed within the inspection scope because

of a planned replacement of

the electronic instrumentation.

The replacement was completed,

and the primary

meteorological instrumentation was returned to service on September

5, 1996.

During the period that the primary meteorological tower was unavailable, the

backup m.teorological instrumentation was opera~le in accordance

with Technical Specification (TS) 3.3.3.4, which requires one of the two channels to be operable.

Radiation monitor recorder traces were reviewed for Radiation Monitors RM-28R,

the particulate sampler; RM-14R, the noble gas activity monitor;

and RM-24R, the

iodine sampler.

Measured radiation activity levels for the monitors remained at less

than

1 percent of the radioactivity release limit during the period covered within the

scope of the inspection.

Licensee Equipment Control Guideline 39-4R7.4B,

Revision 7, which requires that either the primary or redundant

radiation monitor be

operable at all times, was satisfied for the inspected

period.

c.

Conclusions

Effluent and environmental radiation monitors and meteorological monitors met the

operability requirements

of the applicable equipment control guidelines and TS for

the period reviewed by the inspector.

Measured radiation levels for noble gas,

particulate, and iodine were significantly below alarm levels during the period,

indicating that there were no apparent uncontrolled releases of radiation during the

period.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

VIO 50-323 96002-01:

failure to perform TS required channel checks of

incore thermocouples.

Licensee Procedure

STP I-1D improperly allowed the use of

the plant process computer (PPC) to perform the TS required monthly channel

checks of the incore thermocouples.

As a result, the requirements of TS 4.3.3.6

were not being met by the performance of Procedure

STP 1-1D.

The licensee researched

the use of the PPC in performing other TS required

suryeillances

and found that the PPC was also. utilized to perform channel checks of

the subcooled

margin monitor.

In response to these findings, the licensee revised

Procedure

STP I-1D to preclude the use of the PPC to perform the channel checks

of the postaccident

monitoring system instrumentation.

Subsequently,

the licensee

established

a new procedure,

STP R-27A, for conducting the monthly channel

checks of the postaccident

monitoring panel incore thermocouples

and removed that

requirement from Procedure

STP I-1D. A review of Procedure

STP R-27A found

that it adequately met the requirements of TS 4.3.3.6.

-3-

Because

Procedure

STP I-1D allowed the use of either the PPC or the local

postaccident

monitoring panel display, the licensee could not determine when

channel checks of the incore.thermocouples

had, or had not, been performed

adequately.

Consequently,

the licensee concluded that the requirements

of

TS 3.3.3.6 had not been met since initial operation of Units

1 and 2. As a result,

the licensee issued licensee event report (LER) 50-275/84-050-00.

Based upon this

review, LER 50-275/84-050-00

is closed.

08.2

Closed

VIO 50-275 95006-01:

four examples of failure to follow procedural

requirements.

The violation identified four separate

instances where opera Ions

personnel failed to follow procedures.

The licensee determined that the violations

had several different causes

including:

inattention to detail, inadequate

self-

verification, and failure to follow procedure.

One of the four examples was

subsequently

determined to not be a violation based upon additional information

that was not provided to the inspector during the initial inspection.

The inspector reviewed the licensee's corrective actions for the remaining

three examples

and determined that, in each instance, actions had been taken to

prevent recurrence of the problem,

Corrective actions included:

revision to

Operating Procedure C-7C:III, "Condensate

Polishing System Transferring Resin

Beds," issuance

of an Operations Shift Order that reiterated the requirements for

operation of sealed valves, and improvement and clarification of self-verification

criteria. The inspector concluded that the licensee's corrective actions were

appropriate.

II. Maintenance

M1

Conduct of Maintenance

M1.1

Maintenance

Observations

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

~

C0146264 Unit 2 Control Room Ventilation System filter train blank flange

installation

~

PEP R-3E Replacement of Unit 2 moveable incore Detector A

b.

Observations

end Findin s

The inspectors found the work performed under these activities to be accomplished

in accordance

with procedures.

All work observed was performed with the work

package present and in active use.

Technicians were experienced

and

knowledgeable

of their assigned tasks.

The inspectors observed system engineers

-4-

monitoring job progress

and that quality control personnel were present when

required by the procedure.

When applicable, appropriate radiation control measures

were in place.

In addition, selected maintenance

observations

are discussed

below.

M1.1

~ 1

S ent Fuel Pool

SFP

Coolin

Pi in

Freeze Seal

a.

Ins ection Sco

e 62707

On August 14, after establishing

a freeze seal on a spent fuel pool cooling system

pipe, the licensee identified that the pipe had deformed in the vicinity of the freeze

seal location.

The inspector reviewed Procedure

MP M-54.3, Revision 7, "Freeze

Sealing of Piping," NMAC NP-6384-D, "Freeze Sealing (Plugging) of Piping," and

Work Order (WO) C0145900.

Actions taken to establish the freeze seal were

discussed with both the engineering personnel investigating the event and the

director of mechanical maintenance.

b.

