ML16342D432

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-275/96-12 & 50-323/96-12 on 960710
ML16342D432
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 08/26/1996
From: Dyer J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Rueger G
PACIFIC GAS & ELECTRIC CO.
References
NUDOCS 9609230026
Download: ML16342D432 (18)


See also: IR 05000275/1996012

Text

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UNITEO STATES

NUCLEAR REGULATORYCOMMlSSlON

REGION IV

611 RYAN PLAZAORIVE, SuITE 400

ARLINGTON,TEXAS 760114064

August 26,

1996

Gregory M. Rueger, Senior Vice President

and General Manager

Nuclear Power Generation

Bus. Unit

Pacific Gas and Electric Company

Nuclear Power Generation, B14A

77 Beale Street, Room 1451

P.O. Box 770000

San Francisco, California 94177

SUBJECT:

NRC lNSPECTION REPORT 50-275/96-12'0-323/96-12

Thank you for your letter of August 9, 1996, in response to our letter and Notice of

Violation dated July 10, 1996.

We have reviewed your reply and find it responsive to the

concerns raised in our Notice of Violation. We willreview the implementation of your

corrective actions during a future inspection to determine that full compliance has been

achieved and will be maintained.

Sincerely,

Docket Nos.:

50-275

50-323

License Nos.:

DPR-80

DPR-82

J. E. Dyer, Director

Division of Reactor Projects

CC:

Dr. Richard Ferguson

Energy Chair

Sierra Club California

1100 lith Street, Suite 311

Sacramento,

California 95814

960923002b

960826

PDR

ADOCK 05000275

8

PDR

Pacific Gas and Electric Company

-2-

Ms. Nancy Culver

San Luis Obispo Mothers for Peace

P.O. Box 164

Pismo Beach, California 93448

Chairman

San Luis Obispo County Board of

Supervisors

Room 370

County Government Center

San Luis Obispo, California 93408

Mr. Truman BurnshMr. Robert Kinosian

California Public Utilities Commission

505 Van Ness, Rm. 4102

San Francisco, California 94102

Robert R. Wellington, Esq.

Legal Counsel

Diablo Canyon Independent

Safety Committee

857 Cass Street, Suite D

Monterey, California 93940

Mr. Steve Hsu

'adiologic Health Branch

State Department of Health Services

P.O. Box 942732

Sacramento,

California 94234

Christopher J. Warner, Esq.

, Pacific Gas and Electric Company

P.O. Box 7442

San Francisco, California 94120

Robert P. Powers, Vice President

and Plant Manager

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, California 93424

Pacific Gas

and Electric Company

-3-

E-Mail report to D. Nelson

(DJN)

E-Hail report to

NRR Event Tracking System

(IPAS)

bcc to

DMB IE01

'cc distrib. by RIV:

L. J. Callan

DRP Director

Branch Chief (DRP/E,

WCFO)

Senior Project Inspector

(DRP/E.

WCFO)

Branch Chief (DRP/TSS)

Leah Tremper

(OC/LFDCB,

MS:

TWFN 9E10)

Resident

Inspector

DRS-PSB

HIS System

RIV File

M:

Hammond

(PAO.

WCFO)

DOCUMENT NAME:

R:t DCNDC612AK.FRH

To receive copy of document,

indicate In box: "C" = Copy without enctosures

"E" = Copy with enctosures

"N" = No copy

C:DRP/E

HJWong

08

96

D:WCFO

I

D:DRP

KEPerkins

JEDyer

08@696

08/ /96

08/&/96

OFFICIAL RECORD COPY

08/ /96

0

Pacific Gas

and Electric Company

-3-

E-Mail report to D. Nelson

(DJN)

E-Mail report to

NRR Event Tracking System

(IPAS)

.bcc to DMB IEOl

bcc distrib. by RIV:

L. J. Callan

DRP Director

Branch Chief (DRP/E.

WCFO)

Senior Project Inspector

(DRP/E.

WCFO) .

Branch Chief (DRP/TSS)

Leah Tremper

(OC/LFDCB,

MS:

TWFN 9E10)

Resident

Inspector

DRS-PSB

MIS System

RIV File

M.

