ML16341E652

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Insp Repts 50-275/88-07 & 50-323/88-07 on 880306-0409.Three Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items,Lers & Selected Independent Insp Activities
ML16341E652
Person / Time
Site: Diablo Canyon  
Issue date: 05/05/1988
From: Johnston K, Mendonca M, Narbut P, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E651 List:
References
50-275-88-07, 50-275-88-7, 50-323-88-07, 50-323-88-7, NUDOCS 8805230102
Download: ML16341E652 (36)


See also: IR 05000275/1988007

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos.

50-275/88-07

and 50-323/88-07

Docket Nos.

50-275

and 50-323

License

Nos.

DPR-80

and

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

Cali fornia

94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis,Obispo County, California

Inspection

Conducted:

Inspectors:

L.

M. Padovan,

Resident

Inspector

K.

E. Johnston,

Resident

Inspector

P.

P. Narbut, Senior Resident

Inspec or

Approved by:

M.

M. Mendonca,

Chief, Reactor Projects

Section

1

Date Signed

WQ~r EI

Date Signed

Date Signed

~A'"ls s-

Date Signed

~Summer:

Ins ection from March 6 throu

h

A ril 9

1988

Re ort Nos.

50-275/88-07

and

50-323/88-07

Areas Ins ected:

The inspection

included routine inspections of plant

operations,

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

37700,

60710,

61726,

62703,

71707,

71709,

71710,

71881,

73753,

92700,

92701,

93702,

and

94703 were applied during this inspection.

Results of Ins ection:

Three violations were identified.

SS05230i02

SS0505

PDR

ADOCK 05000275

9

DCD

DETAILS

Persons

Contacted

"J.

D. Townsend,

Plant Manager

"J.

A. Sexton, Assistant Plant Manager,

Plant Superintendent

"J.

M. Gisclon, Acting Assistant Plant Manager,

Support Services

"W.

B. McLane, Acting Assistant Plant Manager,

Technical

Services

C.

L. Eldridge, equality Control Manager

"S.

G. Banton,

Engineering

Manager

  • M. E.

Leppke,

Onsite Project Engineer

"K.

C.

Doss, On-site Safety

Review Group

"T. A. Bennett, Assistant

Maintenance

Manager

"0.

A. Taggart, Director, guality Support

M. J.

Angus,

Work Planning

Manager

W.

G. Crockett,

Instrumentation

and Control Maintenance

Manager

"J.

V. Boots,

Chemistry and Radiation Protection

Manager

L.

F.

Womack, Operations

Manager

"T ~

L. Grebel,

Regulatory

Compliance Supervisor

"S.

R. Fridley, Senior Operations

Supervisor

G.

M. Burgess,

Senior

Power Production Engineer

The inspectors

interviewed other licensee

employees

including shift

foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

"Denotes

those attending the exit interview on April 8, 1988.

0 erational

Status of Diablo Can

on Units 1 and

2

Plant Status

Unit 1 shutdown for its second refueling outage

on March 6,

1988.

The

refueling outage

has proceeded

throughout the reporting period and

included

some problems

such

as

an excessive

pressurizer

cooldown,

overpressurization

of the

RCDT, discovery of a

CROM weld leak,

and hot

particle discoveries

discussed

later in this report.

During this report

period the licensee

performed

a forced oxygenation of the

RCS,

successfully

drained to midloop and installed

SG nozzle

dams,

completed

core offloading, and commenced

s'team generator

eddy cur rent inspection

and tube heat treatment.

Unit 2 restarted

on March 6, 1988 (after a March 3,

1988 reactor trip

discussed

in report 50-323/88-04).

Power operations

continued through

the reporting period except for planned periodic reductions

for turbine

valve testing.

During the report period

NRC activities included inspections

and

examinations

by

NRC specialists

in fire protection, radiological

controls, security,

and

a seismic review team.

Results of those

inspections

and examinations will be reported separately.

3.

