ML16341F480

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Insp Repts 50-275/89-31 & 50-323/89-31 on 891017-1211. Potential Violations Noted.Major Areas Inspected:Debris in Unit 1 Containment Recirculation Sump
ML16341F480
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/13/1989
From: Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F479 List:
References
50-275-89-31, 50-323-89-31, EA-89-241, NUDOCS 9001030202
Download: ML16341F480 (32)


See also: IR 05000275/1989031

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report Nos:

50-275/89-31

and 50-323/89-31

EA No.:

89-241

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room

1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units

1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

October

17 through

December

11,

1989

Inspector:

Approved by:

P.

P. Narbut, Senior Resident

Inspector

Yi. N, Nendonca,

Chief, Reactor Projects

Section

1

Date Signed

Summary:

Ins ection fror, October

17 throu

h December

11,

1989

(Re ort Nos. 50-275/89-31

and 50-323/89-31

Areas

I*us ected:

The inspection

was

a special

inspection

conducted

pursuant to the discovery of

debris in the Unit I containment recirculation

sump

by the

NRC inspector.

Inspection

procedures

30703,

37700,

37828,

40500,

61726,

62703,

and

71710 were

used

as guidance

during the conduct of this inspection.

Results of Ins ection:

This inspection identified several. potential violations of regulatory

requirements

with respect

to the containment recirculation

sump

( sump).

The

potential violations identified include:

Failure to assure

that there

were

no gaps

in the Unit

1

sump screen

configuration.

Failure to assure

sump screen

configurations

consistent

with design

requirements.

Failure to assure

that the Units

1 and

2 sumps

were free of debris.

Failure to assure

that the Units

1 and

2 sumps

were not opened during

power operations.

Failure to update

the

FSAR.

Failure to report adverse

conditions

found during operation.

Additional concerns

which warrant licensee

management

evaluation:

The need to assure

consistently conservative

engineering

decisions.

Failure to identify sufficient acceptance

criteria for assuring

design

change construction

met design

requirements.

Failure to update

design drawings.

The

need to improve plant staff awareness

of the importance of

verification signatures.

DETAILS

Persons

Contacted

  • J.

D.

Townsend,

Plant Manager

"D.

M.

Miklush, Assistant Plant Manager,

Operations

Services

"M. J.

Angus, Assistant Plant Manager,

Technical

Services

~B.

M. Giffin, Assistant Plant Manager,

Maintenance

Services

  • M. G. Crockett, Assistant Plant Manager,

Support Services

~M.

D. Barkhuff, Acting equality Control Manager

"D. A. Taggert, Director equality Support

"M. J. Kelly, Regulatory Compliance Engineer

H. J. Phillips, Work Planning Manager

R. Washington,

Acting Instrumentation

and Controls

Manager

"J.

A. Shoulders,

Onsite Project Engineering

Group Manager

M.

E.

Leppke,

Engineering

Manager

S.

R. Fridley, Operations

Manager

~E.

C. Connell, Project Engineer

"M. T.

Rapp,

Chairman,

Ons1te

Safety

Review Group

"P. J. Roller,

System

Engineer

The inspectors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

"Denotes

those attending the exit interview on December 8,

1989.

2.

General

Overview

On October

17,

1989,

the inspector

inspected

the Diablo Canyon Unit 1

containment recirculation

sump.

The Unit was

shutdown for refueling and

in Mode 6.

The containment

sump

had been temporarily

covered with

plastic sheeting

as

a cleanliness

control

measure for the outage.

Consequently,

an inspection of the outer surface

was not possible

at the

time.

The inspector's

examination of the internals of the

sump revealed

debris (including a hacksaw blade

and

a

2 foot by 2 foot cloth) and

an

as-built condition different from that described

by the applicable

licensee

drawing and from that described

in the Final Safety Analysis

Report

(FSAR).

Specifically, the drawing and

FSAR show

a

sump with an

inner 3/16 inch mesh screen

in a "pup tent" arrangement

over each of the

two Emergency

Core Cooling System

(ECCS) suction pipes.

The inner screen

was found not to be installed in Unit 1.

The entire

sump is enclosed

in

steel

grating which is covered with an outer screen of 3/16 inch mesh.

On November

26,

1989,

the outer screen

was found to have openings,

tears

and gaps

(up to

1 inch wide by 5 foot long),

when the temporary

cleanliness

coverings

were

removed

and the outer

screen

and structure

were inspected

by licensee

personnel.

The debris

found in the

sump

and the missing inner screen

coupled with

gaps in the outer screen

for Unit 1 degraded

both trains of the emergency

2

core cooling system for the containment

sump recirculation

mode function.

The licensee

corrected

the configuration deficiencies of the Unit 1 sump,

cleaned

the debri-s

from the

sump

and verified by remote visual

examination (television)

and radiography that the emergency

core cooling

system piping (potentially affected

by the

sump debris)

was in fact

clean.

