ML16341G400

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Insp Repts 50-275/91-37 & 50-323/91-37 on 911010-1118.No Weaknesses Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events & Selected Independent Insp Activities
ML16341G400
Person / Time
Site: Diablo Canyon  
Issue date: 12/13/1991
From: Morrill P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341G401 List:
References
50-275-91-37, 50-323-91-37, NUDOCS 9112310011
Download: ML16341G400 (30)


See also: IR 05000275/1991037

Text

U.

S

NUCLEAR REGULATORY

CONN'ISSION'EGION

V

Report

Nos:

50-275/91-37

and 50-323/91-37

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80

and

DPR-82

Licensee:

Facility Name:

Pacific

Gas

and Electric Company

77 Scale Street,

Room 1451

San Francisco,

California 94106

Diablo Canyon Units

1

and

2

Inspection at;

Diablo Canyon Site,

San Luis Obispo County, California

r

Inspection

Conducted:

October

10 through

November

18,

1991

Inspectors:

H. Mono, Senior Resident

Inspector

Ni. Miller, Resident

Insp ctor

Approved by:

.. or

~

,

ref,

eactor

rogects

ect>on

A

/@ /3/~/

ate

>gne

Summary:

Ins ection from October

10 throu

h November

18

1991

Report

Nos.

50-275/91-37

and 50-323/91-37

~dd:

d

d

d

dd

operations,

maintenance

and surveillance activities, follow-up of onsite

events,

and selected

independent

jnspection activities.

Inspection

Procedures

TI 2515/101,

TI 2515/103,

41500,

61726,

71707,

62703,

71710,

and

93702 were

used

as guidance

during this inspection.

Safet

Issues

Nanaoement

S stem

SINS) Items:

The licensee's

responses

to

Generic Letter 88-17 were reviewed.

Temporary Instructions

2515/101

and

2515/103

were closed

(Paragraph

9).

Results:

General

Conclusions

on Stren ths

and Weaknesses:

The licensee's

startup

testing

o

Unct

was per

orme

wst

good coor ination

and communications

between engineering

and operations

personnel.

Nanaoement

involvement in the

testino

was evident.

Detailed tai lboards

were performed to assure

that those

involved understood

the tests.

No .significant weaknesses

were identified.

9f f23j00f j 9j f~j3

PDR

ADQCK 05000~75

G

PDR

Si nificant Safet

Matters:

None.

Summary of Violations and Deviations:

None.

0 en Items

Summar

One

new open item;

no items closed.

0

DETAILS

Persons

Contacted

  • J.

D. Townsend,

Vice President,

Nuclear

Power Generation

8 Plant Manaoer

Diablo Canyon

Power Plant

~D. B. Niklush;- Manager,

Operations

Services

  • N. J.

Angus,

Yianager, Technical

Services

B.

W. Giffin, Manager,

Maintenance

Services

  • D. H. Oatley,

Nanager,

Support Services

W. G. Crockett,

Instrumentation

and Controls Director

  • W. D. Barkhuff, Quality Control Director
  • R. P. Powers,

Nechanical

Maintenance

Director

D. A. Tagoart,

Director Quality Performance

and Assessment

T; L, Grebel,

Regulatory Compliance Supervisor

H. J. Phillips, Electrical Maintenance Director

  • J. A. Shoulders,

Onsite Project Engineering

Group Manager

S.

R. Fridley, Operations

Director

R.

Gray, Radiation Protection Director

J.

V. Boots,

Chemistry Director

  • J. J. Griffin, Senior Engineer,

Regul.atory Compliance

D. K. Cosgrove,

Safety

and

Emergency Services

Supervisor

R.

W. Hess,

Assistant Onsite Pro'ject Engineer

~i. B. Hock, Nanager,

Nuclear Safety

and Regulatory Affairs

  • T. A. Moulia, Assistant

to Vice President

Operations

J.

N. Welsch, Operations

and Engineering Training Supervisor

R.

P. Flohaug,

Senior Quality Assurance

Supervisor

  • Denotes those

attending

the exit interview.

