ML16342C070

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Insp Repts 50-275/94-11 & 50-323/94-11 on 940320-0423. Violations Noted.Major Areas Inspected:Onsite Followup Events,Operational Safety Verification,Plant Maint, Surveillance Observations & Refueling Preparations
ML16342C070
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/19/1994
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342A515 List:
References
50-275-94-11, 50-323-94-11, NUDOCS 9405250015
Download: ML16342C070 (48)


See also: IR 05000275/1994011

Text

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APPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-275/94-11

50-323/94-11

Operating Licenses:

DPR-80

DPR-82

Licensee:

Pacific

Gas

and Electric Company

Nuclear

Power Generation,

B14A

77 Beale Street,

Room 1451

San Francisco,

California

94177

Facility Name:

Diablo Canyon,

Units

1

and

2

Inspection At:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

March 20 through April 23,

1994

Inspectors:

M. Miller, Senior Resident

Inspector

H. Tschiltz, Resident

Inspector

Approved By.

D.

lrsc

,

1

Reactor Projects

Branch

E

Ins ection

Summar

te

ig

Areas

Ins ected

Units

1 and

2

Routine,

announced,

resident

inspection of

onsite followup of events,

operational

safety verification, plant maintenance,

surveillance observations,

refueling preparations

and operations,

quality

oversite activities, safety

system walkdown, followup on corrective actions

for violations, followup, and in-office review of licensee

event reports.

Results

Units

1 and

2

~0erations:

Operations

personnel

performed well during this inspection period.

Strengths:

Prompt conservative

actions

were

implemented

by the operations

department

to shut

down the Unit 2 reactor within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

when

a leak

was identified in the reactor coolant

system

(RCS).

9405250015

940519

PDR

ADOCK 05000275

Q

PDQ-

Weakness:

~

Communications

and control of fuel movement

were inconsistent with

management's

expectations.

Haintenance:

Certain maintenance

activities were not conducted

in accordance

with

applicable

procedures

and management

expectations

during this inspection

period.

Weaknesses

~

Actions to repair the leak in the Unit 2 reactor'ere

not conducted

using the required clearance for control of the repair work boundary.

As

a result,

argon

gas

was injected into the

RCS, which could have

resulted

in elevated

RCS activity and radiation levels.

~

Maintenance

management

had not clearly communicated

expectations

for

signing work orders to the construction

crew installing an inverter,

resulting in recorded

dates for installation work steps

being back-dated

to the date of performance,

rather than indicating the date of

signature.

Licensee

management

took prompt action to communicate

expectations

to construction

personnel

and, later, to maintenance

personnel.

The licensee's

engineering

organization

responded

well to the emergency

diesel

generator air flow concern;

however,

weakness

was observed

in the conduct of

local leak rate testing

(LLRT) and the evaluation of reduced diesel

generator

loading capability.

Strengths

The engineering

organizations

promptly responded

to concerns

regarding

EDG radiator airflow, contacted

industry experts,

conducted

intensive

testing of diesel

generator radiator air flow, took conservative

action

to recommend

delay of Unit 2 restart,

and maintained Unit 2 in cold

shutdown while

EDG operability testing

was ongoing.

This evidenced

a

conservative

safety perspective.

Weaknesses

~

The operations

and maintenance

organizations

identified inadequate

administrative controls of LLRT temporary modifications by engineering.

Plant management

took actions to clarify expectations

and implement

additional training for LLRT personnel.

-3-

The initial operability evaluation

associated

with Oiesel

Generator

1-3

declared

the diesel

generator

operable for Nodes

5 and

6 at reduced

electrical

loading without consideration

of Technical Specification

(TS)

requirements

for diesel

generator

loading during these

modes

and without

adequate

instruction to operators

regarding selection of electrical

loads which would be appropriate

to shed in the event of a derated

generator.

Licensee

management

agreed with inspectors that this

evaluation

was not appropriate,

and the evaluation

was revised.

The licensee's

quality oversight organization

performed well during this

inspection period.

Strengths

~

The quality organization

evidenced

strong, intrusive involvement,

problem identification,

and corrective action concerning

weaknesses

associated

with the maintenance

area.

Issues

included operability

evaluations of past

improper re-installation of motor-operated

valve

pinion keys,

inspections

to identify cracking in 480

V transformer

insulators,

improper temporary attachments

in the Unit

1 containment,

and lack of visual inspection of snubbers.

Summary of Inspection

Findings:

~

Violation 323/94-11-01

was identified (Section 4).

~

Violation 275/93-32-01

was closed

(Section

10).

~

Licensee

Event Reports

275/94-04,

Revision 0,

and 275/94-05,

Revision 0,

were closed

(Section

11).

Attachments:

~

Attachment

1 - Persons

Contacted

and Exit Neeting

~

Attachment

2 - Acronyms

DETAILS

1

PLANT STATUS

(71707)

1.1

Unit

1

The unit was shut

down throughout the entire inspection period for a refueling

outage

(1R6).

Core offload and reload operations

occurred during this period.

1.2

Unit 2

At the beginning of this inspection period, the unit was operating at

100 percent of rated thermal

power.

On March 26,

1994,

power was reduced to

50 percent to facilitate scraping of marine growth from the circulating water

Pump 2-1 tunnel.

On March 27,

1994,

the unit was shut

down after

identification of RCS leakage.

Following repair of the leak,

and

EDG radiator

air flow testing,

the unit transitioned to Mode

1

and returned to 100 percent

power on April 10,

1994.

2

OPERATIONAL EVENTS (93702)

2. 1

Unit 2 Unusual

Event

Due to Reactor

Coolant

S stem

RCS

Pressure

Boundar

Leaka

e

During

a containment entry for the purpose of troubleshooting

Reactor Coolant

Pump 2-3 seal leakoff indication,

a leak was identified near Reactor Coolant

Pump 2-3, in an area containing piping from several

systems

normally

inaccessible

during reactor operation.

The location of the leak was initially

thought to be valve packing leakage

from the resistance

temperature

detector

(RTD) manifold isolation valve.

This was difficult to confirm due to the high

radiation levels in the area.