0 erational

Safet

Verification

71707

and 71710

~

~

a.

General

During the inspection period,

the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on

a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas

of the facility to

observe

the following:

(a)

General

plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

No violations or deviations

were identified.

4.

Onsite

Event Follow-u

93702

'a 0

Ver

Hi

h Radiation Barrier Doors Unlocked

On March 9,

and on April 1, 1988, the licensee

discovered

very high

radiation barrier doors unlocked.

Technical Specification 6. 12.2

requires that areas

accessible

to personnel

with radiation levels

greater

than

1000 mR/h be provided with locked doors

and that those

doors

remain locked except during periods of approved

access.

Exposure histories of personnel

in the area

were checked

and

no

unusual

exposures

were found.

As corrective action,

the licensee

has initiated independent verification of very high radiation

barrier locking following entry and exit.

The resident inspector

notified regional specialists

for followup.

This issue will be

addressed

in a separate

inspection report.

Unit 1 Pressurizer

Cooldown

On March 10,

1988,

the Unit 1 pressurizer

was inadvertently cooled

down at a rate exceeding

Technical Specification 3.4.9.2

maximum

cooldown of 200

F in any one hour period.

The event occurred

when

the licensee

injected the 20,000

ppm boron Boron Injection Tank

(BIT) inventory.

The root cause for the cooldown was determined to

be that Operations

Procedure

L-5, "Plant Cooldown from Minimum Load

to Cold Shutdown" did not restrict the injection flow rate.

Without

the flow rate restriction,

the pressurizer

heaters

were not able to

maintain

a cooldown of less

than

200

F with the temperature

difference

between

the

RCS and pressurizer

greater

than

200

F.

As corrective actions,

in addition to revising

OP L-5 and reviewing

other operating procedures

and surveillance tests for similar

concerns,

the licensee

requested

Westinghouse

to perform an

evaluation of the above event to demonstrate

pressurizer operability

as required

by TS 3.4.9.2, prior to entry into Mode 4 (Hot

Shutdown).

Preliminary information indicates that there is adequate

mar gin.

An action plan was established

for this event which appeared

to the

inspector

to be comprehensive.

This event

was determined

not to be

reportable

under

10 CFR 50.73 since the licensee

remained inside the

action statement

associated

with TS 3.4. 9. 2.

Initiation of Auxiliar

S ra

on Unit 1

On March 10,

1988, the licensee initiated Unit 1 Auxiliary Spray,

with a differential of less

than 320~F, to terminate

a pressure

transient initiated during cold shutdown

when Reactor Coolant

Pump

(RCP) 1-2 was secured

due to vibration.

The vibration was not

unexpected

since the

RCP's are "tuned" for normal operating

temperature

conditions.

Operators

shut

down

RCP 1-2 on the

recommendation

of the

RCP vibration engineer

although

OP L-5

recommends

that

RCP 1-2 be left in operation to accommodate

spray

f1 ow.

Normal spray

can

be initiated off loops

1 and

2 although the loop

2

spray valve was manually isolated

due to excessive

body to bonnet

leakage.

Spray was being provided from loop 1.

However,

when

RCP

1-2 was secured,

flow through the loop reversed

as designed.

Since

the pressurizer

is between

the Steam Generator

and the Reactor

Vessel

on loop two, pressure

at the surge line increased with

reversed

flow.

This made

normal spray ineffective for controlling

0

the pressure

transient

and auxiliary spray from the charging

pumps

was

used.

Following the transient,

the Shift Foreman

determined that the

differential temperature

between

the spray nozzle

and the

pressurizer

vapor space

was approximately 290'F and definitely less

than 320~F.

TS Table 5.7-1 requires that

a differential temperature

of greater

than 320'F

be logged

as

one of twelve allowable auxiliary

spray actuation cycles.

As corrective actions,

the senior

operations

supervisor

committed to

enhance

OP L-5 to clarify the purpose of leaving

RCP 1-2 in service.

