ML16342D201
| ML16342D201 | |
| Person / Time | |
|---|---|
| Site: | Diablo Canyon |
| Issue date: | 01/23/1996 |
| From: | Brockman K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML16342D202 | List: |
| References | |
| 50-275-95-10, 50-323-95-10, NUDOCS 9602120115 | |
| Download: ML16342D201 (94) | |
See also: IR 05000275/1995010
Text
ENCLOSURE
U.S.
NUCLEAR REGULATORY COMMISSION
REGION IV
Inspection Report:
50-275/95-10
50-323/95-10
Licenses:
DPR-82
Licensee:
Pacific Gas
and Electric Company
77 Beale Street.
Room 1451
P.O.
Box 770000
San Francisco.
Facility Name:
Diablo Canyon
Power Plant,
Units
1 and
2
Inspection At:
Diablo Canyon
Power Plant
~
San Luis Obispo County. California
Inspection
Conducted:
September
18 through October
20 onsite
and in-office
review through
November
17.
1995
Inspectors:
I. Barnes.
Technical Assistant
Division of Reactor Safety
W. Sifre
~ Resident
Inspector
Division of Reactor Projects
K. Weaver.
Reactor Inspector.
Maintenance
Branch
Division of Reactor Safety
Accompanying Personnel:
S.
Boynton. Resident
Inspector
Division of Reactor Projects
Dr.
C.
Doddy
NRC Consultant
P.
Rush. Materials Engineer
Materials
and Chemical
Engineering
Branch
Office of Nuclear Reactor Regulation
Approved:
r
,
y
erector
D vision o
ea
r Safety
23
9g
a e
9602i201i5 960i25
ADQCK 05000275
8
-2-
Ins ection
Summar
Areas
Ins ected
Units
1 and 2:
Regional initiative. announced
inspection to
review the history and material condition of steam generator tubing;
and to
assess
the effectiveness
of licensee
programs in detection
and analysis of
degraded
tubing, repair of defects.
and correction of conditions contributing
to tube degradation.
The inspection additionally included observation of
inservice inspection
work and work activities and followup on previous
inspection findings.
Results
Units
1 and
2
Backcaround
~
Diablo Canyon
Power Plant. Units
1 and 2, utilize four Westinghouse
Model 51 vertical recirculating
per unit.
Each steam
generator
contains
3.388 Inconel
600 U-tubes. with a nominal diameter
and wall thickness.
respectively.
of 0.875 inches
and 0.050 inches
(Section 2.1).
~
Diablo Canyon
Power Plant.
Units
1 and 2.
have been operated with a
primary side hot-leg temperature of 603'F during commercial operation
(Section 2.2).
Tube
De radation
~
The predominant
tubing degradation
modes in Unit
1 have.
to date.
been primary water stress
corrosion cracking (at dented
and
non-dented
tube support plate intersections'elow
the explosive
expansion transition region,
and in the low radius
bends of Rows
1 and
2
U-tubes).
wear at anti-vibration bars.
cold-leg thinning,
and outside
diameter
stress
corrosion cracking at nondented
tube support plate
intersections
(Section 2.5. 1).
~
The predominant
tubing degradation
modes in Unit 2 have.
to date.
been primary water stress
corrosion cracking (at dented tube
support plate intersections'elow
the explosive expansion transition
region,
and in the low radius
bends of Rows
1 and
2 U-tubes), cold-leg
thinning,
and outside diameter stress
corrosion cracking at nondented
tube support plate intersections
(Section 2.5.2).
~
The incidence of Unit
1 primary water stress
corrosion cracking was
significantly lower, to date,
1-3 and 1-4 than in
Steam Generators l-l and 1-2 (Section 2.5.3).
Maintenance
~
The foreign material exclusion program requirements
and practices for
the steam generator
secondary
side were appropriate
and have
been
generally well implemented
(Section 3. 1).
0
-3-
~
Visual inspections of the steam generator
secondary
side were first
performed during Refueling Outage
1R6 in April 1994.
Earlier
implementation of an internal inspection
program could have provided
a
more timely identification and evaluation of J-tube.
barrel riser.
and
nozzle plug erosion/corrosion
phenomena
(Section
3. 1).
~
Licensee nondestructive
examination
personnel
were knowledgeable of
examination techniques
and showed
good adherence
to procedural
requirements
(Section 7.5).
~
Inclusion of operational
experience
in ultrasonic inservice inspection
efforts was considered
commendable
(Section 7.5.3).
En ineerin
The licensee
was viewed to have
been proactive with respect to eddy
current examination
scope.
adoption of new eddy current examination
technology,
and incorporation of industry experience
(Section 4. 1).
The eddy current examination
program requirements
were found to be
generally consistent with the recommendations
contained in Electric
Power Research
Institute
EPRI NP-6201.
Revision 3.
An exception noted
was the absence
of quantitative criteria for handling noisy data.
An
inspection
followup item was identified pertaining to review of the
conformance of the eddy current examination
procedures
to Appendix
H of
Electric Power Research
Institute
EPRI NP-6201,
Revision 3
(Section 4.2.1).
Eddy current examination
program strengths
noted were:
(1) use of only
analysts
who had been certified as qualified data analysts
in accordance
with the requirements
of EPRI NP-6201,
Appendix G: (2) screening for
loose parts in Rows
1 and
2 and the outer two rows of the tube bundle
periphery;
and,
(3) use of two separate
companies
to perform independent
primary and secondary
analysis
(Section 4.2. 1).
An inspection followup item was identified pertaining to review of a
analyses
of conformance of cold-leg thinning indications to
Regulatory Guide 1. 121 (Section 4.3).
The failure of licensee
personnel
for 10 years to identify a procedural
error pertaining to ultrasonic Level I examiner training requi rements
was considered
an indicator of inadequate
attention to detail
when
revising and using procedures
(Section 7.3).
Plant
Su
ort
The licensee
has developed
a good secondary
water chemistry program and
has
been responsive to industry secondary
water chemistry initiatives
(Section 6.1).
0
0
0
~
The chemistry history reflected significant improvements
in secondary
water chemistry performance in the past
5 years,
with the reductions
achieved since
1993 in feedwater iron concentrations
viewed as notable.
The current feedwater iron concentrations
were.
however.
considered to
be still of a magnitude that warranted continued
management
attention
(Section 6.2).
~
The review of overall secondary
side chemistry history was adversely
impacted
by the inability to assess
effectiveness
of chemistry controls
in the first 5 years of plant operation
(Section 6.2).
~
On-line instrument
upgrades
have provided improved sensitivity and
accuracy for monitored parameters
in the steam generator
blowdown,
and condensate
systems
(Section 6.4).
~
The use of a Level III eddy current examiner
from another utility as
a
team member in quality assurance
survei llances of eddy current
examination activities
was considered
commendable.
and
an excellent
practice to follow when performing audits or survei llances of specialist
activities (Section 4.2.3).
Safet
Assessment/
ualit
Verification
~
The historical
eddy current examination
program scope
and ongoing steam
generator
degradation
management
actions were considered
indicators of
both management
awareness
of and support for steam generator
tube
integrity initiatives.
The steam generator
strategic
plan was noted.
howevers
to have not been revised since its issue in 1993 'espite
awareness
that the current
document
does not consider all active
degradation
mechanisms
in its projections
(Sections
4. 1 and 5).
~
The inservice inspection supervisor actively assured
quality of
nondestructive
examinations
and was performing effective oversight of
nondestructive
examination
personnel
(Section 7.6).
Summar
of Ins ection Findin s:
~
Inspection Followup Item 275/9510-01;
323/9510-01
was opened
(Section 4.2.1).
~
Inspection
Followup Item 275/9510-02:
323/9510-02
was opened
(Section 4.3).
~
Open Item 323/9307-08
was closed
(Section 8. 1).
~
Violation 275/9425-01;
323/9425-01
was closed
(Section 8.2).
Attachment:
~
Attachment
- Persons
Contacted
and Exit Meeting
-5-
DETAILS
1
STEAM GENERATOR TUBE INTEGRITY REVIEW (73755,
79501,
79502)
The objectives of this part of the inspection were:
(a) to ascertain
the
history and material condition of the Units
1 and
2 steam generator tubing:
and (b) to assess
the effectiveness
of licensee
programs
in detection
and
analysis of degraded
tubing, repair of defects,
and correction of conditions
contributing to tube degradation.
The inspection
scope
and findings are
documented
in Sections
2 through
6 below.
The results of a previously
conducted
inspection of the effectiveness
of licensee
programs
and training in
regard to detection of and response
primary-to-secondary
tube leakage
were documented
in NRC Inspection Report 50-275/95-04:
50-323/95-04.
2
STEAM GENERATOR MATERIALS AND TUBE DEGRADATION HISTORY
2. 1
Descri tion
Diablo Canyon
Power Plant.
Units
1 and 2, are Westinghouse-designed
pressurized
water reactors.
with an approved
megawatt electric output of 1137
for Unit
1 and
1164 for Unit 2.
The respective
commercial operation dates
were
May 7.
1985, for Unit
1 and March 13,
1986, for Unit Z.
The Diablo
Canyon
Power Plant unit design utilizes four Westinghouse
Model
51 vertical
recirculating
This model of steam generator
contains
3.388
Inconel
600
(ASME Material Specification
SB-163) U-tubes, with a nominal
diameter
and wall thickness.
respectively,
of 0.875 inches
and 0.050 inches.
After insertion of the ends of the U-tubes in drilled holes in an 21.5-inch
thick steam generator
tube sheet forging. the tubes
were initially expanded
against the tube sheet
hole surfaces
by mechanical
rolling for a distance of 2
inches to 4 inches
from the primary side surface of the tube sheets
followed
by welding of the tube ends to compatible composition weld cladding
on the
primary side surface of the tube sheet.
Explosive expansion of the unexpanded
portion of the tubes in the tube sheet
was subsequently
performed onsite at
the Diablo Canyon
Power Plant to eliminate the remaining crevice between the
tube
and the tube sheet hole surface.
Secondary
side tube bundle support structures
consist of seven 3/4-inch
thickness
carbon steel
horizontal tube support plates
and two sets of Inconel
600 anti-vibration bars in the upper tube bundle.
The tube support plates
utilize
a drilled round hole configuration, with a nominal
gap of 0.008 inches
between the outside surface of the tubes
and the surface of the holes.
The
selection of carbon steel for the tube support plates,
in conjunction with a
drilled hole configuration, create
a susceptibility to tube denting due to the
pressure
that can be imposed
on the tubes
as
a result of magnetite growth on
the surface of the holes
and entrainment of corrosion oroducts.
The inspectors
also ascertained
that
16 U-tubes in Unit
1-1
contain 30-inch long "implants."
These
implants were installed onsite by
during Unit
1 construction for the purpose of gaining service
experience with potential alternate
tubing materials.
The
16 U-tubes were cut at approximately
8 inches
above the top of the secondary
face of the tube sheet
on the hot-leg side of the steam generator.
and the
resulting approximately 30-inch long segments of original tubing material
removed from the steam generator.
The removed tube segments
were replaced
by
segments
of alternate tubing materials,
with a welded Inconel
606 sleeve
used
to attach the "implant" to the U-tube.
Four implants were manufactured
from
each of the following candidate tubing materials:
stress
relieved Inconel
600. shot peened
Inconel
600,
Incoloy 800,
and Inconel
690.
2.2
Hot-Le
Tem erature
Licensee
personnel
informed the inspectors that
a primary side inlet hot-leg
temperature (i.e., T-Hot) of 603'F has
been
used at Diablo Canyon.
Units
1
and 2. during commercial operation.
The inspectors
ascertained
from review of
the licensee
"Diablo Canyon
Power Plant Strategic Plan." dated February
13
'993.
that
a recommendation
was
made to evaluate the possible
implementation
of a 4'F reduction in T-Hot to 599'F during the respective sixth refueling
outage for Units
1 and
2 (i.e.
~
1R6 and 2R6).
This recommendation
was noted
by the inspectors
to be consistent with actions
taken by other individual
licensees
to reduce hot-leg temperature
as
an approach to limit initiation and
propagation of stress
corrosion cracking.
The inspectors
questioned
licensee
personnel
regarding the status of the T-Hot reduction
recommendation.
and were
informed that T-Hot reduction
was still an open issue.
but was currently not
a
high priority item.
2.3
T~ti
3 2
The inspectors
requested
to see the procurement
requirements
for the Diablo
Canyon
Power Plant,
Units
1 and 2, steam generator tubing that had been
imposed
by Westinghouse
on its tubing vendor(s).
In response
to the
licensee's
request,
furni shed:
(a) Westinghouse
Tampa Division
Material Specification
2656A95.
"Material-Nickel-Chromium-Iron Tubing,"
Revision 2,
and (b) Westinghouse
Specialty Metals Division Process
Specification
1001-01-B,
"Westro 600T," issued
Oecember
10,
1971.
Both of
these
documents
were marked
as containing proprietary information.
Licensee
personnel
informed the inspectors that tube manufacture
was performed for six
of the Units
1 and
(i.e., Unit 1,
1-1
and 1-2: Unit 2.
2-1, 2-2, 2-3;
and 2-4) by Westinghouse
Specialty Metals Division, with materials production
and initial mechanical
working performed
by Huntington Alloy Products.
Licensee
personnel
stated
that materials production
and complete manufacture of the tubing for the two
remaining steam generators
(i.e.
~ Unit 1.
1-3 and 1-4) were
erformed by Huntington Alloy Products.
Two documents
were obtained
by the
icensee
from Huntington Alloy Products,
which were applicable to the
manufacture of the tubing that was utilized in Steam Generators
1-3 and 1-4.
These
documents
were. respectively,
Procedures
QCP 51. "Quality Control
-7-
Procedure for Bright Annealing of Inconel
600T Steam Generator Tubing,"
Revision 0.
and
QCP 53,
"Tube Bending Procedure,"
Revision 0.
The inspectors
noted from review of Materials Specification
2656A95,
Revision 2. that the specification
invoked
ASHE Materials Specification
SB-163
and was consistent with ASME Sections II and III requirements
with respect to
the furnishing of the material in the annealed
condition and performance of
hydrostatic testing, ultrasonic examination,
and eddy current examination.
The inspectors
noted that the material specification did not identify the
annealing
temperature
to be used for the
ASME SB-163
( Inconel
600) tubes.
The
inspectors
ascertained
from review of Process
Specification
1001-01-B that
this document did define the minimum annealing
temperatures
to be used during
tube manufacture.