The inspectors

interviewed several

other licensee

employees

including

shift supervisors,

shift foremen, reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

and quality

assurance

'personnel.

2.

Operational

Status of Diablo Can

on Units

1

and

2

Unit

1

was at

100K power for essentially

the entire inspection period,

with the exception of

a few days

(November

2-5

and 9-10,

1991).

During

those periods reactor

power

was reduced

to 50K to perform cleaning of

the circulatino water tunnels.

Unit 2 started

the inspection period in Node

5 (refueling 'outage

2R4),

and the reactor

was brought critical on October 20.

Full power was

reached

on October

31.

This was the shortest refueling outage

in Diablo

Canyon history.

Unit 2 continued

at

100K power for the remainder of the

inspection period.

0

On November

12,

1991,

at 2,00 p.m.,

an Unusual

Event

was declared

by

licensee

personnel

due to

a grass

and brush fire within the site boundary

which required offsite assistance.

At. 10:00 a.m..that

day, licensee

personnel

workino with personnel

from the California Department of

Forestry started

a "controlled" burn of brush

and grass

in

a hilly area

outside the plant protected

area,

but within the site boundary.

At

approximately ]:30 p.m., higher than expected

winds caused

the fire to

iump across

the fire break lines.

Addit,ional equipment

from the

California Department of Forestry

was requested.

The California

Department of Forestry provided

an airplane to drop fire retardant,

a

helicopter to drop water, additional fire engines

and bulldozers,

and

additional

crews.

At approximately 4:00 p.m.

on November ]2, 199], the

fire was declared

out.

The

Unusua'1

Event was terminated

at 4:03 p.m..

The fire burned

an additional

7 acres

beyond the

25 acres orioinally

planned.

Plant equipment,

structures,

and transmission

lines were not in

jeopardy.

The

NRC inspector monitored the licensee's

response

to the

event

and determined that the control

room personnel

were maintaining

close

communications

with the fire marshal

overseeing

the fire fighting

activities.

No violations or deviations

were identified.

4.

0 erational

Safet

Verification

71707)

a.

General

Durino the inspection period,

the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on

a daily, weekly, or monthly basis.

On

a daily

basis,

the inspectors

observed

control

room activities to verify

compliance with selected

Limiting Conditions for Operations

(LCOs)

as prescribed

in the facility Technical Specifications

(TS).

Logs,

instrumentation,

recorder traces,

and other operational

records

were

examined

to obtain information on plant conditions

and to evaluate

trends.

This operational

information was then evaluated

to

determine if regulatory requirements

were satisfied.

Shift

turnovers

were observed

on

a sample

basis

to verify that all

pertinent

information of plant status

was relayed to the oncoming

crew.

During each

week, the inspectors

toured the accessible

areas

of the facility to observe

the following:

(a)

General

plant

and equipment conditions

(b)

Fire hazards

and,fire fighting equipment

(c)

Conduct of selected

activities for compliance with the

licensee's

administrative controls

and

approved

procedures

(d)

Interiors of electrical

and control panels

(e)

Pl ant housekeeping

and cleanliness

(f)

Engineered

safety feature

equipment

alignment

and conditions

(g)

Storage

of pressurized

gas bottles

The inspectors

talked with operators

in the control

room .and other

plant personnel.

The discussions

centered

on pertinent t4pics of

'eneral

plant conditions,

procedures,

security, training,

and other

aspects

of the work activities.

During these plant .tours the

NRC inspector

noted

on two occasions

that extension

cords

had

been routed into the Unit 2 diesel

generator

room through the ventilation openings

from the outside.

These extension

cords

appeared

to be associated

with construction

activities for the installation of the sixth dies'el

generator.

In

one case,

the extension

cord had

been

plugged into

a wall outlet,

and the extension

cord was run through the

CO

suppression

system

rolldown door area

and near the diesel fuel o)1 transfer switches.

The inspector

was concerned

that the extension

cords might present

a

fire hazard

or reduce

the effectiveness

of the

CO

suppression

system.

When this concern

was brought to the licfnsee's

attention,

the extension

cords were'removed.