In addition,

an incident summary will be written to address

the

event.

The inspector

noted that event

and proposed corrective

actions

were not being formally tracked

on the licensee's

Action

Request

system

one month following the event.

Although this event

did not result in an auxiliary spray (thermal) actuation cycle, the

corrective actions

needed to prevent

a possible actuation cycle

warrents

formal actions.

These findings were discussed

with the

licensee.

Over ressurization

of the Unit 1 Reactor Coolant Drain Tank

On March 11,

1988, with Unit 1 in mode

5 during the second

week of

the refueling outage,

operations

personnel

were draining down the

safety injection accumulators

in preparation

for maintenance

activities

on accumulator valves.

Normally, during shutdown the

accumulators

are depressurized

and the accumulator contents

are

drained through the reactor coolant drain tank

(RCDT) to the liquid

hold up tanks

(LHUTs) in accordance

with plant operating procedure

(OP) B-3B: III.

In lieu of this prescribed

evolution, since

personnel

were working inside containment,

the decision

was

made to

not vent the accumulator nitrogen to containment,

and to drain the

accumulators

in a pressurized

condition.

Since the

RCDT vent line

was cleared for containment

leak rate testing,

RCDT level indication

was rendered

inaccurate.

During draining, the

RCDT was pressurized

to its relief valve setpoint,

the relief valve failed open,

and

about

140 gallons of water discharged

to the reactor cavity sump

before the evolution was suspended.

A more detailed

evaluation

follows.

As previously mentioned,

accumulator

drain

down during shutdown is

normally accomplished

in accordance

with OP B-3B: III "Accumulators-

Shutdown

and Clearing."

Clearance

Number

10411 was issued for this

activity, but the

OP was not referenced

on the clearance.

However,

the clearance

did require accumulator venting and draining.

Operations

personnel

decided it would not be

a good idea to vent the

accumulator pressurization

nitrogen into containment

since personnel

were working in the area

near the accumulators.

Since the

RCDT was

normally used at power to lower level in a pressurized

accumulator,

a decision

was

made, without shift foreman involvement, to "drain"

the accumulators

under pressure.

An operator at the auxiliary

control board verified the

RCDT was available

and properly aligned

to a

LHUT.

All r emote operated

control valves were observed to be

5

'orrectly

positioned,

and

some water from the

RCDT was

pumped to a

LHUT to verify correct system alignment.

Accumulator

draindown

was initiated,

and

a

RCDT pump was started.

RCDT level appeared

constant,

so

a second

accumulator

draindown

began.

The auxiliary operator

then noticed that

RCDT level

was

rising rapidly and started

a second

RCDT pump.

At that time, it was

noted that reactor cavity sump level

was increasing

and the

accumulator drain operation

was

suspended.

Shortly afterward,

the

shift foreman directed the draindown to continue in accordance

with

the

OP.

After depressur izing the accumulators,

draindown

was

re-initiated

and reactor cavity sump level

began to again increase,

requiring another

draindown termination.

Subsequent

investigation determined

the

RCDT relief valve had failed

open during the initial accumulator drain attempt.

Additionally,

the

RCDT vent header

had been manually isolated for containment

leak

rate testing.

This resulted in an accurate

level indication on the

RCDT, such that level never appeared

greater

than

75K.

The

clearance

for the leak rate testing did not affect remote operated

valves, therefore clearance

tags indicating the unavailability of

the

RCDT vent line were not provided

on the auxiliary control board.

The licensee's

evaluation

determined

operators

failed to follow the

established

accumulator

draindown procedure,

and that tagging or

other indications

on the auxiliary control board were not specified

or provided when the

RCDT vent path was cleared.

At a minimum, the

RCDT pumps should

have

been tagged,

indicating the vent path was

cleared.

Corrective actions

are under evaluation

by the licensee.

Failure to drain the accumulators

in accordance

with the established

operating procedure

is an apparent violation.

(Enforcement

Item

50-275/88-07-01).