Details of specification requirements
for annealing
have
not been included in the inspection report.
as
a result of the inspectors
being informed by Westinghouse
personnel
that this information was considered
proprietary.
The inspectors
selected
three
steam generators (i.e..
1-2.
1-4.
and 2-2) for review of samples of steam generator
tubing certified
material test report data.
The inspectors
noted during review of the sample
data that the reported
chemical
composition
and mechanical
properties
conformed to the requi rements of ASME Haterial Specification
SB-163 and
Materials Specification
2656A95. Revision 2.
The ranges of
0.2 percent yield strength
values for the Steam Generators
1-2. 1-4,
and 2-2
tubing certified material test reports were ascertained
to be, respectively,
35,000-76,000 '5.000-69.000.
and 46,000-70,000.
The respective
ranges of
ultimate tensile strength
values for Steam Generators
1-2,
1-4.
and 2-2 were
91,000-115.000.
89.000-114,000,
and 94.000-111.000.
The inspectors
considered
the ranges of yield strength properties
in the tubing for the two selected
Unit
to be of a magnitude which covered properties that
were typical for both low-temperature
and high-temperature
mill annealed
conditions.
The inspectors
accordingly concluded that these relatively wide
ranges of yield strength properties
were at least partially attributable to
variations in tube annealing
temperatures
and/or times that occurred during
tube manufacture.
The yield strength
values
observed
2-2
tubing data were noted
by the inspectors
to have
a reduced
range
compared to
the Unit
1 tubing material.
The inspectors
concluded that tighter annealing
process
controls
appeared
to have been
used during manufacture of the Unit 2
steam generator tubing.
The inspectors additionally calculated the mean value and standard deviation
for carbon content,
0.2 percent yield strength,
and ultimate tensile strength
for the individual samples of certified material test reports.
The results
obtained
from these calculations
are listed below in Table 1.
The inspectors
noted from these results that the mean 0.2 percent yield strength
and ultimate
tensile strength
values
were lower for the Steam Generator
1-4 tubing than the
comparable properties
calculated
for the tubing in both Steam Generators
1-2
and 2-2.
The inspectors
concluded that it was probable that tube temperatures
and/or annealing
times were typically higher during final annealing of the
1-4 tubing, than those present
during the final annealing of
'0
-8-
the Steam Generators
1-2 and 2-2 tubing.
The lower standard deviation value
for the 0.2 percent yield strength properties
in the Steam Generator
2-2
tubing was considered
by the inspectors
to be further confirmation of the
observation
made
above regarding the use of tighter annealing
process
controls
during manufacture of the Unit 2 steam generator tubing.
Table
1
TUBING CARBON COMPOSITION AND MECHANICAL PROPERTY
DATA
Parameter
SG 1-2
Unit
1
SG 1-4
Unit 2
SG 2-2
Mean
o"'ean
o"'ean
0.2
X Yield
Stren th (KSI)
Ultimate Tensile
Strenath
(KSI)
'arbon
50.0
8.6
47.0
7.0
55.9
4.2
103.0
4.0
97.6
5.1
105.3
3.4
0.033
0.009
0.031
0.009
0.035
0.010
(1)
- Standard deviation.
2.4
Tube-to-Tube
Sheet
Ex ansion
As noted in Section
Z. 1 above,
mechanical rolling was utilized during original
fabrication of the Units
1 and
to partially expand tubes
against
tube sheet
hole surfaces (i.e., the first 2-4 inches of tube starting
at the primary surface of the tube sheet).
The resulting tube-to-tube
sheet
crevices
were subsequently
eliminated prior to unit startup
by explosive
expansion
by Westinghouse of the tubes against the tube hole surfaces.
The
explosive expansion
process
used
was given the name
"WEXTEX" by Westinghouse,
and subsequent
references
in the inspection report to tube expansion
and the
tube expansion transition region utilize this name.
Reviews were not
performed by the inspectors
during the inspection of the technical
and quality
requirements
that were applicable to onsite
WEXTEX explosion expansion
activities.
2.5
Tube
De radation Histor
2.5.1
Unit
1
Prior to operational
service.
the Unit 1 steam generators
contained
one
plugged tube (i .e.,
1-2).
Table 2 below provides the tube
plugging history for the four Unit
as
a function of
0
'0
-9-
effective full-power years of operation at the time of repair.
Table 3
details the number of tubes
removed
from service in terms of applicable
degradation
mechanism.
Eddy current examinations
during Refueling Outage
1R1 identified the presence
of tube denting in the Unit 1 steam generators
at tube support plate
intersections.
The denting was believed to have occurred
as
a result of
condenser
in-leakage during the first cycle of operation,
which created
corrosion conditions favorable for magnetite
growth at tube support plate hole
surfaces.
In response to the observed denting'odifications
were made to the
condenser after the first operating cycle and boric acid additions to the
feedwater were commenced after Refueling Outage
1R2.
The licensee
continued
to monitor tube denting in subsequent
refueling outage examinations,
with no
new dents or growth of existing dents
found since Refueling Outage
1R2.
A
summary of dented
tubes with bobbin coi l signals
over 5 volts is listed below
in Table 4.
Table
2
UNIT 1
STEAN GENERATOR (SG)
TUBE REPAIR HISTORY
Time of
Repair
(Outage)
Preservice
1R1 (1986)
1R2 (1988)
1R3 (1989)
EFPYs"'.00
1.25
2.28
3.45
SG 1-1
SG 1-2
SG 1-3
Tubes
Plugged
Tubes
Tubes
Plugg'ed
Plugged
1
0
5
3(4>
3
SG 1-4
Tubes
Plugged
1R4 (1991)
4.49
0
1
1R5 (1992)
5.87
6
15
1R6 (1994)
7.15
21
36
4
1R7 (1995)
8.47
28
70
3
16
Total
Re airs
60
126
15
27
R Re airs (I"', T"')
1.77.
1.77
3.69, 3.72
0.44,
0.44
0.80.
0.80
(1) - Effective full-power years of operation;
(2) - Inservice:
(3) - Total:
(4) - Net plugged total (i.e.. four tubes
plugged
and one tube unplugged).
-10-
During Refueling Outage
1R2.
one low radius
Row 2 U-tube was plugged
as
a
result of the motorized rotating pancake coil identification of axial primary
water stress
corrosion cracking.
To reduce the susceptibility to stress
corrosion cracking.
the licensee
performed
a thermal stress relief of the bend
regions in all of the
Rows
1 and
2 U-tubes.
This subject is further discussed
in Section 2.6 below.
Despite performance of the thermal stress relief,
an additional four low
radius
Rows
1 and
2 U-tubes requi red plugging during Refueling Outage
1R3.
as
a result of the identification by eddy current examination of the presence
of
primary water stress
corrosion cracking in the bend regions.
In response
to
"Rapidly Propagating
Fatigue
Cracks in Steam Generator
Tubes."
dated February 5,
1988 'he licensee
concluded that five tubes
were
susceptible
to the type of fai lure described
in the bulletin and preventively
plugged the five tubes.
Two tubes
were also plugged
due to anti-vibration bar
wear.
and one tube was plugged
due to a restriction that prevented
passage
of
an eddy current probe.
On May 15.
1989 'he
NRC issued Bulletin 89-01,
"Failure of rlestinghouse
Tube Mechanical
Plugs." in response
to
a plug fai lure at North Anna-1.
The bulletin identified several
steam
generator
tube plug material
heats
which were potentially susceptible
to
stress
corrosion failure.
In Refueling Outage
1R2.
Tube
R2C88 (i .e..
Row 2.
Column 88) in Steam Generator
1-2 was plugged after eddy current examinations
revealed indications that was characterized
as primary water stress
corrosion
cracking in the U-bend region of the tube.
The plugs in this tube were
installed prior to the date of issue of Bulletin 89-01
and were fabricated
from one of the heats (i.e.,
Heat 4523) which was identified in the bulletin
as being susceptible
to failure.
The licensee
removed the plugs during
Refueling Outage
1R3 and reexamined
the tube U-bend region.
The tube
examination data did not reveal
the existence of any degradation
and.
as
a
results
the tube was returned to service.
During Refueling Outage
1R4,
one tube was plugged
as
a result of the
identification of anti-vibration bar wear.
Eddy current examinations
in Refueling Outage
1RS identified that
17 low
radius
Rows
1 and
2 U-tubes required plugging because of primary water stress
corrosion cracking in the bend regions.
This number was considered
by the
inspectors to be
a significant increase
in this type of degradation.
Twelve
tubes experiencing
anti -vibration bar wear were also plugged in this outage.
A total of 68 tubes
were plugged during Refueling Outage
1R6.
The majority of
the corrosion-related
degradation that was found was located in Steam
Generators
1-1 and 1-2.
Further information on this subject is contained in
Section 2.5.3 below.
Active corrosive degradation
mechanisms
identified were
primary water stress
corrosion cracking'utside
diameter stress
corrosion
cracking.
and cold-leg thinning.
Four tubes were plugged
due to outside
diameter stress
corrosion cracking at non-dented
tube support plate
intersections.
which was the first identification in Unit
1 of secondary
side
stress
corrosion cracking.
In this outage
an increase
also occurred in the
number of tubes identified as requiring plugging because of detected
primary
0
-11-
water stress
corrosion cracking (i.e.,
39 tubes
versus
17 tubes in Refueling
Outage
1R5).
The tube locations affected
by primary water stress
corrosion
cracking were:
low-radius
Rows
1 and
2 U-bends.
4 tubes:
below the bottom of
the
WEXTEX transition region.
6 tubes:
dented
tube support plates.
23 tubes;
and
~ nondented
tube support plates'
tubes.
Five tubes were plugged
because
of the detection of crack-like indications in the tubes at nondented
tube
support plate locations for which cause could not be determined.
Cold-leg
thinning was first identified in Steam Generator
1-2 during Refueling
Outage
1R3
- however, indications did not exceed the 40-percent
throughwall
limit until Refueling Outage
1R6 when ten tubes
were required to be removed
from service.
The licensee identified in the Refueling Outage
1R6 report that
the growth rate of these indications
was nominally 17-percent
throughwall per
cycle.
Based
on
a review of the eddy current data for cold-leg thinning
indications
recorded
in previous outages
~ the inspectors
noted that there
was
considerable
scatter in the growth rate data, with several
indications having
exhibited apparent
growth rates in excess
of 40-percent
throughwall per cycle.
Table 3
UNIT
1
INSERVICE PLUGGING HISTORY BY DEGRADATION MECHANISH
Tube Degradation
Hechanism
H.C. Fati ue"'nit
2 Refueling Outage
(2R)
1R1
1R2
1R3
1R4
1R5
1R6
1R7
T" '
0
5
0
0
0
0
5
AVB Wearr>>
0
0
2
1
12
8
12
35
ODSCC/non-dented
TSPs"'
0
0
0
0
4
9
13
ODSCC/TTS'"'
0
0
0
0
0
1
1
PWSCC/R18R2 U-bends"'
1
4
0
17
4
1
27
PWSCC/WEXTEX'
0
0
0
0
0
0
1
1
PWSCC/TS below BWT"'
0
0
0
0
6
4
10
PWSCC/Dented
TSPs"'
0
0
0
0
23
75
98
PWSCC/non-dented
TSPs'"
0
0
0
0
0
6
0
6
Unknown TSP flaws'"'
0
0
0
0
5
0
5
CL Thinnin /TSPs'"'
0
0
0
0
10
14
24
Restriction
0
0
1
0
0
1
0
2
Other
0
0
0
0
0
1
0
1
Tubes
Un lu
ed
0
0
1
0
0
0
0
1
Net Tubes
Plugged
0
1
11
1
29
68
117
227
-12-
(1)
- Preventively plugged in response
to Bulletin 88-02;
(2) - Anti-vibration
bar wear in the U-bend region;
(3)
- Outside diameter stress
corrosion
cracking at non-dented
tube support plates;
(4) - Outside diameter stress
corrosion cracking at the top of tube sheet;
(5) - Primary water stress
corrosion cracking in the
Row 1/Row 2 U-bends:
(6) - Primary water stress
corrosion cracking in the
WEXTEX expansion transition region:
(7) - Primary
water stress
corrosion cracking at the tube sheet
below the bottom of the
WEXTEX expansion transition:
(8) - Primary water stress
corrosion cracking at
dented tube support plates:
(9) - Primary water stress
corrosion cracking at
non-dented
tube support plates:
(10} - Crack-like flaws at non-dented
tube
support plates for which cause
was
unknown;
(11)
- Cold-leg side thinning at
tube support plates:
(12)
- Total.
Other reasons
for tube plugging during Refueling Outage
1R6 were:
restriction,
one tube: anti-vibration bar wear. eight tubes:
and pre-service
related
freespan
inside diameter crack.
one tube.
Table 4
UNIT 1
STEAN GENERATOR (SG}
DENT DISTRIBUTION (DENTS > 5 VOLTS)
TSP/HLS'"
1H
2H
SG 1-1
37
SG 1-2
132
90
SG 1-3
SG 1-4
Total
17.
386
540
5
69
201
3H
7
74
97
189
4H
1
106
5
123
235
5H
4
34
39
50
127
6H
2
7
22
277
308
7H
155
51
116
353
675
Total
211
494
215
1355
2275
(1)
- Tube support plate/Hot-leg side.
During Refueling Outage
1R7,
117 tubes
were plugged
because of detected
anti-vibration bar wear (12 tubes)
and corrosion-related
degradation
(105 tubes).
Of the
105 tubes that were plugged because of corrosion-related
degradation,
81 tubes were affected
by primary water stress
corrosion cracking
(i.e.,
bends in low radius U-tubes,
1 tube:
WEXTEX transition region.
1 tube;
below the bottom of the
WEXTEX transition region,
4 tubes;
and dented tube
support plate locations.
75 tubes).
The inspectors
considered
the increase
from 23 tubes during Refueling Outage
1R6 to 75 tubes in Refueling Outage
1R7
for primary water stress
corrosion cracking at dented tube support locations,
to be the most notable
change in detected
degradation.
A moderate
increase
was
-13-
also noted in required plugging for detected
outside diameter stress
corrosion
cracking, with nine tubes
found to be affected at non-dented
tube support
plate locations
and one tube at the top of the tube sheet.
Fourteen
tubes
were plugged
as
a result of identified cold-leg thinning at tube support
plates.