The licensee

also examined the Unit 2 sump

and found its as-built

configuration

as specified in the

FSAR and applicable

drawings.

The

licensee

found the Unit 2 sump to be clean but subsequent

inspection

by

the resident

found a minor amount of debris

(such

as

a one-half inch

tubing end cap) which was evaluated

as acceptable

by the licensee

due

to'ts

location, size,

and the presence

of the Unit 2 inner screen.

The

inspec'tor considered

the licensee's

evaluation 'to be acceptable.

The

debris

was not removed

because

the Unit was in an operational

mode which

precluded

opening the

sump door.

The Unit 2 emergency

core cooling pipe

potentially affected

by debris

was

examined

by radiography:

One nut was

found in the pipe and allowed to remain

when its size

was determined to

be small

enough to pass

through the residual

heat

removal

pump without

causing

damage,

and to be large

enough to be captured in the residual

heat

removal

(RHR) heat exchanger

and therefore

not detrimental

to

downstream

components.

The licensee

has instituted corrective actions to

improve and expand the existing procedural

instructions for verification

of the containment

sump cleanliness.

In addition,

as

a result of examinations

of the work done in the

sump, it

was determined that the Unit 1 containment

sump,

which has

an access

door

approximately

3 foot by 3 foot,

was

opened twice during the last

operating cycle while in operating

modes requiring emergency

core cooling

system operability.

Unit 2 likewise had its

sump access

door opened at

power at least

one time.

The

sumps

had

been

opened

on these

occasions

for approximately

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> periods to perform corrective maintenance

on

sump level indicators,

and there is

no documentation

that personnel

were

continuously stationed at the

sump location.

The breach of the

sump

barrier defeated

the debris protection function of the containment

sump

making the two trains of the emergency

core cooling system potentially

inoperable for greater

than the technical specification

maximum allowed

time of one hour.

Se

uence of Events

o

June

1974,

the Nuclear Regulatory

Commission

(NRC) issues

Regulatory

Guide 1.82.

The guide

recommends

redundant

sumps.

Oiablo Canyon's

design

was

90X complete at the time.

A licensee

analysis of the

Regulatory Guide, Pacific Gas

and Electric

(PG&E) file 140. 150 dated

July 25,

1974, states

the

sump is

a single structure divided at

sump

center line. It states

further that if one half of. the fine inner

screen

develops

a hole and thus

becomes

ineffective the redundant

system is still operable.

o

September

18,

1975,

Supplemental

Safety Evaluation Report

(SSER)

No.

3 was issued

by the

NRC.

In it, the

NRC staff concluded that the

design of the containment

sump

was acceptable.

The

NRC staff had

studied

the design at that time which consisted

of a coarse

outer

screen

(1/2 inch) and fine mesh inner screen

(3/16 inch) with

separate

cages

over each

pump suction.

In September

1980, Mestern

Canada Hydraulic Laboratories

Ltd.

performed

a study for

PGRE to assess

the probability of vortexing in

the containment

sump.

The configuration studied

was that of a

coarse

outer screen

(1/2 inch) and

a fine inner screen

(3/16 inch)

as originally designed.

The study concluded that the Diablo design

was satisfactory,

provided the inner screens

did not become heavily

blocked by debris'he

report

recommended

that the fine screens

be

moved to the outer structure.

o

February

1981,

design

change

DCO-EC-908 was issued to remove the

inner 3/16 inch mesh

screen

from both units and to add

a 3/16 inch

mesh screen

to the outside trash rack.

This was accomplished

on

Units

1 and

2 and represented

a departure

from the

NRC reviewed

configuration of the

sump.

o

On September

9,

1981,

a license for 5X power was issued for Unit l.

On November 19,

1981, the license

was

suspended

due to the

identification of improper seismic

design inputs.

o

Per the licensee,

in September

1984

an

FSAR update

was submitted

which erroneously left indication of an inner screen

on the

FSAR

contrary to the

1981 design

change.

o

November 2, 1984,

NRC issued

a Full Power License for Unit l.

o

November

7,

1984, Unit 1 achieved initial criticality.

o

April 23,

1985,

NRC issued

a

Low Power License for Unit 2.

o

April 24,

1985,

a Diablo problem control sheet

(DP-2-1193-C)

was

written noting gaps in the Unit 2 recirculation

sump.

o

On June

20,

1985,

the design

change for Unit 2 (DC2-SC-32446

Revision 1) issued to repair

the gaps

was signed off as complete

by

the field engineer.

The design

change

completion also reinstalled

the inner screen

assembly

due to the earlier fai lure to revise the

drawing specification for the inner screen.

Unit 2 now was in a

configuration

as

shown in the

FSAR.

August 20,

1985, Unit 2 achieved initial criticality.