Leak on Unit 1 Control

Rod Drive Mechanism

CROM

On March 12, 1988, during

CRDM ventilation removal the licensee

discovered

a boric acid crystal formation on a spare

CROM

penetration.

The size of the crystal formation was visually

estimated

to be 1 inch wide and five inches

long and appeared

to be

coming from the area of a canopy seal

weld.

The licensee

was aware

of the similar leaks described

in Information Notice 86-108 and its

supplements

and

had planned

a detailed inspection after reactor

vessel

head

removal during the refueling.

This discovery preceded

that action,

however.

On March 16 the licensee

performed additional inspections with

television

cameras

and identified what might be an additional

leak.

The licensee

also

made entry in Unit 2 and performed

swipe surveys

of exhaust ventilation from the

CRDMs.

Based

on comparison of the

swipe surveys

from Unit 1 and the post refueling outage

surveys of

Unit 2, the licensee

concluded that

no measurable

leakage

had

started

on Unit 2.

0

The licensee

developed

an action plan in response

to the situation.

The action plan included contacting other sites

and the

NSSS

supplier (Westinghouse),

investigating

enhanced

leak detection

systems for future use,

and identification of the cause,

and

evaluation of fixes.

Design

Change

Package

(DCP) Number M-39666 was issued

by the

licensee

to cut and

remove

CROM L-5 and J-5

head adapters

(containing the leaking canopy welds)

and butt weld pipe caps

on the

cut head penetrations.

Action Request

A0104552

was issued to

implement the

DCP,

and work was to be accomplished

in accordance

with work order

(WO) C0030719

and Westinghouse

procedure

¹SP 2.7. 1

PGE-1

"CRDM Penetration

Modification at Diablo Canyon."

SP 2.7. 1

PGE-1 was ver ified to contain

a sign-off space for the Authorized

Nuclear Inspector

(ANI) after verification of satisfactory

work

completion.

The inspector

observed that work was being performed in

accordance

with these

documents,

except that activity 2 of the

WO

contained

a gC hold point which had not been

signed off on the

WO

even though work had progressed

beyond that point.

The hold point

required

gC verification of procedural

compliance with special

procedure

SP 2. 7. 1 PGE-l."

In discussing this oversight with the guality Control Manager,

the

inspector ascertained

that quality control personnel

were verifying

work was being performed in accordance

with the

SP 2.7. 1 PGE-l,

as

Westinghouse

gC signoffs were being provided

on the special

procedure.

Accordingly, the unsigned

gC hold point on the

WO was

determined to be redundant

and did not adversely affect the work.

In order .to observe

work activities from a location above the

reactor

head,

the inspectors

entered

a temporary access

platform

installed

on the cable tray area

above the reactor

head.

This area

above the reactor

head

was designated

a Zone

3 "Housekeeping,

Tool

Control/Foreign Material Exclusion" area in accordance

with

Administrative Procedure

(AP) C-10S2 "Housekeeping - General."

AP

C-10S2 specified that for a Zone

3 area, tools, support equipment

and detached

material

inside the zone must be logged in and out.

The

inspector

observed

loose materials within the zone

(such

as

a pocket

knife, razor blade type cutting tool, open allen wrench set,

masking

tape,

and

an air sample

pump) were not entered

on the log provided

at the area.

Each of these

items could have

been accidentally

dislodged

from the Zone

3 tool control area into the refueling

cavity.

This is an apparent violation of AP C-10S2 (Enforcement

Item 50-275/88-07-02).

The inspectors

are following the licensee's

corrective actions.

Subsequent

to the repair of the

CROM L-5 and J-5

head adapters,

the

licensee

made similar repairs to other spare

head adapters

on

CRDMs

L-11 and L-9.

Revisions to the

DCP and

WO were

made to control

these repairs.

Sto

Work on Use of Vendor Technical

Manuals

On March 14,

1988

gC personnel

put a stop work in effect precluding

use of vendor technical

manuals

which had not been verified as

up-to-date.