The licensee's
lead eddy current analyst
reexamined
the population of
cold-leg thinning indications in Steam Generator
1-2 during this refueling
outage.
and concluded that cold-leg thinning was
an active mechanism in the
as evidenced
by the growth of pre-existing degradation
and the
appearance
of new indications.
Other plants with Model
51 steam generators,
which have experienced
tube
denting (e.g..
Salem-l,
North Anna-1 and Sequoyah-1)
in the first one or two
cycles of operation,
have detected
outside diameter circumferential
stress
corrosion cracking
and axial primary water stress
corrosion cracking at dent
locations.
A total of 98 tubes
have
been plugged in the Diablo Canyon
Power
Plant Unit
through seven cycles of operation
as
a result of
the identification of axial primary water stress
corrosion cracking at dent
locations.
The
NRC consultant
reviewed the eddy current data
from tubes that
had
been plugged during Refueling Outage
1R6 because of primary water stress
corrosion cracking that had been detected
at dented
and non-dented
tube
support plate intersections.
Although the
NRC consultant
could not
definitively conclude that dents were present
in all cases'here
were
some
indications that the non-dented
intersections
did, in fact. contain
a small
dent.
Additional discussion of steam generator
tube denting is contained in
Section 2.5.3 below.
2.5.2
Unit 2 History
Prior to operational
service.
the Unit 2 steam generators
contained
no plugged
tubes.
Table
5 below provides the tube plugging history for the four Unit 2
as
a function of effective full-power years of operation at
the time of repai r.
Table
6 details the number of tubes
removed
from service
in terms of applicable degradation
mechanism.
During Refueling Outage
2R1.
two tubes required plugging as
a result of damage
that occur red during removal of a tube lane blocking device.
Thermal stress
relief was also performed of the low radius
bends in the
Rows
1 and
2 U-tubes
during this refueling outage.
in order to reduce the susceptibility to primary
water stress
corrosion cracking.
Despite performance of the thermal stress relief, six tubes
from Rows
1 and
2
required plugging during Refueling Outage
2R2,
as
a result of the
identification of primary water stress
corrosion cracking.
Prior to Refueling
Outage
2R2
~ the
NRC issued Bulletin 88-02.
The licensee initially identified
a total of 24 tubes that were considered
susceptible to the high cycle fatigue
mechanism described
in the bulletin
and preventively plugged these
tubes
during the outage.
A subsequent
analysis
completed
by Westinghouse
(WCAP-12064) 'of the potential for high cycle fatigue damage to the
preventively plugged tubes
revealed that only 5 of the 24 tubes were
susceptible to fatigue damage.
The Office of Nuclear Reactor Regulation
-14-
reviewed the licensee's
response to Bulletin 88-02 and verified the
conclusions of the analysis
by Westinghouse
ir) the safety evaluation,
"Closeout of NRC Bulletin 88-02 for Diablo Canyon
Power Plant. Units
1 and 2."
dated
May 25,
1990.
Consequently,
the licensee
removed the plugs during
Refueling Outage
2R3 from the
19 tubes that had been
shown to be not
susceptible to fatigue damage,
and returned the tubes to service.
The eddy current examinations
in Refueling Outages
2R3 and
2R4 did not
identify any tubes with pluggable indications.
However.
Tube R42/C55 in Steam
Generator
2-1 was preventively plugged during Refueling Outage
2R4 because of
a restriction in the U-bend.
In Refueling Outage
1R5. the plugs were removed
from this tube and it was reexamined.
Although the eddy current probes
initially experienced
some resistance
to passage
through this tube. the tube
was successfully
inspected.
No degradation
was detected.
and the tube was
returned to service.
A reddish-brown
substance
was visible on the probe after
passage
through the tube,
which led the licensee to conclude that the tube had
been obstructed
by
a ferritic object that had corroded
away during the
previous operating cycle.
Table
5
UNIT 2 STEAM GENERATOR (SG)
TUBE REPAIR HISTORY
Time of
Repair
(Outage)
Preservice
2R1 (1987)
2R2 (1988)
2R3 (1990)
2R4 (1991)
2R5 (1993)
EFPYs"'.00
1.02
2.05
3.16
4.43
5.75
Tubes
Plugged
Tubes
Plugged
Tubes
Plugged
3
25
0
0
19(2)
0
0
30
SG 2-1
SG 2-2
SG 2-3
SG 2-4
Tubes
Plugged
9(3)
2R6 (1994)
7.09
10
12
Total
Re airs
C Re airs (Inservice)
21
0.62
43
1.27
31
0.91
19
0.56
(1)
- Effective full-power years of operation;
(2) - Tubes
unplugged during
refueling outage;
(3)
- Net plugged total (i.e., ten tubes
plugged
and one
tube unplugged).
0
-15-
Sixty-two tubes
were plugged during Refueling Outage
2R5
~ with all the tubes
with one exception
plugged because of the detection of corrosion-related
degradation.
The exception pertained to anti -vibration bar wear.
Fifty-one
tubes out of the 62 total were removed
from service
because of the detection
of primary water stress
corrosion cracking indications.
Primary water stress
corrosion cracking was identified in low radius
U-bends
(10 tubes),
the
WEXTEX
expansion-transition
region
(1 tube), in the tubesheet
below the bottom of the
WEXTEX transition
(24 tubes),
and at dented tube support plate intersections
(16 tubes).
A single circumferential indication was identified by motorized
rotating pancake coil examination of the Unit 2 steam generator
tubes in the
area of the
WEXTEX expansion transition region in Steam Generator
2-2.
Four
tubes experienced
outside diameter stress
corrosion cracking at the tube
support plates,
while another tube was plugged for outside diameter stress
corrosion cracking located at the top-of-tubesheet
elevation.
Table
6
UNIT 2
INSERVICE PLUGGING HISTORY BY DEGRADATION MECHANISM
Tube Degradation
Mechanism
H.C. Fati
ue"'VB
Wear<>>
Unit 2 Refueling Outage
(2R)
2R1
2R2
ZR3
2R4
2R5
2R6
Total
0
5
0
0
0
0
5
0
0
0
0
1
3
ODSCC/non-dented
TSPs"'
0
0
0
4
8
12
ODSCC/TTS"'
0
0
0
1
0
1
PWSCC/R18R2 U-bends"'
6
0
0
10
2
18
PWSCC/WEXTEX'
0
0
0
0
1
1
2
PWSCC/TS below BWT"'
0
0
0
24
11
35
PWSCC/Dented
TSPs"'
0
0
0
16
3
19
CL Thinnin /TSPs'"'
0
0
0
5
10
15
Mechanical
Dama
e
2
0
0
0
0
0
2
Other'"'
20
0
1
0
0
21
Tubes
Un lugged
Net Tubes
Plugged
0
0
19
0
1
0
20
2
31
-19
1
61
38
114
(1) - Preventively plugged in response
to Bulletin 88-02:
(2)
- Anti-vibration
bar wear in the U-bend region:
(3) - Outside diameter stress
corrosion
cracking at non-dented
tube support plates:
(4)
- Outside diameter stress
corrosion cracking at the top of tube sheet:
(5) - Primary water stress,
r
-16-
corrosion cracking in the
Row 1/Row 2 U-bends;
(6) - Primary water stress
corrosion cracking in the
WEXTEX expansion transition region;
(7)
- Primary
water stress
corrosion cracking at the tube sheet
below the bottom of the
WEXTEX expansion transition;
(8)
- Primary water stress
corrosion cracking at
dented tube support plates;
(9)
- Crack-like flaws at non-dented
tube support
plates for which cause
was
unknown;
(10)
- Cold-leg side thinning at tube
support plates:
(11)
- Of 20 tubes
plugged in 1R2,
19 tubes were preventively
plugged
due to initial high cycle fatigue concerns
and
1 tube was plugged
because of a restriction.
In Refueling Outage
2R4,
one tube was plugged
because of a restriction.
A total of 21 indications were identified as cold-leg thinning during
Refueling Outage
2R5.
However. only five tubes
required plugging due to
depths in excess of the 40 percent throughwall repair limit.
Cold-leg
thinning is not
a major source of degradation within the industry,
and limited
information is presently
known regarding this phenomenon.
Indications
from
this form of degradation
are volumetric in nature
and
may result from a
combination of corrosion
and mechanical (i.e.. tube motion) mechanisms.
Thirty-eight tubes
were pluggea during Refueling Outage
2R6.
The eddy current
inspections
identified similar degradation
mechanisms
as observed
in the
previous
2R5 outage:
however.
the overall
number of pluggable tubes
decreased
from the previous inspection.
The decrease
primarily stemmed
from a decline
in the number of tubes identified with axial primary water stress
corrosion
cracking.
The respective
plugging numbers
and degradation
locations in
Refueling Outage
2R6 for axial primary water stress
corrosion cracking were
3 tubes at dented
tube support plate intersections.
11 tubes
below the bottom
of the
WEXTEX transition region in the tubesheet.
1 tube in the
WEXTEX
transition region,
and 2 Rows
1 and
2 tubes in the low radius
bend region.
The corresponding
plugging numbers at these locations in Refueling Outage
2R5
were, respectively.
16.
24'.
and
10 tubes.
The number of pluggable tubes
affected
by outside diameter
stress
corrosion cracking increased slightly to
eight (up from four).
Although the licensee
had previously concluded in the
steam generator strategic
plan (see Section 5.0) that outside diameter
stress
corrosion cracking would be the dominant degradation
mechanism in the future,
a significant increase
in pluggable tubes
due to outside diameter stress
corrosion cracking indications
was not apparent
as of Refueling Outage
2R6.
Cold-leg thinning continued to be an active degradation
mechanism in the cycle
of operation prior to Refueling Outage
2R6.
Ten tubes with cold-leg thi nning
depths in excess of 40-percent
throughwall were plugged
as
a result of the
Refueling Outage
2R6 eddy current examinations.
Because of the continued
activity of this degradation
phenomenon,
the licensee
considers it a "special
concern"
as stated in "2R6 Steam Generator
Outage Activities Report," dated
June 3,
1995.
The inspectors
reviewed the Refueling Outage
2R6 outage report
and verified that the licensee
had monitored
and recorded the growth rates of
previously identified cold-leg thinning indications.
0
-17-
A reduced
number of dents occurred in Unit 2 steam generator
tubes atter
the
initial cycles of operation
compared to Unit 1.
The initiation of these
dents
is
a result of the
same
mechanisms
described for Unit 1.
A summary of the
number of dented
tubes is given in Table 7.
Table
7
UNIT 2 STEAM GENERATOR (SG)
DENT DISTRIBUTION (DENTS > 5 YOLTS)
TSP/HLS'"
SG 2-1
SG 2-2
SG 2-3
SG 2-4
Total
1H
0
426
0
0
426
2H
3H
0
1
13
2
3
9
46
60
4H
1
ill
4
7
123
5H
2
0
0
2
4
oH
0
0
0
0
0
Total
551
16
60
634
1
- Tube support plate/Hot-leg side.
2.5.3
Comparison of the Degradation in the Unit
1 and
The licensee
furnished to the inspectors
a compilation of the number of tubes
plugged in the Units
1 and
for each applicable degradation
mechanism.
Summaries of the Units
1 and
2 information are provided,
respectively,
in Tables
8 and 9.
The inspectors
concluded
from review of this
information that there were
some current degradation
differences
between the
two units.
The inspectors additionally noted that tube plugging history. to
date.
suggests
that there
may be differences in susceptibility to primary
water stress
corrosion cracking between
1-3 and 1-4 and the
other six steam generators.
The inspectors
noted that tube wear at anti-vibration bars varied
significantly between units. with Unit
containing
a total
of 35 tubes
plugged for this degradation
mechanism
versus
a total of only
4 tubes in Unit 2 steam generators.
The inspectors
also compared the overall
number of tubes
plugged by unit for primary water stress
corrosion cracking
and noted that the incidence in Unit
1 was approximately twice that of Unit 2
(i.e..
141 tubes
versus
74 tubes).
Unit 1 had,
however.
accrued
8.47
effective full-power years of operation
as of Refueling Outage
1R7 versus
7.09
effective full-power years of operation in Unit 2 at Refueling Outage
2R6.
In
that
81 tubes
were plugged during'Refueling Outage
1R? because
of identified
-18-
rimary water stress
corrosion cracking,
the current overall difference
etween units for this degradation
mechanism
was considered
by the inspectors
to be primarily related to the difference in time of commercial
service.
The inspectors
noted from review of individual Unit
plugging
history that the incidence of primary water stress
corrosion cracking was
significantly lower in Steam Generators
1-3 and 1-4 than in Steam
Generators l-l and 1-2.
The respective
numbers of tubes that have been
plugged through Refueling Outage
1R7 because
of identified primary water
stress
corrosion cracking were two in Steam Generator
1-3 (i.e.,
low radius
Rows
1 and
Z U-bends)
and nine in Steam Generator
1-4 (i.e.. dented tube
support plate intersections).
The comparable
tube totals for primary water
stress
corrosion cracking in Steam Generators
1-1 and 1-2 were, respectively,
35 and 95.
Steam Generators l-l and 1-2 exhibited
a greater
incidence of
primary water stress
corrosion cracking in both the low radius
bends of the
Rows
1 and
2 U-tubes (i.e..
9 tubes
and
15 tubes.
respectively.
plugged)
and
at dented tube support plate locations (i.e..
17 tubes
and
72 tubes.
respectively.
plugged).
Of particular significance to the inspectors
was the
plugging data for primary water stress
corrosion cracking at dented tube
support plate intersections.
As noted in Table 4 in Section 2.5. 1 above.
the
distribution of dents
~ 5 Volts in the Unit
was
as of
Refueling Outage
1R7:
1-1
~ 211:
1-Z. 494:
1-3.
215:
and Steam Generator
1-4.
1355.
The respective
numbers of tubes
plugged for identified primary water stress
corrosion
cracking at dented tube support plate intersections
were,
as of Refueling
Outage
1R7:
1-1
~
17;
1-2.
72:
Steam
Generator
1-3, 0:
and Steam Generator
1-4, 9.
The inspectors
considered that
the latter two plugging numbers
indicated
a significantly greater resistance
to initiation of primary water stress
corrosion cracking in Steam
Generators
1-3 and 1-4 tubing than demonstrated
1-1 and
1-2 tubing.
This view was based,
in part.
on the relative sizes of the dent
populations.
with the respective
percentages
of dented
tubes containing
primary water stress
corrosion cracking found to be 8.06 in Steam
Generator
1-1,
14.57 in Steam Generator
1-2
~
0 in Steam Generator
1-3,
and
0.66 in Steam Generator
1-4.