On August 2,

1985,

an action request

(AR A3520) was issued to

inspect

the Unit 1 containment

sump for gaps greater

than 3/16 inch,

as

a result of the findings in Unit 2.

The inspection

was limited

to the problem areas

found -in Unit 2 and did not identify the gaps

later found in 1989.

The inspection resulted in the identification

and repair of two spots

on the

sump ends.

The personnel

did not

identify the absence

of the inner 3/16 screen

assembly

on Unit 1,

which had just been reinstalled

in Unit 2.

Unit 1 remained

different than the design

drawing and the

FSAR,

and apparently

had

outer screen

gaps at this time.

o

-May 1986,

SSER

No.

33 was issued evaluating allegations.

Allegation

No.

100 dealt with the lack of quality control for painting in the

containment.

The

NRC staff calculated

that the paints inside

containment

could generate

28.2 cubic feet of debris

in Unit 1.

The

NRC staff found the potential

debris acceptable

due to the

likelihood that paint debris

would not enter the

sump nor cause

loss

of "suction if it collected at the bottom of the outer

sump screen.

The

FSAR description of the

sump at that time showed

a containment

sump with an inner and outer fine screen of 3/16 inch and

a

construction

requirement of a maximum gap of 3/16 inch anywhere

on

the surface of the

sump.

o

June 30,

1987, temporary procedure

TP 8706, Revision 0,

was reviewed

by the Plant Staff Review Committee

(PSRC).and

accepted.

The

procedure

allowed the opening of the unit sumps

and adding of

borated water to check the accuracy of sump level transmitters'.

The

procedure

was approved for use

on October 6, 1987, after

a

10 CFR 50.59 evaluation.

The 50.59 evaluation concentrated

on the effects

of adding borated water to containment

including such

items

as the

effect of reduction of containment

volume

by the addition of 5000

gallons of water to the, sump.

Neither the 50.59 nor the

PSRC

apparently

recognized

the potential effects

on

sump operability with

the

sump hatch

open.

o

October

12,

1987, while the reactor

was in Mode 1, the Unit 2

containment

sump hatch

was

opened for approximately

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to

calibrate

the

sump level dete'ctor using

hoses

and

pumps in the

open

sump'TP

8706

was used;

work order

C0022698.

June

16,

1988, while in Mode 5, the Unit

1 containment

sump

was

verified clean, free of structural distress

and corrosion at the end

of the second Unit

1 refueling outage,

in a'ccordance

'with the

technical specification

and the licensee's

procedure

STP-M45

Revision 6, Containment Inspection.

The sign-off for the inspection

was completed

by

a licensed Senior Reactor Operator

(SRO)

and

mechanical

maintenance.

The

sump

was

inspected

from the outside of

the outer screen.

o

July 5,

1988, while in Mode 3, the Unit

1

sump

was

inspected

again

from the outside

and verified clean

by

a different licensed

individual.

o

September

7,

1988, the Unit

1 containment

sump

was

opened for about

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> while in Mode

1 to perform

a calibration of sump level

transmitter

LT940, in accordance

with work order

C 0038090.

PSRC

approved

temporary procedure

TP 8706 was

used to fill and empty the

sump with borated water.

During this time,

hoses

and

a

pump with

temporary lines were in the

sump

and

passed

through the

sump door.

On September

8, 1988,

the

sump

was verified clean.

The shift foreman

had authorized

contairment entry at 1:55 p.m.

on

September

7,

1989.

The pumping equipment

was

logged

as

removed at

1:30 a.m.

on September

8,

1989,

Licensee

personnel

at the exit

stated all such fill and

pump down operation would-be expected

to

take about

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> with the

sump hatch open.

o

Hay 11,

1989, while the reactor

was at 100K power operations,

the

Unit 1 containment

sump was again

opened for about

a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> period

to calibrate

sump level transmitter

LT940 per work order

C 0053302.

A verification of sump cleanliness

from the outside

was performed

by

maintenance

personnel

in this case.

The unit logs

show the level transmitter declared

inoperable at 5:42

p.m.

Based

on the conditions

found by the inspector

on October 17,

1989,

the

sump must have

had debris in it at the time of the

May 11,

1989

licensee verification of cleanliness

discussed

above.

o

October

17,

1989, the

HRC inspector

identified the absence

of the

Unit 1 inner

sump screen

and the presence

of debris inside the outer

sump screen consisting of:

one hacksaw blade,

12 x 1/2 x 1/32 inches,

one wiping cloth, yellow,

2 x 2 feet,

one piece of duct tape,

3 1/2 x 3 1/2 inches,

and

one piece of metal

banding material

12 x 3/4 x 1/64 inches.

o

October 19,

1989,

the Unit 2 contai'nment

sump

was examined

by the

licensee's

system engineer

from outside

the

sump.

The

sump

was

noted to have the inner screen installed.

The

sump

was found to be

free of debris.

o

October

19,

1989, the licensee

found that in February

1981,

design

change

OCO-EC-908

removed the inner screen

from both units.