The stop work was

a result of gC followup of long

standing

commitments to insure the vendor technical

manuals

were

up-to-date.

Cracked

Weld on Diesel Generator

2-2 Lube Oil Filter Su

ort

On March 18,

1988

a maintenance

engineer

discovered

a cracked weld

on one of the three Unit 2 Diesel Generator

(D/G) 2-2 Lube Oil (LO)

filter support feet.

At the time of the discovery,

0/G 1-3, the

swing 0/G,

was out of service for maintenance.

The Plant Safety

Review Committee

(PSRC) determined

based

on the professional

opinion

of the Onsite Project Engineer that

D/G 2-2 would remain operable

during a seismic event.

Subsequently,

the licensee's

corporate

engineering

confirmed the initial determination

by analysis.

As immediate corrective action the licensee

performed

a design

change

by welding a bracket to the existing foot.

In addition

a

visual inspection of the other

D/G lube oil filters was performed.

The licensee

determined

the cause of to be vibration at the lube oil

filter resulting in fatigue failure.

The licensee

is analyzing the

vibration for further corrective actions.

Securit

Event

On March 18,

1988

a reportable security event report was

made.

The

residents

notified regional specialists

for followup.

Hot Particle Identified as Unit 1 Fuel Particle

On March 23,

1988

a hot particle was found on a worker exiting the

Radiological Control Area.

Ho overexposure

was involved per the

licensee's

estimates.

The licensee

temporarily

suspended

work in

the area the particle was suspected

of originating from (the steam

generator

manways).

The licensee

performed surveys

and implemented

additional controls.

Analysis of the particle indicated it to be

a

fragment of Unit 1 fuel.

Regional Specialists

were notified for

followup as necessary.

Diesel Generator

2-2 Fuel Oil Da

Tank Overflow

On March 22,

1988

D/G 2-2 fuel Oil Day Tank overflowed spilling

. approximately

50 gallons of fuel oil onto the pavement outside the

0/G rooms.

The spill was stopped rapidly and the oil was contained

and quickly cleaned

up precluding

a reportable violation of the

Waste Discharge

Permit or a fire.

Earlier, the chemistry department

had requested

that Diesel

Fuel Oil

Storage

Tank Ol be placed

on recirculation.

An Auxiliary Operator

was instructed to place the tank in recirculation in accordance

with

the appropriate

procedure.

The procedure

required

him to "check in

Auto and Closed" all day tank level control valves in order to

isolate the day tanks

from the storage

tank during recirculation.

Since the valves

have

no position indication near their control

switches,

the procedure

implies that the operator verify that the

controller is in automatic

and by visual observation of the valve

which is under floor panels to determine if it is closed.

The

AO

misinterpreted

the statement

and in most cases

to the controllers

from "auto" to "closed" (the controllers

have

a spring return to

"auto").

In the case of 0/G 2-2 he inadvertently took the

controller to "open" without immediately realizing his mistake.

When the

AO turned

on the transfer

pump to initiate recirculation

the day tank for 0/G 2-2 filled and overflowed and cause

a spill.

The operations

department,

as

a result of the spill, issued

an

incident

summary which concluded

by stressing

the maintenance

of the

highest attentions

to operating duties.

In addition the licensee

plans to re-label

the level control valves

and will consider

a

design

change to add position indication at the controllers.

The

inspector finds the licensee's

actions acceptable.

Unit 2 Vital Batter

Seismic Restraint Bracin

Missin

On April 1, 1988, the onsite vital electrical

systems

system

engineer,

during a review of system action requests,

discovered that

a battery surveillance

performed in 1987 found a number of seismic

restraint

braces

and bolts missing from the Unit 2 batteries

2-2 and

2-3.

At 4:30 p.m., the engineer

brought this to the attention of

his management

who recognized

the battery operability implications.

The licensee

took two immediate actions.

First, the Onsite Project

Engineering

Group

(OPEG)

was requested

to take

as built data to

facilitate a seismic evaluation.