The

NRC inspector

also, noted that the seal

on the handwheel for

manual

valve 8728B (Unit

1 residual

heat

removal

pump 1-2 discharge

valve)

was missing with the valve in its required

open position.

Licensee

personnel

subsequently

reattached

the seal.

Based

on this

finding and other licensee findings of missing seals,

the licensee

performed

a verification of approximately

100 sealed

valves

(approximately

30K of the total

number of sealed

valves)

and found

no additional

cases

of missing seals.

b.

Radiolo ical Protection

c ~

The inspectors

periodically observed

radiological protection

practices

to determine

whether the licensee's

program

was being

implemented

in conformance with facility policies

and procedures

and

in compliance with regulatory requirements.

The inspectors verified

that health physics supervisors

and professionals

conducted

frequent

plant tours to observe activities in progress

and were

aware of

significant plant activities, particularly those related to

radiological conditions

and/or challenges.

ALARA considerations

were

found to be

an integral part of each

RWP (Radiation

Work Permit).

Ph sical Securit

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures,

including vehicle

and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area inteority.

Exterior lighting was

checked

during backshift inspections.

No violations or deviations

were identified.

~

~

5.

Onsite Event Follow-up (93702

a.

Missed Containment

Atmosphere

Sample'- Unit

1

On November 3,

1991,

at .2:00 a.m.,

licensee

personnel

idgntified

that manual

containment

atmosphere

samples

had not been Properly

taken

as required

by Technical Specifications

(TS) in that the

manual

samples

were drawn using

a sample cart

when the containment

isolation valves

were closed.

A representative

sample of the

containment

atmosphere

could riot be obtained with the containment

isolation valves closed.

Containment isolation valves

FCV-678, 679,

and

681 were closed

due to work being performed

on the containment

particulate

and

gas radiation monitors

and

on the sample

pump

associated 'with the monitors.

TS 3.4.6.1'specifies

that

when

a containment

atmosphere

monitor is

inoperable,

plant operations

may continue for up to 30 days

as long

as

manual

samples

of the containment

atmosphere

are taken

and

analyzed

every

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

If manual

samples

are not obtained,

the

TS

specifies that the plant should

be shut

down to hot standby

conditions within the next six hours

and to cold shut

down

conditions within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The containment

isol'atioh

valves

were closed

on November

1 at approximately 4:50 p.m.

and

based

on the results of containment

atmosphere

tests,

the licensee

has concluded that the last valid sample

was

drawn

on November

2 at

12:40 a.m..

When subsequent. manual

containment

atmosphere

samples

were drawn

on November

2

and 3, the containment isolation valves

were apparently closed

(based

on the sample results

showing

no

activity).

Therefore the samples

did not represent

containment

atmosphere.

Procedures

specified that the containment isolation

valves

were to be verified to be open;

however, this

was not done.

Approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />

elapsed

between

when the last valid

containment

atmosphere

sample

was taken

and

when the closed

isolation valves

were identified and another valid sample taken.

The results of the samples

showed

acceptable

activity levels in

containment;

therefore,

there

was minimal safety impact

due to the

missed

sample.

However, this event revealed

several

weaknesses..

The operation of the manual

sampling

system

can allow

a

recirculation flow path to be established

such that

'a normal

sample flow rate is indicated

even with the containment

isolation valves closed.

Technicians

thought the isolation

valves

were

open

based

on the indicated flow rate

and did not

verify valve positions

although

procedures

specified that the

proper valve positions

be verified.

Subsequent

testing

by the

licensee

appears

to indicate that the recirculation flow is not

significant during operation of the manual

sample cart with the

containment isolation valves

open.

Technicians

who obtained

a sample

on November

2 at 12:47 p.m.

were not sensitive to the results

which showed

no activity.

This result

was not consistent

with past

samples

and could have

led to the earlier identification of the closed

containment

isolation valves.

0

Communications

between

operations

and chemistry/IEC were not.

adequate

to ensure that appropriate

compensatory

measures

were

taken

when the containment isolation valves for the, sample line

were closed.