Observations

and Findin s

Under WO C0145900, mechanical maintenance

technicians applied a freeze seal to

the SFP demineralizer/filter outlet piping, upstream of Valve SFS-1-19.

The freeze

seal was required to establish conditions needed to repack the valve. As required

by Procedure

MP M-54.3, the work planner completed Attachment 8.1 to provide

direction on the placement of the freeze seal jacket. A sketch of the pipe was

provided in accordance with Step 5.0 of the attachment

and showed the freeze seal

area centered between two pipe hangers. According to the work planner, the length

was based upon a request from the mechanical maintenance

foreman to have an

area cleaned and tested that was approximately three times the length of the jacket.

The work planner was not aware that multiple jackets were to be used for this

freeze seal at the time he completed Attachment 8.1.

To ensure the adequacy of the freeze seal, the maintenance

personnel utilized three

separate

CO, jackets side-by-side to form what they believed would be a single,

long ice plug in the pipe.

Neither engineering

nor the freeze jacket vendor were

consulted on the acceptability of this arrangement.

The as-installed configuration

was not indicated in Attachment 8.1 and was not annotated

in the WO.

In utilizing

three separate jackets, three distinct ice plugs formed.

As the ice plugs grew,

water trapped between the plugs was pressurized

and, consequently,

the yield

strength of the pipe was exceeded.

This resulted in observable

bulging of the pipe

at points between the jackets.

Both Procedure

MP M-54.3 and NMAC NP-6384-D provide guidelines for the

minimum spacing between freeze seals to protect against overpressurization

of the

water volume between the seals.

Neither document provided guidance on the use

of multiple jackets for establishment

of a single freeze seal.

For the SFP piping

-5-

application, the minimum distance between the seals should have been 3 feet.

The

actual distances between the freeze seals was less than

1 foot.

To preclude recurrence of this problem, the licensee has revised

Procedure

MP M-54.3 to explicitly prevent the use of multiple jackets for a'single

freeze seal application.

The associated

training module on freeze seals was also

revised to reflect this precaution.

The licensee assessed

the continued operability

of the deformed, piping and concluded that the deformation caused

by the freeze

seals did not significantly reduce the pipe strength and that the remaining strength,

was adequate for the application.

The affected section of pipe has been scheduled

for replacement

in October 1996.

Conclusions

The use of multiple freeze jackets resulted in the overpressurization

and deformation

of the SFP cooling piping. A violation was identified in that Procedure

MP M-54.3

did not provide adequate

guidance or controls over the attempted application.

This

licensee identified and corrected violation is being treated as a noncited violation

consistent with Section VII.8.1 of the NRC Enforcement Policy (NCV 50-

275/96020-01).

Positive Dis Iacement

PD

Pum

Dischar

e Relief Valve

CVCS-2-RV-8116

Inlet Weld Re lacement

lns ection Sco

e 62707

The inspectors observed portions of work activities under WO C0145272,

"Replace welds on inlet piping to PD Pump Discharge Relief Valve CVCS-2-

RV-8116," and reviewed the related clearance

and history of associated

action requests

(ARs).

Observations

and Findin s

On September

11 the inspectors reviewed the WO and found the level of

detail of the instructions was adequate

for the tasks being performed.

The

instructions for the work contained the applicable requirements for prejob

briefing,.control of foreign material, cleanliness,

clearance,

permits, laydown

area, and use of tools and materials.

The maintenance

personnel were

observed to be correctly performing the instructions in the sequence

listed.

The related clearance was reviewed and the boundaries

were found to

adequately protect both equipment and personnel without unnecessarily

impacting the operability of related equipment.

The clearance tags were

hung at the specified locations in accordance with administrative

requirements.

-6-

The radiological controls for the job appeared

a'ppropriate.

Required

radiological surveys had been performed and personnel at the job-site wore

the required'protective clothing.

Potentially contaminated

areas were

correctly posted,

and appropriate actions were observed to minimize the

spread of contamination.

The tools and material at the job'site were inspected.

Welding rods were

properly tagged and controlled and they corresponded

with the work

instructions and material controls.

The test equipment was calibrated and

tagged,

and the personnel were knowledgeable

of its proper use.

The combustible material permit and welding permit were posted and

adequate

personnel

coverage was provided for the work, including

radiological protection, supervision,

and a monitor for foreign material

exclusion.

Involved personnel were knowledgeable of the necessary work

practices and the history of the equipment problems.

A comparison of Regulatory Guide 1.44, "Control of the Use of Sensitized

Stainless Steel," with the licensee's

program for control of sensitized

stainless steel indicated that the licensee's

program was consistent with the

Regulatory Guide.

The completed work documentation

was reviewed and

was noted to have been properly completed.

In addition, the training record

of the welder performing the work documented that the individual was

qualified to perform the welding.

C.

Conclusions

The observed portions of the work were noted to have been accomplished

in

accordance

with applicable procedures,

and personnel involved with the

maintenance

were knowledgeable

of procedural requirements for the work as well

as the reason for performing the design change.

M1.1.3

Overhaul of Motor 0 crated Dam er VAC-1-MOD-8

a.