The

design

drawing was not properly updated

and the inner screen

was

still shown in one View.

Consequently

as previously discussed

the

screen

was reinstalled

in Unit 2 in 1985.

o

October 21,

1989, the licensee

issued

a justification for continued

operation for Unit 2, recognizing the presence

of the inner screen.

Although this screen

was in accordance

with the

FSAR, the presence

of the screen

was not in accordance

with the 1981 design

change,

DCO-EC-908.

o

October

22,

1989,

the system engineer

performed

a walkdown of the

Unit 2 general

containment

area

looking for general. debris.

The

unit was at full power.

Although the areas

were generally clean,

small articles

were found at various locations

throughout the

containment.

Items included gasket material,

tape,

broken seal

material,

a paper towel, paint chips,

and other potential

flotsam.

The condition of Unit 2 at power is typical

and can

be expected

to

represent

that of Unit 1 as well.

Unit 1 was in a refueling outage,

therefore

the normal state of cleanliness

could be inferred from

that found in Unit 2.

o

November 1, 1989,

the

NRC Resident

Inspector in conjunction with a

licensee

health physics technician

examined the Unit 2 containment

sump which had been declared

clean

by the

PGEE staff.

The inspector

and the technician

found

a utility knife,

a tubing support bracket,

and

a 1/2 inch tubing cap.

All observed

items were larger than 3ll6

inch and.were

judged to be such that they ~ould be stopped

by the

inner

screen

which was installed

on Unit 2.

o

November 2, 1989,

licensee

personnel

inspected

the Unit 1 sump

suction piping for debris using

a television (T.V.) camera.

No

debris

was found.

o

November 4, 1989, Unit 2 recirculation

sump suction piping was

examined

by radiography.

One item was found in the horizontal

run

of piping.

The unit was in Mode 1 power operation

and the item

could not be removed without making

a sump entry, which would

potentially make both trains of the emergency

core cooling system

inoperable.

The item was. determined to be

a low density nut

(aluminum or plastic) of sufficient size to be caught in the

RHR

heat exchanger

and not pass

through.

The items presence

was

evaluated

to be acceptable

for continued operation

by the licensee.

Subsequently,

on November

5, the licensee

issued

a justification for

continued operation for Unit 2.

o

November 16,

1989,

Mestinghouse

provided to

PG8E

a containment

s'ump

debris evaluation (.letter

PGE 89-811) for the hacksaw blade,

wipe

cloth, 'duct tape,

and banding material

found in Unit 1.

The study

assumes

the entrance of the debris cannot

be precluded,

that only

one train of RHR is available

due to a single failure.

The study

concludes that the

RHR pump would likely not be affected.

However,

the wiping cloth and tape

(588 sq.

inches)

could significantly block

flow in the

RHR heat

exchanger

whose inlet tube sheet is 400 sq.

inches.

The cloth has

some porosity but the beneficial effect of

this was not quantified.

The study also indicated that the

RHR heat

exchanger

may have tube degradation

caused

by a piece of hacksaw

blade.

Mestinghouse

determined that other debris'pieces

could pass

through the 0.527 inch diameter

RHR heat

exchanger

tubes.

Mestinghouse

determined that this debris would not cause failure or

binding of the downstream safety injection (SI) or charging

pumps;

however, restart capability might be affected.

Mestinghouse

considered

small valves

(2 inch and smaller)

may become

blocked.

Mestinghouse's

engineering

judgement regarding the fuel was that any

debris trapped would not cause significant core flow blockage.

The study concludes

that the major system

impacts identified were

degraded

RHR flow due to heat exchanger

blockage,

degraded

ECCS flow

due to blocked valves, 'and degraded

hot leg recirculation flow due

to the inability of the SI pump to restart.

The subsequent

consequences

were evaluated

also, indicating long term containment

pressure

could increase significantly and increased

containment

temperatures

could affect environmental

qualifications.

Additionally, flow and

NPSH may be inadequate

causing catastrophic

pump

damage.

o

On November 17,

1989,

a Nuclear Operations

Support

memorandum to

Oiablo Canyon

Power Plant

(DCPP) Support Services

was issued.

The

memorandum

states

that an analysis of the risk significance of the

unavailability of the containment

sump during power operation

was

performed

by probabi listic risk methods.

The results

stated

the

increase

in the annual

core

damage

frequency

was approximately 9.2

E-8 for each

hour the

sump is unavailable

compared to"the total core

damage

frequency of 2.0 E-4 per year.

o

On November 18,

1989,

licensee

personnel

concluded

and told the

NRC

inspector that the expected

post

Loss of Coolant Accident (LOCA)

water level in containment

would be

6 feet

5 3/4 inches.

The height

of the outer

sump screen

is

5 feet

2 inches

per the as-built

drawing.

