ML16341F730

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Insp Repts 50-275/90-08 & 50-323/90-08 on 900311-0421.No Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items & LERs
ML16341F730
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/24/1990
From: Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F728 List:
References
50-275-90-08, 50-275-90-8, 50-323-90-08, 50-323-90-8, NUDOCS 9006120015
Download: ML16341F730 (48)


See also: IR 05000275/1990008

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos:

50-275/90-08

and 50-323/90-08

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and

DPR-82

Licensee;

Pacific

Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

March ll through April 21,

1990

Inspectors:

P.

P. Narbut,

Senior

Resident Inspector

K.

E. Johnston,

Resident

Inspector

Approved by:

en onca,

>e

,

eac or

roJec

s

ec

Ton

a

e

1gne

Summary:

Ins ection from March 11 throu

h

A ril 21

1990

Re ort Nos. 50-275/90-08

and

Areas Ins ected:

The inspection

included routine inspections of plant

opera

sons,

maintenance

and surveillance activities, follow-up of onsite

events,

open items,

and licensee

event reports

(LERs), as well as selected

independent

inspection activities.

Inspection

Procedures

30702,

30703,

35702,

37702,

37828,

40500,

42700,

61726,

62703,

71707,

71710,

92701,

92702,

92720,

and 93702 were

used

as guidance during this inspection.

Safet

Issues

Mana ement

S stem

SINS) Items:

None

Results:

General

Conclusions

on Stren th and Weaknesses:

.Areas of Stren th:

The maintenance

area

was strengthened

by the addition of a new manager.

Specifically the former position of Maintenance

Hanager

was split into two new

-full-time positions consisting of Mechanical Maintenance'anager

and

Electrical Maintenance

Manager.

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9

The licensee's

methods for event investigation were demonstrated

to be

effective in rapidly determining .causes

and corrective actions.

This was

demonstrated

by the investigation

done for a reactor vessel

head lift mishap

in which thermocouples

were

damaged

due to protective covers not being

installed properly.

As will be discussed

in the weaknesses

section which

follows, when the event investigation

methods

were not used,

understanding

and

resolving problems

sometimes

languished.

Certain elements of the licensee's

staff identified and elevated

problems

which were not immediately obvious problems

and the identification of those

problems

speaks

well for the quality of the licensee staff.

Examples of this.

include the identification of motor operated

valve spring pack relaxation

by

maintenance,

the recognition of the design basis

seismic problem when water

was discovered

in containment

spray piping by plant engineering,

and the

recognition

and questioning of test configuration versus operational

configuration differences for the centrifugal charging

pumps

by plant

engineering.

Areas of Meakness

Mechanical

maintenance

engineers

demonstrated

a lack of recognizing

and

expeditiously dealing with already identified problems.

The most notable

example

was the untimely action surrounding

blowdown settings

on Crosby relief

valves.

The potential for inaccurate

settings

was noted by the

NRC residents

in July 1989.

The Unit 1 outage in October

1989 sampled three valves

and

found them inaccurately set.

Nothing was done to finalize Unit 1 corrective

action during that outage opportunity.

NRC follow-up in-February

1990 led to

increased

sampling during the Unit 2 outage

and the knowledge of broader

blowdown setting problems.

A justification for continued operation

and

a

nonconformance

report were not prepared until suggested

by the

NRC on March

20,

1990.

Other examples of mechanical

maintenance

engineers failing to

recognize

problems included:

o

an auxiliary feedwater

check valve which would not fully shut both in the

second

and third refueling outage.

o

RHR valves which had failed operator-to-valve shaft keys, which were

repaired,

but the applicability of the problem to Unit l and to other

similar valves

was not addressed

until brought to the assistant

plant

manager's

attention by the

NRC.

Electrical Maintenance 'Engineers

have not always pursued potentially broader

problems.

This concern

was evident when

a component cooling water pump

circuit breaker failed to close

due to a part failure.

The initial reaction

was to repair the breaker

and treat the case

as isolated.

The electrical

maintenance

manager.

however had the case

pursued

and demonstrated

potentially

generic failures.

Likewise diesel

generator

1-1 tripped in April which was

a

repeat of a 1989 event.

In both cases

the cause

was

a broken wire lug.

The

cause of the broken lug was wire tension which could have

been determined in

1989, but was not,

based

on the belief that .it was isolated.

Si nificant Safet

Matters:

None.

Summar

of Violations and Deviations:

One violation was identified regarding

e opera

s

s y o

e

ue

an

sng Building Ventilation System during the

movement of spent fuel (paragraph

S.a).

0 en Items

Summar

Two items were closed

(one follow-up item and

one

unreso

ve

s

em

and two items were

opened

(one enforcement

item and

one

follow-up item).

Persons

Contacted

DETAILS

"J.

D. Townsend,

Vice President,

Diablo Canyon Operations

8 Pl

"D.

B. Miklush, Assistant Plant Manager,

Operations

Services

.

M. J.

Angus, Assistant Plant Manager, Technical, Services

"B.

W. Giffin, Assistant Plant Manager,

Maintenance

Services

W.

G. Crockett, Assistant Plant Manager,

Support Services

W.

D. Barkhuff, Acting equality Control Manager

T.

A. Bennett,

Mechanical

Maintenance

Manager

D.

A. Taggert, Director equality Support

T.

L. Grebel,

Regulatory Compliance Supervisor

"H. J. Phillips, Electrical Maintenance

Manager

D.

P. Brooks, Acting Work Planning Manager

  • R.

C. Washington,

Acting Instrumentation

and Controls Manager

"J.

A. Shoulders,

Onsite Project Engineering

Group Manager

H.

G. Burgess,

System Engineering

Manager

S.

R. Fridley, Operations

Manager

"R. Gray, Radiation Protection

Manager

E.

C. Connell, Assistant Project Engineer

"L. Cossette,

Plant Engineer

"M. Hug, Regulatory Compliance Supervisor

"R.

D. Cramens,

equality Control

Lead Engineer

"R. Nanniga,

Mechanical

Maintenance

Eng)neer

ant Manager

The inspe'tors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

"Denotes those attending the exit interview on Hay 1, 1990.

0 erational

Status of Diablo Can

on Units 1 and

2

Also during this reporting period,

an enforcement

conference

regarding

security matters

was held on March 16,

1990 and a management

meeting to

review the licensee's

SALP (Systematic Appraisal of Licensee

Performance)

report was held on March 22,

1990.

These meetings

are documented

in

separate

NRC reports.