The licensee's

evaluation of the event, is described

in NPR

DCI-91-TC-N098.

The licensee

has

concluded that this event is not

reportable.

The inspectors

concluded that this item was not

a

violation of the technical'pecifications

since

a valid sample

was

taken before the six hour action statement

would require

shutdown

to hot standby.

Steam

Introduced Into Nitro en

S stem Pi in

- Unit 2

During plant heatup of Unit 2 on October

15,

1991,

a

smoke detector

alarmed inside containment.

Upon investigation

by licensee

personnel,

the paint on nitrogen system piping in containment

was noted to be

smoking.

It was also noted that the nitrogen fill valves to steam

generator

2-2 (valves

2013

and 906) were open.

This allowed steam

at approximately

400 degrees

F and 400 psi from steam generator

2-2

to enter the nitrogen

system piping.

Licensee

personnel

closed

the

nitrogen fill valves to prevent further heatup of the piping.

The nitrogen line is used to provide

a nitrogen blanket for the

steam generators

during outages

and also provides

a backup method

for operating certain valves in the reactor coolant

letdown system.

The letdown system valves

are inside containment

and are normally

operated

by instrument air.

The nitrogen line is not used during

normal plant operations,

and its outboard

containment isolation

valve is sealed

closed.

The nitrogen fill valves

were manipulated

during system vent

and fill operations

and apparently

were not

restored

to the closed position.

The licensee

performed

a detailed

walkdown of the nitrogen

system

piping which included disassembly

of some piping connections

to

determine

the extent of steam

and water intrusion.

The piping

arrangement

in the plant apparently provided

a loop seal

which

prevented

water from reaching

solenoid valves for the letdown valve

actuators.

The licensee

evaluated

the impact of the elevated

temperature

and water intrusion

on the piping and components

in the

nitrogen

system

and determined that the event did -not significantly

damage piping or components

except

the nitrogen pressure

regulators.

The licensee

disconnec4ed

lines to pressure

regulator

5199

and also

capped

the nitrogen lines to the letdown valves to preclude similar

problems

in the future.

The lines were blown down to remove

any

remaining water.,

and the letdown valves

were cycled to assure

no

damage

was sustained.

The event

and evaluation

are described

in AR

A0248331.

The

NRC inspector

reviewed the licensee's

evaluations

and

had

discussions

with licensee

personnel.

The evaluation

appeared

to be

thorough

and complete.

Based

on inspector discussions,

.the

licensee

revised

procedure

AP-9, Loss of Instrument Air, 'to indicate

that the affected

letdown valves

were

no longer provided:.with

a

backup nitrogen supply in Unit 2.

The inspector

had

no further

questions

regarding this event.

No violations or deviations

were identified.

6.

Maintenance

62703)

The inspectors

observed

portions of,

and reviewed records

on, selected

maintenance

activities to assure

compliance with approved

procedures,

Technical Specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance

activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and 'replacement

parts

were appropriately

certified.

These activities include:

Work Order

R0096039 - Cleaning

CCW Heat Exchanger

2-1

Work Order R0071268 -

CCW

Pump 1-2 Oi 1

Sample

No violations or deviations

were identified.

7.

Surveillance

61726)

~

~a.

Observations

By direct observation

and record review of selected

surveillance

testing,

the inspectors

assured

compliance with TS requirements

and

plant procedures.

The inspectors verified that test

equipment

was

calibrated,

and acceptance

criteria were met or appropriately

dispositioned.

These tests

include:

STP M-15:

Integrated

Safeguards

Test

STP R-30:

Startup

From Refueling

( Initial Criticality)

STP R-6:

Low Power Physics Testing

OP L-2:

Hot Standby to Startup

Mode

TP T0-8902,

Rev.

1:

RHR Water

Hammer Testing

STP 1-2D:

Power

Range

Channel Calibration

'7

b.

Testino Auxiliary Feedwater

AFW)

S stem Valves

No

On October-27,

1991, the 'inspector

observed testing of Valves

associated

with the the turbine-driven auxiliary feedwater

(AFW)

system in Unit 2.