Hammond

(PAO.

WCFO)

DOCUMENT NAME:

R:K DCNDC612AK.FRH

To receive copy of document,

indicate In box: "C" = Copy without enclosures

"E" = Copy with enctosures

"N" = No copy

C:DRP/E

HJWong

08

96

D:DRP

D:WCFO

KEPerkins

JEDyer

08/&/96

08/ /96

08@&6

OFFICIAL RECORD COPY

08/ /96

0

Pacific Gas and Hectric Company

August 9, 1996

PG8 E Letter DCI=96-167

245 Market Street. Room 937-N9B

San Francisco, CA 94105

.ila///ug ilrlclnm

Mail Code N9B

P.O. Box 770000

San Francisco. CA 94177

415/973-4684 Fax 415/973-2313

Gregory M. Rueger.

Senor Vice President and

General Manager

Nuclear Power Generation

U.S. Nuclear Regulatory Commission

ATI'N: Document Control Desk

Washington, D.C. 20555

Docket No~ 50-275, OL-DPR-80

Docket No. 50-323, OL-DPR-82

Diablo Canyon Units 1 and 2

Re

I to Notices of Violation and Notice of Deviation in NRC Ins ection Re ort Nos. 50-275/96-

12 and 50-323/96-12

Dear Commissioners and Staff:

NRC Inspection Report Nas. 50-275/96-12 and 50-323/96-12, dated July 10, 1996, and

amended on July 11, 1996, included two Severity Level IVviolations regarding implementation

of the Unit 1 Main Steam Safety Valves (MSSVs) Augmented Testing and Inspection Program.

The inspection report also included a notice of deviation regarding PG8 E's failure to obtain

valve-specific correction factors during the Unit 1 seventh refueling outage (IR7) for 11 of 20

MSSVs contrary to a commitment made in PG8 E letter DCL-95-241, dated November 1, 1995.

PG8 E's response, summary cause analysis, and corrective actions associated with the

violations and deviation are enclosed.

The specifics associated with events leading to these

violations and the deviation have already been discussed

in detail at the July 1, 1996,

Predecisional Enforcement Conference held in Arlington, Texas.

PG&E wants to emphasize its recognition and appreciation of two points expressly mentioned in

the inspection report.

First, PG8 E as the licensee has the continuing and ultimate responsibility

to ensure that the Diablo Canyon Power Plant is operated at all times in accordance with its

Technical Specifications.

In this instance, PG8 E did not fulfillthis responsibility, because of a

lack of formality in developing and implementing the augmented MSSV testing program.

Second, PG&E recognizes and willcontinue to emphasize the absalute need for assuring that

all communications between PG8 E and the NRC are made in a prompt and accurate manner,

are made to the appropriate NRC persannel, and are properly documented.

Sincerely,

CC:

Steven D. Bloom

L. J. Callan

Kenneth E. Perkins

Michael D. Tschiltz

Diablo Distribution

INPO

Enclosure

WEC/2237/N0001 327

Enclosure

PG8,E DCL Letter 96-167

REPLY TO NOTICES OF VIOLATIONIN

NRC INSPECTION REPORT NOS. 50-275/96-12 AND 50-323/96-1 2

Qn July 11, 1996, as part of NRC Inspection Report (IR) Nos. 50-275/96-12 and

50-323/96-12, NRC Region IV issued two Severity Level IV Notices of Violation (NOVs)

and one Notice of Deviation (NOD) to Diablo Canyon Power Plant (DCPP), Units 1

and 2. The statements of violation and deviation and PG&E's responses

are

documented below.

STATEMENT OF VIOLATIONA

10 CFR Part 50, Appendix B, Critenon XVI, states, in part, that measures shall be

established to assure thaf condifions adverse to qualify are promptlyidentified and

corrected.

l.

Confrary to the above, on April2; 1996, fhe licenseeidentified a condition adverse to

quality wifh respect to the liftsetpoinfs on 3 of5 Unit 1 main steam safefy valves tested

(main steam lead 1), and did nof take prompt acfion to determine whether the same

condition existed on the main sfeam safefy valvesin main steam leads 2, 3, and 4.