Diablo Canyon Unit 1 started

the reporting period at full power and

continued at power during the reporting period.

Unit 2 was in its third

refueling outage for the entire period.

During this reporting period the licensee

made organizational

and

personnel

changes.

The maintenance

department

was changed in that

separate

positions for a mechanical

maintenance

manager

and electrical

maintenance

manager

were created.

Therefore,

the assistant

plant manager

for maintenance

now has separate

managers for electrical,

mechanical,

and

I8C maintenance,

in addition to a work planning manager

and

a manager of

materials services.

3.

0 erational

Safet

Verification

71707)

~

~

lj

a.

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas

of the facility'o

observe

the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(d)

Interiors of ei~ctrical

and control panels.

(e)

Plant housekeeping

and cleanliness.

(f)

Engineered safety feature

equipment alignment

and conditions.

(g)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

b.

Radiolo ical Protection

The inspectors periodically observed radiological protection

practices

to determine whether the licensee's

program was being

implemented in conformance with facility policies

and procedures

and

in compliance with regulatory requirements.

The inspectors verified

that health physics supervisors

and professionals

conducted frequent

plant tours to observe activities in progress

and were generally

aware of significant plant activities, particularly those related to

radiological conditions and/or challenges.

ALARA consideration

was

found to be an integral part of each

RWP (Radiation Work Permit).

c.

Ph sical Securit

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

including vehicle and personnel

access

screening,'ersonnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was checked during backshift inspections.

No violations or deviations

were identified.

4.

Onsite Event Follow-u

(93702)

During the report period, there were

a number of events involving

,.

equipment important to safety,

where the equipment

was found in a

degraded

condition or had failed either during testing or in the course

of operation.

For the items discussed

below, the inspectors

confirmed

that the licensee

had initiated its problem identification and corrective

action programs in accordance

with 10 CFR Part 50, Appendix B, Criterion

16, "Corrective Actions" and the licensee's

procedure

NPAP C-12.

The

program is initiated with an Action Request

(AR).

equality Evaluations

(gE) and Nonconformance

Reports

(NCR) are

used to document

cause

and

corrective action, with NCRs used to address

the more significant

problems.

When appropriate,

the licensee initiated a Justification for

Continued Operation

(JCO).

In each

case the inspector confirmed that the

licensee

had addressed

the cause

and safety significance of the event

and

had taken corrective actions to prevent recurrence,

addressing,

as

appropriate,

the generic applicability to Diablo Canyon

and the industry.

a.

Unit 2 Motor 0 crated Valve Fails to 0 en

On March 12, 1990, during periodic surveillance testing, Unit 2

valve SI 8805B (refueling water storage

tank to charging

pump

suction) failed to open.

The licensee

performed follow-up

investigations,

but these investigations

did not appear to be

completely thought out prior to commencing action.

Consequently

some information was lost (such

as the torque switch condition and

the thermal overload condition).

The licensee

actions

were examined

by an

NRC motor operated

valve specialist

and will be reported in

detail in a separate

report.

The licensee did not develop

an

absolute

cause for the motor operated valve's failure to open, but

did perform extensive

maintenance

and testing to verify valve

operability for restart.

The need to perform preplanned

and

prescribed trouble troubleshooting

was discussed

with the licensee

management

at the exit interview.

Licensee

management

stated that

they recognized

the faHure to obtain valuable information and would

evaluate

program changes.

b.

S ill of Water in Containment

On March 12, 1990, during pump

down of the Unit 2 recirculation

sump

for the refueling outage water was

pumped to the reactor

coolant

drain tank (RCDT).

The

RCDT was not intended to be the terminus for

the

sump water.

An overfill and spill occurred.

The event

had

no

safety significance,

but did indicate confusion between

maintenance

and operations

personnel.

Personnel

had apparently

moved hoses

without notifying operations.

The assistant

plant manager for

maintenance

stated

he was unable to determine

who moved the hoses

or

why.

He had questioned

the outage control center personnel

and

maintenance

personnel.

Licensee

management

personnel

took no further actions to determine

the cause of the spH

1 due to the lack of safety significance.

The

inspectors

understood

the licensee's

position but noted that this

was

a second

apparent

example

where maintenance

personnel

were not

apparently

meeting management's

expectations.

Auxiliar

Feedwater

(AFW

Terr

Turbine Steam

Su

1

Check Valve

oun

uc

en

Reference:

NCR DC2-90-MM-N023

On March 14,

1990, following the removal for a design

change of the

AFW terry turbine steam supply check valves,

one of the check

valves,

FW-2-5166 was found stuck open.

It was subsequently

determined that the valve disc was not bound to the extent that it

would not have performed its design function to isolate the

AFW

steam supply from a faulted steam generator.

Upon disassembly,

maintenance

engineering

found that the bushings

for the hinge p";n had rotated

and had bound the hinge assembly.

In

a history search,

the licensee

found that in 1984 the bushings for

FW-2-5166

had been

machined for an unspecified

reason.

As a result,

an excessive

gap in the arm/hinge block/bushing assembly

allowed

enough clearance for the bushing shoulders to rotate out of

position.

Although bushing rotation was noted during the Unit 2 second

refueling outage,

no corrective actions

were taken at that time.

The problem almost did not come to light during this outage.

The

Assistant Plant Manager for operations

recognized

the problem and

brought it to light after discussions

with maintenance

engineers.

The licensee

performed

a history search

and confirmed that

no other

check valves of similar design

had been previously machined.

The

licensee

also will revise check valve inspection procedures

to

measure

the gap in the hinge arm assembly.

The missed opportunity

to discover this problem during the previous refueling was noted at

the exit interview.

The importance of instilling the proper safety

perspective

in maintenance

personnel

was discussed.

Feedwater,

Check Valve Missin

Pin

Reference:

gE f0007385

On March 15, 1990; during a planned inspection of Unit 2 important

check valves,

the pivot pin and retaining pin were found missing

from one ear of the disc/seat

assembly of main feedwater

pump

discharge

check valve FW-2-506.

Both pins were subsequently

found

downstream in the feedwater piping.

The cause

was attributed to the

previous post maintenance

placement of the pivot pin anti-rotation

tack welds (essentially,

the tack welds,

as they were placed,

did

not prevent the pin from rotation).

The corrective actions

included

revisions to inspection

and maintenance

procedures.

The licensee

determined that this problem was limited to the two main feedwater

pump discharge

check valves.