The testing

was performed.to obtain v/lve

performance

data in response

to

NRC Generic Letter 89-10.

This

testino

was performed during power operations

(at approximately

30K

power)

so that

steam would be available to run the turbine-driven

AFW pump.

Testing

was

implemented

by licensee

procedures

HP E-99.01,

Revision

0,

MOV Flow Test - TDAFW Flow Control Valves LCV-106, 107,

108,

and

109;

MP E-99.02, Revison',

MOV Flow Test - TDAFW Steam Supply

Valves

FCV-37, 38,

and 39;

and

STP P-6A, Revision 4, Performance

Test of Steam-Driven Auxiliary Feed Pump.'he

conduct of testing is

described

in procedure

NPAP C-3,

"Conduct of Plant

and Equipment

Tests."

The inspector

reviewed the test procedures

and concluded

that the procedures

appeared

to meet the requirements

of NPAP C-3.

The inspector

noted that the testing

appeared

to have

been

appropriately

controlled in that

a tai lboard discussion

was

conducted

both with the control

room staff and with technicians

stationed

at the valves.

Expected plant performance,

alarms,

and

test termination contingency actions

were discussed.

In addition,

a control

room shift change

was anticipated

and during the first

tai lboard discussion,

operators

determined

the appropriate

plant

conditions to suspend

testing during the shift change.

After the

shift change,

another tai lboard

was held with the

new shift which

reviewed the expected

plant performance,

alarms,

and test termination

contingency actions.

The inspector

observed that experience

gained

from earlier valve testing,

regarding minimizing plant transients,

was discussed

during each of the tailboard discussions.

A

representative

of licensee

management

wa's present

at each tailboard

discussion

and during the entire test evolution.

During the changes

in plant equipment status

and the resulting minor

plant transients,

operators

maintained stable plant conditions

and

coordination with 'technicians

at the valve stations.

Overall control

of testing

was effective

and

appeared

to maintain the priority on

safe operations.

The control

room operators

conservatively recognized

the need to

demonstrate

valve operability after the restoration of the system

back to original conditions

and cycled the -valves to demonstrate

operability.

violations or deviations

were identified.

8.

Enoineerino Safet

Feature

Ver ification

71710)

During this inspection period selected

portions of the containment

spray

system for Units

1

and

2 were inspected

to verify system configuration,

equipment condition, valve

and electrical

lineups,

and local breaker

positions.

violations or deviations

were identified.

8

9.

Loss of Deca

Heat

Removal

(Generic Letter 88-17)

(TI 2515/101

and T12

5

3

b.

Backaround

8

On October

17,

1988,

the

RRC issued'Generic Letter 88-17 .regarding

the potential

loss of decay heat

removal during nonpower operations.

This generic letter

was

due in part to

an event at Diablo Canyon in

April 1987 which highlighted previously unrecognized

concerns

associated

with reduced reactor coolant

system

(RCS) inventory

conditions.

As directed

by the generic letter, the licensee

responded

in submittals

dated

January

6, 1989, regarding expeditious

actions,

and

on February 6,

1989, regarding

proorammed

enhancements.

In addition,

the licensee

provided supplemental

responses

in letters

dated

January

17

and

Yiay 31,

1991.

NRC letters

dated April 26,

1989,

and August 22,

1991,

document

the completion of the

NRC's

review

and

acceptance

of the l,icensee's

responses.

Review

The

NRC inspector

reviewed the licensee's

responses

to Generic

Letter 88-I7 in accordance

with Temporary Instructions

2515/101

and

2515/103 to verify completion of the licensee's

actions

and to

verify that trainina

and procedures

were appropriate

to prevent

and

mitigate

a loss of decay heat removal.

Training lesson

plans

were

reviewed,

class

attendance

lists were checked,

and

a training video

tape

was reviewed.

The inspector

reviewed current plant procedures

and held discussions

with operations

personnel

to verify the

acceptability

of procedural

limitations, precautions,

and actions.

In general,

the licensee's

training

and procedures

were found to be

complete

and adequately

covered

the areas

specified in the generic

letter.