Specifically, fhe main steam safety valves on main steam lead 2 were not tested until

April 11, 1996, when 3 of5 were found ouf-of-tolerance, and the main steam safety

valves on main steam leads 3 and 4 were not fested untilApril14, 1996, when 5 of5

valvesin main-steam lead 3 and 1 of5 valvesin main steam lead 4 were found ouf of-

tolerance.

This is a Severity Level /Vviolafion (Supplement I).

REASON FOR THE VIOLATION

PG8 E agrees with the violation as stated in the IR.

PG8 E has determined that the cause of the delays in testing the additional steam leads

was a lack of formality and rigor in developing and implementing the Augmented

Testing Program for the main steam safety valves (MSSVs). Though the procedure for

performing the augmented testing was well defined, PG&E did not adequately define

the actions that should be taken should adverse test results be obtained.

PG&E failed

to recognize that although it had committed to discuss test findings with the NRC before

expanding the scope of testing, its primary responsibility was to assure compliance with

the Technical Specifications (TSs).

PG8 E should have promptly expanded the testing

to assure that additional out-of-tolerance (QQT) conditions were identified and

corrected.

The circumstances

surrounding this failure to promptly expand testing are

addressed

in the following sections.

Enclosure

PG8E DCL Letter 96-167

Back round

In September of 1995, PG8E submitted to the NRC License Amendment Request

(LAR) 95-06, "Request for Emergency Review and Approval of Change to Technical Specification 3.7.1.1, Table 3.7-2- Increase in Setpoint Tolerances for Main Steam

Safety Valves." LAR 95-06 explained that despite efforts to resolve the problem, MSSV

testing results were continuing to show a pattern of high initial lifts. The LAR requested

relaxation of.the TS tolerances and presented the necessary supporting safety

analyses.

On October 1, 1995, the NRC issued License Amendments (LAs) 108 and

107 to PG8 E. The new TSs relaxed the MSSV as-found tolerances from+/-1 percent

to +/- 3 percent (+3/-2 percent for the lowest set valves).

As a condition of the LAs, PGKE was required to perform augmented inspection and

testing on the MSSVs on a more frequent basis than that required by the ASME Code

.

for at least one operating cycle. The NRC required that PG8 E provide additional

details on the program by November 1, 1995.

On November 1, 1995, PG8 E submitted

letter DCL-95-241, "Main Steam Valve Augmented Testing and Inspection Program."

In the letter, PG8E explained that the testing program would provide information on the

time dependency aspects of high initial liftphenomenon observed during past on-line

testing.

PG8 E stated itwould perform augmented testing on the Unit 1 valves one

steam header at a time on a staggered test basis to provide varying time periods

. between header tests.

PG8E also stated that testing to meet the requirements of

TS 3.7.1.1 and the ASME Code for all the Unit 1 MSSVs would be conducted just prior

to the eighth refueling outage (1R8). PG8 E further stated that ifthe MSSV lifts are not

within +/-'

percent, but are within+I-3 percent (+3/-2 percent for the lowest set

MSSVs), the valves would be reset.

No test expansion beyond the five valves on the

test header would be done in an effort to preserve the time related aspect of the test

data.

Should a valve or valves liftoutside the as-found TS tolerance, the valve(s)

would be returned to+/-1 percent tolerance and the'scope of additional testing would

be discussed with the NRC staff prior to expanding the testing.

The NRC responded to PG8E's proposal on December 26, 1995. The NRC response

reiterated PG8 E's proposal and concluded by stating that the NRC staff had reviewed

the licensee's submittal dated November 1, 1995, and had determined that the

augmented testing and inspection plan described therein was acceptable.

T~iP

Qn April 2, 1996, PG8 E conducted its first round'of augmented testing of Unit 1 Steam

Lead

1 in accordance with approved work orders and Maintenance Procedure M-4.18,

'Verification of LiftPoint Using Ultra Star Assist Device for the Main Steam Safety

Valves."