Auxiliar Saltwater

(ASW) Seismic

Su

ort Bolt Crackin

Reference:

AR A0184193

NCR DCO-90-EN-NOOS

On March 22, 1990, during the disassembly for maintenance

of

auxiliary saltwater

(ASW) pump 2-2, the

pump casing brace ring bolts

were found to be badly corroded.

It was subsequently

determined

that the installed

Grade

630 stainless

steel bolts are not

appropriate for service in a saltwater

submerged

environment.

The

licensee's

review also determined that the bolts had been replaced

in the previous

outage.

The original bolts were

304 stainless

steel

bolts and were replaced with Grade

630 bolts.

The licensee

determined that all other

ASW pumps

had also

had bolts replaced with

Grade

630 material.

The licensee identified and replaced all other Grade

630 bolts in

submerged

service in the

ASW sy'htems for both units.

An analysi

performed of the

as found conditions of the bolts determined that

the

ASW systems

would have performed their design functions during a

seismic event.

An NCR was initiated to investiqate

why Grade

630

bolts were allowed to be used in submerged

service

and to determine

appropriate corrective 'actions.

The inspector will review the

licensee's

NCR during the course of routine inspection activities.

Limitor ue Valve 0 erator

S rin

Pack Relaxation

On March 23, 1990, the inspectors

became

aware of a potentially

generic problem dealing with relaxed spring packs

on limitorque

valve operators.

The licensee

discovered

the condition on a valve

being disassembled

and inspected

during a routine maintenance.

The

condition observed

was,a physically loose spring pack which was

astutely

noted to be wrong by the mechanics

performing the work.

Discussions

were held with the licensee,

the residents,

regional

supervision

and

NRC headquarters

personnel.

An NRC specialist

was

sent to the site to perform

a special

inspection for the potentially

qeneric issue of spring pack relaxation.

The results of that

inspection will be reported separately.

The resident inspectors

examined the licensee's

rationale for

continued operation of Unit 1 and the justification for restart of

Unit 2 and found the licensee's

positions acceptable.

Protective'"Bullet Noses"

Se grated

From Core Exit Thermocou le

ea

s

ur>n

reac or vesse

ea

Reference:

gE f0007448

On March 26,

1990, during a,Unit 2 reactor vessel

head lift,

temporary protective "bullet noses"

separated

from the core exit

thermocouple

leads.

The "bullet noses 'ere installed to protect

the thermocouple

leads during the

head

movement.

The bullet noses

had been incorrectly installed.

The licensee

determined that the

installation problems resulted

from inadequate

installation

instructions

aggravated

by the conditions which existed

when the

bullet noses

were installed;

the installers

were required to use

respirators

and the position of the scaffolding placed the

installers in an awkward position.

Corrective actions

included

procedure

revisions

and training enhancements.

Three thermocouples

were identified as potentially damaged.

However the licensee

evaluation

concluded that operation with three inoperable

thermocouples

was acceptable.

Reactor Coolant

Pum

(RCP) Motor Rotor Delamination

References:

NCR DC2-90-EM-N017

JCO 90-07

On March 26,

1990, during the inspection of tPg Unit 2 RCPs,

motors

2-1, 2-2 and 2-4 were .found to have loose structural

and electrical

parts called finger plates

and motor laminations.

The condition was

found to a limited extent

on the 2-3 motor,

and the motor required

minor repair.

The Unit 1 and Unit 2 loop three motors

had been

swapped prior to the initial startup of Unit 1 in 1985.

Therefore

it was suspected

that since limited problems

were found on the 2-3

motor, the 1-3 motor would be likely to have

more severe rotor

defects similar to the other Unit 2 motors.

Likewise, it was

suspected

that the other Unit 1 motors would not have substantial

defects.

The vendor performed

an analysis to determined the

probable failure mode of a motor with defects

as described

above

and

concluded it to be an electrical fault without lockinq the rotor.

Since the design basis

assumes

one locked rotor, continued Unit 1

operation

was determined to be acceptable,

since

a locked rotor or

the concurrent failure of more than one

pump was determined to be

improbable.

.'The licensee

committed to inspect the Unit 1 motors

during the Unit 1 fourth refueling outage in February 1991.

Trojan

was the only other plant with this specific motor design

and they

were supplied with information on how to detect

and correct the

rotor defects.

Although it was suspected

that the cause of the

defects

was related to the manufacturing process,

the specific cause

had not been determined

and the licensee

was continuing to pursue

the issue with the vendor.

y ~

Com onent Coolin

Water

Pum

Circuit Breaker

On March 31, 1990, following planned preventative

maintenance

in the

breaker cubicle, the 4kv circuit breaker for component cooling water

pump 2-3 failed to close

when actuated

from the control

room.

The breaker

was declared

inoperable

and

an action request

(AR) was

written.

Investigative actions

showed the cause to be

a fai lure of

a gear in the charging motor.

The licensee's first reaction

was

that such fai lures are infrequent

and would be self-revealing

when

breakers

are racked in.

Consequently

no further action, other than

this breaker's

repair,

would be required.

Licensee

maintenance

.'ersonnel

in reviewing past history identified another breaker in a

non-safety application which underwent

a similar failure.

Consequently

licensee

maintenance

management

was considering

elevating the problem to a quality evaluation level at the end of

the reporting period.

The inspectors will follow-up licensee

action

in the course of future inspection activity.

Chromated

Water

S ills

On April 3, 1990,

a chromated water spill was

announced

over the

plant public address

system.

An inspector examination of the spill

was initiated.

The spill was from the service coolinq water system;

a non-safety

system.

The spill was the second spill sn as

many

weeks involving the

same modification and startup testing personnel.

The inspector discussed

the event with the lead startup enneer

and

the general

construction

manager

and confirmed that a quality

evaluation

had been written (gED7440)

and root cause

determined.

Action to prevent recurrence

had not yet been determined but the

startup

engineer

confirmed that the interface

between operations

and

startup personnel

would be re-examined.

Diesel Generator

(D/G

1-1 Tri

ed While Runnin

in Test

References:

gE f0007424

ACR DCI"90-EM"N026

On April 3, 1990,

D/G 1-1 tripped during a post maintenance

run when

its generator differential current relay actuated.

The cause

was

determined to be

a broken wire lug for the secondary

side of the

current transformer.

The licensee's

inspection

found evidence that

the wire had been taut and that cabinet vibration caused

the lug to

break (the cabinet is mounted

on the D/G).

All other D/G current

transformers

were inspected

and wiring adjustments

were

made to

ensure

no similar, conditions existed.

