ML16342A516

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 940320-0423.Violation Noted:Valve SI-2-8809B Was Not Shut Prior to Initiating Repair Work & Argon Purge Was Connnected to Safety Injection Line W/O Use of Work Controls
ML16342A516
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/19/1994
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342A515 List:
References
50-323-94-11, NUDOCS 9405250013
Download: ML16342A516 (4)


Text

APPENDIX A NOTICE OF VIOLATION Pacific Gas and Electric Company Diablo Canyon Unit 2 Docket:

50-323 License:

DPR-82 During an NRC inspection conducted from Parch 20 through April 23,

1994, a

violation of NRC requirements was identified.

In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions,"

10 CFR Part 2, Appendix C, the violation is listed below:

Diablo Canyon Technical Specification 6.8. 1 states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2, dated February 1978.

Appendix A of Regulatory Guide 1.33, Revision 2, recommends procedures for performing maintenance that can affect the performance of safety-related equipment be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

1.

Clearance 00044155 was written by the work planning group to be used during the repair of the leak on the Unit 2 reactor coolant system safety injection inlet to Loop 2-3.

The clearance required that Valve SI-2-8809B be closed during the repair of the leak.

Contrary to this requirement, on Harch 31, 1994, while establishing conditions to perform the repair of the leak, the clearance was not followed in that Valve SI-2-8809B was not shut prior to initiating the repair work.

Additionally, an argon purge was connected to the safety injection line without the use of work controls.

The combination of these two occurrences resulted in approximately 50 cubic feet of argon being injected into the reactor coolant system, which could have resulted in elevated reactor coolant system radiation levels.

This is a Severity Level IY violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Pacific Gas and Electric Company is hereby required to submit a written statement or explanation to the U.S.

Nuclear Regulatory Commission, ATTN:

Document Control

Desk, Washington, D.C.

20555 with a copy to the Regional Administrator, Region IV, and a copy to the NRC Resident Inspector at the facility that is the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice).

This reply should be clearly marked as a "Reply to a Notice of Violation" and should include for each violation:

(1) the reason for the violation, or, if contested, the basis for disputing the violation, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved.

If an adequate reply is not received within the time specified in this Notice, an order or a Demand for 94052500i3 940519 PDR ADOCK 05000275 Q

PDR

Information may be issued to show cause why the license should not be

modified, suspended, or revoked, or why such other action as may be proper should not be taken.

Where good cause is shown, consideration will be given to extending the response time.

Dated at Arlington, Texas, thisy~day af 4