Other locations in Steam Generators
1-1 and 1-2 where primary water stress
corrosion cracking
has
been identified were:
below the bottom of the
WEXTEX
expansion transition region (i.e.,
seven
tubes
and three tubes,
respectively.
plugged): the
WEXTEX expansion transition region (i.e.,
one tube in Steam
Generator
1-1 only plugged):
and at non-dented
tube support plate
intersections
(i .e.,
one tube
and five tubes,
respectively,
plugged).
Table
7 lists the number of tubes that have been identified to contain hot-leg
side dents
~ 5 Volts in the Unit 2 steam generators
as of Refueling
Outage
2R6.
With the exception of Steam Generator
2-2, which contained
551
dents,
the incidence of denting
was significantly lower than was found in the
Unit
Although cracking at dented tube support plate
intersections
is not necessarily
a function of dent voltage,
the limited
number of dents
a 5 Volts in Steam Generators
2-1. 2-3.
and 2-4 (i.e.,
-19-
respectively,
7,
16,
and 60) suggest
that the long-term incidence of primary
water stress
corrosion cracking at dented tube support plate intersections
should
be limited in these three Unit 2 steam generators.
Table 8
UNIT 1
TUBE DEGRADATION BY MECHANISM
Tube Degradation
Mechanism
Mi h
C cle Fati
ue'VB
Wear'
0
1
0
4
7
9
15
35
SG
SG
Total
1-1
1-2
1-3
1-4
ODSCC/non-dented
TSPs'
6
1
0
13
ODSCC/TTS'
0
0
0
PWSCC/R18R2
U-Bends'
15
2
0
PWSCC/WEXTEX'
0
0
0
PWSCC/TS Below BWT'
3
0
0
PWSCC/Dented TSPs'7
72
0
9
PWSCC/Non-'dented
TSPs'
5
0
0
Unknown TSP flaws"
3
2
0
0
C.L. Thinnin /TSPs"
7
13
1
3
26
10
98
24
Other"
Total Plugged
60
125
0
2
1
0
15
27
227
(1)
- Preventively plugged in response
to Bulletin 88-02:
(2)
- Anti-vibration
bar wear in the U-bend region;
(3) - Outside diameter stress
corrosion
cracking at non-dented
tube support plates;
(4) - Outside diameter stress
corrosion cracking at the top of tube sheet:
(5) - Primary water stress
corrosion cracking in the
Row 1/Row 2 U-bends;
(6)
- Primary water stress
corrosion cracking in the
WEXTEX expansion transition region;
(7)
- Primary
water stress
corrosion cracking at the tube sheet
below the bottom of the
WEXTEX expansion transition:
(8) - Primary water stress
corrosion cracking at
dented tube support plates;
(9)
- Primary water stress
corrosion cracking at
non-dented
tube support plates:
(10)
- Crack-like flaws at non-dented
tube
support plates for which cause
was unknown; (ll) - Cold-leg side thinning at
tube support plates:
(12)
- Two tubes
were plugged in Steam Generator
1-2 due
to probe restrictions
and one tube in Steam Generator
1-3 due to a freespan
indication that was pre-service
related.
0
-20-
As noted in Table
1 in Section 2.3 above,
the mean 0.2 percent yield strength
and ultimate tensile strength
values for a sample of Steam Generator
1-4
tubing were found to be lower than the corresponding
values determined
from
samples of Steam Generators
1-2 and 2-2 tubing.
The inspectors
concluded that
it was probable that higher tube annealing
temperatures
and/or longer
annealing
times were used by Huntington Alloy Products
during final annealing
of the Steam Generator
1-4 tubing than the values
used
by Westinghouse
Specialty Metals Division during final annealing of the Steam Generators
1-2
and 2-2 tubing.
Lower 0.2 percent yield strength properties
would be expected
to result in a lower susceptibility
to primary water stress
corrosion
cracking,
which would at least partially explain the lower incidence of this
type of degradation
1-3 and 1-4.
The relatively large
range of 0.2 percent yield strength
values
noted during review of the Steam
Generator
1-4 certified material test report data,
in conjunction with a
calculated
standard deviation of 7 KSI. suggested.
however.
to the inspectors
that other factors
had to be contributing to the apparent difference in
degradation susceptibility.
Table 9
UNIT 2
TUBE DEGRADATION BY MECHANISM
Tube Degradation
Mechanism
Hi h
C cle Fati ue'G
2-1
0
5
0
5
SG
Total
2-2
2-3
2-4
AVB Wear'
0
3
1
4
ODSCC/non-dented
TSPs'
4
5
2
12
ODSCC/TTS'
1
0
0
1
PWSCC/R18R2
U-Bends'
5
5
5
18
PWSCC/WEXTEX
0
1
0
1
2
PWSCC/TS Below BWT'l
5
9
10
35
PWSCC/Dented
TSPs'
19
0
0
19
PWSCC/Non-dented
TSPs'
0
0
0
0
Unknown TSP flaws"
0
0
0
0
0
C.L. Thinnin /TSPs"
5
8
2
0
15
Other"
Total Plugged
21
43
31
19
114
1
0
2
0
3
(1)
- Preventively plugged in response
to Bulletin 88-02;
(2) - Anti-vibration
bar wear in the U-bend region:
(3)
- Outside diameter stress
corrosion
0
0
-21-
cracking at non-dented
tube support plates:
(4)
- Outside diameter stress
corrosion cracking at the top of tube sheet:
(5)
- Primary water stress
corrosion cracking in the
Row 1/Row 2 U-bends;
(6)
- Primary water stress
corrosion cracking in the
WEXTEX expansion transition region:
(7)
- Primary
water stress
corrosion cracking in the tube sheet
below the bottom of the
WEXTEX expansion transition:
(8) - Primary water stress
corrosion cracking at
dented tube support plates;
(9)
- Primary water stress
corrosion cracking at
non-dented
tube support plates:
(10)
- Crack-like flaws at non-dented
tube
support plates for which cause
was unknown.;
(11)
- Cold-leg side thinning at
tube support plates;
(12)
- Two tubes
plugged in Steam Generator
2-1 and one
plug in Steam Generator
2-3 due to probe restriction in U-bend.
2.6
Licensee Actions Taken to Increase
Tubin
Stress
Corrosion Crackin
Resistance
The inspectors
were informed by licensee
personnel
that onsite shot peening
was performed
on the inside diameter of all Units
1 and
tubes in the area of the tube sheet
through the tube expansion transition
region.
Hoth hot-leg
and cold-leg sides of the U-tube bundle were peened.
with the purpose
being to increase
resistance
to initiation of primary water
stress
corrosion cracking by inducing surface
compressive
stresses
(i.e..
a
tensile stress
is required to be present for stress
corrosion cracks to
initiate).
The Units
1 and
2 shot peening activities were performed,
respectively,
during Refueling Outages
1R5 (1992)
and
2R5 (1993).
The
inspectors
considered that achieving
any beneficial effects
from shot peening
would be strongly dependent
upon whether primary water stress
corrosion cracks
had already
commenced to form during the five cycles of operation that
preceded
the shot peening.
The Unit 2 degradation
data presented
in Table
6
in Section 2.5.2
shows that primary water stress
corrosion cracks were
detected
below and in the
WEXTEX expansion transition region during Refueling
Outage
2R5. the outage in which the shot peening
was performed.
The
inspectors
therefore considered
the detection of further primary water stress
corrosion cracking at these
locations during Refueling Outage
2R6 not to be
surprising.
As shown in Table 3 in Section 2.5. 1, primary water stress
corrosion cracking was not detected
in and below the
WEXTEX transition region
in the Unit
as of Refueling Outage
1R5 when shot peening
was performed.
The subsequent
detection of primary water stress
corrosion
cracking at these locations during Refueling Outages
1R6 and
1R7 was viewed by
the inspectors
as probably indicative that cracks were present at the time of
shot peening
~ but were of sizes that were below the eddy current detection
limit.
also performed onsite thermal stress relief of the low radius
Rows
1 and
2 U-bends in each Unit
1 and
during,
respectively.
Refueling Outages
1RZ (1988)
and
2R1 (1986). in order to
increase
the resistance
of the bend regions to primary water stress
corrosion
cracking.
The Units
1 and
2 degradation
data contained,
respectively,
in
Tables
3 and
6 show.
however. that primary water stress
corrosion cracking has
0
-22-
continued to be detected
in low radius
U-bends despite
performance of the heat
treatment.
The inspectors
did not believe that sufficient information was
available to determine with any certainty the reason for the continuing
detection of this type of degradation'ut
considered
a possible explanation
was
a continuing slow growth of cracks that initiated prior to performance of
the heat treatment.
Reviews were not performed
by the inspectors of the procedural
requirements
and process
controls that were in effect for accomplishing the shot peening
and stress relief activities.
3
VISUAL EXAMINATION OF THE SECONDARY SIDE OF THE STEAN GENERATORS
3. 1
Review of Pro
ram
Re uirements
and Ins ection Data
The inspectors
reviewed Procedures
ISI VT-5. "Steam Generators
Secondary
Side
Internal Inspection." Revision I: and AD4. ID6. "Foreign Material
Exclusion
Program." Revision 2.
The inspectors
performed
a visual inspection of the
upper internals of Steam Generator
1-4. including the foreign material
exclusion barriers.
and interviewed personnel
during the closeout of Steam
Generator
1-2 for Refueling Outage
1R7.
The inspectors
noted that Procedure
ISI VT-5 was first utilized during
Refueling Outage
1R6 in April 1994.
Secondary
side inspections of steam
generators
had not been performed in either unit prior to that outage.
The
licensee's
current program appeared
to be responsive
in addressing
secondary
side degradation
issues.
Howevers earlier implementation of the program could
have provided for a more timely identification and evaluation of J-tube.
barrel riser.
and nozzle plug erosion/corrosion
phenomena.
An evaluation
by the inspectors of the licensee's
program and practices for the secondary
side of the steam generators
showed
that measures
taken to preclude foreign materials
from entering the feedwater
annulus during maintenance
and inspection were appropriate.
The inspectors
were informed that steel
wedges.
specially fitted for the annulus,
are used in
conjunction with wood planking and nylon reinforced drop cloth to provide the
foreign material exclusion barrier.
Inspectors
observed
the barrier in place
during an inspection of Steam Generator
1-4.
Based
upon discussions
with
licensee
personnel
and observation of the closeout of Steam Generator
1-2. the
inspectors
noted that material accountability
was reestablished
prior to
removal of the foreign material exclusion barrier.
Subsequent
to the removal
of the drop cloth,
a visual inspection of the planking and wedges
was
performed
and debris
removed.
Planking
and wedges
were then
removed
and final
closeout
completed.
Review by the inspectors of the results of visual inspections that were
performed of the secondary
surfaces of steam generator
tube sheets
during
refueling outages
revealed that minimal foreign objects
had been observed
0
-23-
during commercial operation.
To date,
no objects
have
been
observed of a size
and type that could impair tube integrity.
Overall. the inspectors
considered
that the data
was indicative of effective implementation of foreign material
exclusion program requirements
for steam generators.
4
REVIEW OF TUBE EXAMINATION HISTORY.
PROGRAM REQUIREHENTS,
AND DATA
4.1
Review of Tube Examination Histor
During Refueling Outage
1Rl in 1986,
the licensee
performed
a full-length
bobbin coil examination of a
16 percent
sample of active tubes in each
steam
generator.
This sample size exceeded
the Technical Specification
minimum
sample size requirement of 3 percent
when each individual
is examined.
Initial Unit 2 inservice examinations
during
Refueling Outage
2R1 utilized a sample size for full-length bobbin coil
examination which ranged
from 22 to 100 percent of active tubes in the steam
generators (i.e..
2-1
~
25 percent:
2-2
~
22
percent:
2-3.
100 percent:
and Steam Generator
2-4.
25 percent).
Full-length bobbin coil examinations
during Refueling Outages
1R2 through
1R4
utilized sample sizes in individual steam generators
which ranged
from 22 to
31 percent of active tubes.
Similar bobbin coil sample sizes
were utilized in
Unit 2 during Refueling Outages
2RZ through
2R4 (i .e..
20 to 25 percent of
active tubes).
In addition. the licensee initiated during Refueling Outages
1R2 and
2R2
a motorized rotating pancake coil examination of the low radius
bend region in all of the
Rows
1 and
2 U-tubes.
This type of examination
was
utilized to increase
the assurance
of detection of primary water stress
corrosion cracking.
The inspectors
noted that examinations of the low radius
bends in the
Rows
1 and
2 U-tubes
have also been performed during each
refueling outage
subsequent
to Refueling Outages
1R2 and
2R2.
During
Refueling Outages
1R4 and 2R4. the licensee
added to the examination
program
motorized rotating pancake coil examinations of a 20 percent
sample of WEXTEX
expansion transition regions
on the hot-leg side of each
The
motorized rotating pancake coil examinations of the
WEXTEX expansion
transition region were added to increase
assurance
of detection of
circumferential
stress
corrosion cracking.
During Refueling Outage
1R5. the sample size for full-length bobbin coil
examinations
ranged
from 28 to 45 percent of active tubes in individual Unit
1
During Refueling Outage
2RS. the bobbin coil sample size
was increased to 100 percent of the active tubes in each Unit 2 steam
generator.
Motorized rotating pancake
coi 1 examinations
during Refueling
Outages
1R5 and
2R5 of the hot-leg side
WEXTEX expansion transition regions
utilized. respectively.
sample sizes of 22 and 41 percent of active tubes.
Beginning in Refueling Outage
2R5. the licensee
fut ther augmented
the
examination
program to include motorized rotating pancake
coi 1 examinations of
dented tube support plate intersections
on the hot-leg side of the steam
generators.
The purpose of these
examinations
was to increase
assurance
that
any stress
corrosion cracking associated
with dents would be detected.
All
-24-
hot-leg side intersections
in Tube Support Plates
01 through 06, which
exhibited
a dent signal amplitude
> 5 volts during bobbin coil examination.
were examined
by motorized rotating pancake coil during Refueling Outage
2R5.
During Refueling Outages
1R6 and 2R6,
100 percent of the active tubes in each
were examined full length using
a bobbin coil.
The steam
generator
sample sizes
used for motorized rotating pancake
coi 1 examination of
the
WE)(TEX expansion transition region ranged
from 22 to 23 percent of active
tubes in the Unit
and from 22 to 46 percent of active tubes
in the Unit 2 steam generators.
