ML16341E685

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Insp Repts 50-275/88-13 & 50-323/88-12 on 880509-13.No Violations or Deviations Noted.Major Areas Inspected:Vital Areas & Equipment,Licensed Operator Training,Spurious Containment Ventilation Isolations & Followup of Open Items
ML16341E685
Person / Time
Site: Diablo Canyon  
Issue date: 05/26/1988
From: Burdoin J, Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E684 List:
References
50-275-88-13, 50-323-88-12, GL-88-03, GL-88-3, IEB-85-001, IEB-85-1, IEB-88-003, IEB-88-3, NUDOCS 8806100139
Download: ML16341E685 (12)


See also: IR 05000275/1988013

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report Nos. 50-275/88-13,

50-323/88-12

Docket Nos. 50-275,

50-323

License

Nos.

DPR-80,

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street

Room

1451

San Francisco,

California

94106

Facility Name: Diablo Canyon Units

1 and

2

Inspection at: Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Condu

ed:

y 9

,

19

Inspectors:

.

F.

B rd in, Reactor Inspector

Approved by:

N. N. Nendonca,

Chief

Reactor Project Section

1

Date Signed

~-/w g

/s'8'ate

Signed

~Summar:

Ins ection Durin

Period of Na

9-13,

1988

Re ort Nos. 50-275/88-13

an

- 2

8-

Areas

Ins ected:

An announced

inspection

by .one regional

inspector of

various vita

areas

and equipment in the plant, licensed operator training,

spurious

CVIs, and follow-up of open items

and bulletins/generic letters.

Inspection

Procedures

Nos.

71707,

41701,

90712,

92701,

92703,

61726

and 30703

were used

as guidance for the inspection.

Results:

No violations or deviations

were identified..

The licensed operator

tra>

>

gnpnrogram

was weil planned,

documented

and acceptably

implemented.

The

licensee's

short term and .long term programs

to correct spurious

Containment

Ventilation Isolations

(CVIs) were adequate.

SS06100139

SS0526

PDh

ADOCK 05000275

9

D'

DETAILS

1.

Individual s Contacted

Pacific

Gas

and Electric

Com an

(PGSE)

.

  • J

D

J. A.

  • W. M.

. T. A.

S.

R.

  • T. L.

S.

W.

S.

D.

J.

N.

P.

W.

D.

D.

R.

C.

M. T.

J.

E.

J.

M.

W. J.

J.

R.

L. R.

Townsend,

Plant Manager

Sexton,

Plant Superintendent

McLane, Acting Assistant Plant Manager,

Technical

Support

Bennett, Assistant Naintenance

Manager

Fridley, Senior Operating Supervisor

Grebel,

Regulatory Compliance Supervisor

Hamilton,

Power Production Engineer

Wilson, Regulatory Compliance

Engineer

Neill, Document Control, Super visor

Provence,

Records Analyst

Malone, Regulatory Compliance

Engineer

Washington,

Senior

Power Production

Engineer

Hug, Regulatory Compliance Engineer

Molden, Operator Training Supervisor

Becerra,

Senior Training Instructor, Operations

Kelly, Regulatory Compliance

Engineer

Hinds, Regulatory Compliance Engineer

Exner, Training Administrative Supervisor

Various other engineering

and quality control personnel.

  • Denotes attendees

at exit meeting

on May 13, 1988.

2.

Area Ins ection

71707)

An independent

inspection

was conducted

in Units

1 and

2 Turbine and

Auxiliary Buildings.

The inspection

examined

areas

and equipment for

debris, potential

hazards, oil and water leakage,

and equipment

condition, e.g., oil level, valve position,

and electrical

connection

configuration

and cleanliness.

The equipment

and areas

inspected

included:

A.

Five Emergency

Diesel

Generator

Rooms.

B.

Six 4160 Volt Switchgear

Rooms.

C.

Combined Two-unit Control

Room.

D.

Two Containment Spray

Pumps (Unit 2).

E.

Three Charging

Pumps (Unit 2).

F.

Four Safety Injection Pumps.

G.

Four Residual

Heat Removal

Pumps

H.

Five Component Cooling Water Pumps.

. I.

Six Auxiliary Feedwater

Pumps.

J.

Six Emergency Battery Rooms.

K.

L.

N.

N.

0.

p.

Six 480 Volt Vital Bus

Rooms

Two Cable Spreading

Rooms.

Two Hot Shutdown

Panel

Areas.

Two 480 Volt Load Center Areas.