The

DG 1-1 problem was

determined to have also occurred in 1989 and as

a result,

a

non-conformance

report was issued to address

the lack of a root

cause investigation following the first event.

Vital Batter

Char er 232 Overloaded

Reference:

NCR DC2-90-EM-N028

On April 3, 1990, while placinq Unit 2 battery charger

232 in

service

on battery 2-3, following- its battery discharge test,

four

of the six battery charger

fuses failed.

The output current

was

noted to be above

500 amps.

The battery charger

was rated for a

maximum of 440

amps

DC. It was subsequently

determined that the

battery charger's

current control module,

which had been replaced

on

November

12, 1988,

had not been correctly calibrated to limit

current output.

The battery charger overloaded in its attempt to recharge

the

depleted battery.

The lic'ensee

determined that the current control module for battery

charger

232 had been the only one which had been replaced

and

therefore

had confidence that the other nine safety related battery

chargers

would charge correctly.

Additional confidence

was provided

by the fact that

no other chargers

achieved

an overload condition

when recharging depleted batteries:

The licensee

also determined that battery charger

232 could have

failed following a loss of all

AC power event,

when it would have

been required to supply both the depleted batteries

and emergency

loads,

depending

on the length of the loss of AC power.

However,

the redundant battery charger

231 could have been

used to supply the

loads.

Additionally, the licensee

determined that for other

analyzed

events,

battery charger

232 would have

been able to perform

its design functions.

The licensee initiated a non-conformance

report to investigate

the

cause

and corrective actions.

The inspector will followup the.NCR

during the course of routine inspection.

Reactor Coolant

Pum

(RCP) Thrust Runner

On April 3, 1990, during the

RCP motor inspections,

the licensee

noted marring of the

RCP motor thrust shoes.

The licensee

and the

vendor determined that the indications were limited to the thrust

shoe babbit and not in the shoe itself.

The licensee

had

a second

vendor resurface

the thrust shoes

and was informed by that vendor

that the as found condition of the shoes

was acceptable

and not

unusual.

The licensee postulated

from the evidence

and discussions

with the vendor that cavitation at the leading edge of the thrust

shoe

was causinq'he

indications.

Further, the licensee

performed

motor modifications in the previous

outage which they feel

terminated the progression of the problem.

This was supported

by a

comparison of pictures of the thrust

shoes

from the Unit 2 second

refueling outage

and the current condition of the thrust shoes

during this outage.

Ventilation Lineu

Shift Due to an Inverter Volta e

S ike

Reference:

NCR DC2-90-OP-N020

On April 4, 1990, the Unit 2 Control

Room Ventilation System

(CRVS)

unexpectedly transferred

from its normal ventilation lineup to the.

pressurization

lineup and the Fuel Handling Building Ventilation

System

(FHBVS) transferred

from its normal ventilation lineup to the

iodine removal lineup.

Other control

room alarm annunciations

indicated that vital instruments

powered

by AC panels

PY-21 and

PY-21A had undergone

a current transient.

At the time of the event,

Unit 2 was in a refueling outage with a high level of maintenance

activity.

The licensee

was unable to determine

the cause of the

current transient.

A non-conformance

report

(NCR DC2-90-OP-N020)

was initiated to

address

the cause,

safety significance,

and corrective actions.

The

licensee

determined

the event to be an engineered

safety features

actuation

and will submit a Licensee

Event Report (LER).

The

inspector will review the cause

and corrective actions following the

submittal of the

LER.

RHR valves

HCV-670

637

and 638

roblems

Reference:

gE f0007456

On April 3, 1990, during the performance of containment

spray

testing, Unit 2 residual

heat

removal

(RHR) valves

HCV-670, HCV-637,

and HCV-638 were observed to be leaking excessively.

HCVs 637 and

638 are the throttle valves for RHR trains

1 and

2 respectively.

HCV-670 is the

RHR heat exchanger

bypass

valve.

The combined

leakage past the seats

of the three valves, which were in their

closed position,

was measured to be 1800

gpm, with HCV-670 leaking

the greatest.

All three valves are the

same

model butterfly valve with an air

actuator.

Hechanical

maintenance

(NM) found that for HCV-670, the

key .which interlocks the valve shaft to the actuator lever had

sheared.

HCVs 637 and 638 were found with identical problems;

the

key was found outside its lever slot and had allowed the shaft to

rotate in relation to the actuator lever.

For all three valves the

cause

was attributed to fatigue of the key and wear of the lever

slot.

The .inspector discussed

the valve problems with HN on April 26. It

was evident from the discussion that although the immediate cause

was understood

to some extent,

the licensee

had not yet adequately

addressed

the root cause,

the safety significance,

the generic

applicability, and the corrective actions.

Specifically, the review

had not addressed

the following;

The installed

key material

was not the material specified in

the most recent plant drawings.

Mhether the safety function of the valves

had been

compromised.

If other plant valves

may be subject to the

same failures.

10

o

The operability of the Unit 1 valves

and any inspections

or

testing

needed to confirm their operability,

The inspector discussed

the adequacy

of HM's review of these

problems with the Assistant Plant Manager

(APH) for Maintenance

Services.

As

a result of this discuss>on

and the APM's further

investigation,

an

NCR was initiated to address

the issue.

The

inspector will followup the licensee's

review during the course of a

future inspection.

Containment

Fan Cooler Unit

CFCU 2-2

Breaker Control Transformer

ause

a

>re

>n

s uice

Reference:

AR A0186280

On April 6, 1990,

a small fire was discovered in the breaker cubicle

for Unit 2

CFCU 2-2.

The fire resulted

from a ground in the primary

side of the breaker control transformer.

The fire was extinguished

when the breaker

was racked out.

Electrical maintenance

was in the

process

of trouble shooting the breaker following spurious

breaker

trips.

Electrical maintenance

concluded that the spurious trips had

resulted

from the degraded

control transformer.

The licensee

also concluded that the control transformer failure was

an isolated event,

arguing that there are

many transformers of this

type operating without recurring failures.

Based

on the above,

broader corrective action was considered

unnecessary.

Containment

Leak Rate Test

On April 10, 1990, Unit 2 completed its integrated

leak rate test.

Licensee

engineers

reviewed the data

and concluded the results

were

satisfactory.

Inadvertent Ventilation Lineu

Shift

On April 17, 1990, the licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency

report

due to an automatic ventilation lineup change

from normal to

safeguards

mode in,both the control

room and fuel handling building

ventilation

systems.