The Refueling Outage
1R6 motorized rotating
pancake coi 1 sample sizes
used for examination of dented hot-leg side
intersections
ranged in the four steam generators
from 10 to 26 percent of the
intersections
in Tube Support Plates
01 through
07 with bobbin coi 1 dent
signal
amplitudes
~ 5 volts.
All steam generator hot-leg side intersections
in Tube Support Plates
01 through 07, which exhibited
a bobbin coi 1 dent
signal amplitude
~ 5 volts, were examined
by motorized rotating pancake coil
during Refueling Outage
2R6.
During the onsite inspection.
the inspectors
reviewed the examination
requirements
that had been developed for Refueling Outage
1R..
These
requirements
were documented
in a licensee
memorandum
dated October
16.
1995.
which was entitled.
"1R7
SG Tube Eddy Current Inspection Criteria."
Revision 2.
The inspectors
noted from the review that
a full-length bobbin
coil examination of 100 percent of the active tubes
was specified in each
A sample size of 28 percent
was selected
for Plus Point
motorized rotating pancake
coi l examinations
in each
steam generator of the
WEXTEX expansion transition region.
The inspectors
ascertained
that the
sampling requirements
for the
WEXTEX expansion transition region were
implemented in accordance
with Westinghouse
Owners
Group guidelines.
The
sample size selected
for Plus Point motorized rotating pancake
coi 1
examinations of dented hot-leg side intersections
was
100 percent of the
intersections
(with dent signal
amplitudes
~ 5 volts) in each
in Tube Support Plates
01,
02.
and 03.
The sampling criteria additionally
required sampling
be performed
above
Tube Support Plate 03. if necessary.
to
achieve
a sample of 20 percent of the hot-leg side dented intersections.
The
low radius
bends in all
Rows
1 and
2 U-tubes were specified to be examined
by
motorized rotating pancake coil and all anomalies
noted in the
WEXTEX
expansion transition region were required to be examined
by the Plus Point
motorized rotating pancake
coi l.
Overall. the inspectors
concluded that:
(1) the historical examination
program scope
was considered
an indicator of management
awareness
of and
support for steam generator
tube integrity initiatives;
and (2) the licensee
has
been proactive with respect to examination
scope,
adoption of new eddy
current examination technology,
and incorporation of industry experience.
0
0
-25-
4.2
Review of Examination
Pro
ram
Re ui rements
4.2. 1
Current
Program
and Process
The inspectors
and
NRC consultant
reviewed the eddy current examination
program requirements
for Refueling Outage
1R7 which were contained in:
(1) Document
DCPP-Guide-001.
"Data Analysis Guidelines." Revision 95. 1 dated
October
7,
1995;
(2) Procedure
AD5. ID4,
Tube Inspections,"
Revision 2; (3) Procedure
N-ET-4,
"Eddy Current Data Analysis of Diablo Canyon
Units
1 and
Tubing," Revision
1; (4) Westinghouse
Document
DAT-GYD-005. "115/+Pt./80HF
RPC Probe Analysis Guidelines." Revision
0: and,
(5) Westinghouse
Nuclear Services
Division Procedure
HRS 2.4.2
PGE-35,
"Eddy Current Inspection of Inservice
Nonferromagnetic
Tubing
for Diablo Canyon Units 182." Revision 4.
The inspectors
also compared the
current program against the recommendations
contained in Electric Power
Research
Institute
EPRI NP-6Z01.
Examination Guidelines."
Revision 3.
't was ascertained
during this review that the licensee
data analysis
guidelines
were generally consistent
with the recommendations
contained
in
Electric Power Research
Institute
EPRI NP-6Z01. Revision 3.
The data analysis
guidelines
were noted to contain legible Lissajous figures
and standard
drawings that were considered to provide appropriate
guidance to analysts.
The most significant omission in the licensee
data analysis guidelines
was the
absence of any quantitative guidance
regarding the Electric Power Research
Institute
EPRI NP-6201
recommendation
for establishment
of criteria for noisy
data.
The inspectors
also noted that. in addition to the licensee
data
analysis guidelines
(DCPP-Guide-001,
Revision 95. 1), Westinghouse
data
analysis guidelines
(DAT-GYD-005, Revision 0) were also in effect for analysis
of motorized rotating pancake
coi 1 data,
resulting in some overlap and
redundancy.
Eddy current examination
program strengths
noted during the
review included:
(1) use of only analysts
who had been certified as qualified
data analysts
in accordance
with the requirements
of EPRI NP-6201,
Appendix G;
(2) screening for loose parts in Rows
1 and
2 and the outer two rows of the
tube bundle periphery;
and (3) use of two separate
companies to perform
independent
primary and secondary
analysis.
Site-specific training and testing of primary and secondary
eddy current data
analysts
were performed by the licensee
Level III eddy current examiner.
Assessments
of the training and testing materials
were not performed during
the inspection.
The inspectors
and
NRC consultant
reviewed the process
and equipment that were
applicable to Refueling Outage
1R7 eddy current data acquisition
and analysis.
Data acquisition
and primary analysis
were performed
by Westinghouse,
with
secondary
analysis
performed
by Anatec International.
Both primary and
secondary
analysis
were performed remotely at the Westinghouse
Waltz Hill
facility in Pennsylvania.
using
a dedicated
telephone line for data
transmission.
Resolution analysis for differences in "calls" between primary
and secondary
analysts
was performed onsite
by Westinghouse
and Anatec
-26-
International
Level III analysts.
It was ascer tained that motorized rotating
pancake coil examinations of straight sections
in Refueling Outage
1R7
utilized
a three-coil
probe.
The three-coil
probe contained
a 0. 115-inch
diameter
pancake coil.
a Plus Point coil, and
a high frequency shielded
0.080-inch diameter
pancake coil.
The inspectors
considered that the probe
should enhance
detection capability compared with previous examinations'ue
to the increased
signal-to-noise ratio of the Plus Point coil and the ability
of the high frequency
pancake coil to detect shallow inside diameter cracking.
Bend regions were examined with a two-coi 1 probe containing
a 0. 115-inch
diameter
pancake coil and
a Plus Point coil.
The
NRC consultant
considered
that the scope of electric discharge
machined axial
and circumferential
inside
diameter
and outside diameter
notches
in the licensee
standards
for motorized
rotating pancake coil examinations
was excellent.
and would be very useful
for
probe setup
and defect sizing.
During the inspections
the
NRC consultant
ascertained
that Westinghouse
was
utilizing 100-foot extension
cable for the bobbin coil examinations.
This
cable length was permitted
by the applicable job data sheet.
Prior to the
start of motorized rotating pancake coil examinations.
personnel
were questioned
concerning
the extension
cable length that was planned to be
used for that series of examinations.
in that the applicable Aestinghouse
job
data sheets
for this examination
method specified that
a 50-foot extension
cable
be used.
The
NRC consultant
was initially informed that
a 100-foot
extension
cable would also be used for the motorized rotating pancake
coi 1
examinations.
because
of an
ALARA concern that had been expressed
by health
physics personnel.
The inspectors
requested
licensee
personnel
to review the
matter
and determine whether
a 50-foot extension cable could be used without
posing
an ALARA problem.
since the increased
extension
cable length could
result in some degradation of motorized rotating pancake
coi 1 data quality.
After review. licensee
personnel
determined that the motorized rotating
pancake coil examinations
could be appropriately
accomplished
using
a 50-foot
extension cable.
While this issue
does not raise regulatory concerns. it is
indicative of a lack of a thorough evaluation
and proactive
management
of
contractor activities.
The
NRC consultant
noted that the Westinghouse
Anser software permitted
analysts to view C-scan (or isometric) plots
as they were being rotated,
which
allowed the analysts
to get
a better
idea of the contours of the plots and
limited the ability of artifacts to "hide" defects.
The mix residual
in the
Anser software
was ascertained
by the
NRC consultant to be typically
0.43 volts, with the residual
appearing to increase with increase
in probe
speed.
The residual
masks small defect indications
and contributes additional
error in the measurement
of defect depth. with the error noted by the
NRC
consultant to be at
a maximum if the defect
was near the edge of a support.
The
NRC consultant
considered
the mix residual to be of a magnitude which
would make detection of outside diameter stress
corrosion cracking at tube
supports
more difficult for signals
less
than one volt.
During the onsite inspection.
the inspectors
noted that Westinghouse
Procedure
MRS 2.4.2
PGE-35.
Revision 4, did not require
use of low capacitance
0
-27-
probe extension cable for motorized rotating pancake coil examinations (i.e.,
Appendix
E of MRS 2.4.2 PGE-35,
Revision 4, specified
a capacitance
value of
26 pico farads/foot
+ 10 percent for the cable).
Additional review of eddy
current equipment criteria was performed subsequent
to the onsite inspection.
Included in the offsite review was the licensee
response
dated
June
29.
1995
'o
Generic Letter 95-03 'Circumferential
Cracking of Steam Generator
Tubes. "
The inspectors
noted that the licensee identified in its response that it will
use
augmented
inspection techniques
that are consistent with industry
recommendations
and that are qualified to Appendix
H of the Electric Power
Research
Institute Guidelines.
Appendix
H qualifications that had been
previously seen
by the inspectors uti lized low capacitance
extension cable.
Conformance of the Westinghouse
eddy current examination procedures
to the
qualification criteria contained in Appendix
H of Electric Power Research
Institute
EPRI NP-6201.
Revision 3.
was not specifically checked during the
onsite inspection.
An additional exit meeting
was held by telephone
on
January
17 '996. to inform the licensee that review of the conformance of the
eddy current examination
procedures
to Appendix
H of Electric Power Research
Institute
EPRI NP-6201.
Revision 3.
was considered
an inspection followup item
(275/9510-01:
323/9510-01).
4.2.2
Response
to Generic Communications
The inspectors
performed
a limited review of the licensee's
handling of NRC
generic communications pertaining to steam generator
tube degradation
problems.
The sample
used for this review consisted of Bulletin 89-01
'Failure
of Westinghouse
Tube Mechanical
Plugs."
and
Information Notices 90-49,
"Stress
Corrosion Cracking in
Tubes."
and 91-67.
"Problems With the Reliable Detection of Intergranular
Attack
( IGA) of Steam Generator Tubing."
The review indicated that the licensee
had appropriately
responded to
Bulletin 89-01, with removal of Westinghouse
Inconel
600 mechanical
plugs from
Unit
1 complete
and removal of the remaining
14 Unit 2 cold-leg side plugs
scheduled to be completed during Refueling Outage
2R7 in Spring 1996.
The
inspectors
noted that the licensee
immediately responded to Information Notice 90-49 by implementing (in the 1991
and subsequent
Units
1 and
2
refueling outages)
a motorized rotating pancake coil examination of the
expansion transition region of at least
20 percent of the tubes.
The
inspectors
considered
the licensee
actions to be appropriate
for optimizing
detection sensitivity for circumferential cracking.
No specific additional
actions
were taken
by the licensee in response to Information Notice 91-67.
The inspectors
considered
the licensee's
bases for this determination (i.e.,
(a) the historical
non-use of a voltage amplitude threshold for analysis of
bobbin coi 1 data,
and (b) the existing use of revised Electric Power Research
Institute guidelines for interpreting bobbin coil indications at tube support
plates attributed to outside diameter stress
corrosion cracking/intergranular
attack) to be reasonable.
0
0
-28-
4.2.3
Eddy Current
Program Oversight
The inspectors
observed that oversight of the eddy current examination
contractors
during Refueling Outage
IR7 was performed
by both steam generator
engineers
from the licensee's
secondary
engineering organization
and by
a
nondestructive
examination engineer
from the licensee's
Technical
and
Ecological Services organization in San
Ramon, California.
The latter
individual. who held certifications
as
a Level III eddy current examiner
and
Electric Power Research
Institute qualified data analyst,
was the author of
the licensee's
data analysis guidelines
and had administered
the site specific
training and testing of data analysts.
No documentation
was
seen during the
onsite inspection that would allow an assessment
of the scope of the oversight
activities by the licensee
personnel.
The inspectors
ascertained
that the quality assurance
organization
had
increased its oversight of steam generator activities during the sixth
refueling outage in both units.
A team surveillance
(SQA-94-0091)
was
performed of Unit 2 steam generator activities during Refueling Outage
2R6.
which included in its scope:
eddy current
and ultrasonic examinations.
chemistry controls.
the foreign material exclusion program.
computer programs.
and high impact team meetings.
A surveillance
(SQA-94-0020)
was also
ascertained
to have been performed
by the quality assurance
organization of
eddy current examination activities during Refueling Outage
1R6.
The
inspectors
reviewed the surveillance reports
and found them to be well written
and indicating thorough review in the eddy current examination
area.
The
inspectors
considered
the use of a Level III eddy current examiner
from
another utility as
a team member in both of these survei llances to be
commendable.
and an excellent practice to follow when performing audits
or
survei llances of specialist activities.
The inspectors
also reviewed the
planned
scope for an audit of steam generator activities that was to be
performed during Refueling Outage
1R7,
and attended
the audit entrance
meeting.
The inspectors
considered
the planned
scope,
which included audit of
eddy current examination activities at the Westinghouse
Waltz Hill facility,
to be comprehensive.
4.3
Review of Tube Examination
Data
The
NRC consultant
reviewed several full-length bobbin coil scans
and also
several three-coil
probe motorized rotating pancake coil examinations of
WEXTEX expansion transition regions.
The bobbin coil examination data quality
was considered
good, with the noise level (using the maximum vertical signal)
observed to be under
0. 17 volts for the sample of scans that was examined.
During review of the three-coil motorized rotating pancake coil examination
data'he
NRC consultant
noted that the high frequency coil appeared to give
additional information about indications, particularly in distinguishing
whether
an indication was located at the inside diameter or outside diameter
0
-29-
surface of the tube.
In addition, the high frequency coil was noted to allow
the analyst to more easily distinguish
between lift-offsignals
and shallow
inside diameter cracks.
Only one potential
inside diameter indication was
observed
by the
NRC consultant during the onsite inspection,
and it indicated
less than 10-percent
throughwall.
The
NRC consultant also reviewed during the inspection
a sample of data
from
Refueling Outage
1R6 pertaining to primary water stress
corrosion cracking
that was detected at dented
and nondented
tube support plate intersections.
The results of this review are documented
in Section 2.5. 1 above.
During the review of Unit
degradation history, which is
discussed
in Section 2.5. 1 above,
the inspectors
noted high apparent
growth
rates
had occurred in some cold-leg thinning indications.