Because

of the licensee's

past

experience

with problems

when operating with

a reduced

RCS invenstory,

licensee

personnel

were

very sensitive to the potential

problems

and the

need for prompt

actions to limit any adverse

consequences;

The inspector verified that training had

been

conducted shortly,

after the April 1987 event at Diablo Canyon

and that reduced

RCS

inventory trainino continues

to be

a part of initial and

requalification trainino for licensed operators.

Specific training

in this

area

was conducted for licensed operators just prior to the

recent Unit

1 refueling outage

which occurred

in spring 1991.

In

addition, training of non-licensed

personnel,

such

as auxiliary

operators

and maintenance

personnel,

regarding

reduced

RCS inventory

operations

was also verified.

There

are

no specific administrative

provisions which require additional training prior to conducting

reduced

RCS inventory operations.

However,

based

on discussions

with licensee

personnel, it appears

that licensee

personnel

are

sufficiently sensitive to the potential

problems that the

need for

additional training would be considered

prior to actually or

potentially enterino

a reduced

inventory mode.

Such training

occurred prior to the Unit

1 refueling outage

in early 1991

even

thouoh reduced

inventory operations

were not planned.

Further

guidance

does

not appear to be necessary

at this time.

The inspector's

review of the applicable refueling,

abnormal

operating,

and administrative

procedures

showed that in general,

the

guidance

contained

in the generic letter

had

been incorporated'into

site procedures.

Appropriate precautions

and limitations'ad

been

specified to prevent,

monitor,

and mitigate the consequences

of

a

loss of decay heat

removal while under reduced

RCS invenihry

conditions.

However, the inspector

noted that in some

pr'ocedures

clarification and revision still needed

to be performed,

and

procedures

needed to be checked to assure

consistency

of

information.

The licensee

agreed to evaluate

and take appropriate

actions to address

these

issues.

The areas

of comment

are described

below:

New procedures

were developed

in the areas

of outage planning

(Administrative Procedure

ADS.DC52)

and diagnoses

of problems

with decay heat

removal

when in Modes

5 and

6 (Abnormal

Operating

Procedures

OP

AP SD-0 through 5).

These

procedures

.

contain additional

information not provided in other procedures,

such

as the

need to wait 42 days after shutdown

and to have

three containment

fan cooler units operating if the containment

water sealed

penetration

is to be used.

Abnormal Operating Procedure

AP-16, "Malfunction of the

RHR

System,"

needs to be revised to indicate it is applicable only

in Modes 1-4.

Operations

Procedure

A-2:III, "Reactor Vessel - Draining to

Half Loop Operations

with Fuel in Vessel,"

does

not have

sufficient guidance

in establishing

and maintaining containment

closure for other than the major penetrations.

Additional

guidance

appears

necessary

to assure

that other penetrations

which could

be open to outside

containment,

such

as

when

maintenance

on valves is being done,

are appropriately

controlled

such that the penetrations

could

be closed, if

required.

In addition, operations

management

recognizes that,

because

of the limited pressure

retaining capability of the

penetration

using only a water seal,

additional

guidance is

needed to effectively seal

the penetration

should containment

pressurization

occur.

This penetration

is used only during

outages

to bring temporary lines into containment,

such

as for

steam generator

cleaning activities.

Procedure

AP SD-2,

"Loss of RCS inventory," should include

guidance

to open valve HCV-142 to establish

a gravity feed flow

path to the charging

pumps (step 7g).

Instructions for monitorino and trending

RHR pump motor

amps

are not described

in procedures.

10

The current mid-loop trouble alarm

(PK 02-21A) setpoint

specified for RCS temperature

is 190 degrees

F, although

procedure

A-2:III specifies that

RCS temperature

should

be

maintained

less that ]60 degrees.

In addition, the. alarm

setpoint for the wide ranoe

and narrow range reactor

vessel

refueling level indication system

(RVRLIS) has

not been

establi,shed

in the plant computer.