The ventilation lineup change

was caused

by

I8C technicians

inadvertently shorting leads to radiation monitor

RH-51.

The short caused

a voltage disturbance

on the vital

instrument panel'hich initiated the lineup changes.

The'icensee's

immediate actions

were appropriate

and the licensee's

follow-up actions will be examined in response

to their event report

and

Non Conformance

Report

DC 2-90-TI-N025.

Wirin

Se aration Not Sufficient

On April 20,

1990, the licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency

report

for Unit 2,

The report was based

on finding the wiring for relays

for low temperature

over-pressure

protection

(LTOP) not properly

separated

per

IEEE standards.

The licensee

had also found and reported the problem in Unit 2

earlier in the day.

The Unit 2 condition was repaired.

The Unit 1

condition has

been included on a forced outage

work list and will be

corrected at the next opportunity.

The inspectors will follow-up the licensee's

root cause evaluation

through the licensee

event report and

non conformance

report.

5.

Haintenance

62703)

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures;

technical specifications,

and appropriate

industry codes

and. standards.

Furthermore,

the inspectors verified maintenance activities were

~

~

~

~

~

erformed by qualified personnel,

in accordance

with fire protection

and

ousekeeping

controls,

and replacement parts were appropriately

certified.

The inspectors

examined maintenance activities in conjunction with the

plant events

reported in paragraph

4.

In particular,

those examinations

included the maintenance .aspects

of motor operated

valve problems (4a),

RCDT overfill (4b), stuck check valves (4c), missing check valve parts

(4d), auxiliary saltwater

pump restraint bolting repair (4e), limitorque

valve spring pack relaxation (4f), reactor vessel

disassembly

work (4q),

reactor

coolant

pump rotor repair {4h), 4kv circuit breaker repair (4>),

diesel

generator repair (4k), vital battery charger repairs (41), reactor

coolant

pump thrust bearing repair (4m), butterfly valve repair (4o), fan

cooler transformer

replacemeh't

(4p), and wiring separation

repair for

protection relays (4r).

In addition detailed maintenance

observations

were

made for motor

operated

valve testing

and repair by an

NRC specialist.

That activity

will be reported separately.

a.

Relief Valve Blowdown Settin

s

During the reporting period, the inspector

examined

licensee

progress

in resolving Crosby relief valve blowdown settings.

The problem was first identified in Inspection Report 50-275/89-16

in July 1989.

The inspector questioned

the setting of the Unit 2

letdown relief valve due to an event in which the valve would not

reseat at normal. system pressure.

The licensee

commenced

an

examination of the subject at that time.

Three Crosby relief valves were examined during the Unit 1 refueling

outage in October to December

1989.

The as-found

blowdown settings

were not in accordance

with licensee

procedures

and were set high

such that the relief valves would have chattered

had they lifted.

No further examination

was

done during the Unit 1 outage.

The

maintenance

engineers

logic for not examining additional valves

was

that the valves would liftat the proper setpoint

and the improper

blowdown would only cause chatter.

12

During the Unit 2 refueling outage in March 1990, the licensee

examined all Crosby relief valves with adjustable

blowdown settings

in Unit 2.

The reason for the expansion of the sample

was the discovery that

the licensee's

procedure for setting Crosby relief valves

was in

error and did not recognize that each individual valve had

a unique

blowdown ring setting.

The Unit 2 valves

had been set to Unit 1

values.

The events to this point raised two concerns.

First, it took from

July 1989 to March 1990 to discover that the licensee's

procedures

were wrong and the valves were improperly set for blowdown.

Secondly,

the Unit 1 outage

had

come

and gone

and left valves with

improper blowdown settings in Unit 1.

On March 20,

1990, in response

to a request for an operability

evaluation

by the resident inspector,

the licensee

issued

a

justification for continued operation,

JCO 90-04RO, for Unit 1

operations with potential

blowdown setting problems

on Crosby relief

valves.

The

JCO was reviewed by the resident inspectors

and judged

to be acceptable.

Copies of the

JCO were provided to regional

and

headquarters

technical

personnel

and the subject

was discussed

with

regional supervision.

The licensee

subsequently

issued

a

Nonconformance

Report,

NCR DC2-90 MM-N013, on the subject of the

Crosby relief valve blowdown settings.

The licensee

had not yet

determined final root cause or final permanent corrective action.

Subsequent

licensee

actions regarding

Crosby relief valves appear to

be acceptable.

All Unit 1 valves will be properly set by the fourth

refueling outage in 1991,

and

a new maintenance

procedure will be

prepared

and training conducted

by the

same date.

Licensee

nonconformance

analysis did not appear to address

two

management

issues:

o

En ineerin

Res onsibilit

Engineering

involvement in the problem is not addressed

in the

nonconformance.

Engineering culpability should

be examined

since they were the organization which specifically provided

the wrong information for Unit 2 in the Diablo Canyon vendor

manual for Crosby relief valves

(DC663 219-601,

Revision 2,

dated

June

15, 1987).

o

Untimel

Maintenance Action

The licensee action in resolving the apparent

blowdown problem

appeared

to be untimely.

The problem revealed itself in July

1989 and was not addressed

comprehensively

during the Unit 1

outage

even through all three valves

sampled

had improper

blowdown settings.

13

The two management

issues

above were discussed

at the exit

interview.

The licensee

committed to .include the management

issues

in the nonconformance

report.

The inspector also discussed

the

opinion that the facts surrounding the development of the blowdown

setting problem

show the

need for improved management

oversight of

mechanical

maintenance

activities to recognize,

raise

and deal with

issues.

No violations or deviations

were identified.

6.

Survei1

1 ance

(61726)

By direct observation

and record review of selected

surveillance

testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

Surveillance testing observed

during this period included the performance

of the Unit 2 Integrated

Leak Rate Testing

and the integrated test of

engineered

safeguards

and diesel

generators

(STP M-15).

Both tests

involved major coordination efforts during the refueling outage.

Both

tests

were successfully

performed.

No findings were identified.

In addition surveillance testing aspects

of the events

discussed

in

paragraphs

4 and 8 were examined.

The surveillance

aspects

included

visual examination of check valves - paragraph 4d., diesel

generator

1-1

testing - paragraph 4k., 'battery testing - paragraph 41., safety valve

testing - paragraph

8b., containment

spray surveillance testing-

paragraph

8d.,

and charging

pump testing - paragraph

8.e.

No violations or deviations

were identified.

7.

0 en Item Follow-u

(92703

92702

a.