Second, efforts were initiated to

procure bracing

and bolts from a Unit 1 battery not required to be

operable

(Unit 1 was defueled at the time).

By 6:30 p.m.,

OPEG

had

made

a preliminary determination,

without

having completed calculations,

that the batteries

would survive

a

seismic event.

Early in the morning of April 2, the parts

had been

procured

from Unit 1.

The batteries

were never

determined to be

inoperable.

Had this determination

been

made,

entry into Technical Specification 3.0.3 would have

been required.

The inspector

found

the licensee's

immediate actions to be prudent

and timely.

On April 4 the engineering analysis

determined that the as-found

condition would have

been seismically acceptable.

A subsequent

analysis

performed determined that the Unit 1 battery

used to supply

parts

was also acceptable.

On April 4, the licensee initiated a Non Conformance

Report

(NCR).

The

NCR intends to address

how the braces

and bolts were

removed

and

why when they were identified to be missing were the seismic design

implications not considered.

The licensee

was in the process

of this investigation at the time of

this report.

The inspectors will follow the licensee's

NCR process

to confirm that the above questions

are acceptably

addressed.

Two violations and

no deviations

were identified.

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

a.

Diesel Generator

1-3 Fuel In ection Tell-Tale

On March 20,

1988 while performing return to service testing of

Diesel

Generator

1-3,

a maintenance

engineer

observed

fuel "misting"

from the fuel injector tell-tale port on the number

5R cylinder

head.

The engineer

determined

and documented

on an action request

that the misting condition did not represent

a fire hazard

and that

an earlier engine analysis

had proven acceptable

engine performance.

On March 21,

1988 the

D/G 1-3 was

removed

from service to trouble

shoot the tell-tale indication.

Cylinder head

5R had been replaced

during the previous

D/G outage

due to a leaking jacket water to fuel

injector sleeve fitting.

The work order to trouble shoot the fuel

oil leakage

required the removal of the cylinder head cover and

disassembly

of the fuel injector.

A maintenance

mechanic

discovered that the original fuel injection

rod was not sealing completely against

the

new cylinder head.

With

the concurrence

of gC and mechanical

engineering

the work order

was

revised to include

a step to lap the fuel injection rod seat of the

cylinder head.

The inspector

observed

the performance

of this

activity.

The 0/G was returned to service

on March 23,

1988 following testing

in which no evidence of tell-tale "misting" was observed.

b.

Unit 1 Containment

Personnel

Hatch

On March 26, 1988, the inspector

observed portions of a preventive

maintenance activity performed

on the containment

personnel

hatch.

It was performed to return the door to service prior to lifting the

reactor vessel

head.

During the performance

of this activity it was

discovered that an interlock lever was not falling into a slot on a

disc which rotates with the inner door when the handwheel

on the

inner door is taken to the closed position.

The inter lock provides

mechanical verification that the inner door is closed

and allows the

outer door to be opened.

The disc

had

somehow rotated out of

position and the slot. would not line up to the lever.

A maintenance

mechanic,

in frustration took a pipe, approximately

three feet long, staged to be used for scaffolding,

and hit the disc

in order to rotate it back into position.

This was

done in the

10

presence

of his foreman

and

a number of other mechanics,

radiation

protection

(RP) technician,

in-service inspection (ISI) technicians,

and guality Control

(gC) inspectors.

To have adjusted

the disc

correctly, the mechanic

should

have

loosened

the set screw holding

it in place,

rotated the disc,

and retightened

the set screw.

The inspector discussed

the mechanics activitieswith both the

mechanic

and his foreman.

Both the foreman

and the mechanic stated

that the

use of the pipe was not correct.

They expressed

that

mitigating circumstances

existed in that the personnel

hatch

had

become

a critical path maintenance

item, tools were not readily

available (they were in containment in an SCA), and that

a

differential pressure

existed across

the outer door which created

a

potential

hazard if it was opened.