Therefore,

the top 'of the

sump would be under water and

an

open

sump screen

door could expose

the

RHR pump suction pipes to

debris,

should

a

LOCA occur.

o

November

21,

1989,

a letter was issued

from the

PG8E Project

Engineer to the Assistant Plant Manager for Technical

Services

stating that it was unlikely that the debris

found in the Unit 1

sump would have

a significant impact on safety,

based

on a review of

the Mestinghouse

assumptions

which apparently

were considered

by the

licensee 'to be overly conservative.

The letter indicated that the occurrence

of an accident

requi ring

the recirculation

sump

was

low.

The letter also indicated the

ingestion of the wiping cloth and tape

were not likely, even with

the missing inner 3/16,inch

mesh screen

due to the existing inner

grating.

The grating is typical walkway grating of egg crate design

made of 1', by 3/16 inch steel

spaced

1-3/16 inch center to center

with cross

bars

spaced

4 inches center to center.

The letter also

states

the probability of the metal pieces

being carried to the

piping inlet are

low.

The letter states

the rag will probably block

a small

area of the heat exchanger.

The letter further indicates

, that if a single failure is not assumed,

then the loss of one train

(due to debris) is tolerable.

The letter also indicates that for

the large break

LOCA the fai lure of the SI pumps to restart will not

be

a problem due to the ability of the

RHR system to provide flow to

a depressurized

RCS.

The

PGIIE letter concludes

that there

was not

a

significant risk.

o

November 21,

1989,

the licensee

made

a four hour

non-emergency Title

10 Code of Federal

Regulations

(CFR) Part 50.72 report regarding the

Unit 1 containment

sump:

The licensee

reported the presence

of the

debris

and reported their assessment

that it would be unlikely that

the debris would have

a significant impact on safety.

They also

reported the Mestinghouse

analysis results

except that, they took

cr edit for the availability of a second

RHR heat exchanger.

o

November 26,

1989,

the licensee

performed

an as-built inspection of

the Unit 1 containment

sump.

Gaps

were found which were present

since construction.

One gap,

about

1 inch wide by 5 feet long,

and

two gaps,

2 1/2 x 3 inches,

were the biggest identified.

Several

rips,

as large

as

1/2 x

2 1/2 inches,

in the outer screen

were

noted.

Other defects

such

as missing bolts were noted.

The specific results

are recorded

on licensee as-built sketches

SKC-43642-1

through SKC-43642-5.

Additionally, a section of structural

grating (which is used to

support the 3/16 inch screen)

was found missing.

The licensee

has

not yet assessed

the consequence

of the missing grating.

o

On November 28,

1989, the licensee

proposed

that the Unit

1

sump

configuration for restart of the unit should

be without an inner

3/16 inch screen.

Subsequent

to discussions

with NRC, the licensee

decided

to install the inner screen

and issued

design

change

DCI-EC-43770 to accomplish that task.

o

On December

1, 1989, the Unit

1

sump

had outer gaps

repaired

and the

inner screen reinstalled

by design

change.

On December

2, the

cleanliness

of the

sump

was personally verified by the Assistant

Plant Manager for Technical

Services

and quality control personnel.

o

On December

11,

1989 the licensee

provided

a preliminary assessment

of the consequences

of the as-built gaps

found on November

26 in the

Unit

1 containment

sump outer screens.

The licensee

concluded that

there

had

been

no significant risk of system

damage

due to debris

larger than 3/16 inch being able to pass

through the outer screen

gaps.

The licensee's

conclusior

was

based

on their procedural

requirement to maintain

a clean containment

and

an assessment

of

accident related debris

such

as paint and insulation.

The licensee

subjectively judged that paint ingestion

would not have noticeable

effects,

nor would increased

ingestion of calcium silicate

insulation.

The licensee

did not plan to have Westinghouse

perform an analysis

of the potential

consequences

of the as-found outer screen

gaps.

The licensee

planned to finalize their own analysis

in the

nonconformance

report written for the containment

sump concerns.

o

On December

14,

1989 the licensee

provided

a copy of an emergency

procedure

(ECA-1. 1) which provides contingencies

for operator action

to mitigate the consequences

of a

LOCA with the "Loss of Emergency

Coolant Recirculation".

This procedure

provides actions

to restore

emergency

coolant recirculation capability, to delay depletion of

the

RWST by adding

makeup

and reducing outflow, and to depressurize

the

RCS to minimize break flow.

Summar

of Concerns

Overall this inspection

has

demonstrated

weaknesses

in the implementation

and maintenance

of design

bases,

and the conduct of safety related

surveillances.

The licensee

should give consideration

to assessing.

the

causes

of the following problem areas,

including an assessment

of the

potential

breadth of the errors

which occurred in their respective

timeframes.

a

~

Potentiall

Ino erable

Emer enc

Core Coolin

S stems

Diablo Canyon technical specification 3.5.2 requires

two emergency

. core cooling sub-systems

be operable

including an operable

flow path

from the containment

sump during the recirculation

phase of

operation.