As part of this
review, the worst-case
data (i.e.
~ Tube
R34C18 in Steam Generator
1-2), which
exhibited
an apparent
change
from "no detectable
degradation"
at Tube Support
Plate
01 on the cold-leg side during Refueling Outage
1R6 to
a
68 percent
throughwall defect indication in Refueling Outage
1R7.
was reviewed
by the
NRC
consultant.
The
NRC consultant
noted
from review of the Refueling Outage
1R6
data that
a 1.5 volt signal
was generated
at this location. but with a phase
angle which indicated
a depth that was too shallow to be "called" by an
analyst.
The
NRC consultant
confirmed from the Refueling Outage
1R7 data that
the tube defect
now measured
at 68-percent
throughwall
and appeared
to be
located near the edge of the tube support plate.
The
NRC consultant
concluded
that the high apparent
growth was at least partially related to the masking
effect of the mix residual.
(Note:
Effects of mix residual
are discussed
in
Section 4.2. 1 above).
The inspectors
questioned
licensee
personnel
subsequent
to the onsite inspection
about plans to address
the apparent
rapid growth of
cold-leg thinning indications.
The inspectors
were informed that:
(1) preliminary analysis
by Westinghouse
(of the 68 percent throughwall
indication worst-case
indication in Steam Generator
1-2 Tube R34C18) indicated
that the structural
requirements
of Regulatory Guide
1. 121 were still
satisfied;
(2) the growth curve for cold-leg thinning indications
showed small
growth for larger existing indications,
making it questionable
whether
plugging less than 40-percent
throughwall indications offered any benefit;
and.
(3) Westinghouse
had been instructed to perform
a structural
analysis
and
growth study.
Licensee
personnel
were informed on January
17,
1996, that
review of the Westinghouse
preliminary analysis
and structural
analysis
and
growth study were considered
an inspection followup item (275/9510-02;
323/9510-02).
5
STEAN GENERATOR DEGRADATION HANAGEHENT
5. 1
Steam Generator Strate ic Plan
During the onsite inspection,
the inspectors
were provided with a document
entitled'Steam
Generator Strategic
Plan," dated
February
13,
1993.
This
document described
the licensee's
plans for the future in the area of steam
-30-
generator
tube degradation
management
at the Diablo Canyon
Power Plant.
The
document contained projections of the expected
number of defective tubes which
would require plugging by the end of the plant life, and described mitigative
efforts for containing future degradation
mechanisms.
Based
on the degradation
projections in the report, the licensee
concluded
that the life of the Diablo Canyon
Power Plant steam generators
would extend
to the end of the operating license if aggressive
mitigation efforts were
undertaken.
The noted mitigation efforts included:
reduction of corrosion
product transport,
prevention of caustic tube support plate crevice
conditions,
and reduction of oxidant concentrations
by hydrazine addition and
minimizing air in-leakage.
The primary degradation
mechanism
was projected to
be outside diameter stress
corrosion cracking at the tube support plate
intersections.
This projection was primarily based
on the current status of
the Diablo Canyon
Power Plant steam generator
tubes
and data provided from
other nuclear plants with Westinghouse
Model
51 steam generators.
The
licensee predicted
an end-of-life plugging total in the Diablo Canyon
Power
Plant steam generators
of less
than
17 percent of the total tubes.
Approximately 85 percent of this end-of-life plugging total
was predicted
would occur
as
a result of outside diameter stress
corrosion cracking at the
tube support plates.
Several
recommendations
were made for limiting the
extent of outside diameter stress
corrosion cracking in the future.
The
mitigation measures
listed in the report included:
enhancement
of the
condensate
polishers,
reduction of air in-leakage into the condensers.
continuing to follow the secondary
water chemistry guidelines
issued
by the
Electric Power Research
Institute and Westinghouse,
and investigation of a
potential
T-Hot reduction to 599'F.
The inspectors
noted that the steam generator strategic
plan considered
the
following degradation
mechanisms:
outside diameter stress
corrosion
cracking/intergranular
attack at the top of the tubesheet,
outside diameter
stress
corrosion cracking/intergranular
attack at the tube support plate,
primary water stress
corrosion cracking in the
WEXTEX expansion
region of the
tube sheet.
primary water stress
corrosion cracking in the tube U-bend
regions.
and anti-vibration bar wear.
The inspectors
reviewed
a summary of
pluggable indications in the previous Unit
1 and
2 outages
and concluded that
the dominant acti ve degradation mechanisms'o
date.
were primary water stress
corrosion cracking below the bottom of the
WEXTEX expansion transition region,
primary water stress
corrosion cracking at dented tube support plate
intersections,
and cold-leg thinning.
The absence of apparent
consideration
of these degradation
modes in the licensee's
original projections
was viewed
by the inspectors
as potentially affecting the overall conclusions of the
strategic plan.
During the review of steam generator
business
team activities, which is
discussed
in Section 5.2 below.
a meeting
summary dated July 8,
1994,
was
noted by the inspectors
which indicated that Westinghouse
had comoleted
a
review of the licensee's
steam generator strategic plan.
-31-
determined that the key conclusions of the plan were sound, with the exception
that primary water stress
corrosion cracking should
be considered
as
one of
the dominant future degradation
mechanisms
in the Diablo Canyon
Power Plant
The strategic plan recognized that,
although the degradation
projections
were
based
on data
from similar pressuri zed water reactors,
the final conclusions
regarding the end-of-life state of the Diablo Canyon
Power Plant steam
generators
primarily relied on best engineering
judgement.
The strategic
plan
also identified that degradation
rates
would be closely monitored to verify
that actual
rates
stayed at or below expected
levels,
and that the plan would
be updated annually to reflect the most recent industry steam generator
degradation
experience.
The inspectors
ascertained,
however, that the
strategic
plan had not been
updated since its original issue
on February
13,
1993.
Licensee
personnel
informed the inspectors that outage reports
were
being used to document the results of program actions that had been taken
on
strategic plan issues'ith
open issues
identified in steam generator
business
team minutes.
Licensee
personnel
additionally indicated that
a determination
was
made in 1994 to assign
a lower priority for updating the strategic plan.
due to the other vehicles
used to document results of program actions
and open
issues.
The inspectors
reviewed the steam generator
outage activities reports
that had been written for Refueling Outages
1R6 and
2R6 and found them to be
both comprehensive
and well written.
The reports
were noted to contain
detailed
information on degradation
mechanisms
and status,
but only partially
compared actual results with strategic plan projections.
The inspectors
concluded that the steam generator strategic
plan would.
without regular revision to maintain it as
a living document,
be of limited
value to management
in determination of needed
program actions for maintaining
the integrity of the Units
1 and
5.2
Business
Team
On September
14 and 15,
1993 'epresentatives
from the licensee
and
met to form a steam generator
business
team.
The team was formed
to:
provide
a forum for discussion of Units
1 and 2 steam generator
tube
inspection data.
emerging issues,
and industry events;
and to make
recommendations
regarding future steam generator
chemistry,
operations,
and
outage activities at the Diablo Canyon
Power Plant.
The steam generator
business
team formally convened for the first time in December
1993.
Subsequent
meetings
have occurred approximately every
6 months, with the most
recent meeting taking place June 8-9.
1995.
The inspectors
reviewed the meeting
summaries
from each of the steam generator
business
team meetings.
The meeting
summaries
indicated that much of the
discussions
regarding
tube degradation
and inspection
issues
focused
on recent Diablo Canyon
Power Plant steam generator
tube inspection
results
and findings at other U.S. pressurized
water reactors.
In addition,
the steam generator
business
team also discussed
potential mitigation efforts
in the meetings.'he
inspectors
concluded
from review of Procedure
TS1. ID3,
-32-
Program," Revision
1. the meeting
summaries,
and discussions
with licensee
personnel,
that the steam generator
business
team meetings
were
a key part of the licensee's
overall approach
toward
managing
tube degradation.
6
REVIEW OF SECONDARY WATER CHEMISTRY CONTROLS AND HISTORY
Many impurities that enter
the secondary
side of steam generators
can
contribute to corrosion of steam generator
tubes
and support plates.
While
the concentration of impurities needed to cause corrosion problems is normally
much higher than that present
bulk water. concentration of
impurities to aggressive
levels is possible in occluded
areas
where dryout
occurs.
Typical areas
where dryout and resulting concentration of impurities
can occur are tube sheet crevices,
tube support plate crevices.and
sludge
piles.
Impurities known to contribute to tube denting (i.e., squeezing of
tubes at tube support plates
and tube sheets
as
a result of the pressure of
corrosion products)
are chlorides. sulfates'nd
and its oxides.
Pitting of steam generator
tubes
has
been attributed to the presence
of copper
and concentrated
Concentrated
sulfates
and sodium hydroxide are
believed to be major causes
of intergranular stress
corrosion cracking
and
intergranular attack in steam generator
tubes.
Iron oxide deposits
and sludge
promote local boiling and concentration of impurities.
leading to these
damage
mechanisms.
6. 1
Pro
ram Evolution
The inspectors
reviewed the licensee's
secondary
water chemistry control
program requirements
and initiatives.
It was ascertained
that the secondary
water controls utilized all volatile tr eatment with hydrazine.
Ammonia was
used for pH control
from initial commercial operation unti 1 replacement
by
ethanolamine
in August 1993 (Unit 1) and in March 1994 (Unit 2).
The
inspectors
compared
the Diablo Canyon
Power Plant historical secondary water
chemistry program requirements
against the criteria contained in the Electric
Power Research
Institute
"PWR Secondary
Water Chemistry Guidelines."
These
guidelines
were initially issued in October
1982 as
EPRI NP-2704-SR, with a
different document
number assigned
for each issued revision (i.e.. Revision
1
~
EPRI NP-5056-SR;
Revision 2.
EPRI NP-6239;
and the current Revision 3.
EPRI TR-102134).
To accomplish this task, the inspectors
compared selected
revisions of Operating Procedure
OP F-5: II, "Chemistry Control Limits and
Action Guideline for the Secondary Side." against the Electric Power Research
Institute document that was in effect at the time.
The Procedure
OP F-5: 11
revisions included in the review were:
(a) Revision
0
~ which was effective on
January
28.
1984, against
EPRI NP-2704-SR;
(b) Revision
1, which was effective
on April 13,
1987,
against
EPRI NP-5056-SR;
(c) Revision 4
~ which was
effective on March 30.
1989.
and Revision 5, which was effective on
January
10.
1990, against
EPRI NP-6239:
and (d) Revision ll, which was in
effect on September
8.
1995. against
EPRI TR-102134.
-33-
The inspectors
determined that.
in addition to the limits contained in the
Electric Power Research
Institute guidelines,
the licensee
secondary
side
chemistry program initially included monitoring and Action Level
1 limits for
sulfate. silica. iron.
and copper in the steam generator
blowdown samples.
Further review established
that,
as the Electric Power Research
Institute
secondary
water chemistry guidelines
and the licensee
secondary
side chemistry
program evolved,
the two were in full conformance
upon issue of Revision
5 of
Procedure
OP F-5: II in January
1990.
The inspectors
ascertained
that the licensee
had adopted
several Electric
Power Research
Institute
recommended initiatives in its secondary
chemistry
program.
These initiatives included:
implementation of boric acid addition
to the secondary
side in 1988 in response
to denting.
adoption of 100 ppb
minimum hydrazine levels in December
1992 'nitiation of molar ratio control
in August
1993 using
ammonium chloride injection.
and replacement of ammonia
by ethanolamine for pH control in August 1993 (Unit 1) and in March 1994
(Unit 2).
Overall the inspectors
considered
that the licensee
had developed
a good
secondary
water chemistry program
and had been
responsive
to industry
secondary
water chemistry initiatives.
6.2
Secondar
Side Chemistr
Histor
The inspectors
reviewed the history of the Diablo Canyon
Power Plant. Units
1
and 2, steam generators
with respect to significant chemistry events
and
compliance with the Electric Power Research
Institute secondary
water
chemistry guidelines.
Details on off-normal chemistry are discussed
below in
Section 6.5.
Prior to the onsite inspections
the inspectors
were informed
that retrieval of chemistry records for the first 5 years of commercial
operation would be extremely time consuming
and labor intensive.
due to the
records
management
system that was in effect at the time.
Other offsite
records that were germane to secondary
chemist y performance in this time
period had also not been retained after reorganization
and consolidation of
chemistry engineering discipline responsibilities
at site.
To avoid burdening
the licensee.
the inspectors
did not request that data
be assembled
for the
first 5 years of operation.
This action impacted both the completeness
and
effectiveness
of the review of secondary
side chemistry history, in that the
majority of secondary
side chemistry problems
occurred during the ear ly years
of plant operation,
As part of this review, the inspectors
requested
available historical
information from the licensee
for annual
average
blowdown chemistry values.
The information provided in response
by the licensee for Units
1 and
2 is
listed below in Tables
10 and
11.
0
-34-
Table
10
UNIT 1 AVERAGE STEAM GENERATOR
BLOWDOWN CHEMISTRY VALUES AT > 30K
POWER
Par ameter"'urrent
Limit
CGA
S/cm
< 0.8
Cl
~
b
< 20
SO.
b
< 20
Na.
b
< 20
Molar Ratio"'.1
- 0.7
Na'/Cl
0. 28
2.56
3.38
1.58
1.28
0 crating Cycle
5
6
0.24
0.28
1.14
1.12
1.69
1.53
0.84
0.51
1.10
0.73
0.39
1.14
0.55
0.25
0.35
(1)
-
CC (cation conductivity).
Cl
(chloride).
SO,
(sulfate).
Na
(sodium):
(2)
- Determined
from -;he ratio of molar concentration of sodium to molar
concentration of chloride.
Table
11
UNIT 2 AVERAGE STEAM GENERATOR
BLOWDOWN CHEMISTRV VALUES AT > 30K
POWER
Parameter'"
Current
Limit
0 eratin
C cle
4
5
6
CC. pS/cm
< 0.8
0.26
0.24
0.24
0.35
0.75
Cl
.
b
< 20
1.89
SO,
b
< 20
2.07
Na'.
b
< 20
2.58
Molar Ratio"'. 1
- 0.7
2.54
Na /Cl
1.28
1.04
1.23
1.73
1.17
1.38
0.53
0.44
1.29
0.71
0.31
0.37
1.65
1.03
0.50
0.34
(1)
-
CC (cation conductivity).