Ins ection Sco

e 62707

The inspector reviewed the following work documents

and procedures:

- WO R0159930: VAC-1-MOD-8 Damper Overhaul

- MP E-53.10M, Rev 10A, "Limitorque SMB-00 and SB-00 Valve Operator

Maintenance"

- MP E-53.10A, Rev 19, "Preventive Maintenance of Limitorque Motor Operators"

-7-

b.

Observations

and Findin

s

Technical Maintenance

(TM) personnel were observed

during the installation of the

actuator worm shaft and the clutch tripper assembly for the Limitorque SMB-00

actuator that operates

Damper YAC-1-MOD-8. This portion of the work was being

repeated since, when attempting to operate the actuator following the initial

overhaul, it could not be placed in the manual mode.

Discussion with the cognizant

engineer identified that this was the first time that the actuator had been overhauled

since the plant had started operation.

Actuator Disassembl

During actuator disassembly it was noted that the tripper lever spacer had not been

installed.

Correspondence

referred to by the licensee from Limitorque indicated that

the installation of the tripper lever spacer was not required as long as proper

alignment could be obtained.

In addition, during the actuator disassembly,

an

additional spacer was noted to have been previously installed that was not specified

in the actuator diagrams.

The additional spacer had been installed between the

inner tripper cam and the bearing spacer.

After technicians consulted with

engineering,

neither the tripper lever spacer nor the additional spacer were used in

the reassembly of the actuator.

Mixed Lubricants

Upon disassembly,

technicians noted a mixture of Beacon 325 and Mobil 28 grease

in the actuator limitswitch gearbox.

Prior to reassembly,

the gearbox was cleaned

and greased

using Mobil 28 lubricant.

Discussion with the cognizant engineer

indicated that the Beacon 325 grease

had most likely been used by the valve

manufacturer since it had not been utilized by the licensee.

The mixing of grease by

addition of Mobil 28 lubricant had most likely been performed during the licensee's

prior maintenance

activities.

The combination of the two types of lubricants,

although not desired;- was evaluated

as not to have impacted valve operability since

the grease was noted to remain in a liquid state.

Although the combination of the

greases

resulted in a thinner more liquid substance,

it was considered

acceptable

since the actuator was not required to be environmentally qualified.

VAC-1-MOD-8 was one of two actuators that had not been overhauled

since

actuator maintenance

was turned over to the maintenance

department prior to the

plant commencing commercial operation.

The cognizant engineer indicated that all

other motor-operated

valve and damper actuators had been overhauled

by the

maintenance

department since that time, and the other nonoverhauled

actuator had

been satisfactorily inspected.

Based upon the information provided, there does not

appear to be a concern for the use of mixed grease

in other actuators.

-8-

Clutch Tri

er Assembl

Installation

During installation of the worm shaft, the previously installed tripper cams and

tripper fingers were inspected

and noted to be worn.

One of the tripper cams had

been slightly deformed, apparently by contact with the tripper fingers.

The tripper

fingers were also noted to be rounded, thus reducing the contact. area on the tripper

adjustment arm. The inspector concluded that a more thorough inspection of the

tripper fingers and tripper cams would have indicated the need for replacement

during initial overhaul of the actuator.

The cognizant engineer agreed that the parts

should have been replaced.

Following replacement of the tripper cams and the

tripper lever assembly, the actuator was verified to satisfactorily operate in the hand

mode.

C.

Conclusions

The initial reassembly of VAC-1-MOD-8 without replacing the worn components

is

considered to be a poor maintenance

work practice. In addition, the presence

of

mixed lubricants in the limitswitch gearbox is indicative of a prior weakness

in the

licensee's motor-operated

actuator maintenance

activities.

M1.2

Surveillance Observations

a 0

Ins ection Sco

e 61726

Selected surveillance tests required to be performed by the TS were reviewed on a

sampling basis to verify that:

(1) the surveillance tests were correctly included on

the facility schedule;

(2) a technically adequate

procedure existed for the

performance of the surveillance tests; (3) the surveillance tests had been performed

at a frequency specified in the TS; and (4) test results satisfied acceptance

criteria

or were properly dispositioned.

The inspectors observed the following surveillances:

STP l-9-L922, Revision 2, Refueling Water Storage Tank 1-1 Level Channel

LT-922 Calibration

STP P-RHR-12, Revision 4, "Routine Surveillance Test of RHR Pump 1-2"

b.

Observations

and Findin s

The inspectors found that the surveillance reviewed and/or observed were

scheduled

and performed at the required frequency.

The procedures

governing the

surveillance tests were technically adequate,

and personnel performing the

surveillance demonstrated

an adequate

level of knowledge.

The inspectors'also

noted that test results were appropriately dispositioned.

-9-

MS

Miscellaneous Maintenance Issues (92902)

M8.1

Closed

VIO 50-.275 95016-02:

Nl audio count'rate secured contrary to TS and

'rocedural requirements.

During operational tests of Nuclear Instrument

CI;annels Nl-31 and NI-32, TM personnel failed to follow procedures

and, as a

result, the audible count rate provided by these instruments was secured for

approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> during a period required by TS.