Enclosure

PG&E DCL Letter 96-167

When testing found three of five MSSVs OOT high on the initial lifts, PG8 E reset the

valves, documented the as-found OOT conditions on action requests (ARs), and

requested analyses to be performed on results by the San Francisco based Regulatory

and Design Services'R8DS) Transient Analysis (TA) Group. The R8DS TA Group

performed a preliminary analysis (projecting results over 20 valves), determined the

results were within the design bases of the plant, and forwarded the findings to the site

on April4, 1996.

On April 8, 1996, PG8 E initiated a conference call with the NRC to

discuss the Unit 1 MSSV as-found data, analysis results, and the possible expansion of

testing.

PG&E informed the NRC that data on five additional valves would be collected

and that PG8 E would notify the NRC of the test results.

On April 10 and 11, 1996, PG&E tested Main Steam Lead 2. The initial lifts of three of

five MSSVs were high OOT. PG8 E reset two of the OOT valves and the other was left

at+ 1.4 percent.

(See response to NOV "B"contained herein.)

PG&E documented the

as-found OOT conditions on ARs and submitted the data to the TAgroup for analysis..

On the morning of April 12, 1996, PG8E and the NRC held another conference call to

discuss the latest findings and further testing.

PG8 E informed the NRC that testing on

the remaining ten valves on Steam Leads 3 and 4 would resume on April 14, 1996, and

that results should be available on April 15 or 16, 1996.

At 1730 PDT, on April 12, 1996, PG8 E made a 10 CFR 50.72 report to the NRC that

the as-found liftpressures ofsix of ten Unit 1 MSSVs (Main Steam Leads

1 and 2)

exceeded the:TS setpoint tolerance of +1- 3 percent and that preliminary analysis of the

data indicated that the condition constituted a condition outside the design basis of the

plant. At approximately 2130 PDT, on April 12, 1996, another conference call was held

between the NRC and PG8 E in response to the NRC requesting additional information

on MSSV testing, the basis for the 50.72 report, and the operability determination for

the untested ten MSSVs on Steam Leads 3 and 4. PG8 E indicated at this time that

arrangements

were being made to test Steam Leads 3 and 4 valves on April 14, 1996.

On April 14, 1996, PG8 E conducted testing on Steam Leads 3 and 4. On Steam

Lead 3, five of five MSSVs lifted high OOT. PG8 E reset four of the five MSSVs and left

one at 1.2 percent.

(See response to NOV "B"contained herein.)

On Steam Lead 4,

one of five MSSVs lifted high OOT. PG8 E reset the one OOT MSSV. The test results

were documented on ARs and the data was submitted to the R8 DS TA group for

analysis.

A conference call was held with the NRC on April 16, 1996, to discuss the

latest test results.

On April 18, 1996, the R&DS.TA Group forwarded preliminary analysis results to the

site that indicated peak steam pressure remained within the 110 percent design

'ressure

if credit was taken for either direct reactor trip from turbine trip or for the 40

percent steam dump valves.

PG8 E discussed the analyses results with the NRC on

April 19, 1996 and reported the results April 25, 1996 in LER 1-96-003-00, "Technical

. Enclosure

PG8 E DCL Letter 96-167

Specification 3.?.1.1 Not Met During Testing of MSSVs Due to Setpoint DriA; Unit 1

MSSVs Outside Design Basis Due to Setpoint Drift."

Lessons Learned

While acknowledging in the lR that PG8E did pursue testing of all Unit 1 MSSVs, the

NRC noted that its concern was with the aggressiveness'and

timeliness of PG8 E's

pursuit of the potential OOT conditions. The lR further stated that it appeared from the

NRC's perspective that PGRE engineering personnel had lost sight of PG8E's ultimate

responsibility to maintain the facilitywithin the requirements of the TSs and that this

occurred largely because of a lack of formality and rigor in developing and

implementing the Augmented Test Program.

The IR states that a number of important

decisions in this matter were made by one individual, including decisions regarding

operability, and that these decisions were not appropriately documented nor were they

subjected to further evaluation.