Core Reload Confi uration

Unresolved

Item 50-275/89-26-01

Closed

On November 17, 1989, during the Unit 1 core reloading operation,

the senior power production engineer

(SPPE)

and the refueling- senior

reactor

operator

(SRO) placed

a fuel element in a position

prohibited by the core loading procedure

(OP B-8D Sl).

With only

six vacancies left in the core,

a fuel assembly

(one cycle used)

was

placed temporarily next to the core baffle.

Although OP B-SD Sl

allows the temporary placement of fuel elements to facilitate the

placement of a bowed element,

the procedure

requires that two

vacancies

exist on either side of the temporary storage position.

With only six vacancies

open, this was not possible.

This procedure violation was identified by the

SPPE during a

subsequent

core reload evaluation.

An evaluation

was performed

by

the fuel vendor and determined that the move essentially .lowered

reactivity (as

had been judged by the

SPPE during the move)

and was

therefore

not safety significant.

A gE (f0006994)

was written which

'nitiated corrective action to clarify OP B-8D S1 reqarding the

placement of fuel elements at the end of fuel load w)th limited core

b.

vacancies.

After the procedure

was revised, prior to the Unit 2

outage,

training was provided for individuals involved in the fuel

load.

Although the

SPPE

and

SRO failed to follow procedure,

the event

was

identified by'he licensee,

there

was

no safety significance,

and

the licensee

took appropriate corrective action in a timely manner.

Therefore, this item is closed.

II

Main Annunciator

T

ewriter Testin

(0 en Item 50-323/89-21-01

ose

Following the August 21,

1989 manual trip of Unit 2, the main

annunciator

typewriter did not record alarms during the critical

portion of the event.

An electronic

memory card,

designed to

maintain alarm information until the alarm typewriter caught

up,

had

failed and approximately

40 seconds

worth of alarm information was

lost.

As a result of the event,

the licensee

implemented

a periodic test

to assure

the availability of the memory cards.

As permanent

corrective action, the licensee

replaced

both the Unit 1 and

2 main

annunciator typewriter systems with state of the art equipment.

The

system,

which has redundant processors,

is not subject to the

same

fai lure mode

and the testing

was discontinued.

Thss item is closed.

No violations or deviations

were identified.

8.

En ineerin

and Desi

n Control

37700

37702)

a.

Fuel Handlin

Bui ldin

Ventilation

S stem Ino erable Durin

Fuel

ovemen

On March 14, 1990, during a walkdown of the Unit 2 Auxiliary

Building, the inspector

noted that hoses

used for the Unit 2 steam

generator fill and drain evolution passed

from the 100 foot

elevation containment penetration

area,

through

a door, to the motor

driven auxiliary feedwater

(AFW) pump room.

The inspector also

observed that the

AFW pump rooms appeared

to be within the fuel

handling building and the door, propped

open by the hoses,

appeared

to be

a barrier between the fuel handling building and the auxiliary

building.

At the time of the the inspection,

fuel was being handled

in the spent fuel pool and the fuel handling building ventilation

system

(FHBVS) was required to be operable.

The inspector

asked the Assistant Plant Manager for Technical

Services to confirm that the door between the 100 foot penetration

area

and the

AFW pump room served

as

a

FHBVS boundary

and to,

determine

whether the open door affected

FHBVS operability.

Subsequent

to the inspector's

questions,

the licensee

determined

that the door in question

was indeed

a

FHBVS barrier.

Additionally,

the licensee identified a second

open

FHBVS barrier door and

determined that the open doors

made indeterminate

the ability of the

15

FHBVS to maintain

an 1/8 inch differential pressure,

as required

by

the Technical Specification.

The licensee

took immediate action to

shutdown the

FHBVS supply fans,

leaving the exhaust

fans on, to

ensure that

a greater

than 1/8 inch differential pressure

was

established.

The safety function of the supply fans is specifically

to cool the

AFW pump rooms.

Since the plant was in Mode 6,

refueling,

the

AFW system

was not required to be operable.

The

supply fans are not taken credit for in the ventilation design basis

for the spent fuel pool.

Technical Specification

3. 9. 12, "Fuel Handling Building Ventilation

System,"-allows fuel movement within the spent fuel pool provided

the

FHBVS is operable.

To demonstrate

operability, every eighteen

months

TS 4.9. 12.d.3 requires that the licensee verify that the

FHBVS maintains the spent fuel storage

pool area at a negative

pressure

of greater

than or equal to I/8 inch water gauge relative

to the outside

atmosphere

during system operation.

FSAR Section

15.4. 5. 2. 2, "Fuel Handling Area Accident, 'tates

that,

"Doors in

the fuel handlinq area

are closed to maintain controlled leakage

characteristics

sn the spent fuel pit region during refueling

operations

involving irradiated fuel."

In response

to the inspector's

questions,

a test

was performed to

establish

what effect having the doors

open

had on the ability of

the

FHBVS to maintain

a 1/8 inch negative pressure

with the supply

and exhaust

fans operating.

The test determined

+hat under these

conditions,

the

FHBVS could maintain only a 1/16 inch negative

pressure.

This indicates that while fuel was being handled in the

spent fuel pool, from March 12 to March 15,, 1990, the

FHBVS was not

able to maintain the

TS required 1/8 inch negative pressure.

This

is an apparent violation (Enforcement Item 50-323/90-08-01).

Subsequent

to the inspector

s findings, the licensee initiated a

non-conformance

report and prepared

a licensee

event report (Dated

April 16, 1990).

As a result of these

events,

the inspector questioned

the adequacy

of the review the licensee

performed in April 1989 of the final

safety analysis report

(FSAR) for commitments which may not have

been incorporated into procedures.

The review was performed in

response

to an enforcement action which also involved the failure to

implement

an.'FSAR commitment, which was associated

with the

Auxiliary Saltwater

System.

During the

FSAR review, the licensee

recognized

the commitment in FSAR section 15.4.5.2.2.

regarding the

control of FHBVS doors.

However, plant engineering limited their

attention to control of large roll-up doors

and did not address

other

FHB doors.

The inspector

reviewed the non-conformance

(NCR) report which

implemented the licensee's

commitment to review the

FSAR

(DCO-89-TN-N015) and the

NCR which addressed

the design

discrepancies

identified during that review (DCO-89-TN-N081). It

was not apparent to the inspector that all of the discrepancies

found (154)

had received the appropriate

review for safety

16

significance

and reportability.