In addition, the mechanic

was

very familiar with the personnel

hatch

and determined that his

actions

would not harm the door.

In review of these

circumstances

the inspector

determined that the

adjustment

could have

been

done correctly.

Furthermore,

the use of

excessive

force on the door displayed poor practices.

As follow-up, the inspector discussed

these

events with the

maintenance

manager,

the

gC manager,

and the Unit 1 outage

manager.

Based

on these

discussions

and independent

actions initiated by

mechanical

maintenance

and gC, the following actions

were taken:

The individual was counseled.

Maintenance

held a tailboard to discuss

the event

and proper

maintenance

practices.

An incident summary

was issued to maintenance.

gC inspectors

discussed

the importance of responding to events

such

as this.

The door was inspected

and

no damage

was identified.

Although immediate corrective actions

appeared

to be limited, the

licensee's

follow-up was acceptable.

c.

Other Maintenance Activities

Other maintenance activities were observed

during the course of

event follow-up, the control rod drive mechanism

seal

weld repair

(see Section 4.e),

and inspection of'nstrumentation

and Controls

activities (see Section 12).

No violations or deviations

were identified.

6.

Surveillance

61726

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

0

11

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

Unit 1 Auxiliar Salt Water

Pum

1-1 Inservice Testin

The inspector

observed portions of the Auxiliary Salt Mater System

(ASW)

Pump l-l Inservice Testing (IST) performed prior to the return

to service of the

pump following motor maintenance.

In followup of

this surveillance,

the inspector

reviewed the system design

bases

and compared

them to operational

practices.

At the

end of the

inspection period the inspector

had posed

two questions

to the

licensee

concerning the effects of allowable biofouling in the

ASW

side of the Component Cooling Water

(CCW) Heat Exchanger

on the heat

removal capacity of the heat exchanger.

Inservice Test

The test,

to comply with the requirements

of ASME Section XI, has

the operators

establish

greater

than 11,000

gpm

ASW flow and then

confirm that the differential across

the

ASW pump is within minimum

and

maximum valves.

The

ASW flow measurement

was

made using

a

temporary annubar inserted

in the flow upstream of the heat

exchanger.

It was discovered,

when flow measurements

were

substantially

less

than 11,000

gpm, that the annubar

had failed.

A

circumferential

weld joining the extension

rod to the flow element

had failed apparently

due to flow induced vibration.

The licensee

determined

the annubar to be

a temporary instrument

and

made

an on

the spot change to Surveillance Test Procedure

(STP)

P-7B to have

the instrument

removed following testing.

In addition,

an effort

was initiated to install

a mounting bracket to store the annubar

following testing.

Following replacement

of the annubar,

the test

was again attempted

and 11,000

gpm was not achieved.

The heat exchanger

was cleaned

and

rated flow was achieved,

however differential pressure

across

the

pump remained at the alert level.

As a result,

the engineering

department

made the decision to disassemble

and rebuild the

pump.

Desi

n Basis

uestions

The inspector

reviewed the design basis for the

ASW system.

Diablo

Canyon

FSAR Chapter 9.2 states that the system is designed for the

post-design

basis

loss of coolant accident

(LOCA) instantaneous

heat

rejection

assuming

the loss of one diesel

generator.

The postulated

peak heat rejection rate is 2.52 x 10 8 Btu/hr.

Witn an ocean

temperature

of 70 degrees

F. this would have required 10,580

gpm

through

one heat exchanger.

The inspector

asked

two questions:

1.

If the

pump test

STP-P7B

was performed

on with clean heat

exchanger

and

ASW flow of exactly 11,000

gpm was established

what would be the flow achieved with the delta pressure

across

the heat exchanger at its alarm setpoint of 167 inches of

water?

12

2.

The design basis

heat

load is 2.52 x 10 8 Btu/hr and the vendor

heat exchanger

specifications

indicate

a heat

exchange

rate of

2.588 x 10 8 Btu/hr,

a margin of less

than

3X.