The IR further stated that in regard to this violation, the NRC noted that a similar

condition was discovered in September 1995, when 19 of 20 Unit 1 MSSVs were found

OOT on their initial liftand an analysis showed that this condition would have resulted

in the steam generators exceeding 110 percent of their design pressure.

Thus, PG8 E

should have been more sensitive to the possibility that this same condition existed

when Main Steam Lead 1 was tested on April2, 1996, and three offive MSSVs were

found OOT high, and should have expanded testing to the other leads more promptly.

PG8E agrees with the statements above.

PG&E acknowledges that mistakes and

errors in judgment were made in implementing the MSSV Augmented Testing Program

and has learned several important lessons from this experience.

First, PG8E inappropriately allowed an unacceptable degree of "informality"to be

associated with this Augmented Testing Program and thus did not apply its normal rigor

to the process.

PG8 E now recognizes that the "augmented" nature of this test program

does not relieve it of its responsibility as a licensee to promptly and correctly address

any test results that call into question system operability. Because of the potential for

the discovery of inoperable valves during testing, PG8 E should have been better

prepared for, and should have vigorously pursued, identification and correction of any

additional OOT conditions to assure that the plant continued'to operate within the limits

of the TSs.

Second, where uncertainty existed, prior to beginning the tests PG8E should have

taken the Initiative to clarify its underStanding of the test process to be used with

appropriate NRC personnel.

Enclosure

PG8E DCL Letter 96-167

P

CORRECTIVE STEPS TAKENAND RESULTS ACHIEVED

'I.

PG8E has conducted performance counseling with the individual who made

several of the key decisions during th'e test program.

2.

3.

4.

PG&E has now formalized its Augmented Test Program into Surveillance Test

Procedure (STP) M-77A, Revision 0, "Augmented Test Program for Main

Steam Safety Valves (MSSV)'." The PG&E letter to the NRC (DCL-96-156)

dated Aly16, 1996, transmitted this procedure and Maintenance Procedure

M-4.18, Revision 14, 'Verification of LiftPoint Using Ultra Star Assist Device for

the Main Steam Safety Valves."

STP M-77A includes provisions for scope expansion.

It also states that MSSV

testing shall be considered "in progress" until'all of the valves, including any

expansions,

have been tested.

It states that it is management's

expectation, due

to the importance of the testing, that the testing should continue 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> per

day, 7 days a week, unless test results indicate a design basis concern.

Ifa

design basis concern is indicated, testing willbe completed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of

the identification of the concern.

Though we believe communication

inadequacies regarding augmented testing expectations existed between PG&E

and the NRC, in this situation,. as the licensee it is PG&E's responsibility to

ensure that a common understanding exists.

's

prescribed in M-77A:

a)

Operations and management willbe informed of OOT conditions.

')

Prompt operability assessments

will be generated as necessary.

c)

Time limits have been set on the determination of operability of each

steam lead and test expansion to other steam leads.

A project manager as been appointed to specifically manage the MSSV

Augmented Testing Program.

DATE WHEN FULLCOMPLIANCEWILLBE ACHIEVED

PG8E is currently in full compliance.

The procedure was approved and became effective on July 16, 1996.

It was successfully used on July

18, 1996, to test the MSSVs on Unit 1 Lead 3.

Enclosure

PG8E DCL Letter 96-16T

STATEMENT OF VIOLATION8

Diablo Canyon Technical Specification 3/4.7. 1, Table 3.7-2 requires, in part, that steam

line safety valve liftsettings be returned "Withins1% following main steam line Code

safety valve testing.

Contrary fo the above, on April 11, 1996, and on April14, 1996, the licensee found

main steam safety valves MSS V-223 and MSS V-14 ouf oftolerance by 1.4% and 1.2%

respectively.

Following the testing, the licensee did not reset them within the allowed

tolerance of +1% ofthe specified seffing before returning fhem to an operable status.

Thisis a Severity Level IVviolation (Supplement I)

REASON FOR THE VIOLATION

PG8 E agrees with the violation as stated in the IR.