Evaluating these procedural

violations, the licensee determined that the first example was caused

by personnel

error in that the technicians,

recognizing

a discrepancy

in a procedural step, did not

obtain an on-the-spot-change

(OTSC) to allow them to perform the step as desired.

The second example was most likely caused

by inadequate

self-verification.

The licensee subsequently

issued an OTSC to Procedure

STP I-4A to:

(1) allow the

audio count rate setting on the instrument to be adjusted,

as necessary,

to produce

a discernable

change

in the audio count rate, and (2) add an independent

verification requirement during the audio count rate channel restoration.

Additionally, the technicians were counseled

on the need to process

an OTSC when

work being performed is not clearly specified by the applicable procedure.

In

addition, a general tailboard was conducted with TM personnel

regarding the issues.

Prior to Refueling Outage 2R7, Procedure

STP I-4A was revised to enhance

equipment turnover requirements

contained

in the "Return to Service" section.

The

inspector verified the completion of these corrective actions and reviewed the

revised portions of Procedure

STP I-4A. The licensee's

corrective actions appeared

to be reasonable

and sufficient to preclude recurrence of the violation.

M8.2

Closed

VIO 50-275 95016-03:

failure to follow fire protection requirements for

fire doors.

During housekeeping

activities in the Emergency Diesel

Generator

(EDG) 1-1 room, personnel blocked open a fire door without informing the

fire protection specialist or the shift foreman.

The licensee determined that the root

cause of the violation was inadequate

guidance inthe governing procedure for fire

system impairment.

Specifically, Procedure

OMS.ID2 did not clearly define when a

fire door is considered

blocked or impaired. Consequently,

the personnel

performing

the housekeeping

activities did not believe that the their activities impaired the

function of the fire door.

Based upon this finding, the licensee revised Procedure

OMS.ID2 to specify when a fire door is considered impaired,

The licensee also

provided information to plant personnel

on this event, including the definition of fire

door impairment, in a March edition of the plant's Nuclear News letter. The

inspector verified the completion of the licensee's corrective actions and determined

that the actions were appropriate to preclude recurrence of the violation.

-10-

ill. En ineerin

E1

Conduct of Engineering

E1.1

4160V Vital AC S stem Review

a.

Ins ection Sco

e 71707

37551

The inspector conducted

a review of the design, maintenance,

and operation of the

on-site 4160 V vital AC power system.

This review included the following

documents:

Updated Final Safety Analysis Report (U-SAR), Chapter 8.3, Onsite Power

Systems

Design Criteria Memorandum S-63, 4160 V System

DCP H-049059, Rev. 0, 4 kV Switchgear and Cable Spreading

Room Air

Flow

DCP E-047079, Rev. 0, Setting of Secondary

Undervoltage

Relays

DCP E-049237, Rev. 1, Tap Adjustment on the Standby Startup Transformer

DCP C-043902, Rev. 1, 4 kV Switchgear Embedment

Plate Welds

DCP M-047098, Rev. 0, 4 kV Switchgear Door Fasteners

~

TP TD-9607, Providing 125 VDC Power From SD21 to SD22 Vital Loads

Quality Evaluations: 00007408, Q0010602

~

4160 V System Surveillance Procedures

~

4160 V System Operating Procedures

The inspector also conducted

a detailed system walkdown of the 4160 V vital

switchgear and interviewed the system engineer.

This review did not specifically

address the electrical portions of the EDGs.

b, 'bservations

and Findin s

The 4160 V vital AC power system is designed to provide reliable power to various

safety-related

components.

Major loads on the 4160 V buses include emergency

core cooling system pumps, component cooling water pumps, auxiliary saltwater

pumps, auxiliary feedwater pumps, and the 480 V vital buses.

Normal power to the

buses

is fed from the unit main generator or 500 kV transmission system via the

unit auxiliary transformer.

Backup power is supplied from the offsite 230 kV

-11-

transmission system via the standby startup transformer and from the EDGs.

Each

of the three 4160 V buses has a dedicated

EDG that will automatically supply

power to the bus in the event of a loss of voltage.

Plant TS for the 4160 V system were found to be consistent with the requirements

of the Updated Final Safety Analysis Report (UFSAR). Procedures

STP M-13A,

STP M-13F, STP M-13G, STP M-13H, and STP M-75 adequately

addressed

the

requirements of TS 4.8.'l.1.1.

Operating procedures

were also found to be of

sufficient detail to provide adequate

guidance to operators in the startup, operation,

and shutdown of the 4160 V system.

Since the start of commercial operation, the licensee has identified several design

deficiencies in the 4160 V system and has proactively pursued their resolution.

Examples include the replacement of the underrated

250 MVA GE Magne-Blast

circuit breakers with 350 MVASF, breakers, improvement of the seismic withstand

capability of the 4160 V switchgear, and a modification to provide annunciation

when the breaker closing spring fails to charge.

During and following the

installation of the new 350 MVA SF~ breakers, several problems were revealed in

the interface between the new breaker and the stationary auxiliary switch.