NCR DCO-89-TN-N081 stated that it

addressed

only the

'design related discrepancies",

a total of 72,

and that

NCR DCO-89-TN-N015 addressed

the remainder.

However, while

DCO-89-TN-N015 appears

to have addressed

the cause

and corrective

actions for the implementation of commitments

made in the

FSAR, it

did not address

the safety significance

and reportability of the

commitments

not implemented.

In the specific case of the

FHB

roll-up doors, there

was

no consideration of the possibility that

because

the roll-up doors

had not been procedurally controlled

through the first two refueling outages for both units, that they

may have

been

open,

rendering the

FHBVS inoperable.

In the exit meeting,

the licensee

was requested

to address

in

response

to the notice of violation contained in this report, the

control of the

FHB roll-up doors during the first two refueling

outages

and the adequacy of the safety analysis for all

FSAR

discrepancies

identified.

Additionally, the licensee

was requested,

to address

the adequacy

of the

FSAR review and the design

memo

review conducted in 1989.

b.

Pressurizer

Code Safet

Valve Testin

Through discussions

with the licensee

and examination of the

periodic testing performed

on pressurizer code'afety

valves,

the

inspector

became

aware of a change in the licensee's

method of

testing pressurizer

code safety valves.

4

The change

has to'o with the definition of when the valve is

considered

to have "lifted".

The licensee previously considered

the

"lift"point the pressure

at which "popping'f the relief occurred.

The valves ordinarily have

a water loop seal

and .the initial lifting

of the stem

and the passing of the loop seal water occurs first and

does

not involve "popping" the valve which occurs later.

Dependent

on which definition is used,

"popping" or "stem movement," there is

about

an 80 psi difference in the apparent liftpressure.

The- licensee

has

chosen to use the definition of first stem

movement.

In effect, therefore,

pressurizer

valves will be set 80

psi higher than in previous outages.

The licensee

engineers

concluded that thiC will help prevent the simmering of relief valves

experienced

in previous fuel cycles.

The licensee

performed

an

evaluation

and

had

a safety evaluation performed by Westinghouse.

The evaluations

concluded that the change in liftpoint definition

was acceptable for existing safety analysis

and was in accordance

with ASME Code definitions.

The licensee's

position is described in PG&E Womack to Giffin letter

dated

March 21, 1990,

(147497),

and Westinghouse

McHugh to Womack

letter dated

March 23,

2990 (PGE-90-580).

The information and the licensee's

position appeared

reasonable.

The information was forwarded to regional specialists

for

information.

17

Fuel Handlin

Buildin

Brid e Crane

Problems

Overview

During the fuel loading operation for Unit 2, the spent fuel pool

building bridge crane control system locked

up while attempting to

lower a fuel element into the fuel transfer

upender.

To recover,

the licensee

installed

a controlled electrical

jumper and performed

a safety evaluation to allow the fuel element to be lowered.

The

inspector

reviewed the fuel movement operations

conducted in the

spent fuel pool with the Assistant Plant Man'ager

(APH) for Technical

'ervices,

the spent fuel pool system engineer,

and equality Assurance

personnel,

and

a number of problems

were indicated.

Although the lowering of the fuel element

appears

to have

been

performed in acceptable

manner,

the inspector's

review of the events

leading

up to the locked

up crane control event indicates there were

a number of precursor

problems.

Discussed

below are apparent

~

~

~

~

~

~

~

~

~

roblem areas

which indicate that operation of the spent fuel pool

ridge crane

was not performed in a fully controlled manner.

The

discussion is based

on interviews with the APH, the system engineer,

and gA.

In some instances

the information received

was

contradictory.

Due to the limited time of the"inspection

and the

complexity of the issues,

these findings are therefore characterized

as preliminary.

Ade uac

of Startu

Testin

Extensive modifications were

made to

e

ue

an

ing sys

em, )ncluding the spent fuel pool bridge crane

control system,

at the end of the Unit 2 second refueling outage

(December

1988).

However, testing of the systems

was not completed

during the second refueling outage

and was scheduled for the start

of the third refueling outage, prior to its use.

Two apparent

hardware

problems

(discussed

below) were not discovered

during

startup testing.

These

problems

may have

been caught

and corrected

if a complete dry run had been performed using the bridge crane to

move the

dummy fuel element into the upender.

This was apparently

not done.

Hardware

Problems:

During fuel movement, it was noted that when

ggH ti f t

p d,th

1d

tf

3

to 6 inches

beyond the stopping point.

The system engineer

indicated that the crane

brake was designed to stop the element in

1.5 inches.

Additionally, the digital limit controller for the

bridge crane,

as set

up by the startup engineer,

did not allow the

fuel element to clear the upender

when the element

was lifted in

slow speed.

To correct this problem, the system engineer raised the bridge crane

control

system

upper limit to allow a fuel element to clear the

upender in slow speed.

It was subsequently

discovered that if the

crane

was raised in fast speed,

the coast past the upper stop would

put the crane in a position where the electronic controller did not

know what position it was in.

As a result, the controller would not

allow the crane to be moved.

This is the condition reported

as

18

"lockup".

As corrective action, prior to core reload, the fuel

movement

crew was given verbal instructions to assure

fuel elements

were raised in slow speed.

However,

midway through the reload this

was not successfully

accomplished

and crane control locked

up with

an element in the elevated position.

Desi

n Chan

e Turnover:

After the core offload, but prior to the

core re oa

,

ectncal

Maintenance

(EM) was asked to investigate

the bridge crane.

No problems

were found.

System engineering

indicated that the turnover from startup engineering to

EM regarding

the design of the spent fuel pool bridge crane

may have

been

inadequate.

Procedural

Com liance:

The system engineer indicated that after the

core

o

oa

,

o

ow>ng the departure of the fuel movement

crew

(supplied

by a service vendor),

he became

aware that the contractor

had not been following the fuel handling procedure.

During the core

offload, the contractor

had discovered that the upper control limit

would not allow a fuel element to clear the upender if the element

was raised in slow speed

as required by the procedure.

To

compensate,

the fuel movement

crew raised fuel elements

in fast

speed,

relying on the crane's

coast past the upper limit to allow

the fuel element to clear the upender.

When the system engineer

became

aware of the problem,

he reprogrammed

the controller to set

a

higher liftpoint.

This was performed without a change to a

procedure

which specifies

the limit settings.

Upon the return of the fuel movement

crew for the core reload,

a

problem was found with the crane's

underload

bypass

feature.

The

startup

group was asked to investigate

the problem.