The setpoints of the valves, as measured with the Ultra Star (or AVK)test equipment,

were not altered at the tim'e of testing because PG8E believed that adjusting the valves

would have resulted in less conservative setpoints than those previously recorded

when the valves were set on live steam at the Westinghouse Western Service Center

(WSC). However, PG8E failed to document in a formal 10 CFR 50.59 safety

evaluation that this decision met the requirements of the TSs.

Further explanation of

this event follows.

PG8 E stated in LER 1-96-003-00 that test personnel were only able to develop

correction factors (CFs) for 9 of 20 Unit 1 valves during the October 1995 testing at the

WSC.

(Also see the response to the NOD contained in this letter.) Of the nine valves

for which CFs were obtained, the data collected showed a maximum AVKsetpoint

variation of +l- 1.4 percent from the settings achieved on steam alone. Therefore,

PG8 E judged that during in-situ testing, valves without CFs that are returned to +l- 1

.percent of their measured setpoint using AVKwould be susceptible to the+I-1.4

percent error introduced by the AVKtest methodology.

That is, a valve returned to

within+i-1 percent could have an additional error of up to+i-1.4 percent added to its

liftsetpoint.

During the in-situ testing, PG8 E considered the foregoing information and the as-found

data in deciding whether or not to reset the valves.

PGBE reasoned that it would b

m re conservative to leave valves unadjusted for which the as-found setpoints were

i wou

e

less than + 1.5 percent and chose to accept instead the more accurate live-steam

settings recorded at the WSC.

Similarly, PG8 E reasoned

it would be more

conservative to adjust valves for which the as-found setpoints were'greater than+ 1.5

percent.

As MSSV-223 and MSSV-14 were two of the eleven valves without CFs and

Enclosure

PG8 E DCL Letter 96-167

P

their as-found setpoints were less than+1.5 percent, they were left unadjusted.

Other

valves without CFs forwhich as-found setpoints greater than +1.5 percent were

accordingly reset to within+/-1 percent.

Though PG&E continues to believe the

reasoning used to not readjust the two valves was correct and that the requirements of

the TSs had been met, PG&E failed to document the decision and the basis in a formal

10 CFR 50.59 safety evaluation.

PG8 E believes this event occurred in part because of the failure to have a formal,

documented Augmented Test Program plan considering all the potential issues that

would develop during testing.

Had PG&E developed a more formal test plan, the issue

of when or when not to reset the valves would have been thoroughly thought through

and formally documented prior to test results being received and time pressures

being

felt.

From this experience, PG&E has learned that it should have documented in a

10 CFR 50.59 safety evaluation that the accepted settings for MSSV-223 and MSSV-14

were those established at the WSC and not those recorded as "as-left" in Maintenance

Procedure M-4.18. This experience also underscores the importance of more formal

test planning, as discussed

in PG&E's response to Violation A.

CORRECTIVE STEPS TAKENAND RESULTS ACHIEVED

1.

MSSV-223 and MSSV-14 were retested on April21, 1996. The valves were left

with settings within +/- 1 percent of setpoint.

2.

STP M-77Awas written and approved to formalize the, test program.

It explicitly

states the acceptance

criteria for as-left settings using the AVKtechnology.

3

The principal individuals involved with the in-situ testing of MSSV-223 and

MSSV-14 participated in the preparation of STP M-77A and.in the preparation or

reviews of the response

to this NOV. Therefore, they are cognizant of the

lessons learned.

DATE WHEN FULL COMPLIANCEWILLBE ACHIEVED

PG&E is currently in full compliance.

Enclosure

PG&E DCL Letter 96-167

STATEMENT OF NOTICE OF DEVIATION

PG8 2 Letter DCL-95-241 dated November 1, 1995, stated thaf "The following

additional MSSV testing willbe completed dunng 1R? and 2R? oufages at fhe

Westinghouse fest facility:

1)

Valve signature

profiles

willbe defermined on live sfeam and with fhe AVKtest

equipmenf

2)'he magnitude ofthe AVKfest equipmenf bias willbe determined."

Confiary to fhe above, on November 24, 1995, the 1R7 outage was complefed, but the

licensee had determined the magnitude ofAYKtest equipmenf bias on only 9 of 20

Unit 1 MSS Vs. As ofJuly 1, 1996, the licensee had not submitted a requesf forrelief

from ifs commifmenf fo defermine AVKfest equipment bias during 1R7.