These

problems were aggressively pursued by the licensee with corrective actions that

were both thorough and technically justified. A review of the associated

design

change

packages for these modifications found that they were technically complete

and that they adequately

addressed

any impact on the licensing basis of the

system.

The inspector walked down the 4160 V switchgear in both units, including the

ventilation lineup for room cooling.

No extraneous

materials affecting fire loading or

seismic interaction were noted in any of the switchgear rooms.

Switchgear

deficiencies were properly identified and tagged.

No deficiencies were noted that

had not already been identified.

The system engineer was very knowledgeable

on both system requirements

and

component design basis,

He has been assigned to the 4160 V system for 6 years

and is also the system engineer for the electrical portions of the EDGs.

He had

played an active rote in each of the design changes

to the system and was able to

discuss the technical details of each.

The system engineer walked down the

system on a nominal monthly basis and maintained

a quarterly system report on the

status of design changes

and resolution of deficiencies.

Conclusions

Current design and testing of the 4160 V vital,AC power system

is in conformance

with the UFSAR and plant TS. The licensee has been proactive in identifying and

correcting degraded

conditions and system design deficiencies.

Engineering,

operations,

and maintenance

staffs have demonstrated

the ability to coordinate

efforts in the implementation of design changes

and problem resolutior.

-12-

E1.2

CVCS S stem Review

a.

Ins ection Sco

e 71707

37551

The inspectors reviewed documentation

related to the CVCS, including:

ARs: A0403181,A0394714, A0394405, A0398021, A0384085,

A0384084, A0402973, A0410262, A0122862, A0314487, A0326480 and

A0393237

~

System Engineer Quarterly Reports

~

Quality Evaluations Q0011894, Q0011791, 00011639

~

Nonconformance

Report N0001955

~

UFSAR Section 6.3, Emergency Core Cooling System; Section 9.3.4,

Chemical and Volume Control System; and Table 6.2-39, Containment Piping

Penetrations

and Valving

~

Plant Staff Review Committee (PSRC) TS Interpretation 96-08, Revision 0

Surveillance Procedures

STP M-54, Verification of RCP Seal Injection

Flows By Resistance

Measurements,

Revision 18

Temporary Modification/Plant Jumpers 94-44, 96-14, 96-28

The inspectors walked down portions of the system in both Units

1 and 2

and observed equipment operation, valve alignments, AR tags, and overall

material condition of the equipment.

b,

Observations

and Findin s

Selected ARs on the CVCS system'were reviewed with the system engineer.

The system engineer was knowledgeable

of the status of these items and of

the equipment history for his system.

At the time of the review there was a

total, for both Units

1 and 2, of approximately 300 outstanding

ARs on the

CVCS system, some dating back to 1989.

Of the older ARs that were

reviewed,

a majority had been assigned

as low priority items.

Based on a

limited sample, the prioritization of these ARs appeared

appropriate

due to

the minor nature of the problems.

CVCS TS Re uirements

Applicable TS were reviewed.

During the review, the inspector noted that

the PSRC had approved

an interpretation of TS 3.4.6.2 e. that addressed

-13-

acceptable

CONTROLLED LEAKAGE. The TS states that the reactor coolant

system leakage shall be limited to 40 gpm CONTROLLED LEAKAGE at a

system pressure

of 2235 ~ 20 psig.

The licensee's interpretation of the TS is that its purpose

is to ensure that the

CONTROLLED LEAKAGE is less than 40 gpm under postloss of cooiant accident

conditions.

The basis for the interpretation is supported

by the TS bases, which

indicate that the limitfor controlled leakage is to ensure the safety injection flow

will be greater than that assumed

in the analysis in the event of a loss of coolant

accident.

Therefore,

in situations where the CONTROLLED LEAKAGE is calculated

to be less than 40 gpm, with charging aligned in the post accident mode, but flow

measurements

taken at 2235 psig indicate the flow rate is greater than 40 gpm, the

licensee considers the test results acceptable.

The inspector questioned the validity

of the TS interpretation in that it appeared to deviate from the surveillance as

currently written in the TS to ensure

CONTROLLED LEAKAGE at 2235 a 20 psig is

less than 40 gpm.

The most recent surveillance results for Units

1 and 2 indicated

that the CONTROLLED LEAKAGE was less than 40 gpm.

The evaluation of the

licensee's

interpretation of TS 3.4.6.2.e is being considered

as an inspection

followup item (IFI 50-275/323 96020-02).

CVCS S stem IValkdown

A walkdown of portions of the system was performed for both Units

1 and 2

and found the valve alignment to be correct, including accessible

containment isolation valves.

The operating pumps had adequate

oil levels

and cooling flows. The overall material condition of the equipment was

good, with the exception of dry boric acid indications on numerous valves.

Although most of these valves were tagged and tracked on a master AR,

12 valves were identified as having indication of dry boric acid leaks and

were neither tagged nor included in the master AR. After this concern was

raised with the licensee, the valves with evidence of boric acid leakage were

added to the master AR.

Various documents were reviewed that identified the containment, isolation

valves in the CVCS system.