Turbine Building at Elevations 85'nd

140'W/GE

Penetration

Areas Units

1 and

2 at Elevations 100'nd

85'Unit

2 only)

Housekeeping

and equipment status

appeared

to be acceptable.

No violations or deviations

were identified.

3.

Licensed

0 erator Trainin

41701

This is

a continuation of inspection in the area of licensed operator

training first reported in Inspection

Report Nos. 50-275/88-06

and

50-323/88-06.

The inspector

examined recent performance

evaluations

and documentation

of requalification training for six licensed operators

selected

as the

inspection

sample.

1)

The simulator performance

evaluations

examined

appeared

to be

thorough,

comprehensive

and included evaluation

in how well the

trainee

understood

the subject/system

of concern,

alertness

to react

to simulated plant conditions,

thoroughness

in correcting simulated

abnormal

conditions.

The trainee

was also evaluated for his ability

to function as

a team in correcting simulated

abnormal

plant

accident conditions.

2)

The requalification program is scheduled

over

a period of one year.

The

1986 program which extended

well into 1987 year was made-up of

seven six week sections.

Each section

covers

a particular series of

courses

such as:

Industry events,

procedure(s)

revisions, licensing

event reports,

fundamentals,

plant systems,

general

employee

training, simulator operations,

design

change notices, etc.

The

operators

are rotated every five weeks to spend

one week in

requalification training.

Periodic written examinations

are

required in this training program.

The inspector also reviewed the process

that

a trainee

who fails an

examination

must follow in order to take

a makeup examination.

The

training instructor(s) identifies for the trainee,

areas of weakness

where additional self study is required of the trainee before

a

makeup examination will be administered.

A makeup examination is

required to be taken

and

passed within twelve weeks following the

failed examination.

It is concluded that the licensed operator training met and satisfied

the

requirements

of Section

13 of the

FSAR. It is further concluded that the

licensee's

licensed operator training program is well planned,

documented

and acceptably

implemented.

This item is closed.

No violations or deviations

were identified.

~

'

S urious Containment Ventilation Isolations

90712

Spurious

containment ventilation isolations

(CVIs) have

been

an ongoing

problem in both units since the plants first went operational.

The

causes

of the CVIs have

been identified as voltage spikes that have

occurred

on both the power circuits to the containment vent-radiation

monitors

and the signal circuits from the detectors.

Some of these

voltage spikes

are switching generated

spikes.

Short term corrective measures

to reduce

the CVIs have

been to replace

the C-14,

1 microfarad capacitor with a ten microfarad capacitor in the

input circuit of the rate meter of the radiation monitors.

This

modification was performed under

DCN, DC2-OJ-40119 in Monitors RE-ll, 12,

14A, 14B,

28A 28B for Unit 2 during the first refueling outage in the

summer of 1987.

The modification did reduce

the number of spurious

containment ventilation isolations for Unit 2 that were initiated from

voltage spikes

on the signal circuits.

The

same modification is being performed

under

DCN, DC1-0J-39119,

on Unit

1 containment ventilation radiation monitoring system during the present

(second)

refueling outage.

It is expected that

a similar reduction of

spurious

containment ventilation isolations will result from this

modification.

The licensee is continuing to review and evaluate different techniques

for reducing/eliminating voltage spikes

on the power circuits of the

radiation monitoring system.

The licensee's

long term corrective

program for this problem is to

purchase

and install

a new containment ventilation radiation monitoring

system.

This corrective action has

been initiated; and to date the

specifications for the

new system

have

been developed

and written.

The

next step is to go out for competitive bid.

This corrective

program

has

a five year period associated

with it, so completion of the program is

expected

during the early nineteen nineties.

Based-on this review the

following LERs which reported

spurious

CVIs for Unit 1 are closed:

88-05-LO and 88-10-LO.

Based

on an in-office review, the following LERs were closed

out by the

project inspector during this inspection; 87-05-Ll (Unit 2) and 87-15-L1

(Unit 2).

.The

LERs were reviewed for event description,

root cause,

corrective actions

taken,

generic applicability and timeliness of

reporting.

No violations or deviations

were identified.

Closed

50-275/87-01-02,

Control Of U -to-Date Vendor Manuals

92701

Follow up of this item showed that phase

one of the updating of vendors

manuals

program (vendor manual

review program)

scheduled for completion

by June

1,

1988 was

on. schedule.

Phase

One consists

of an integrity

check of current information for approximately eighty vendors

manuals,

selected

by plant personnel.