The. two emergency

core cooling systems

in Unit

1 appear to have

been

degraded

since initial star tup on November 7,

1984 because

of the

gaps in the outer

sump screen.

This is

a potential violation.

b.

Potential

Sum

Inner Screen

Discre ancies

c

~

The Unit

1 inner screen configuration

was different from that in the

FSAR and that of Unit 2.

The acceptability of the various

screen

configurations

should

be assessed

and specified

by the licensee

so,

that there is

no confusion

on the

sump design

bases,

function,

and

operability.

This is

a potential violation.

Potentiall

Unacce table Verification of Sum

Cleanliness

.

Technical specification

4 .5.2.c requires

a visual inspection

be

performed to verify that

no debris is present

which could cause

restrictions of the emergency

core cooling system

(ECCS) suctions

during

a loss cf coolant accident

(LOCA).

Loose debris

including

a hacksaw blade

and wiping cloth were found

in the Unit

1 containment

sump

by the

NRC inspector

on October

17,

'989.

The debris

could cause restrictions of the

ECCS suctions

durino

a

LOCA.

The

sump

had

been

inspected

arid verified cleari by

licensee

personnel

on May'l, 1989.

This is

a potential violation.

d.

Potential

Failure to Declare

Emer enc

Core Coolin

S stem

Ino erabi it

Technical specification 3.5.2 requires

two emergency

core cooling

subsystems

be operable

in Miodes 1,

2 and 3, including an operable

flow path from the containment

sump during the recirculation

phase

of operation.

If both trains of the Emergency

Core Cooling System

(ECCS) are inoperable,

technical specification 3.0.3 applies,

and

requires that within

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action

be initiated to place the unit in

a mode in which the action statement

doesn't

apply.

The tm

ECCS subsystems

were potentially not operable

while in Mode

1 for about

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

each

on October

12,

1987 for Unit 2 and

on

Sept. ember 7, '1988 an) May 11,

1989 for, Unit

1 and action

had not

been initiated to place

the Units in a mode where the action

statement

does

not apply.

Th'is condition

was

due to the opening of

the containment recirculation

sump screened

access

hatch to allow

the addition of and subsequent

pump

down of borated water with hoses

for the calibration of the

sump level detectors.

This is

a

potential violation.

e.

Potentiall

Non-Conservative

En ineerin

Decisions

'0

The inspector

concluded that the licensee's

engineering

decision to

remove inner

sump screens

in 1981 appear

to have

been

a

non-conservative

engineering

decision which did not fully consider

basic

defense

in depth strategy defined

by

NRC requirements

and

guidance.

Further,

the inspector

concluded that the licensee's

preliminary engineering

decision to return Unit

1 to

power after

refueling without an inner

sump screen

in place

may have likewise

been

a non-conservative

engineering

decision in regard to thoroughly

evaluating

the need for defense

in depth.

Potential

Failure to

S ecif

Construction

Desi

n Chan

e Acce tance

Criteria

To implement

a design

change

in 1981, prior to lice'nsing,

the method

used to maintain configuration control was:

o

To issue

a design

change.

o

Construction

would formulate

a work package

based

on applicable

specifications

and general

construction

procedures.

o

After construction,

inspection

would occur against

the

specifications

and procedures.

o

Construction

would generate

detailed as-builts of the

modification.

o

Engineering

would receive,

review,

and accept as-built drawings

and incorporate

them into the applicable

design

drawing.

This was the process

used for the relocation of the

sump screens

done in 1981.

The design

drawing was not properly updated

in that

reference

to the inner 3/16 inch mesh

screen

was not removed in one

detail

o< the design

drawing 443259,

Revision 4, issued

t1arch

16,

1981,

The

1981 desion

change

process

reflected

a practice

not totally

uncommon in the 'early 1980s of field design followed by engineering

analysis

and approval or modification if required.

ln the case of the containment

sump,

the critical construction

parameter

("The

max gap opening

anywhere

on the surface of the

sump

shall

be 3/16.")

was not defined

by engineering for the field unti 1

December

15,

1986

when Revision

8 of the containment

sump drawing

443259

was issued.

The revision

was issued at that time to reflect

the Unit 2 design

changes

of 1985

made to close

the gaps.

As

explained

in the sequence

of events,

the licensee

missed

the

opportunity to discover

and correct the Unit

1 gaps

in 1985.

The apparent failure to specify adequate

construction

acceptance

criteria for the containment

sump screen

gaps

led to the as-built

condition discovered

in 1989 of large

gaps

in the outer screen.

E

g.

Potential

Failure to Pro erl

U date

Desi

n Documents

The failure to properly update

the design drawing for the

containment

sump led to the reinstallation of inner screens

in Unit

2 in 1985.

h.