Operations

management

concluded that

a plant

shutdown

was prudent

and reached

Node

3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

Immediately after

reactor

shutdown,

on

a containment entry for further investigation,

the leak

location was determined to be not from the

RTD manifold, but from a

nonisolable

cracked

socket weld on

a 3/4-inch vent line cornected to Safety

Injection Accumulator 2-3 injection line.

Operations

concluded that

a plant

shutdown would have

been required

by TS since the 0.3

gpm leak was nonisolable

pressure

boundary leakage.

An unusual

event

was declared.

Upon transition to

Mode

5 on March 28 1994, the licensee

terminated the unusual

event

and

began

establishing

conditions for repair of the leak.

Failure analysis of the

cracked weld, performed

by Westinghouse,

revealed that the cause of the leak

was

a weld defect

on the inner diameter of the weld,

an area not required to

be inspected

during fabrication.

2'.1

Conclusion

The licensee

operations staff initiated

a conservative

reactor plant shutdown

following discovery of the

RCS leak.

Immediately after reactor

shutdown,

a

more precise

leak location was identified.

The licensee

Operations staff

0

promptly declared

an Unusual

Event

upon determination that the leak was

unisolable

RCS leakage.

Evaluation of repair efforts are described

in

Paragraph

4.

2.2

Unantici ated

Hi

h Radiation Area Durin

Chemical

and Volume Control

S stem

CVCS

S stem Fill and Vent

At about

4 p.m.

on April 11,

1994, the licensee identified that

a high

radiation area

had occurred in a radiologically controlled area hallway,

originating in reactor

cleanup piping mounted

along the hallway.

The area

was

posted

promptly upon discovery,

a root cause

evaluation initiated,

and

a

visiting NRC health physics inspector

and resident

inspectors

were informed.

Based

on the configuration of the radiation area localized to

a hot spot,

and

the low traffic in the area,

the licensee

determined that

no personnel

had

been over exposed.

Earlier that day, at 2:50 a.m.

on April 11, before

CVCS fill and vent

operations

had

commenced,

Operations

alerted Health Physics to the potential

for changing radiation

areas

caused

by the fill and vent.

Apparently no

radiation protection surveys

were accomplished

in that area after that

announcement

until the routine survey around

4 p.m. the

same day, which

identified the hot spot.

Licensee root cause

investigation determined that the area radiation levels

had risen sharply,

at approximately the time the

CVCS fill and vent procedure

had

been

underway, while testing the

CVCS diversion valve function.

The

licensee

determined

the most likely cause of the hot spot,

which is discussed

in the following paragraph.

Forced oxygenation,

which was performed before

shutdown to decrease

RCS piping

radiations levels,

probably caused

highly activated iron oxides

(magnetite)

to

deposit in the deborating demineralizer.

A newly replaced

0.2 micron filter

upstream of the hot spot

and downstream of the deborating demineralizer

was

later found to have failed.

It is likely that

a water slug was generated

by

the fill and vent procedure,

which could have

caused

the magnetite to break

loose

from the resin

bed

and travel to the filter.

The filter may have

ruptured at that time or an earlier time.

This would have allowed the

magnetite to travel past the filter to the area of piping which was the source

of the hot spot.

The filter vendor

and the licensee

concluded that the

filter, bowed out

as if overpressurized,

had

been

exposed to reverse flow,

since the normal flow path is from the outside of the cylindrical filter to

the inside of the filter.

A reverse

flow path

may have occurred during

hydrostatic testing of the volume control tank.

Check valve leakage

was

suspected

during the hydrostatic test.

Licensee investigation is continuing

and appears

to be conducted

in a thorough manner.

At the time that the hot spot

was identified,

no formal notification was

made

to the

NRC.

The licensee's

emergency

plan was not consistent with the safety

significance of the event,

since the only emergency

plan guidance available

was

ambiguous

and would have resulted

in a highly conservative

recommendation

of an Alert level of emergency

response.

The licensee

determined that

declaration of an Alert was incorrect,

since

no chance of off site radiation

release

was possible for this hot spot.

After inquiries from the

NRC, the

licensee later discussed

the basis for not declaring

an Alert with NRC

management.

The basis

appeared

appropriate.

The licensee

agreed to revise

the emergency

response

plan to more clearly and appropriately

address

these

types of situations.

The licensee's

corrective action in this area will be

reviewed during the next scheduled

NRC inspection of the emergency

response

area.

The health physics

aspects

of this issue

are addressed

by the

NRC inspection

report issued

by the Region-based

NRC health physics inspector.

The licensee

received

a violation for the unposted radiation area,

issued

in the

NRC hea)th

physics Inspection

Report 50-275/94-12;

50-323/94-12.

2.2.1

Conclusion

The licensee radiation protection organization did not appropriately

survey

for changes

in radiation levels

when warned

by the operations staff.

The root

cause of this deficiency will be followed by the

NRC hea')th physics

and

emergency

preparedness

inspection efforts.

Licensee investigation into the

cause of the hot spot was prompt

and appears

to be continuing in a

responsible,

appropriate

fashion.

Corrective action observed to date

appeared

appropriate.

3

OPERATIONAL SAFETY VERIFICATION

(71707)

3. 1

Control of Plant Confi uration

and Status of

E ui ment

Im lemented

in the

Control

Room

Inspectors

performed frequent control board walkdowns in the control

room to

observe

Operations

control of plant configuration, clarity of clearance

tags,

appropriate availability of plant equipment

and instrumentation

during

shutdown

and operating

modes,

and effective, conservative transitions

through

the various

modes of operation.

Both units transitioned

through several

operating

modes during this inspection period.

Inspectors

found operators

to

be knowledgeable

and control of plant equipment to be appropriate.

Equipment

tags clearly referenced

applicable clearances

and noted additional cautions

and restrictions.

The

TS and the outage safety plan was followed for both

units with respect

to availability of plant equipment.

3. 1. 1

Conclusion

The control

room boards

were maintained

in an appropriate

fashion during both

unit outages.

Control board indication

and control for plant equipment

and

instrumentation

were appropriately tagged,

and restrictions

were clearly

documented

or referenced for cases

where multiple safety controls were

applicable.