'I

REASON FOR THE DEVIATION

PG& E agrees with the deviation as stated in the IR.

PG&E failed to obtain the AVKtest equipment bias and Unit 1 valve-specific CFs for 11

of 20 valves due to equipment problems at the test facility. ln addition, PG&E

personnel failed to document and effectively communicate internally and to the NRC

that the commitment would not be met as required by procedure.

Testin

Back round

ln October 1995, during the Unit 1 seventh refueling outage (1R7), all 20 MSSVs were

removed and shipped to.the WSC in Beaumont, Californi. Testing was to be

performed during a nominal two-week window (October 8, 1995, to October 20, 1995)

to obtain AVKtest equipment bias and to perform Code testing to satisfy the

requirements of the TSs.

Near the end of the first week of testing (approximately October 13, 1995), pG&E

engineering personnel collecting the AVKbias information had determined that none of

the data collected was valid because

the steam accumulator on the test stand for this

data collection was too small in capacity to give valid data.

This information was

relayed to the'esponsible

director at DCPP..

The director, after discussions with test personnel at WSC, recognized that only limited

scope testing could be accomplished at WSC during the remaining week of the

available testing window and directed that half of the valves (those for Steam Leads

3 and 4) be returned to DCPP once the Code safety testing and steam signature testing

Enclosure

PG8E DCL Letter 96-167

had been completed using a larger test stand.

It was anticipated that the remaining

AVKvalve-specific bias data could be collected at the site when the valves were re-

installed at DCPP.

It was later determined, however, that in-situ testing for collection of

the bias information could not be done.

Afterthe valves for Steam Leads 3 and 4 were shipped back to DCPP, personnel at the

WSC devoted the remaining time, using the larger te'st stand, to testing and obtaining

complete data for the valves on Steam Leads

1 and 2. On October 20, 1995, the

remaining ten'valves for Steam Leads

1 and 2 were returned to DCPP. At this point in

time, because of the time constraints for testing the valves at the WSC and data being

lost for one valve, PG8 E had collected AVKdata for only 9 of 20 valves.

On November 1, 1995, PG8 E sent the letter (DCL-95-241) containing the commitment

which is the subject of this NOD.

PG8E Investi ation

The investigation into this event revealed that there were deficiencies in PG8 E's

performance in addition to its failure to collect the AVKequipment bias data for all 20

valves.

PG8 E failed to modify the November 1, 1995, letter to the NRC when it was

known to PG8E that testing had been completed at WSC and that only a portion of the

AVKvalve-specific bias data had been collected. Atthe time engineering continued to

believe that the data in question could be obtained once the valves were reinstalled at

DCPP.

PG8 E also failed to notify the NRC of the missed commitment and to

implement corrective action to obtain the data before the end of 1R7 on

November 26; 1995.

The reason for PG8 E's failure to obtain a complete and valid set of AVKequipment

bias data is addressed

in. the testin'g background presented above.

PG8 E believes the

other failures were attributable to a breakdown of proceduralized communications.

PGBE procedure XI1.ID1, "Regulatory and Correspondence

Processing," directs that

the responsible individual or department should contact R8 DS ifthey cannot complete

a commitment action prior to its firm due date.

PG8E has determined that prior to the

end of 1R7 on November 26, 1995, full and effective communication of the status of the

MSSV Augmented Testing Program did not occur among engineering personnel,

R8 DS, and management.

Had this communication occurred as prescribed, PG8 E

would have communicated this information'to the NRC, and:PG8E management would

have had an opportunity to implement corrective action.

This breakdown of communication was also the reason why PG&E failed to generate

an AR to track the commitment to obtain the Unit 1 AVKtest equipment bias information

as stated in the November 1, 1995 letter. PG8 E stated at the Enforcement Conference

Enclosure

PGB,E DCL Letter 96-167

that RB DS had failed to generate an AR. PGB E has since determined that. an AR was

purposely not written for the Unit 1 valves because of a miscommunication between

R&DS and Secondary Engineering.