The system

engineer

noted that when the crane

was returned to service following

investigation

by the startup group, the limit settings

were

different than those set by the system engineer

and were also not

those specified by the procedure.

Inade

uate

Communications:

During the fuel movement,

there were

examp

es

o

apparen

dna equate

communications.

The first example

was the apparent

lack of communication of the difficulty experienced

by the fuel movement

crew in raising the fuel element

above the

upender.

There

was also evidence of inadequate

communications

between

the startup group,

EM, and the system engineer.

ualit

Assurance

Involvement:

The equality Assurance

department

per orme

our surveys

ance

coverage of spent fuel handling

operations.

The gA department did not have any outstanding

issues

related to the problems discussed

above.

The lead

gA auditor was

unaware of some of the problems

and questioned

the accuracy of

information supplied to the system engineer.

The inspector concurred with the

APM for Technical

Services that

a

review of these

events

was not immediately necessary

given the

impending restart of Unit 2 and that fuel movement would not

commence

on Unit 1 until 1991.

However, the inspector

observed that

efforts should

be made in a timely way to prevent the loss of

19

impetus for corrective actions.

In the exit meeting,

the

APM

committed to initiate an

NCR to address

the issues

discussed

above.

This item will remain

open pending the completion of the licensee's

review (Unresolved Item 50-323/90-08-02).

Containment

S ra

Header in an Unanal

zed Condition

Overview

During Local

Leak Rate Testing of the Unit 2 Containment

Spray

(CS)

system containment penetration isolation valves,

engineers

discovered water downstream of the

CS isolation valves.

Upon

further inquiry by plant engineering, it was realized that based

on

Hosgri design considerations,

the

CS piping inside containment

was

not qualified to withstand the design basis

seismic event with water

in the pipe.

Details

On April 3, 1990, the licensee

drained the inside containment

portion of the Unit 1

CS piping and discovered

approximately

30

gallons of water in one train and 160 gallons in the other.

In

accordance

with 10 CFR Part 50.72, the licensee

made

a 1-hour

non-emergencey

report on Unit 1 and

a 4-hour

non-emergency

report on

Unit 2, after determining that the condition was

an "unanalyzed

condition that significantly compromised plant safety."

Subsequently,

an engineering analysis

was performed,

taking into

consideration"the

amount of water found.

The analysis

concluded

that while the

CS piping would have

been stressed

beyond the design

allowables, it would not have been stressed

to the point of yield.

Although the licensee

could not make

a positive determination of how

the water managed to get beyond the outside containment isolation

valves, it was concluded that isolation and check valve surveillance

tests

were the most probable

cause.

Supporting this was that the

water level discovered in the Unit 1 piping was calculated to reach

the 150'evel, 10'elow the minimum level of the

RMST.

This

suggested

that the head of the

RMST and not a

CS pump had pushed the

water downstream of the isolation valve.

Supporting the conclusion

that this had occurred during valve testing and not as

a result of

isolation valve leakage

was that

a week following the discovery of

water in Unit 1

CS piping,

no additional water was discovered.

To address

cause

and corrective action, the licensee initiated an

NCR (DCO-90-TN-N-019).

Additionally, the event was determined to

require

an

LER.

A February 10,

1982

memo from the plant manager to the corporate

office documented portions of the

CS design basis including the need

to maintain the

CS piping inside containment dry.

However, the

requirement to maintain the

CS piping dry was never implemented into

plant procedures.

On March 24, 1989, in response

to an

NRC

inspection finding regarding the design basis of the auxiliary

saltwater

system,

the licensee

committed to and performed

a review

20

of engineering

correspondence

and communications specific to

constraints

on plant operations.

This was

done to verify that

no

other operational

requirements

identified by design

memorandum

were

missed.

The February 10, 1982,

memo was not included in this

review.

Section

Ba. of this report describes

a similar issue.

The

FSP'eview

performed

as

a result of the

same set of corrective ac'ns

did not identify the

need to control all

FHB doors.

At the xit

meeting for this report, the licensee

was requested to include in

their response

to the notice of violation contained in section

8a.

an evaluation of the adequacy of the

memo and

FSAR review performed

in 1989.

Char in

Pum

Recirculation

Lines

While performing functional testing of the emergency

core cooling

system

(ECCS) during the Unit 2 refueling outage it was noted

bP the

plant engineering staff that the tested

ECCS configuration did riot

match the configuration that would result from a safety injection

signal.

Specifically the centrifugal charging

pump (CCP) minimum

flow recirculation isolation valves

do not receive

an automatic

close signal

and are normally open during plant operations,

whereas

the tested configuration was with the

CCP recirculation valves

closed.

The licensee

then questioned

the ability of the charging

system to perform its design function as explained below.

In the original plant design;:the

CCP recirculation valves were

automatically closed

on a safety injection signal.

In 1981, in

response

to

NRC I8E Bulletin 80-18,

where it was recognized that the

CCPs could be dead

headed

against

high reactor coolant system

'ressure,

the licensee

removed the recirculation safety injection

isolation signal to the recirculation isolation valves.

An analysis

was performed that determined that the

ECCS could perform its design

function with this configuration.

During the third refueling outages for both Units,

new higher

enrichment fuel was added to the core.

The revised safety analysis

for the

new fuel assumed that the recirculation valves would close

on a safety injection signal.

As a result, the analysis

took credit

for more high head injection than would have

been available.

The licensee

requested

the

NSSS vendor provide

a supplemental

analysis of the

FSAR accident analysis,

taking into consideration

the. open recirculation line.

The analysis

concluded that the design

basis

had been met.

An NCR was initiated to identify why an

accurate

ECCS configuration

had not been provided for the

new fuel

analysis

and to determine appropriate corrective actions.

The

inspector will review the

NCR during the course of routine

inspection.

g ~

21

f.

Block Mall Ins ection

The Office of Nuclear Reactor Regulation

(NRR) reviewer and the

Region

V Projects

Section I Chief inspected

masonry block walls with

ductility ratios greater

than three.

This review did not find any

apparent situations

where large safety components

would be

significantly affected

by the collapse of the masonry walls.

The

inspection identified concerns

on the length of restrainina

angles

at the bottom of walls A06A and

B and the connection detaH of the

ventilation duct at the top of these walls.

The walls between the

cable spreading

rooms are also

an

NRC concern.

These

concerns

we'll

be reviewed under

NRR's evaluation of this issue.

No violations or deviations

were identified.

11.

Exit (30703)

On Hay 1, 1990,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.