3.2

Ina

ro riate Documentation of Containment

LLRT Jum er

Jum er 94-019

On Harch

16, during routine Operations

department

review of the jumper logs,

operations identified that

a jumper had

been

documented

but had not received

proper reviews

by operations.

Operations

issued Action Request

A0331842 to

document

the deficiency.

Later review determined that the jumper supplied

pressure

for containment isolation valve local leak rate testing in

containment,

being performed

by engineering

and maintenance.

The pressurizing

gas

was supplied through the spare

Containment

Penetration

80.

Further investigation revealed that poor communications

had occurred

between

Engineering

and Haintenance

concerning

jumper documentation

and existing

procedural

controls for the

LLRT, resulting in submission of incomplete jumper

documentation.

guality Evaluation

11270

was issued to determine the root

cause of the inadequate

communications.

Engineering

and maintenance

management

discussed

appropriate

expectations

and

controls for planning

and documentation

of LLRT jumpers,

as well as conduct of

LLRT evolutions, with their staffs.

To determine the safety significance,

the inspector evaluated existing

controls of the

LLRT process

regarding the jumper.

Further review determined

that the entire process of connection,

control, disconnection,

and use of the

jumper was controlled by several

plant procedures,

including:

Procedure

STP G-12, "Operation of the Portable

Leak Test Monitor," Revision 3;

several

procedures

for individual penetration testing,

such

as

Procedure

STP V-651A, Revision 3, "Penetration

51A Containment Isolation Valve

Leak Testing," which, for example,

included Step 11.3. 15 "replace seal

on

SI-1-153,"

and Step 11.3. 18 "verify removal of all test instrumentation," with

sign offs on each step.

The inspector questioned

whether the controls for ensuring

containment

integrity were established

for the spare penetration,

and noted that

Procedure

OP K-108,

"Sealed

Valve Checklist for Manual

Containment Isolation

Valves," Revision 3, Step 2. 1, stated

"This sealed

valve checklist verifies

inside containment

manual isolation valves are in the correct positions

and

sealed ... for Modes 1,2,3

and 4."

Step 6. 1 stated

"Visually verify position

of containment isolation valves in Appendix 9. 1," which included the

Penetration

80 spare

instrument lines.

These controls

appeared

comprehensive

and appropriate.

The safety significance of the inadequate

jumper documentation

is very low in

that multiple levels of control of the jumper exist in plant procedures.

3,2. 1

Conclusion

Operations

promptly identified incorrect documentation of a plant jumper.

Engineering

and maintenance

management

took steps

to correct inadequate

communications

between

the two groups coordinating

LLRT work.

The safety

significance of this issue is low, but provides

an example of a communication

and work control problem identification and corrective action.

3.3

EDG Radiator Air Flow

Licensee testing of

EDG radiator air flow identified lower than expected

flow

values.

The licensee initiated several

tests of EDG air flow, including

testing of Unit 2

EDGs, during the unscheduled

Unit 2 shutdown.

The

engineering staff conservatively

required Unit 2 to remain shut

down until

EDG

operability was thoroughly addressed.

An operability evaluation

was issued

identifying that,

above the 78'F ambient design temperature,

air flow may not

be adequate

to remove heat from the radiator.

The Final Safety Analysis

Report design basis

concluded that temperatures

above 78'F would occur only

for 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> per year, with a maximum temperature

of 91

F.

Temperatures

at the

site

had not exceeded

78

F for

an extended

period.

On April 1,

1994, during

a review of EDG 1-3 operability evaluation,

documented

on Action Request

A0333816,

the inspector

noted that the licensee

concluded that the

EDG was operable,

with reduced radiator air flow during

Modes

5 and 6, provided generator

loading was maintained less

than

1400

kw.

The operability evaluation further stated that generator

loading could

be

increased

to above

1400

kw provided operations

monitored jacket water

temperature

every

30 minutes

and loads

were reduced

as reqiiired to maintain

diesel

engine jacket water temperature

less

than 177'F.

This operability

evaluation

had

been

reviewed

and concurred

in by the Manager of Nuclear

Engineering Services.

The inspector identified that

TS 3.8. 1.2,

Surveillance 4.8. 1.2, requires that, during Modes

5 and 6,

a diesel

generator

be capable of being loaded to greater

than or equal to 2484 kw.

The inspector

questioned

the validity of the operability assessment

based

on the

TS

electrical'loading

requirements.

The inspector also questioned

whether

any instructions

had

been provided to

operations

department

personnel

expected to initiate compensatory

actions for

generator

load conditions of greater

than

1400

kw.

Apparently,

no guidance

had

been provided to operators

even though vital component

loads

on the

associated

bus

had

been estimated

to be close to 1800

kw during Modes

5 and 6.

Guidance for load shedding

was provided to operators within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of the

inspector raising the issue.

The operability evaluation

was issued

and questioned

by inspectors

when the

Unit

1 core

was off-loaded

(No Mode).

Although the operability evaluation

documented it's applicability for Modes

5 and 6, the

TS requirements

were not

applicable at that time.

As a result of the concerns

raised

by the inspector,

the licensee

revised the

operability evaluation.

Licensee calculations

completed during the first week of April 1994,

concluded

that, with roll up doors

opened to provide air flow, diesel

performance

would

meet design basis

loading requirements

up to the maximum temperature

of 91'F

identified in the Final Safety Analysis Report.

During

a meeting

on April ll, 1994, to discuss

more detailed

aspects

of the

EDG air flow test results with the licensee,

NRC inspectors

raised the

following issues:

~

The need for issuing formal guidance

in procedures

to the operators

to

determine

which loads

should

be shed.

~

Apparently, the

EDG cooling air supply had not been tested

or calculated

for conditions

when more than

one diesel

is running.

This may not be

conservative,

since three diesels

may start

and all use the

same cooling

air source

when operators

open doors for extra cooling.

~

The calculated

basis for EDG oper ability during periods

when outside

ambient temperature

was greater

than S5'F relied

on

EDG operation with

engine jacket water temperatures

at 205 F, which is greater

than that

recommended

by the

EDG vendor (190'F).

The inspector questioned

whether

this condition was considered

acceptable

by the vendor.

Operability of EDGs depends

on operator actions to open roll-up doors

upon alarm of the diesel jacket water high temperature.