Current procedures

require

an additional

manager

to be present

whenever

midloop operations

are conducted;

however,

the

licensee

has

informed the

NRC that this commitment is no longer

necessary

based

on the administrative

actions

taken to prevent

and mitigate

a loss of decay heat removal.

This-is not yet

reflected in procedures.

During discussions

with licensee

pe'rsonnel,

the

NRC inspector

was

informed that evaluations

were being performed to assess

the

capability of the pathway resulting from the removal of'ressurizer

safety relief valves to function

as the hot leg vent path.

This

pathway would be in place of detensioning

the reactor

vessel

head

studs.

Removal of the safety relief valves is being explored

as

an

alternative

because

detensioning

of the reactor

head

and the

associated

steps

are viewed by the licensee

as

more complicated

and

with

a higher possibility for errors.

Because

an

RCS vent path

as

a

result of detensioning

the reactor

head

was discussed

in the

licensee's

response

to the generic letter, the licensee

was

requested

to inform the

NRC in writing should another

method of

venting

be proposed,

such

as through the safety relief valve

openings.

c.

~Summar

In general,

training

and procedures

covering reduced

RCS inventory

operations

appear

appropriate.

Progress

has

been

made in the

structure of procedures

and in refining the previous

procedures

to

reflect more current information

and analyses.

While this progress

appears

beneficial overall,

procedures

are currently in

a

transition.

The licensee

stated that appropriate

changes

to

procedures, will be made to address

the inspector's

comments,

as well

as those

changes

already being considered.

In the past,

because

the

licensee

has

not planned to perform reduced

RCS inventory operations

with fuel in the reactor vessel,

the procedure

revisions

have not

been

a high priority.

However, there is

a possibility that these

reduced

inventory operations

would be needed

unexpectedly

due to

a

steam generator

tube leak or reactor coolant

pump seal

problem'.

It

is expected that the procedures

would be reviewed

and updated prior

to the performance

of reduced

inventory operations.

It is also

noted that reduced

inventory. operation

may be planned

in the latter

staoes

of the next'refueling

outages

should extended

steam generator

inspection

and maintenance

activities occur.

0

11

'

This closes

the review of the licensee's

responses

to Generic Letter 88-17.

The licensee's

corrective actions to the'above

comments will

be reviewed in future inspections

(Followup Item 50-275/'91-37-01).

No violations or deviations

were identified.

10.

Startup Activities - Unit 2

93702

71707)

a ~

b.

Hi

h Pressurizer

Safet

Relief Valve Tailpipe Temperature

- Unit 2

'uring the startup of Unit 2 from the recent refueling outage,

licensee

personnel

noted that pressurizer

safety relief valve 8010C

had

an elevated tailpipe temperature

indication of 'approximately

200-220

degrees

F.

Total leakage to the pressurizer relief tank

(PRT)

was monitored

and

was found to be 0.008-0.025

gpm.

Based

on

previous licensee

analyses,

a loop seal

on the safety relief piping

wil1 exist

up to

a leakage rate of 0.05

opm.

The

NRC inspector

had discussions

with licensee

personnel

to

determine

the significance of the leakage

and the monitoring which

would be performed during plant operations.

Based

on these

discussions,

the licensee will continue to monitor tailpipe

temperatures

and record

PRT in-leakage

rates

as already provided for

in alarm response

procedures.

In addition, the licensee

has

installed

a containment

monitor to display loop seal

temperatures

to

assure

that the loop seals exist.

Loop seal

temperatures will be

recorded

during routine entries into containment.

The

NRC inspector

.verified that the temperature

information was being recorded.

In

addition, the inspector verified that the licensee

had provided

operators

with specific guidance that the relief valves might not be

operable if high loop seal'emperatures

are observed.

Current

.tailpipe temperatures

for valve 8010C indicate

a downward trend.

Licensee

personnel

indicated that actions

had

been

taken to resolve

the leakage

problem

and that engineering activities are continuing

to determine

whether additional-system

or valve design

changes

would

be beneficial.

It is noted that Unit 1 safety relief valves

8010A

and

B also

have elevated tailpipe temperatures

(170-180 degrees

F).