Cl
(chloride),
S04
(sulfate),
Na
(sodium);
(2)
- Determined
from the ratio of molar concentration of sodium to molar
concentration of chloride.
The data
from both Units
1 and
Z showed
an improving trend over the last
5 years with respect to control of secondary
water chemistry.
The molar ratio
data
suggested
that alkaline crevice conditions
had been present in earlier
years of power operation.
Reduced
average
molar ratio values
were observed
by
the inspectors to have occurred in Cycle 6 (i.e., the cycle in which molar
ratio control was
implemented using
ammonium chloride injection).
The
inspectors
noted.
however. that the reduction in molar ratio values
appeared
to be related
more to reduction in blowdown sodium concentrations
than from
increases
in chloride content created
by ammonium chloride injection.
The
concurrent reductions
in blowdown sulfate concentrations
during the last two
-35-
operating cycles suggested
to the inspectors
that the improvements in blowdown
chemistry were primarily related to improvements
in condensate
polisher
operational
practices.
The inspectors additionally requested
available trend information for
from the licensee.
in order to gain
some understanding
of the amount of corrosion product transport to the steam generators.
Trend
data
from 1989 to the present for both units was furnished in response
by
chemistry staff.
The trend data.
which consisted
simply of connected
data
points,
showed high iron contents
were historically present
in the feedwater
in both units.
Although the data
format and scatter
impacted interpretations
the inspectors
concluded that feedwater iron concentrations
in both units were
typically in the range of 10-20 ppb through approximately the end of 1992,
with Unit
1 iron values
appearing slightly higher than those in Unit 2.
The
data for this period showed
an essentially stable condition, with no
noticeable
upward or downward trend in iron concentration.
Reduction in
were noted by the inspectors
to have occurred
following the replacement of ammonia
by ethanolamine
for pH control in August
1993 (Unit 1) and March 1994 (Unit 2).
Recent
iron concentrations
were typically in the 5-6 ppb range for Unit
1 and 6-7 ppb for Unit 2.
The
inspectors
also noted.
however. that Unit 2 feedwater iron concentrations
had
declined
as
low as the 3-4 ppb range
by Summer
1994 and then proceeded
to
trend
up to the current 6-7 ppb range.
Licensee
personnel
informed the
inspectors
that this was due.
in part, to ethanolamine
breaking
down to
organic acids at
a. faster rate in Unit 2,
and which resulted in higher steam
cation conductivity values in Unit 2 for a given ethanolamine
concentration.
A current limit for steam cation conductivity of 0.3 ymho/cm requi red by the
turbine warranty resulted in Unit 2 having to operate with feedwater
ethanolamine
concentrations
of 1.7
ppm versus 2.1-2.2
ppm in Unit 1.
The inspectors
requested
historical information from the licensee
regarding
the weight of sludge
removed by sludge lancing from each
during refueling outages.
The data provided by the licensee for the Units
1
and
are listed below in Tables
12 and
13.
The data
indicated to the inspectors
that total Unit
sludge
removal
quantities during refueling outages
have typically been higher than the
amounts
removed from the Unit 2 steam generators.
Although historical
appeared
to the inspectors to have
been slightly
higher in Unit
1 than Unit 2, the differences did not appear
to the inspectors
to be of a magnitude that would account for the sludge variance.
Overa'Il, the
data did not indicate to the inspectors that any clear trend was occurring in
either unit in sludge
removal
amounts.
The inspectors
also reviewed the sludge
removal
data with respect to the
Units
1 and
2 implementation
dates for injection of ethanolamine.
This review
was performed to ascertain
whether the reduction in feedwater iron content.
that was noted to have occurred after beginning
use of ethanolamine
~ was
reflected in reduced
sludge quantities.
Ethanolamine
was introduced into
Unit
1 in August 1993. approximately
7 months before Refueling Outage
1R6.
The inspectors
noted from review of the data in Table
12 that 492 and
-36-
654 pounds of sludge,
respectively.
were removed during Refueling Outages
1R6
and
1R7.
The values for sludge
removal
from the previous five refueling
outages
ranged
from 376 to 850 pounds,
with the mean
removal quantity
calculated to be 729 pounds.
A test
was conducted during Refueling Outage
1R7
which involved use of dimethylamine during wet layup of the steam generators.
The purpose of the test
was to evaluate
whether the dimethylamine would help
dissolve or loosen iron deposits
tubes.
The inspectors
did
not have specific information on the results of the test.
and so could not
assess
whether the dimethylamine
use contributed to an increase
in sludge
removed during lancing operations
in Refueling Outage
1R7 compared with the
previous refueling outage.
The inspectors
concluded that review of sludge
removal
data
from additional Unit
1 refueling outages
would be required before
a determination
could be made of the effects of ethanolamine
use
on sludge
accumulation.
Ethanolamine
was not introduced into Unit 2 until March 1994.
approximately
6 months before the last refueling outage (i.e.. Refueling
Outage
2R6).
The time frame of this change
precluded current assessment
of
the effects of ethanolamine
use.
The inspectors
also reviewed the results of chemical
analyses
that were
performed
on sludge
samples
-.hat had been
removed
from the Units
1 and
2 steam
generators
during each refueling outage through
1R6 and
2R6.
The most
significant feature of the analyses
noted
was the progressive
decrease
in
sludge copper content in successive
refueling outages (i.e.
~ the percent
(as oxide) by weight declined in Unit
1 sludge
from 18. 1 in Refueling
Outage
1Rl to 0.9 in Refueling Outage
1R6,
and in Unit 2 sludge from 21.8 in
Refueling Outage
2Rl to 0.57 in Refueling Outage
2R6.
Progressive
reductions
were also noted in the sludge
from both units
during successive
refueling outages.
The high original copper contents
in the
sludge were ascertained
to be related to the original use of copper alloys for
the feedwater heater tubes.
These tubes
were replaced with Type 439 stainless
steel
during the first refueling outage in each unit.
quantities
were also believed to have originated
from feedwater heater
tubes,
in that the original tubing used
was cupronickel
and brass,
a copper-zinc
alloy.
The inspectors
were informed that the only remaining copper
alloys
were in condenser
tube sheets
and condensate
coolers.
Table
12
WEIGHT (LBS)
OF SLUDGE REMOVED FROM UNIT 1
(SGs)
1Rl
1R2
UNIT 1 REFUELING OUTAGE (1R)
1R3"
1R4
1R5"'R6
1R7
276
286
211
68
226
151
161
1-2
234
154
262
98
241
84'
260
1-3
166
163
169
106
220
100
90.5
1-4
149
247
143
104
124
157
142.5
Total
825
850
785
376
811
492
654
-37-
(1)
- Sludge values
include sludge
removed
by pressure
pulse cleaning;
(2)
- Sludge
removed
by the CECIL process
versus
conventional
sludge lancing.
Table
13
HEIGHT (LBS)
OF SLUDGE
REMOVED FROM UNIT 2 STEAM GENERATORS
(SGs)
Unit 2 Refueling Outage
(2R)
2-1
2Rl
117
2R2r>>
135
2R3
40
2R4
2R5'R6
97.5
142"'-2
2-3
2-4
144
95
182
59
85
83
39
41
127
39
69
121.5
122.5
105
78.5
85
Total
~67
52:
177
237
420
473
(1)
- Sludge values
include siuaae
.emoved
by pressure
pulse cleaning:
(2)
- Sludge values
include sludge
removed
by bundle flushing.
Overalls
the inspectors
considered
that the chemistry history indicated that
the licensee
has significantly improved secondary
chemistry performance
in the
past
5 years. with the reductions
achieved
since
concentrations
viewed as notable.
The current feedwater iron concentrations
were.
however.
viewed to be still of a magnitude that warranted continued
management
attention.
6.3
Self Assessment
of Mater Chemistr
Pro
ram
The inspectors
performed
a limited review of the licensee audit and
surveillance
history pertaining to the primary and secondary
water chemistry
control programs.
In review of the audit and surveillance findings. the
inspectors
observed
no findings which would bring into question the quality of
the water chemistry programs.
6.4
Chemistr
Laborator
Instrumentation
The inspectors
toured the secondary
water chemistry laboratory
and reviewed
the in-line process capabilities with licensee staff.
The inspectors verified
from the review that the necessary
instrumentation
was installed in the
process
lines or available in the laboratory. for analysis of the diagnostic
and control parameters
specified in the secondary
water chemistry control
program.
The inspectors
ascertained
that analog in-line instruments
were
originally used to monitor the
pH
~ conductivity.
and oxygen content of
Recent instrumentation
upgrades
included
a complete upgrade of the
in-line instruments
in 1988 and
a condensate
polisher computer upgrade in
1993.
The in-line instrument
upgrade
provided improved sensitivity and
0
-38-
accuracy for monitored parameters
in the steam generator
blowdown, feedwater,
and condensate
systems (i.e.,
sodium and chloride monitoring improved from + 3
ppb to + 0.5 ppb with sensitivity to 5 ppt).
In 1992.
an on-line ion
chromatography
system
was installed.
This upgrade
enabled chemistry personnel
to monitor contaminants
to the parts per trillion level in the steam generator
blowdown, feedwater,
and condensate
systems.
6.5
Off-Normal Secondar
Chemistr
Histor
The inspectors
requested
licensee
personnel
to provide available
information
regarding significant out-of-specification conditions which have occurred
during commercial service.
The criteria used
by the inspectors
to define
significant were values which exceeded
Action Levels
2 and
3 limits in the
Electric Power Research
Institute secondary
water chemistry guidelines.
The
number of hours exceeding Action Levels
Z and
3 in each cycle for Units
1 and
Z are listed in Tables
14 and
15 below.
The inspectors
noted during review of
the data discussed
in Section 6.2 that minor out-of-specification conditions
were promptly corrected.
This was further illustrated by the relatively few
hours in which conditions in excess
of Action Levels
2 and
3 existed.
From
a
review of supporting information provided by the licensee.
the inspectors
noted that each unit has encountered
sea water intrusions
caused
by condenser
tube leaks which resulted in the pass
through of sodium and chloride ions to
the steam generators.
In addition. Unit 2 experienced
a resin intrusion event
in July 1993 which resulted in an increase
in sulfate concentration
in the
Table
14
UNIT 1 STEAN GENERATOR OFF-NORMAL SECONDARY WATER CHEHISTRY HISTORY
Cycle
Hours Exceeding
Level
2
Hours Exceeding
Level
3
CC(l)
13
- (2)
Cl. "'a'"'0
CC(1)
Na1)
cation conductivity; (2)
blowdown
sulfate:
(3)
blowdown chloride:
(4)
blowdown sodium.
-39-
Table
15
UNIT 2 STEAM GENERATOR OFF-NORMAL SECONDARY WATER CHEMISTRY HISTORY
Cycle
Hours Exceeding
Level
2
Hours Exceeding
Level
3
CC(1)
48
- (2)
Cl
(3)
Na "'C(l)
12
Na'"'6
(1)
- Steam generator cation conductivity: (2)
blowdown
sulfate:
(3)
blowdown chloride:
(4)
blowdown sodium.
7
INSERVICE INSPECTION-OBSERVATION OF
WORK AND WORK ACTIVITIES (73753)
The objective of this inspection
was to determine whether the inservice
inspection examinations
were performed in accordance
with Technical
Specifications,
The American Society of Mechanical
Engineers
(ASME) Boiler and
Pressure
Vessel
Code.
requirements
imposed
by
NRC and industry initiatives.
and correspondence
between the Office of Nuclear Reactor Regulation
and the
licensee
concerning relief requests.
This part of the inspection
and the
followup activities documented
in Section
8 of this report were performed
by a
single inspector during October 16-20,
1995.
7. 1
Inservice
Ins ection Pro ram
The licensee's
inspection
program incorporated the requirements
of the
1977
Edition of the
ASME Code through
and including the
Summer
1978 Addenda. with
the exception that
Code Class
1 and
2 pipe weld requirements
were determined
by the 1974 Edition through
Summer
1975 Addenda of the
ASME Section
XI Code.
This was the third inspection period of the first 10-year inservice inspection
program interval.
7.2
Personnel
ualifications and Certifications
The inservice inspection examinations
observed
were performed
by
nondestructive
examination
personnel
who were employed
and certified by the
licensee.
The inspector
reviewed the qualification files of the seven
individuals who performed the examinations
observed
during this inspection.
-40-
The files contained
the appropriate
examinations
and certifications for the
observed
nondestructive
examination
methods.
The records
showed that the
personnel
had been certified in accordance
with American Society for
Nondestructive
Testing
Recommended
Practice
SNT-TC-IA. 1980 Edition.
7.3
Personnel
ualifications
and Certifications Procedure
Discre anc
The inspector
reviewed Procedure
2. 1, "Qualifications and Certifications of
Personnel'
" Revision 7.
This procedure established
the requirements
for
nondestructive
examination
personnel
training and qualification. Table l.
"Training and Experience
Hinimum Levels," in Procedure
2. 1 identified the
minimum training hours that were applicable for each type of examination
and
qualification level.
The inspector
reviewed Procedure
ISI C-855.
"Inspection of Nondestructive
Examinations Activities." Revision 6.
Procedure
ISI C-855 stated.
that.
"This
procedure
assures
the
NDE work done by examination contractors
wi 11
be
properly controlled and monitored for conformance to Code and approved
procedures
and specifications
as required
by the
PG&E Quality Assurance
Program."
This procedure
also contained
an inservice inspection/
nondestructive
examination standard
inspection checklist which identified the
minimum training hours for each examination
type and qualification level.
These
requirements
pertained to contractors
who were certified under programs
other than the licensee's certification program.
The inspector
compared the minimum training hours listed in Procedure
2. 1 and
Procedure
ISI C-855 and noted
a difference in the requirements
between the two
procedures
for ultrasonic Level I minimum training hours.
Procedure
2. 1 had
identified 40 formal training hours
and Procedure
ISI C-855 noted
20 required
training hours.
The inspector questioned
licensee
representatives
concerning
this difference in procedural
required training hours.
The licensee
representatives
stated that Procedure
ISI C-855 was in error.
Action
Request
A0383185 was initiated and Procedure
ISI C-855 was revised to reflect
the required
40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />.
The licensee
representatives
stated that
a
transposition error occurred
when Procedure
ISI C-855 was revised in July
1984.
The licensee
representatives
indicated that the only known uses of the
inadequate
procedure for ultrasonic examination
personnel
was during
ultrasonic examination of the reactor vessel
in the first and thi rd
examination periods.