However, the

alarm circuit was not safety related

and does not undergo routine

surveillance to ensure it will perform it's required function.

Similarly, the roll-up doors were not qualified for design basis

functions.

Various design basis

scenarios

for the doors

and alarm

circuit had not been evaluated

regarding seismic, fire protection,

equipment qualification,

and control

room evacuation

requirements.

~

The capability for alarm circuit reflash

was not known, i.e., whether or

not

a separate

alarm on that circuit would preclude annunciation of a

jacket water temperature

{or other temperature)

alarm.

No acceptance

criteria appeared

to be stated for the cleanliness

of the

air pathways

in the

EDG radiators,

although debris in the radiators

may

ffect air flow through the radiator.

Several roll up doors were involved in supplying air to radiators;

however,

the doors required to be opened

were not identified clearly and

specifically.

It was not clear that appropriate

conservatism

was

used in the

calculations for the radiator

performance,

such

as dry air, wind

effects,

or other heat transfer conservatism.

It was not clear that the vendor

had concurred in the air flow and

diesel

performance calculations.

-10-

~

The licensee

had not shared air flow measurement

and radiator

performance

information with other licensees

with similar diesel

radiator designs.

~

Past surveillance test performance of diesel

generators

while air

temperatures

were above 78'F had not been reviewed to validate

operability calculations.

The licensee

provided satisfactory resolution of each of the above issues,

obtained

vendor concurrence

with performance

conditions

and expectations,

or

is performing detailed calculations

and evaluations to address

the concern.

Testing

was later performed with all three Unit

1

EDGs running, with

satisfactory air flow results.

Other licensee identified technical

issues

are

under review or undergoing calculations.

The information has

been

shared with

the industry.

The licensee

has initiated

a hot weather plan, to be effective

upon

alarm indication in the control

room for ambient temperature

greater

than

78oF

A search of past operations

during high ambient temperatures

indicated that,

during

a 7-hour run at 85'F ambient temperatures,

jacket water temperature

reached

and stabilized at 200'F,

which the vendor concurred

was acceptable

for

sustained

operation.

This satisfactory

EDG performance

occurred without

opening roll up doors.

3.3. 1

Conclusion

The licensee

appeared

to have promptly addressed

the operability issues.

However, inspectors

were able to identify several

potential

issues,

which

indicated

some weaknesses

in the completeness

of engineering

and technical

work.

Overall, licensee

engineering

involvement appeared

to be acceptable.

3.4

Flow Oscillations in

EDG Radiators

The licensee identified that air flow through the

EDG radiators

evidenced

pressure oscillations.

The fans were designed for a pressure

drop of

1.8 inches of water

and were installed in a configuration which resulted

in

approximately 2.4 inches of water.

The licensee

tested

fan blades at lower

angles to determine if oscillations could be reduced,

but minimal benefit was

gained,

and air flow was reduced.

The licensee

returned the blades to the

original configuration.

Detailed inspection of the blade

hubs

was performed,

and

no indications of

fatigue or growth of existing surface discontinuities

was identified.

Despite

the lack of fatigue indications,

the licensee

implemented

a previously

approved

design

change during the unscheduled

Unit 2 outage,

replacing Unit 2

EDGs fan hubs with more robust design

hubs.

This design

change

had already

been

performed

on Unit

1 during the scheduled

outage.

The licensee

concluded,

and obtained

vendor concurrence,

that continued operation of the

EDGs with

flow oscillations would not be detrimental

to long term

EDG operation.

3.4.1

Conclusion

The licensee

appeared

to have appropriately

addressed

these

issues

with

timely, intrusive engineering

involvement.

3.5

Reactor

Vessel

Level Indication

S stem

On April 20,

1994, during preparations

to perform

RCS maintenance

at reduced

inventory while at

an

RCS level of 109 feet

(RCS loops full, and

2 feet above

the midloop level of 107 feet), the licensee

found that the narrow range level

indicator,

LT 400, did not properly agree with the other narrow range

transmitter or the wide range transmitter.

Operations staff halted the

procedure for continuing to midloop operations

while the

RCS was at

109 feet,

until the level indication was repaired.

Licensee

management

of maintenance,

engineering,

and operations

became actively involved, along with plant staff,

in agreeing that operations

would remain halted until the problem was

resolved.

Troubleshooting

revealed that the indicator consistently

indicated

about

a

1.5-inch lag in actual level, resulting in the indicated level being

approximately 1.5 inches

high under conditions of decreasing

level,

a

nonconservative

indication.

The level indicator consisted of a reference

leg

in which

a float containing

a magnet

rose

and fell with reference

leg level.

The magnet

actuated

magnetic

sensors

outside the reference

leg, allowing

visual indication of the level.

The licensee

duplicated

the observed

oFfset

in a bench test

by changing the axial orientation of the float, resulting in

the magnet not facing the sensors

and changing the sensed

magnetic field.

Efforts to realign the float in the plant were not successful.

The lag offset

was consistently

repeated

during troubleshooting

in the plant,

and, after

contact with the vendor, plant Engineering,

Operations,

and Instrument

and

Control staff concluded that the indicator's calculated

instrument error

should

be increased

to include the observed error and procedures

revised

accordingly before entering midloop operations.

After revision of the

procedures

to raise the minimum level of the

RCS level midloop operating

band,

which resulted

in narrowing the operating

band,

operations

at reduced

inventory were initiated.

No further problems

were identified during reduced

inventory operations.

3.5. 1

Conclusion

Major work activities were halted

when plant management

concluded that further

investigation

and testing of the level indicated

was required.

This was

a

conservative

and responsible

approach

to plant safety during reduced

inventory.

0

-12-

4

PLANT MAINTENANCE

(62703)

During the inspection period,

the inspecto}

observed

and reviewed selected

documentation

associated

with maintenance

and problem investigation activities

listed below to verify compliance with regulatory requirements,

compliance

with administrative

and maintenance

procedures,

required quality

assurance/quality

control department

involvement,

proper

use of safety tags,

proper equipment

alignment

and use of jumpers,

personnel

qualifications,

and

proper retesting.