Those manuals

were given top priority for

~

'

updating

because

of the importance of this equipment to plant safety

and

operations.

Phase

Two of vendor manual

review program initiated during February

1988

consisted of an evaluation

by the various engineering disciplines of

Nuclear Engineering

and Construction Services

to ensure vendors'anuals

for all Class

I (safety related)

equipment will be identified and

made

available to Diablo Canyon

Power Plant

Document Control.

The scheduled

target date for identifying all the vendors

manuals

was the middle of

Hay.

A review of the present

status of this phase of the vendor manual

review program

has revealed that

Phase

Two was

on schedule.

Phase

Three of the vendor manual

review program

was in the stage of being

developed

and implemented.

Part of this phase

as

proposed

was to

continue the level of review being conducted

on Phase

One material

through

Phase

Two (safety related) materials

on an acceptable

schedule.

This phase of the program also proposed

a system to ensure that complete,

accurate,

and current vendor materials

are maintained

and available for

all plant equipment

and components.

The inspector

concluded after examining the licensee's

program for

control of up-to-date

vendor manuals that the licensee's

actions

were

sufficient. This item is closed.

No violations or deviations

were identified.

6.

Follow-u

of Bulletin(s

and Generic Letters(s

(92703

A.

Closed)

50-275/323

NRC Bulletin 88-03 "Inade uate Latch

En

a ement

ln

~om an

e

atc

sn

e

a

s

anu acture

enera

ectric

This Bulletin requested

licensees'o

perform inspections

to ensure

that all

GE latching-type

HFA relays installed in Class

1E

applications

have adequate

latch engagement,

and that those relays

which failed to meet acceptance

criteria be repaired or replaced.

The licensee's

letter (DCL-88-098) of April 21,

1988 stated that the

HFA type latching relays

noted in the Bulletin were not used in

Class

1E applications at Diablo Canyon Units

1 and 2.

The inspector

examined

the latest version of the licensee's

"Equipment Restricted

From Nuclear Safety Applications"

(NPAP

D-11/NPG 4.5) which identified the

GE

HFA type latching relays

and

source

document

as

NRC Bulletin 88-03.

NPAP D-11/NPG 4.5 was

established

'to identify and control the use of equipment not

acceptable

for use in Nuclear Safety Application.

The licensee

response

and actions

were acceptable.

This Bulletin is closed for Units

1 and 2..

S

~

'

B.

Closed

Generic Letter 88-03,

"Steam Bindin

Of Auxiliar

Fee water

F

um

s

This issue

was inspected

in the field in April 1986 in response

to

IE Bulletin 85-01,

and

was reported

and closed in Inspection Report

50-275/86-12

and 50-323/86-13

dated April 24,

1986.

The inspector conferred with the licensee

and determined that the

requirement for the operator to perform

a manual

temperature

check

of the auxiliary feedwater piping each shift remained in effect,

and

was included

on the auxiliary operators'rounds

sheet."

Also the

installation of temperature

sensors

on each

AFW pump discharge

piping for continuous monitoring of temperature

had

been

completed

for both units.

Alarm annunciation

occurs

on annunciator 'window

PK-0916 in the control

room if the pipe fluid temperature

reaches

200'F.

The annunciator

response

procedure

to window PK-0916

directed the plant operator to vent the

AFW piping (and

pump casing,

if necessary)

should

leakage

occur.

The temperature

sensors

and

annunciator

response

procedures

satisfied

the recommendation for

recognizing

steam binding and for restoring the

AFW system to

operable status,

should

steam binding occur.

This Generic Letter is closed for Units

1 and 2.

No violations or deviations

were identified.

7.

Reactor Tri

S stem Instrumentation

Technical

S ecifications

TS)

Survei

ance

61

The inspector assisted

the resident inspector in a meeting with the

licensee

and reviewed the time (frequency)

requirements

to satisfy

TS

Surveillance 4.3.1.2 for the three channels

of steam generator

level

transmitters

used in the reactor trip system (Unit 1).

This issue

was

not completely resolved

so will be reported in detail in the resident

inspectors

report(s)

50-275/88-11

and 50-323/88-10.

8.

Exit l1eetin

30703

The inspector

conducted

an exit meeting

on May 13, 1988, with the members

of the plant staff as indicated in Paragraph

One.

During this meeting,

the inspector

summarized

the scope of the inspection activities

and

reviewed the inspection findings and described

in this report.

The

licensee

acknowledged

the concerns identified in the report.

'I