On November 6, 1995, when a Unit 2 tracking

document was generated,

RBDS personnel were informed that the Unit 1 testing had

b

been completed.

RBDS then concluded that the gathering of all AVKtest equipme t

ias information was also completed.

Consequently,

RBDS did not generate a tracking

ip

en

document for a task that supposedly had already been completed.

CORRECTIVE STEPS TAKENAND RESULTS ACHIEVED

PGB E has addressed

the operability of MSSVs without valve-specific CFs in

Operability Evaluations (OEs) 96-04, "Operability of Main Steam Safety Valves

that Do Not Have Valve Specific Correction Factors," and 94<2, "Operability of

Main Steam Safety Valves with Potentially High Initial LiftSetpoints." These

OEs conclude that using AVKssuggested

CF (mean seat area) to set the valves

is appropriate and that the plant can operate safely.

2.

PGB E willcollect AVKequipment bias data for the remaining 11 valves during

1R8.

PGB E has generated

a commitment tracking document to track this

commitment.

I

4.

A nonconformance report has been generated to address missed commitments.

5.

PGB E has appointed a project manager to specifically manage the MSSV

Augmented Testing Program.

Reca

in

Current MSSV Commitments

Units 1 and 2 MSSV augmented testing involving one'steam header at a time will

be conducted on a staggered test basis to provide varying time periods between

header tests.

Ifthe MSSV lifts are not within +/- 1 percent, but are within +/- 3

percent (+3/-2 percent for the lowest set MSSVs), the valves willbe reset.

Should a valve or valves liftoutside the+/- 3 percent tolerance, the valve(s) will

be returned to +/- 1 percent tolerance.

2.

It is intended that augmented testing provide information on the time

dependency aspects of the high initial liftphenomenon observed during past

on-line testing.

This testing willprovide a set of on-line test data for each of the

five valves on each lead prior to the eighth refueling outages (1R8 or 2R8) on

the respective units. However, ifthe results of the augmented testing on a

specific lead indicate that test expansion to other leads is necessary

to conform

to TS requirements, test expansion willpromptly occur, and PGB E willtreat the

results obtained for operability evaluation as ifthese tests were TS

Enclosure

PG&E DCL Letter 96-167

surveillances.

Should testing'of valves on additional leads be necessary,

the

further expansion willpreclude PG&E from collecting the time-deperidency data

needed for analyzing the high initial liftphenomenon.

3.

PG8 E's efforts to determine the root cause of the high initial lifts is on-going.

(Reference PGBE letter DCL-95-241 dated November 1, 1995, "Main Steam

Safety Valve Augmented Testing and Inspection Program.") A summary of the

results of the root cause evaluation activities and corrective actions willbe

providad upon completion of the analyses and evaluations.

4

PG&E willtest all MSSVs upon return to Mode 3 (Hot Standby) from any Mode 5

(Cold Shutdown). This testing willcontinue until the analysis is complete and

corrective actions (replacement of valve seating material, etc.), ifany, are taken.

NRC concurrence for discontinuation of this testing willbe obtained.

5.

Commitments made at Enforcement Conference on July 1, 1996:

a)

Regarding "AVKTest Methodology Validation," PG&E willcomplete the

uncertainty analysis.

b)

c)

d)

e)

PG&E willcomplete the seating materials replacement evaluations.

PG&E willconduct MSSV-specific performance evaluation.

C

PG&E willconduct potential MSSV Parts Improvement Program.

i

PG&E willmonitor industry MSSV experience.

f)

Technical staff training:

1)

As one of the "CF Corrective Actions," PG8 E willreview

appropriate licensing commitment implementation and NRC

communication requirements.

2)

As one of the "Conduct of Test Program Corrective Actions," PG&E

willconduct training on the missed commitment event focusing on

technical data'evaluation,

formal communication, and compliance

with commitments.

3)

As one of the "SV Operability 8 Timeliness Corrective Actions,"

PG8 E will conduct training on operability determination

procedures.

(Partially or fully completed as this response

is

prepared.)