Potential

Failure to

U date the

FSAR

The failure to update

the

FSAR description

and drawings of the

containment

sump pursuant

to 1981 design

changes

led to faulted

assessments

of the

sumps

design

bases

on the part of the licensee's

engineering

personnel

and

NRC reviewers.

This is

a potential

violation.

l!

Potential

Failure to

Re ort Adverse Conditions

Found Durin

~0ereti on

The April 25,

1985 problem report for Unit 2 and the August 2,

1985

action request for Unit

1 were both issued after licenses

were

issued for the units.

The problems identified reflected

on the

operability of the

ECCS system but were not reported to the

NRC.

This is

a potential violation.

j.

Potential

Failure to Perform Proper

Ins ections

and Ins ection

~Si

no, fe

A number of relatively recent occurrences,

in addition to the

1985

failure to 'identify sump screen

g'aps,

indicate that plant personnel

performing inspections

and sign-offs in procedures

were not

performing their duties in a precise

manner

and were'aking

broad

and non-conservative

interpretations

of the verification statements

of procedures.

For example

on June

16,

1988 the containment

sump and

RHR suction

piping was verified clean

and free of structural

distress

and

corrosion

by mechanical

maintenance

and senior operator

licensed

personnel.

The procedure

annotations

indicate the inspection

was

performed

from outside

the

sump by flashlight.

The inspector

found

it difficult to 'assure

an adequate

inspection of the

RHP, piping in

this case

given the screening

and grating visual interferences

and

the distances

involved.

Although no debris

was found in the pipe in

1989 inspections

by remote television devices,

the inspection

performed in 1988

was not suitable to attest to piping cleanliness.

The

same

method of inspection

was again

used

and the

same

inadequate

verification was

made

by

a different licensed individual

on July 5,

1988,

On Nay 11,

1989 the cleanliness

of the

sump

was attested

to by

maintenance

personnel

after level indicator calibration.

Licensee

evaluation indicates that the debris later found in October

1989

was

in the

sump at this time.

Previous

inspector findings such

as the violation issued for a

QC

inspector attesting

to

a valve cleanliness

without visually

inspectino

the valve body (50-275/88-03)

and current problems with

misaligned valves which had

been verified and signed for by

12

operators, 'indicate that the proper instincts to precisely perform

. verifications

have not consistently

been demonstrated

by personnel-

at Diablo Canyon.

Descri tion of Safet

Functions

The Diablo Canyon

FSAR section 6.2.3.2.2:1

describes

the containment

recirculation

sump.

It states

that the

sump is

a large collecting

reservoir designed

to provide

an adequate

supply of water with a minimum

amount of particulate matter to the safety injection system,

the charging

system,

the residual

heat

removal

system,

and the containment

spray

system during the recirculation

mode of emergency

core cooling system

operation following a loss of coolant

accident."'he

FSAR states

the-sump is approximately

50 feet from components

that

could become

sources

of debris.

It further states

a baffle arrangement

surrounds

the

sump to prevent floating debris,

high density particles

or

anything larger than 3/16 inch from entering the

sump.

It states

that

the two )4 inch suction pipes are located

on opposite

sides of the

sump

to prevent

any unforeseen

blockage of one from affecting both containment

spray trains.

The

FSAR indicates

that the fluid from .the

sump

passes

into the

14 inch

residual

heat

removal'(RHR)

pump suction piping.

The flow passes

through

the

RHR pumps to the heat exchangers.

The flowpath continues

to the

suction of the safety injection system

(SIS)

pumps.

The SIS

pumps

discharge

to the hot legs of the reactor coolant system

(RCS), irito the

core

arid out through the ruptured

RCS loop onto the containment floor and

to the containment

sump.

The

FSAR describes

the flowpath to the centrifugal charging

pumps

similarly from the

RHR heat exchangers

to the suction of the charging

pumps to the cold legs of the

RCS.

The

FSAR describes

the

RHR flow path similar to the flow path from

the'HR

heat exchanger

to the cold or'hot legs.

The

FSAR describes

the flowpath to the containment

spray system

similarly.

The flow continues

'from the

RHR heat

exchangers

to the

containment

spray

headers-

and out the 3/8 inch spray nozzles.

In

recirculation

mode,

the

RHR pumps instead of the Containment

Spray

(CS)

pumps are

used for motive force.. The screen

mesh size of 3/16 inch for

the

sump screens

was sized to preclude plugging of the 3/8 inch spray

nozzles.

Redundanc

of the

Sum

The

FSAR section 6.2,3.3.7

in discussing reliability states:

"To ensure

that the failure of a portion of the protective screen

a'ssembly

(Figure 6.2-11) will not negate

the effectiveness

of the

ensnare

assembly,

separate

outer and inner assemiblies

are provided.