The documents were consistent with the plant

drawings and with each other, with the exception of two minor editorial

errors in AD13.DC1, Attachment 7.10, "Containment tsolation Valves."

These deficiencies were identified to the licensee for correction.

The jumper log was reviewed for temporary modifications to the CVCS

system,

Three temporary pressure

instruments were noted to have been

installed to improve monitoring of the CONTROLLED LEAKAGE during

surveillance testing and to allow monitoring of the differential pressure

.

across the reactor coolant letdown filters 1-2 and 2-2 when Fi:ters 1-1 or 2-1

are isolated.

The temporary letdown filter differential pressure

gauges were

installed in April 1994 and May 1996 for Units

1 and 2, respectively.

The

-14-

use of a temporary jumper for over 2 years, in'lieu of installing a design

change,

appeared to be a protracted length of time to utilize a temporary

jumper.

However, the inspector noted that design changes

had been

initiated, and the licensee had scheduled

replacement of the temporary

gauges with permanent installations within the next month.

Centrifu

al Char

in

CC Pum

and Positive Dis lacement

PD

Pum

Issues

The licensee has taken several positive steps to ensure that the material condition

of the CC pumps and the PD pumps is properly maintained,

as demonstrated

by the

following actions:

ao

The licensee had previously identified erosion of the restricting orifice in the

recirculation flow path for each CC pump.

Following identification,

recirculation line flow testing was performed in order to determine if the

pump recirculation flow rates were within allowable limits. Testing indicated

that CC pump recirculation flow had increased

but not to the point of

causing flow rates to be outside of allowable limits. The testing appeared to

adequately

assess the impact of the degradation

on flow rates for the

existing conditions.

The licensee has scheduled

replacement of the orifices

during the next refueling outage for each unit.

b.

In response

to industry problems described

in NRC Information

Notices 94-76: Recent Failures of Charging/Safety Injection Pump

Shafts, 80-38: Cracking in Charging Pump Cladding; and 94-63: Boric

Acid Corrosion of Charging Pump Casing Caused

By Cladding Cracks,

the licensee

has replaced one cc pump on each unit with pumps that

have stainless steel casings and internal assemblies.

C.

Following identification of an indication on a pipe weld associated

with the Unit 1 PD pump, the licensee attempted to perform an

ultrasonic examination of the Unit 2 piping.

Due to the inaccessibility

of the weld for ultrasonic examination and the potential concern for a

similar problem with the Unit 2 weld, the licensee replaced the socket

weld in question with a butt weld as a precautionary measure.

Conclusions

The licensee's initiatives to improve system reliability were noteworthy.

Significant

effort had been put forth to improve the reliability of the system and facilitate

running the PD pump to provide normal charging flow and limit operation of the CC

pumps during normal plant operation.

In addition, the system engineer was very

knowledgeable of the system and the status of outstanding

deficiencies.

One

weakness

was noted in that a number of boric acid leaks were noted that had not

be;:n identified by the licensee and entered into their tracking and evaluation AR.

-1 5-

ICES

Engineering Support of Facilities and Equipment

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

plant practices, procedures,

and/or parameters to the UFSAR description.

During

the inspection period, the inspectors reviewed the applicable sections of the UFSAR

that related to the inspection areas discussed

in this report.

There were no

inconsistencies

noted between the wording of the UFSAR and the plant practices,

procedures,

and/or parameters

observed

by the inspectors.

E8

Miscellaneous Engineering Issues (92903)

E8.1

Closed

LER 50-275 94006-00:

CC pump outside of design basis due to throttling

of component cooling water (CCW) to subcomponents.

The LER was written to

report the licensee's determination that CCW flow to the CC pumps had been

reduced by throttling to the point where the CCW flow rate may not have been high

enough to adequately

cool the CC pump subcomponent

heat exchangers

in the

event of an accident to maintain postaccident

CC pump operability.

The original LER, which reported only the licensee's discovery of the problem and

immediate corrective actions, was submitted to the NRC on July 22, 1994.

Revision

1 to the LER was submitted on June 15, 1995, and addressed

the root

cause, safety significance and corrective actions for the event.

As a part of the

corrective actions, the licensee performed testing that confirmed the adequacy

of

the existing nonthrottled CCW flow to cool the CC pump subcomponents.

Although

the CCW flow to CC pump heat exchangers

remains less than that recommended

by the vendor, the licensee has consulted with the vendor and obtained concurrence

that the existing flow is sufficient to ensure the CC pump remains operable during a

design basis accident.

Final review of this issue will be performed prior to the

closure of Revision

1 of the LER.

IV. Plant Su

ort

R'I

Radiological Protection and Chemistry Controls

R1.1

Control of the Moveable Incore Detector S stem

MIDS

Ke

a.

Ins ection Sco

e 71750

In conjunction with a maintenance

observation associated

with the replacement

of

the Unit 2 MIDS Detector A, the inspec:or reviewed Procedure

RCP D-230,

Revision 9, "Radiological Control for Containment Entry" and AR A0394318 to

evaluate the radiological controls requirements for the work.