Specifically, the inspector witnessed

portions of the following maintenance

activities:

Unit

1

~ Diesel

Engine Generator

Inspection

(18-Month interval)

~ Inspection/Replacement

of 480 Volt Bus

G Insulators

~ IY-13 Cable Installation

and Termination

Unit 2

~ Replacement

of Safety Injection Vent Line

~ FCV-439 Motor Operator Inspection

~

EDG 2-1 Postmaintenance

Test

(PMT 27.21)

4. 1

Inverter IY-13 Installation

On April 4,

1994, during review of a work order which included connection of

wiring associated

with Inverter IY-13, the inspector noted that the foreman

verification of the clearance

had not been

signed for more than

1 week after

the start of the work,

and subsequent

work order steps

had

been performed.

The inspector questioned

the foreman in charge of the work, who indicated the

signature

should

have

been

made prior to starting the work.

Subsequent

review

of the work package

revealed that the foreman back-dated

his signature for

having verified the clearance

to March 26,

1994,

although the work order step

was signed

on April 4,

1994.

Discussions with licensee

management

revealed

that this situation did not meet their expectations.

The management,

however,

indicated that the foreman stated that

he had verified the clearance

prior to

starting the work and

had not signed the work package

at that time.

The inspector also inquired of the foreman

when the work was scheduled

to be

completed.

The foreman indicated that the work should

be completed within the

next several

hours.

While reviewing the work package,

the inspector

noted

that

a significant number of steps

had not been

signed

as complete.

The

inspector questioned

the foreman concerning

the lack of signatures.

The

0

-13-

foreman indicated that most of the work had

been

completed

but not signed for

and that

he was in the process of verifying the work which had

been

performed

by the other shift.

The inspector raised

the concern to licensee

management

regarding the lack of discipline of the involved workers in that they were not

completing sign-offs for their work as work was completed.

Additionally,

later review by the inspector

found that the dates for some of the recently

signed

steps

had

been

back-dated

to an earlier time.

The inspectors

were concerned that construction

workers

had not under stood

management

expectations

that steps

would be signed off as

soon

as they were

completed,

and dated

on the date they were signed,

rather than allowing steps

to be signed

days later

and dated

back to the date the step

was completed.

Licensee

management

expressed

concern that workers

had not understood

these

expectations,

particularly in light of past procedural

compliance

issues.

On

April 7,

1994,

a bulletin was issued to all nuclear construction

services

personnel

outlining the expectations

that steps

would be signed

and dated

as

soon

as practicable

upon completion of the step,

as well as the potential

safety

and work control

consequences

associated

with improper completion of

sign-offs.

The inspectors

questioned

whether the plant maintenance

personnel

were also fully aware of these expectations.

The licensee

stated that the

contents of the bulletin would be discussed

with plant maintenance

personnel

as well as construction

personnel.

These actions

adequately

addressed

the

inspector's

concerns.

4.1.1

Safety Significance

There is no safety significance specifically- associated

with the lack of a

signature for the clearance verification step,

since the

same clearance

number

and clearance

points

had

been

used to remove the old inverter,

IY-13, and the

step in that work order which required the foreman to walk down the clearance

had

been

perFormed

and signed

as complete at the start of the work.

The

construction

crew was

aware of that the

same clearance

was being

used in the

installation of the

new inverter.

4.1.2

Conclusion

The licensee

had not clearly conveyed expectations

associated

with timely sign

off and correct dating of work order steps.

Although the construction

work in

the field appeared

to have

been properly completed,

the inspector

identified

a

case of lack of sign off of a step

and late sign off and back-dating of some

steps of a work order which replaced

a safety-related

inverter.

The licensee

actions in response

to the concern

appeared

appropriate.

The safety

significance of these

specifsc findings was negligible, since work appeared

to

have

been

completed appropriately

and the identical sign off in a separate

work order referring to the

same clearance

had

been signed

by the foreman.

-14-

4.2

Re 1acement of Safet

In'ection

SI

Accumulator 2-3 In'ection Vent Line

On March 31,

1994,

the inspector

reviewed operator logs

and interviewed the

shift supervisor following an unexpected

delay in the work schedule for the

replacement

of SI Accumulator 2-3 vent line.

The Shift Supervisor indicated

that the delay was caused

in part by the concern for hydrogen off-gassing

in

the

RCS and, later,

by presence

of a vacuum in the vent line which was

observed after removal of the vent line pipe cap.

The delay was

due to

concerns

regarding the potential for introduction of material into the

RCS

while the pipe was being cut with the presence

of a vacuum in the pipe.

Subsequent

discussion

with the Directors of the Operations

and Mechanical

Maintenance

Departments

revealed that no clearance

had

been

used to perform

the leak repair.

A clearance

had been written by the work planning group for

the performance of the work but was not used.

The decision to not implement

a

clearance for performance of the work was

made at the prejob briefing by

Operations

Department

personnel.

This is

a violation of the work procedure.

The Operations

and Mechanical

Maintenance

managers

said that the decision to

not set the clearance

was based

on concern

over disturbing the failed weld for

analysis.

As a result, residual

heat

removal

{RHR) cold leg injection to

Loops

3 and

4 was not isolated

from the maintenance

area

and flow past the

safety injection pipe penetration

created

a vacuum in the vent line.

An additional

concern

over the need to purge hydrogen from the vent line had

been raised at the prejob briefing.

Individuals in the prejob briefing

decided to remove the hydrogen

from the line by establishing

an inert gas

purge prior to cutting the pipe.

The use of a nitrogen purge

was then

discussed

with the Mechanical

Maintenance

manager

and agreed

upon.

Subsequent

to the discussion,

personnel

involved with the work decided to use

argon

as

the purge gas.

Argon was readily available,

since it was planned to be used

as

a cover gas during the welding,

and necessary

hoses

and regulators

were

already

staged

at the work site.

Management

was not consulted following the

decision to use

argon vice nitrogen

as the purge gas.

The argon purge

equipment

was connected

and purging was

commenced

at

a rate of 50 cubic feet

per hour.

No instructions specifying the use,

connection,

or removal of argon

purge equipment

were issued.

After purging argon for approximately

40

minutes,

the welding personnel

questioned

the continued existence of a

negative

pressure

in the vent line and contacted

operations

personnel

to

investigate.