In addition,

the inner assembly contains

a steel divider that

prevents

a hole in the screen

assembly

over one

RHR pump suction

13

pipe from influencing the effectiveness

of the screen

over the

redundant

pipe."

Figure 6.2-11 of the

FSAR shows 3/16 inch wire mesh installed

on the

outside

sump structure

(refe'rence

Section

A, Elevation

B, Section

E and

Detail 2)

and 3/16 inch wire mesh installed

on the inner wedge grating

structure

(reference

Detail 1).

Note

6 of the drawing states,

"The max

gap opening

anywhere

on the surface of the

sump shall

be 3/16."

Section

G of the drawing

shows

1/4 inch steel

plate dividing the inner

sump

assembly

into two separate

assemblies.

Consequently,

the inspector

concluded that

( 1) the

FSAR describes

functionally redundant

design features

of the containment

sump,

and (2)

this appears

to be,a desirable

feature which was

an important

consideration

in the

NRC review of containment

sump design.

The

NRC standard

review plan

(SRP) for Safety Analysis Report

(SAR)

review states

that the containment

system

branch

(CSB) will:

"CSB reviews the system provided to allow drainage of containment

spray water

and emergency

core cooling water to the recirculation

suction points

(sumps).

CSB reviews

the design of the protective

screen

assemblies

around

the- suction points.

CSB reviews plan

and

elevation

drawings of the protective screen

assemblies,

showing the

relative positions

and orientations of the trash

bars or grating

a'nd

the stages

of screening,

to determine that the potential for debris

clogging the screening

is minimized.

CSB also

reviewst the drawings

to determine that suction

pints

do not share

the

same

screened

enclosure.

The effectiveness

of t e protective screen

assem

y will

be determined

by comparing

the smallest

mesh size of screening

provided to the clogging potential of pumps,

heat exchangers,

valves,

and spray nozzles.

The methods of attachment of the trash

bars or grating

and the screening

to the protective

screen

assembly

structure

should

be discussed

in the

SAR and

shown

on drawings.

A

discussion of the adequacy

of the surface

area of screening

with

respect

to assuring

a low velocity of approach of the water to

minimize the potential, for debris

in the water being

sucked against

the screening

should

be presented.

Regulatory

Guide 1.82 (Ref.8)

represents

guidelines for the acceptability of the design of

containment

sumps."

(Underlining added)

Regulatory

Guide 1.82

"Sumps for Emergency

Core Cooling and Containment

Spray Systems

issued

in June

1974 states

as part of its guidance:

"Redundant coolant

sump screens

and

pump suction pipes

should

be

separated

as uuc

as prac~tica

to reduce

the possihi'lity that

a

partially c ogged

screen

or missile

damage

to one screen

could

adversely affect other

pump circuits."

(Underlining added)

In addition,

10 CFR 50 Appendix

A General

Design Criteria, Criterion 35,

Emergency

Core Cooling requires

a system to provide "abundant

emergency

core cooling,"

The criterion requires:

14

"Suitable redundancy

in components

and features,

and suitable

interconnections,

leak detection, isolation,

and containment

capabilities

shall

be provided to assure

that for onsite electric

power system operation

(assuming offsite power is not available)

and

for offsi te electric

power system operation

(assuming

onsite

power

is not available)

the system safety function can

be accomplished,

assuming

a single failure."

Likewise, Criterion 38, Containment

Heat Removal, requires

a system

be

provided to remove heat

from the containment

and also specifies that

same

redundancy

and protection against single failure requirements.

The definition of single failure provided in 10 CFR 50 Appendix

A as it

deals with passive

components

like the containment

sump states:

"A single failure means

an occurrence

which results, in the loss of

capability of a component to perform its intended safety functions.

Fluid and electric

systems

are considered

to be designed

against

an

assumed

single failure if neither

( I) a single failure of

any active component....

...nor (2)

a single. failure of a passive

component

(assuming active components

function properly), results

in

a loss of the capability of the system to perform its safety

functions."

A referenced

footnote states

however:

"The conditions

under which

a single failure of a passive

component

in

a fluid system

should

be considered

in designing

the system

against

a single failure are under development."

It was clear to the inspector that the single failure conditions

applicable to the containment

sump were develo

ed

and defined in

Regulatory

Guide 1.82 specifying "redundant

coo ant

sumps

screens,

separated

as

much

as practical."

Since the Diablo

FSAR described

"redundant

sump screens,

separated

as

much

as practical," the information available

to

NRC reviewers

indicated

that Diablo Canyon

was to implement

NRC requirements

and guidance for

redundancy

and separation

of containment

sump screens.

Further,

the

FSAR

indicated that the licensee

was to provide. defense

in depth against

possible

screen failure and the incapacitation of two trains of emergency

core cooling.

On December 8,

1989

an exit meeting,was

held with the licensee's

representative

identified in paragraph

1.

The inspector

summarized

the

scope

and findings of the inspection

as described

in this report.