The licensee

is monitoring the elevated tailpipe temperatures

and

is recording

PRT in-leakage for Unit 1.

Durino the

above discussions,

licensee

personnel

indicated that

an

evaluation

was being drafted which was intended to demonstrate

that

safety relief valves would still be operable without loop seals.

The licensee

plans to submit this eval.uation to the

NRC when completed.

Failure of Feeder

Breaker from Auxiliar

Transformer to 0 en

-. Unit 2

On October

23,

1991, during the attempt to transfer

the

4

kV vital

bus

H from the auxiliary transformer to the startup transformer,

the feeder

breaker

from the auxiliary transformer failed to open.

During subsequent

attempts

to open the auxiliary feeder breaker,

the

breaker

was observed

to have

smoke

coming from the cubicle.

The

DC

control

power for the breaker

was

removed with the breaker still

providing power to bus

H.

The auxiliary feeder

breaker

was manually

tripped,

and

power

was provided to bus

H by the startup transformer.

12

The licensee's

investigation of the breaker failure revealed. that

the trip coil appeared

to have

become slightly misaligned with the

armature

assembly.

This misalignment

could- be sufficient to catch

the dropping armature,

when the trip coi 1 is energized.

'Since only

the force of gravity pulls the armature

out of the trip qoil,

a minor

interference

or misalignment

can reduce the

amount of arohture travel

and cause

the breaker to fail to trip.

This failure mech'anism

was

demonstrated

on. another similar breaker.

The failure of this breaker to trip is significant in that power to

a vital bus would not be provided.

Under plant conditions which

would cause

a transfer to the startup transformer,

such

as a.fault,

the failure of the breaker

to open could cause

an overcurrent

condition if the startup

power system

attempted

to also provide

power to the

bus or if the fault continued to exist

on the

4 kV

system.

In addition, the diesel

generator

would be unable to

provide power to the

bus

because

of an interlock which prevents

diesel

oenerator

breaker closure if the auxiliary feeder breaker is

closed.

Therefore,

power to one of the three

4

kV vital buses

would

not

be provided.

The licensee

performed testing of the replacement

breaker

and

a

visual inspection of the alignment of similar breakers

in Units

1

and 2.

No other alignment problems

were identified.

The licensee's

evaluation is described

in

NCR DC2-91-EM-N095.

The

NRC inspectors

verified that visual inspections

without breaker

removal

could

determine

whether the coi 1

and armature

were properly aligned

and

that the licensee's

corrective actions

appeared

appropriate.

No violations or deviations

were identified.

ll.

Operator Simulator Trainin

41500

The

NRC inspector. observed requalification training for licensed

operators

which involved

a three

hour simulator

scenario

and

a one hour

critique session

(Lesson

No. LS-4-5A).

The scenario

involved the

successive

loss of

a component cooling water system

heat

exchanger,

a

generator

load reject,

a small

break

LOCA,

a large break

LOCA,

and

finally a loss of startup

power.

This training session

involved both

operations

personnel

and training instructors.

The crew positions

manned

were shift foreman,

senior control operator,

control operator,

auxiliary

control operator (2),

and shift technical

advisor.

The training scenario

emphasized

the

use of procedures

and the ability of

the crew to transition from one

emergency

procedure to another.

The crew

demonstrated

the understanding

of the

need to adhere

to procedures

in

a

stepwise

manner

and were able to transition

between

procedures.

The

critique session- highlighted the technical

issues

related to the scenario

and also the

need to follow procedures

even for routine evolutions.

The

inspector

noted that in the critique session

there

was little discussion

related to crew interactions

or individual performance.

Based

on

discussions

with the trainina supervisor

and

a supervisor

involved in the

13

training session

witnessed

by the inspector, it appeared

that the licensee

i~i~-ii'c~~ that more

can

be done to strengthen

the crew interactions

area.

The training manager

and operations

management

indicated that this area

had

been reviewed in the past

by the operations director

and this:area

would be

given further operations

management

attention.

12.

Exit

On November

22,

1991,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspector

summarized

the

scope

and findings of the inspection

as described

in this report.

I

I