Operations

personnel

then told the welders to secure

the purge

and investigated

the cause of the

vacuum in the line.

It was determined that

Loop

3

RHR flow past the SI pipe connection

was creating the negative

pressure

in the vent line.

Valve RHR-2-8809B, which was initially planned to be shut

in accordance

with the unimplemented

clearance,

was then shut.

This secured

RHR flow to Loops

2 and

3 and eliminated the

vacuum in the vent line.

Work to

replace

the vent line was then

resumed.

During restart operations,

removal of argon from the

RCS was performed

by

filling and venting the volume control tank.

-15-

4.2.1

Conclusion

Investigation of the work activities revealed that there

was confusion over

the maintenance activity requirements

in several

areas

which contributed to

failure to set the proper clearance

for the work and the improper use of argon

as

a purge gas.

In cases

where

a purge is required,

the work order normally

specifies

the installation

and removal of purge equipment.

The inspector

questioned

the lack of a clearance

and the adequacy of both the planning

and

the procedures

for performing the work.

Personnel

involved in the decision to

use

argon

as

a purge

gas were not aware of the potential radiological

consequences

due to the high energy activation of argon after it is exposed

to

a neutron flux.

The failure of the licensee

to implement the required clearance,

thus allowing

argon

gas into the

RCS,

was

a violation of TS 6.8. I, which requires that

procedures

be implemented for the

recommended

processes

of Regulatory

Guide 1.33.

Regulatory

Guide 1.33,

paragraph 9.a.,

recommends

that procedures

associated

with maintenance

of equipment

important to safety

be properly

preplanned

and controlled (50-323/94-11-01).

5

SURVEILLANCE OBSERVATIONS

(61726)

Selected

surveillance tests

required to be performed

by the

TS were reviewed

on

a sampling basis to verify that:

(1) the surveillance tests

were correctly

included

on the facility schedule;

(2)

a technically adequate

procedure

existed for performance of the surveillance tests;

{3) the surveillance tests

had

been

performed at

a frequency specified in the Technical Specifications;

and

{4) test results satisfied

acceptance

criteria or were properly

dispositioned.

Specifically, portions of the following surveillances

were observed

by the

inspector

during this inspection period:

Unit

1

~ Reactor Cavity Hanipulator Crane

~ Diesel

Generator

Radiator Air Flow

Unit 2

~ Control

Room Ventilation Functional

Test

5. 1

Surveillance of Reactor Cavit

Mani ulator Crane

During routine inspection activities, the inspector

reviewed documentation

of

replacement

of several

relays in the motor circuitry of the refueling

manipulator crane

(WO C0121933).

Although the crane is not safety related, it

is controlled

by TS,

and it's function of lifting and moving reactor fuel is

important to safety.

The inspector questioned

whether the crane

had

been

returned to service without performance of a formal surveillance test.

After

completion of relay replacement,

the crane

vendor

and reactor engineers

had

informally performed parts of an integrated

crane

performance test,

Procedure

STP H-27,

"Fuel Handling System Interlock Verification and

Functional Test,"

and maintenance

personnel

had performed required

postmaintenance

testing of the relay circuity and motor circuits.

Reactor

engineers

and engineering

management

explained that,

since

none of the relays

associated

with the

TS required overload

and underload circuitry (associated

with fuel lift) had

been replaced,

the operability of the crane did not

require formal surveillance testing.

Surveillance Test N-27 was performed in

a formal manner later,

as

a conservative

measure.

The inspector identified that the formality of the control of crane

operability was less

than desirable,

since the clearance

to remove the crane

from service for relay replacement

had referenced

the

TS surveillance test,

performed several

days earlier

on the

TS underload

and overload interlock

circuits,

as the basis for returning the crane to operable

status after the

relay replacement.

This was not appropriate

documentation

of equipment

oper ability, and engineering

management

agreed that proper formal

documentation of operability would be discussed

with engineering staff.

An additional

concern

was identified by the inspector.

During preparation of

some work orders, identification of applicable

postmaintenatrce

surveillance

test requirements

may be inadequate.

Planners

determine

the need for a

surveillance test

by determining if the equipment is safety related or listed

in Equipment Control Guidelines,

developed for administrative control of

important equipment

which is not listed in TS.

The inspector pointed out that

surveillance

requirements

for equipment

which is not safety related but is

included in TS would not be readily identified.

The licensee

acknowledged

this vulnerability,

and documented this in an action request,

for correction,

5. 1. 1

Conclusion

The Reactor

Engineering evaluation of the

TS requirements

and the effect of

the maintenance

on the reactor cavity manipulator crane operability appeared

to be technically adequate,

although the formality of documentation

was not in

accordance

with management

expectations.

6

SAFETY SYSTEM WALKDOWN, 125

V DC SYSTEM

(71710)

The inspector reviewed the Final Safety Analysis Report,

TS,

and design

control

memorandum

(OCN S-67) ensuring there

was consistency

between

the

different documents.

TS surveillance

requirements

were reviewed along with

the surveillance

procedures

which accomplished

them.

The modifications to the

125

V DC system being performed during the Unit I outage

were discussed

with

the system engineer

concerning

the scope of the modifications, alternate

power

supplies,

and the changes

to emergency

procedures

associated

with the

modifications.

One administrative discrepancy

was found wher e the design

control

memorandum

referenced

a

TS table which did not exist.

This

discrepancy

was pointed out to the licensee.

The licensee initiated an action

-17-

request

to track correction of the deficiency.

Inspectors

walked down safety-

related

125

V DC circuitry in Unit

1 containment

and in the auxiliary building

to evaluate

the condition

and locations of selected

125

V DC circuitry.

The

inspectors

performed

a visual inspection of the internals of two battery

chargers

and

a

125

V DC distribution panel.

No deficiencies

were noted.

6. 1

Conclusion

The

125

V DC system

appeared

to be in good order

and the system engineer

appeared

knowledgeable.

7

PREPARATIONS

FOR REFUELING

(60705)

The inspectors

reviewed the licensee's

preparations

for refueling to determine

if adequate

safety

and procedural

control

was properly implemented

in

preparation for refueling.