-16-

b.

Observations

and Findin s

Step 5.3.1.b.2 of Procedure

RCP D-230 requires the MIDS keys to be in the

possession

of trie'Radiation Protection

(RP) Foreman during all containment entries.

As these keys are controlled by the unit shift foreman (SFM), the RP Foreman signs

for and takes possession

of the keys prior to a containment entry.

AR A0394318

was initiated in February 1996 to document the fact that another key controlled by

the SFM would also operate the MIDS power switch. The SFM who initiated the

AR recommended that the MIDS key lock be changed to preclude the possibility of

inadvertent operation of the MIDS drives while personnel were in the containment.

As an immediate corrective action, the SFM would subsequently

issue both keys to

the RP Foreman.

However, this action was neither proceduralized

nor documented

in the AR, and no further action was taken at that time to determine if the MIDS key

was duplicated in other applications.

On September

12, 1996, the SFM informed the RP department that there were two

more keys, controlled by the control room assistant, that would fit in the MIDS

. power switch lock. The RP General Foreman updated AR A0394318 to reflect this

discovery; however, he did not document any corrective actions taken in response.

On September

19, the inspector questioned the shift supervisor on what actions

had been taken to ensure adequate

control of the MIDS key during containment

entries.

Operations personnel

determined that the control room assistant's

keys

were initiallyturned over to the SFM and then were subsequently

removed from the

SFM's key locker and stored as spares.

Following the inspector's inquiry, the

licensee discovered that the Unit 2 MIDS power switch key was also duplicated for

use in other applications.

On September 24, in response to the number of duplicate keys identified for the

MIDS power switch, Procedure

RCP D-230 was updated to require an administrative

tagout to provide adequate

control of the MIDS during containment entries.

No

occurrences

were identified where the MIDS had been operated during personnel

entries into the containment.

C.

Conclusions

The scope of the licensee's

investigation and corrective actions in response to the

duplication of the MIDS power switch key was too narrow to adequately

bound the

- problem and ensure positive controls over the MIDS during containment entries.

This was considered

a weakness

in the licensee's corrective action program.

-17-

R3

RP&C Procedures

and Documentation

R3.1

Primar

Coolant Sam

le Procedure

P

a.

Ins ection Sco

e 71750

On September

27, the inspector observed

the drawing of a reactor coolant system

daily sample at the Unit

1 primary'ample sink.

Procedure

CAP E-1, Revision 118,

"Sampling of Primary Systems," was also reviewed.

b.

Observations

and Findin s

The "chemistry technician was knowledgeable

of the procedure

and demonstrated

proper radiological controls while working in the sample sink. A sufficient volume

of coolant was purged through the sample line to ensure

a representative

sample

was drawn.

The technician utilized an "issued-for-use"

copy of Procedure

CAP E-1, located in

the primary sample room, to draw the reactor coolant sample.

An "issued-for-use"

stamp was affixed to the cover page of the procedure,

indicating that it had been

verified to be current; however, the copy was that of Revision 11A and not 118.

The latest revision, 11B,'ad been implemented in April 1996.

A comparison

between the two revisions found only minbr administrative changes that did not

impact the intent of the procedure.

Procedure AD2.ID1, Revision 4, "Procedure

Use and Adherence," requires "issued-

for-use" procedures to be verified current.

Step 5.1.1.a states that, when a

procedure

is taken from a controlled manual and is to be used in the performance of

work, the cognizant supervisor or designated

individual shall verify that It is the

current revision immediately prior to starting work. Step 5.1.1.c states that

"procedures

in use longer than the "issued-for-use" interval shall be verified to be

the current revision..."

Both the verifier and the technician failed to identify and

update the superseded

revision of Procedure

CAP E-1 in the Unit 1 primary sample

room.

The failure to verify and update "issued-for-use" copies of controlled

procedures

was also documented

in NRC Inspection Report No. 50-275/96-06; 50-

323/96-06 with regard to the axial flux difference limits curve posted at the control

operator's station.

c.

Conclusions

The failure to verify and update the "issued-for-use" copy of Procedure

CAP E-1 in

the primary sample room was determined to be a violation of Procedure AD2.ID1

(VIO 50-275/96020-03).

-18-

R8

Miscellaneous

RPBcC Issues

R8.1

Housekee

in

in Radiolo ical Work Areas

a.

Ins ection Sco

e 71750

The inspector toured the radiologically controlled area and observed the

housekeeping

and radiological work practices in areas established to accomplish

maintenance

on contaminated

equipment.

b.

Observations

and Findin

s

The inspector observed that the radiological conditions in the 140 foot elevation of

the fuel handling building had improved from that noted in NRC Inspection

Report 50-275/96-03; 50-323/96-03.

Tools and protective clothing were noted to

be appropriately stored.

Radiological boundaries

were properly maintained in that

the areas were clearly marked and posted and there were no items laid across the

boundaries.

General cleanliness of the area had also been improved and the amount

of radioactive material that was being stored in the area had been significantly

reduced.

C.