The licensee
representatives
also indicated that the
vendors
who performed the reactor pressure
vessel
examinations
had their
programs
audited
and approved
by the quality assurance
organization.
and were
on the nuclear qualified suppliers list.
Subsequent
to the end of the onsite
inspection,
licensee
personnel
reviewed the certification records for the
personnel
who had performed the reactor pressure
vessel
ultrasonic
examinations'nd
determined that all personnel
met the requirements of
SNT-TC-1A.
The inspector concluded that the failure of licensee
personnel
to identify the
procedural
error for 10 years
was
an indicator of inadequate
attention to
detail
when revising and using procedures.
-41-
7.4
Inservice
Ins ection Procedures
Review
The inspector
reviewed the nondestructive
examination
procedures
used during
the performance of the observed
examinations.
The procedures
reviewed
included the following:
~
Procedure
N-MT-1. "Magnetic Particle Examination." Revision 6:
~
Procedure
N-PT-1, "Liquid Penetrant
Examination." Revision 5A:
~
Procedure
N-UT-l. "Ultrasonic Examination Procedure
For Pipe Welds."
Revision 8:
~
Procedure
N-UT-4. "Ultrasonic Examination of Pressure
Vessel
Welds Other
Than Reactor Vessels."
Revision
3A:
~
Procedure
N-UT-8. "Automated Ultrasonic Data Acquisition and Analysis
Procedure."
Revision 4:
~
Procedure
"Visual Examination During Section
XI System
Pressure
Test." Revision 4: and.
Procedure
"Visual Examination of Component
and Piping
Supports."
Revision 8.
Based
on the review. the inspector concluded that the procedures
were
consistent with the requirements
of ASME Code
and had been
approved
by the
appropriate
licensee
personnel.
7.5
Observation of Nondestructive
Examinations
The inspector
observed
the nondestructive
examination personnel
perform
nondestructive
examination activities in the field.
These
observed
examinations
were conducted
using the liquid penetrant.
ultrasonic
(both
manual
and automated),
magnetic particle,
and visual examination
methods
on
Class
1, 2,
and
3 piping and components.
The inspector
noted that prior to
the examinations,
the examiners
performed inspections to verify correct weld
identification, surface cleanliness,
surface temperature,
and industrial
safety
and radiological conditions.
7.5. 1
Magnetic Particle Examinations
The inspector
observed
the performance
by nondestructive
examination personnel
of magnetic particle examinations
on the following system piping and
components:
Code Class
Line/Weld No.
Description
2
K15-225-28V
Hanger
No.
1028.
Line Attachment
2
556/WICG-92-4A
1-4 Feedwater
Supply Line
0
-42-
The inspector noted that nondestructive
examination
personnel
used
an
and appropriately verified that it was capable of lifting a 10-pound weight
prior to the examinations.
The inspector verified that approved color
contrast magnetic particles
were used
and nondestructive
examination personnel
verified magnetic flux lines
and pipe temperature prior to examinations.
The
inspector also verified that the examination results
were appropriately
documented
and reviewed in accordance
with procedures.
No recordable
indications were noted during the examinations.
7.5.2
Dye Penetrant
Examinations
The inspector
observed
the performance
by nondestructive
examination personnel
of a liquid penetrant
examination
on the following system piping weld:
Code Class
Line/Weld No.
Description
2
508/58N-52A
Integral Attachment
Weld to
Residual
Meat Removal
Line
The inspector
noted that the nondestructive
examiner performed
a thorough
inspection for weld identification. surface preparation.
cleanliness.
and
temperature prior to start of liquid penetrant
examinations.
Subsequent
to
the surface
inspections
the examiner applied approved cleaner to assure
the
surface
area
was clean prior to application of the penetrant fluid.
The
inspector noted that appropriate
dwell times were allowed for the liquid
cleaners
developer in accordance
with the procedure.
No recordable
indications were noted by the examiner.
7.5.3
Ultrasonic Examinations
(Manual
and Automated)
The inspector
observed
the performance
by nondestructive
examination personnel
of manual
and automated ultrasonic examinations
using both shear
and
longitudinal wave forms on the following system piping welds:
Code Class
Line/Weld No.
Description
I
WIB-374SE
Pressurizer
Spray Line to Inlet Nozzle
I
Girth I
Pressurizer
Bottom Head to Shell
2
WICG-92-4A
1-4 Feedwater
Supply Line
The inspector noted that nondestructive
examination personnel
performing the
observed
examinations
adhered to procedural
requirements.
The inspector
noted
that the examiners
were very knowledgeable of the examination techniques
and
procedural
requirements.
During the manual ultrasonic inspection of the pressurizer
spray line to
inlet nozzle welds, the examiner noted
and documented
observed
geometric
indications.
The inspector did not observe this examination.
Based
on
evaluations
performed
by nondestructive
examination personnel,
the geometric
indications were attributed to thermal sleeve
attachment
and were not
0
-43-
recordable.
However,
licensee
representatives
were aware of a previous
operational
event at another facility in 1993 where subsequent
to
nondestructive
examinations
during heatup
a leak was identified in the
pressurizer's
safe-end
near where
a pressure-operated
relief valve header
connected to the pressurizer.
Based
on that operational
event
and concerns
for cracks in nozzles
having similar configurations,
licensee
representatives
performed further examinations of the pressurizer
spray line to inlet nozzle
Ultrasonic examination
was performed using the licensee's
automated
ultrasonic examination
and data acquisition system.
The inspector
was
informed that the area to be examined
was indicating approximately
800 milli rem on contact.
However, the inspector
observed
the nondestructive
examination
personnel
display good ALARA practices while performing this
examination.
Based
on review and evaluation of the examination data taken
during the subsequent
examinations
nondestructive
examination personnel
concluded that the geometric indications identified with both the manual
and
automated ultrasonic examinations
were thermal
The inspector considered that the licensee's
inclusion of operational
experience
for inservice inspection efforts was commendable.
7.5.4
Visual Examinations
The inspector
observed nondestructive
examination personnel
perform visual
examinations
on the following welds
and system piping:
Code Class
Line/Weld No.
Description
ISI Test
58
Containment
Spray Discharge
Functional
Pressure
Test Visual Examination
Hanger
14-47SL
Component Cooling Water Line Snubber
Replacement
Preservice
Visual Inspection
During the containment
spray discharge
functional pressure test.
the inspector
noted that the line was pressured
to approximately
250 psi
and the pressure
maintained for approximately
20 minutes.
which was in excess of the minimum
time requirements
specified in the procedure.
No system
leakage
was
identified.
During the preservice visual examination for the component
cooling water line snubber
replacement.
the examiner noted that Hanger
14-47
had been mislabeled
as "14-74."
The nondestructive
examiner appropriately
documented this observation
on the visual examination report.
No other
problems
were identified.
The inspector noted that nondestructive
examination
personnel
who performed the observed visual examinations
displayed
a
questioning attitude
and attention to detail.
7.6
Safet
Assessment/
ualit
Verification
During the observed
examinations,
the inspector
noted that on several
occasions
the licensee inservice inspection supervisor
was observing
and
monitoring nondestructive
examination personnel.
The inspector also noted
that the inservice inspection supervisor
was cognizant of ongoing activities
0
-44-
and status of scheduled
examinations.
Based
on these observations.
the
inspector concluded that the inservice inspection supervisor
was actively
assuring the quality of examinations
and was performing effective oversight.
8
FOLLOMUP
-
HAINTENANCE
(92902)
8. 1
Closed
0 en Item 323/9307-08:
Fuel Handlin
Area Exhaust
Carbon Filter
Bank Test Failure
8.1.1
Original Open Item
This open item involved
a subsequent
review of the licensee's
corrective
action associated
with test failure of the charcoal filters in the ventilation
system.
The charcoal filters were tested prior to fuel movement during
Refueling Outage
2R5.
The results of the analysis,
which were received after
refueling activities
had begun.
concluded that the efficiency of the charcoal
was slightly below the Technical Specification requirement.
8. 1.2
Licensee Action
As part of the licensee's
corrective action.
the charcoal filter bank was
replaced.
Unit
1 and Unit 2 Procedures
STP 0-41.
"Fuel Handling Building
Ventilation System
-
DOP and Halide Penetration
Tests."
were revised to
caution that results of the test should
be received prior to moving fuel so
that adequate
time for filter replacement
was available.
8. 1.3
Inspector Action During the Present
Inspection
During this inspection.
the inspector verified that the Unit
1 Procedure,
STP H-41. Revision
13,
and the Unit 2 Procedure,
STP M-41. Revision
1,
included consideration for the receipt of the charcoal filter test results
prior to moving fuel.
In addition, the inspector verified that the charcoal
filter test results
had been received
and evaluated prior to moving .fuel in
the current Refueling Outage
1R7.
8.1. 4
Conclusions
Based
on the inspector's
review. it was concluded that Unit 1 and Unit 2
Procedures
STP H-41 had been appropriately revised
and that the charcoal
filter test results
had been received
and evaluated prior to moving fuel in
the current Refueling Outage
1R7.
-45-
8. 2
Closed
Violation 275 323/9425-01:
Inade uate Measures
For Control lin
Reactor Coolin
S stem Water
Leaka
e durin
Hachinin
0 erations
and
Failure to Initiate an Action Re uest for a Previous Simi1ar Occurrence
8.2.1
Original Violation
This violation involved a failure to provide documented
instructions
appropriate to the circumstances
for the resistance
temperature
detector
modification on Unit 2 that resulted in reactor coolant system water spilling
out of the Loop
1 hot leg during machining operations.
In addition, this
violation involved the failure to initiate an action request
during the
previous Refueling Outage
1R6,
when
a reactor coolant system water spill
occurred during the Unit 1 resistance
temperature
detector modification
project.
8.2.2
Licensee Action
Licensee representative
concluded that
a more thorough prejob planning process
could have prevented
the spill of contaminated
water.
As part of the
licensee's
corrective action.
a thermowell drain adapter
and discharge line
were installed to control reactor coolant system water leakage for the
remaining modifications project activities.
A case
study of this event
was
prepared for review by plant personnel
to heighten
awareness
of the need for
proper work planning
and the need to initiate problem identification
documentation.
Administrative Procedure
AD7.NC2,
"Conduct of Work," was
issued to provide specific guidance to plan for handling unanticipated
amounts
of water when
a fluid system is breached.
8.2.3
Inspector Action During the Present
Inspection
During this inspection.
the inspector
reviewed Procedure
AD7.NC2 and verified
that the procedure
addressed
planning for handling
an unanticipated
amount of
water during
a fluid system breach.
The inspector questioned
licensee
representatives
concerning
any water spills that might have occurred
subsequent
to these
two events.
Licensee representatives
indicated that none
have occurred.
8.2.4
Conclusions
Based
on review of Procedure
AD7.NC2 and the case
study prepared for this
event,
and the fact that no subsequent
water spills from fluid system
boundaries
have occurred.
the inspector concluded that the licensee's
corrective actions
were adequate.
ATTACHMENT
PERSONS
CONTACTED AND EXIT MEETING
1
PERSONS
CONTACTED
l. 1
Licensee
Personnel
D. Adamson,
Nondestructive
Examination Supervisor,
Technical
and Ecological
Services
~J. Arhar,
Engineer,
Turbine Support
Systems
- S. Cortese.
Chemistry Engineer,
Chemistry
and Environmental Organization
- R. Exner, Supervisor,
Turbine Support
Systems
- W. Fujimoto. Vice President
and Plant Manager
"J. Gardner,
Senior
Chemistry Engineer,
Chemistry and Environmental
Organization
¹D. Gonzalez,
Inservice Inspection Supervisor.
Nuclear Steam System Supplier
System Engineering Services
- C. Harbor,
NRC Interface.
Regulatory Services
~A. Hardy. Quality Assurance
Engineer.
Nuclear Quality Services
C. Hartz. Quality Assurance
Engineer.
Nuclear Quality Services
- J. Hays. Director, Chemistry and Environmental Organization.
Operations
Services
D. Helete.
Engineer.
Turbine Support
Systems
- J. Kang. Nondestructive
Examination Engineer.
Technical
and Ecological
Services
¹T. McKnight. Quality Assurance
Supervisor.
Nuclear Quality 'Services
¹P.
Nugent, Senior Engineer,
Regulatory Services
¹G. Toison, Audit Team Leader.
Nuclear Quality Services
- T. Polidoroff, Senior Engineer,
Nuclear Technical
Services
D. Taggart
~ Director, Nuclear Safety Engineering,
Nuclear Quality Services
¹D. Vosburg. Director. Nuclear Steam
System Supplier System Engineering
Services
- ¹J.
Young. Director, Quality Assurance,
Nuclear Quality Services
1.2
Contractor
Personnel
J.
Semelsberger,
Site Outage
Manager,
1.3
NRC Personnel
M. Tschi ltz, Senior Resident
Inspector
¹J. Russell,
Acting Senior Resident
Inspector
In addition to the personnel
listed above.
the inspectors
contacted
other
personnel
during this inspection period.
- Denotes
personnel
that attended
the exit meeting
on October
17.
1995.
¹ Denotes
personnel
that attended
the exit meeting
on October 20.
1995.
"¹ Denotes
personnel
that attended
the exit meetings
on October
17 and
October 20.
1995.
-2-
- Denotes
personnel
that attended
the exit meetings
on October
17.
1995,
and
January
17,
1996.
2
EXIT HEETING
Exit meetings
were conducted
on October
17,
1995, in regard to the steam
generator
tube integrity inspection
and on October 20.
1995, in regard to
observation of inservice inspection work and work activities.
During these
meetings,
the inspectors
reviewed the scope
and findings of the report.
An
unresolved
item was discussed
in the October
20 '995 'xit meeting which was
subsequently
resolved
based
on additional
information provided by the
licensee.
The licensee
was notified on October
27.
1995 'hat the subject
item was considered
resolved.
An additional exit meeting
was held by
telephone
on January
17,
1996, to inform the licensee that.
as
a result of
in-office review. inspection followup items would be identified in regard to:
(a) eddy current examination procedure
conformance to Appendix
H of
EPRI NP-6201,
Examination Guidelines." Revision 3: and.
(b) review of Westinghouse
analyses
for cold-leg thinning indications.
The
licensee did not express
a position on the inspection findings documented
in
this report.
Nuclear steam
system supplier documents
were reviewed during the
inspection which were marked to indicate they contained proprietary
information.
No information was included in the inspection report that was
considered proprietary.
0