The inspectors

examined surveillance test

completion,

equipment

checkouts,

fuel handling

and inspection operations,

shift manning requirements,

crew briefings, prerequisite lists,

outage safety

planning, control of reactivity, quality oversite

involvement,

and other

areas.

The inspectors

also examined preparations

for fuel movement in the

containment refueling areas,

the fuel handling building,

and the control room.

The licensee

procedures,

outage planning,

and training addressed

control of

reactivity, fuel inventory,

movement of fuel modules,

communications

between

refueling crew, control

room crew, fuel handling building crew and reactor

engineering monitors.

The engineering

and control

room staff had

been trained

and appeared

to have the tools to maintain rigorous control of the observed

evolutions.

7. 1

Conclusion

The preparations

for refueling appeared

well planned

and appropriate.

8

REFUELING OPERATIONS

{60710)

8. 1

Overview

The inspectors

observed refueling operations

to evaluate

the control of fuel

modules

and reactivity, refueling equipment operability, effectiveness

of

procedures

and communications,

and overall safety of fuel manipulations

and

reactivity control.

All of these

areas

appeared

to be effectively

implemented.

8.2

Nonconservative

Fuel Handlin

Practices

In one instance,

when

a fuel module was being loaded into Core Location F-8

with difficulty, a reactor

engineer

observed

the refueling crew place the

difficult module to the side

and place

a different fuel module in Core

Location F-8, to determine if the original module

was

bowed.

The reactor

engineer

immediately identified that,

by procedure,

no module

may be loaded

into

a location next to other modules

unless it is in that module's final core

0

-I8-

location.

Additionally, the reactor engineer identified that the control

room

had not been

informed that the

new module

was to be tried in Core

Location F-8, which was

a violation of the intent of the procedure to have the

control

room staff aware at all times of what fuel module moves were to occur.

These

concerns

were promptly documented

in Action Request

336402.

It was later discovered that the refueling crew in containment

had discussed

the

use of the next fuel module

as

a test for a bowed module

and determined

that placement of the fuel in Core Location F-8 would not violate intent of

the refueling procedure,

since the module would not be loaded,

since it would

not be unlatched.

The refueling crew was

aware that the reactivity control of

this temporary module configuration

was within TS and

bounded

by core

analysis,

assuming

the existing boron concentration of the refueling cavity.

The inspector discussed

the fuel movement issue with reactor engineering

management,

who considered that the refueling crew should

have informed the

control

room of the intended

movements of fuel, regardless

of the intent to

not unlatch the module in Core Location F-8.

Also, licensee

management

considered

that

a dummy module should

have

been

used rather than

a new fuel

module to test for bowed fuel to minimize the chance of damage to fuel

modules.

The movement of the

new fuel to Control Location F-8 determined that the

module

was not bowed.

Core alterations

were halted,

and closer inspection

found

a I/O-inch fastener

on the lower core plate which had interfered with

fuel alignment.

The fastener

was retrieved,

and inspection for additional

foreign material

was conducted.

No additional material

was identified.

The

fastener

was activated,

indicating that it had

been irradiated for at least

one cycle.

The licensee

concluded that

no fastener

of this design

was

used in

any safety-related

application,

and it had not detached

from reactor coolant

system internals.

The identification of the source of the fastener is

continuing.

8.2. 1

Conclusion

The safety significance of the placement of fuel in Core Location F-8 was

minimal, since the reactivity analysis

was bounded,

and the refueling crew was

fully aware of the negligible reactivity consequences

of this. fuel movement.

Though licensee

management

expectations

for communications

and control of fuel

movement

and

use of dummy modules to minimize the chance of fuel

damage

were

appropriate

and were communicated

to refueling crews,

the crew did not meet

these

expectations.

The resolution of the fastener

on the core support plate

was being resolved appropriately.

8.3

Conservative

Res

onse to Elevated

Counts

on

a Source

Ran

e Channel

On two occasions

the inspector

observed

licensee

operations

personnel

suspend

refueling operations

due to elevated

counts

on one of the source

range nuclear

instrumentation

channels.

Refueling operations

in both instances

remained

secured until the source

range

channel

level returned to its reference level,

0

-19-

in agreement

with the other channel.

The licensee initiated actions to

determine

and resolve the cause of the elevated

counts in both instances.

The

signal

on the source

range circuit appeared

to have

been

low level electrical

interference.

However,

core alterations

were not resumed until the circuit

was clear.

8.3. I

Conclusion

The response

to elevated

counts

on

a source

range

channel

during refueling

operations

was conducted

in an appropriately conservative

manner.

9

OUALITY OVERSITE

(40500)

The inspector reviewed findings of quality oversite group audits

and

surveillances

to determine if the audits were sufficiently probing

and

implemented conservative

safety expectations.

Separate

issues

are discussed

below.

9. I

Snubber

Ins ections

During an audit of snubber inspections,

the licensee quality organization

identified that

some

snubbers

had not been visually inspected

as required

and

had

been declared

operable without conclusion of the visual portion of the

inspection,

without signing off the step requiring completion of the visual

inspection.

The corrective action involved completing visual inspection

and

counseling

mechanical

maintenance

management

and staff on proper documentation

and completion of safety-related

work.

No significant safety issues

were

identified.

9.2

Refuelin

Crew Activities

A quality oversite surveillance identified that the refuelling crew involved

in the improper location of the fuel module in the core location, discussed

earlier,

had also

been involved in the lack of proper foreign material

exclusion postings described

in an earlier report

and in

a miscommunication

regarding identification of specific fuel module designations

during receipt

inspection fuel handling.

Further review of the root cause of the

communication

issues

was initiated

by the Independent

Safety Engineering

Group

to determine if a

common thread

and corrective action could be identified for

this refueling crew.

9.3

Motor-0 crated

Valve Motor Pinion

Ke

Ins ections

An operability assessment

was issued to address

a

10 CFR Part 21 identified

vulnerability in motor-operated

valves in which motor pinion keys

may not have

been properly installed.

The Plant Staff Review Committee

and the Independent

Safety Engineering

Group identified that the scope of inspection of valves

and

the identification of vulnerability of specific valves

was not conservatively

addressed

in the evaluation.