Conclusions

The general housekeeping

and radiological work practices

in the fuel handling

building contaminated

work areas had significantly improved.

F1

Conduct of Fire Protection Activities

F1.1

Fire Watch Performance

a ~

Ins ection Sco

e 71750

On September

16, during a tour of the Unit 1 turbine building, the inspector

"'bserved maintenance

personnel performing welding on the service air supply to the

oily water separator.

The requirements of the welding and open flame permit

associated

with the work were evaluated to determine whether they were being

met.

b.

Observations

and Findin s

The Welding and Open Flame, Permit had been properly approved by a Fire

Protection Specialist, and required that a trained fire watch be stationed during the

work with a portable fire extinguisher in the work area.

Although several personnel

were in the room housing the oily water separator during the welding, a fire.watcli

was not readily identifiable.

Additionally, the required portable fire extinguisher was

outside the room, under the temporary work bench that had been set up for the job.

-19-

The portable extinguisher was, in fact, further from the work site than a permanent

fire extinguisher that was mounted on the exterior wall of the room.

The inspector

noted that the permit had not been initiated to indicate that these requirements

had

been met prior to the start of work.

Procedure

OMS.ID1, Revision 4, "Fire Loss Prevention," delineates the fire

protection requirements

during welding activities.

Section 3.3A of Attachment 7.1

to Procedure

OMS.ID'I states that the fire watch is responsible for being readily

identifiable (e.g., wearing a red vest or readily identifiable hard hat, arm band, etc.).

Section 4.3.7 states that "prior to the start of actual welding or open flame work

the worker or the fire watch shall initial the right side of the [Welding and Open

Flame Permit) after inspecting the area and confirming each of the requirements

designated

have been completed."

The failure of the maintenance

personnel to

properly designate

a fire watch and to verify that the requirements of the Welding

and Open Flame Permit had been met prior to commencing work was considered

a

violation of Procedure OMS.IDI.

co

Conclusions

The failure to properly designate

and identify a fire watch during welding activities

and the failure to verify and initial that the fire protection requirements

had been

met prior to commencing work was a violation of Procedure

OMS.ID1. This failure

constitutes

a violation of minor significance and is being treated as a noncited

violation consistent with Section IV of the NRC Enforcement Policy (NCV 50-

275/96020-04).

The placement of the portable fire extinguisher outside the room

where the welding was being performed was considered

a poor work practice.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management, at the

conclusion of the inspection on October 2, 1996.

The licensee acknowledged

the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

~

'

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. P. Powers, Manager, Vice President

DCPP and Plant Manager

J. R. Becker, Director, Operations

D. K. Cosgrove,

Supervisor, Safety and Fire Protection

S. R. Fridley, Manager, Outage Services

W. A. Ginter, Engineer, Nuclear Steam Supply Systems

Engineering

T. L. Grebel, Director, Regulatory Services

J. A. Hays, Director, Chemistry and Environmental Services

J. R. Hinds, Director, Nuclear Quality Services

S. C. Ketelsen, Supervisor,

Nuclear Quality Services

D. B. Miklush, Manager, Engineering Services

J. E. Molden, Manager, Operations Services

M. N. Norem, Director, Mechanical Maintenance

D. A. Vosburg, Director, Nuclear Steam Supply Systems

Engineering

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92901: Followup - Plant Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

~Qened

50-275/96020-01

NCV

Inadequate

work instructions and procedures for

installation of a freeze seal on SFP piping

50-275/96020-02

50-323/96020-02

50-275/96020-03

50-275/96020-04

IFI

PSRC interpretation of TS 3.4.6.2 regarding controlled

leakage

VIO

Failure to use the latest revision of CAP E-1 primary

sample procedure

NCV

Failure to follow fire watch procedures

0

-2-

Closed

50-275/96020-01

NCV

Inadequate

work instructions and procedures for

installation of a freeze seal on SFP piping

50-323/96002-01

VIO

Failure to perform required monthly channel checks of

in-core thermocouples

50-275/95006-01

50-275/9501 6-02

50-275/9501 6-03

50-275/96020-04

50-275/84050-00

VIO

Four examples of failure to follow procedure

VIO

Nuclear Instrument audio count rate secured when

required by TS

4

VIO

Fire door blocked open without authorization

NCV

Failure to follow fire watch procedures

LER

Failure to meet TS 3.3.3.6 surveillance requirements

50-275/94006-00

LER

CC pump outside of design basis due to throttling of

component cooling water to subcomponents

LIST OF ACRONYMS USED

AR

CC

CCW

CVCS

EDG

LER

MIDS

OTSC

PD

PDR

PPC

PSRC

RHR

RP

SFM

SFP

TM

TS

UFSAR

WO

action request

centrifugal charging

component cooling water

chemical and volume control system

emergency diesel generator

licensee event report

moveable incore detector system

on the spot change

positive displacement

public document room,

plant process computer

Plant Staff Review Committee

residual heat removal

radiation protection

shift foreman

spent fuel pool

technical maintenance

Technical Specification

Updated Final Safety Analysis Report

work order

Pq

J