Subsequent

inspections

and discussions

with

licensee

management

resulted

in additional

valves being inspected,

and

one

key

0

-20-

was found operable

but improperly installed in a valve inspected

as

a result

of the quality group's

involvement.

9.4

Ins ection for Crackin

of 480

V Transformers

The potential for cracking of insulators

in 480

V transformer s was identified

and inspections

were conducted.

The guality Control staff identified that,

because

of mechanical

interferences

and minor accumulated

dust,

the

inspections

could be conducted without adequate visibility to identify

cracking

on the top and sides of the insulators.

Intrusive involvement by gC

resulted

in removal of the layer of dust

and improving the visibility of the

insulators.

Further involvement by the

NRC regarding crack acceptance

criteria,

and lack of identification of potential root causes

for the

cracking,

led to Engineering performing

a calculation concluding that the

insulators

were sufficiently supported to perform their safety function under

design basis conditions despite

the cracks.

9.5

Tem orar

Attachments in Containment

During an audit of containment

work practices,

guality Assurance staff noted

that several

temporary attachments,

such

as electrical

extension

cords,

service air,

and other temporary service connections

not being properly

attached to supports

and attached

to inappropriate

supports,

such

as

instrumentation lines

and other plant equipment.

The guality Assurance staff

took steps to identify improperly routed attachments

and informed the work

crews

and applicable

management

of the improper practices.

This resulted in

correction of improper work practices

and re-emphasizing

management

expectations

regarding

work in containment.

9.6

Conclusion

Each of these

issues

were of low safety significance.

However, the

involvement of quality oversite groups

was intrusive, timely,

and

conservative.

Corrective action appeared

timely and commensurate

with safety

significance.

As

a result of involvement

by the quality groups,

the safety

performance of the plant was improved.

10

FOLLOWUP ON CORRECTIVE ACTIONS FOR VIOLATIONS

(92901)

)0. 1

Closed

Violation 275 93-32-01

Failures to Follow Procedures

The

NRC identified four instances

of the licensee's

failure to follow

procedures,

which was issued

as

a citation with NRC Inspection

Report 50-275/93-32.

In a letter dated

February 4,

1994, the licensee

acknowledged

the violation and stated that corrective action

had

been

completed for the specific violations cited

and that corrective action

had

been initiated for the overall

concern of failure to follow procedures.

For

each of the specific instances

of failure to follow procedures,

the licensee

documented

actions which addressed

the concern.

The licensee

stated that

these

actions

would correct the identified violation and help preclude future

-21-

violations.

The inspector

reviewed

and verified these

actions.

The

licensee's

actions

appeared

to be appropriate

and properly implemented.

ll

IN-OFFICE REVIEW OF LICENSEE EVENT REPORTS

(90712}

The following licensee

event reports

were closed

based

on in-office review:

~

275/94-04,

Revision

0

Main Steam Safety Valves Outside Design

Bases

Due to Vendor Identified Deficiency

~

275/94-05,

Revision

0

Failure to Control Reactor

Vessel

Inventory During Draindown

Due to

Personnel

Error

ATTACHMENT 1

1

PERSONS

CONTACTED

l. 1

Licensee

Personnel

G.

H.

Nucl

J.

D.

Cany

W.

H.

Tech

  • R. P.
  • J. S.
  • G. H.

R.

N.

  • W. G.

S.

R.

"R. D.

  • T. L.
  • B. W.

P.

B.

  • C. R.
  • J. A.

R.

W.

  • J.

R.

  • K. A.

M. E.

  • D. B.
  • J f
  • T. A.

P. T.

D.

H.

  • S.

R.

P.

G.

R. A,

  • J ~ A.

D.

P.

  • D. A.

E.

R.

1.2

NRC Personnel

Rueger,

Senior Vice President

and General

Manager,

ear

Power Generation

Business

Unit

Townsend,

Vice President

and Plant Manager,

Diablo

on Operations

Fujimoto, Vice President,

Nuclear

nical Services

Powers,

Manager,

Nuclear guality Services

Bard, Director, Mechanical

Maintenance

Burgess,

Director,

Systems

Engineering

Curb,

Manager,

Nuclear Technical

Services

Crockett,

Manager,

Technical

and Support Services

Fridley, Director, Operations

Glynn III, Supervisor,

guality Assurance

Grebel,

Supervisor,

Regulatory Compliance

Giffin, Manager,

Maintenance

Services

Grable,

Engineer,

Mechanical

Maintenance

Groff, Director, Plant Engineering

Hays, Director, Onsite guality Control

Hess, Assistant Director, Onsite Nuclear Engineering Services

Hinds, Director, Nuclear

Safety Engineering

Hubbard,

Engineer,

Regulatory

Compliance

Leppke, Assistant

Manager,

Technical

Services

Hiklush, Operations

Manager,

Acting Plant Manager

Holden, Director, Instrumentation

and Controls

Houlia, Assistant to Vice President,

Plant Management

Nugent,

Engineer,

Regulatory Compliance

Oatley, Director, Materials Services

Ortore, Director, Electrical Maintenance

Sarafian,

Senior Engineer,

Nuclear guality Services

Savard,

Director, Technical

Services

Shoulders,

Director, Onsite Nuclear Engineering Services

Sisk, Senior Engineer,

Regulatory

Compliance

Taggart, Director, Onsite guality Assurance

Willis, Engineer,

Mechanical

Haintenance

  • M. Hiller, Senior Resident

Inspector

H. Tschiltz, Resident

Inspector

J. Winton,

NRR Inspector Intern

In addition to the personnel

listed above,

the inspectors

contacted

other

personnel

during this inspection period.

  • Denotes personnel

that attended

the exit meeting.

2

EXIT MEETING

An exit meeting

was conducted

on April 22,

1994.

Ouring this meeting,

the

inspectors

reviewed the scope

and findings of the inspection.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to,

or reviewed by,

the inspectors.

0

ATTACHNENT 2

ACRONYNS

CVCS

EDG

LLRT

RCS

SI

TS

Chemical

Volume and Control

System

emergency

diesel

generator

Local

Leak Rate Test

Reactor Coolant System

safety injection

Technical Specifications