What amount of

fouling was

assumed

in the heat exchanger

design?

This is an

Open Item (follow-up Item 50-275/88-07-03).

The licensee

committed to respond to the inspectors

questions

during

a telephone

conference

call

on April 13,

1988.

b.

Other Surveillance Activities

Other surveillance activities were observed

by the inspectors

as

a

part of inspection of inservice inspection activities (see Section

13) and inspection of Instrumentation

and Controls activities (see

Section 12).

No violations or deviations

were identified.

7.

En ineerin

Safet

Feature Verification

71710

a.

Unit 2 Hi

h Head In ection

S stem Walkdown

The inspector performed

a walkdown of the physically accessible

portions of the Unit 2 High Head Injection System including

electrical

breakers

and control

room indication.

No violations or deviations

were identified.

8.

Radiolo ical Protection

71709

The inspectors periodically observed radiological protection practices

to

determine whether the licensee's

program

was being implemented in

conformance with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted

frequent plant tours to observe

activities in progress

and were generally

aware of significant plant

activities, particularly those related to radiological conditions and/or

challenges.

ALARA consideration

was found to be an integral part of each

Radiation

Work Permit.

No violations or deviations

were identified.

9.

Ph sical Securit

71881

Security activities were observed

for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

including vehicle and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

No violations or deviations

were identified.

10.

Licensee

Event

Re or t Follow-u

92700

and 92701

4

13

Status of LERs

Based

on an in-office review, the following LERs were closed out by

the resident inspector:

Unit 1:

88-07

Unit 2:

88-01, 88-02

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

No violations or deviations

were identified.

11.

Inde endent

Ins ection

37700

60710

and 92700

a.

Reactor

Vessel

Refuelin

Level Indicatin

S stem

RVRLIS

In preparation for the licensee's

planned drain to midloop condition

for the Unit 1 refueling outage the inspector

examined

and walked

down the installation of the

RVRLIS system for Unit l.

Subsequent

to the Unit 2 loss of RHR event

on April 10,

1987 the

licensee

had implemented

many improvements

in the control of mid

loop operation.

One of the improvements

was the installation by

design

change of a dedicated

temporary

system for measuring reactor

vessel

level during the drain

down to and at midloop conditions.

The licensee's

system consists of permanently installed equipment;

narrow range;, wide range

and tygon tube level indicating systems

connected

to independent

location in the reactor hot and cold legs.

The system

includes

readouts

and alarms in the control

room,

a

television monitor (of the tygon tube scale)

in the control

room and

level recorder traces.

Prior to the inspectors

walkdown, involved licensee

engineer

technicians

and management

had performed exhaustive

walkdowns to

ensure

an adequate

system.

b.

Insufficientl

Detailed

Se uencin

of Mork for Drain Down to

Midloo

Conditions

In reviewing the licensee's

commitments

made in response

to the

April 10,

1987 loss of

RHR event

and the licensee's

response

to

Generic Letter 87-12 dealing with operations

at midloop, the

inspector

determined that the licensee

did not have plans to

carefully control the sequence

of steam generator

manway removal

and

steam generator

nozzle

dam installation.

Likewise the inspector

determined

the licensee

had not sequenced

reactor vessel

head work

to insure

a sufficient vent path

was available prior to installing

the last hot leg nozzle

dam.

The possible

consequences

of improper sequencing

could be the

sudden

expulsion of the already

reduced

RCS inventory (at mid loop

14

operation)

through

a steam generator

cold leg nozzle.

This could

occur with the loss of the

RHR system for any appreciable

length of

time.

This situation

was brought to the attention of licensee

management

and the licensee

revised the sequence

of operations

appropriately.

Im ro er Desi

n Calculation

To provide sufficient venting area in the reactor vessel

head,

the

licensee

performed calculations

to demonstrate

sufficient vent area

would be available

from the process

of opening the incore

thermocouple ports (mechanical

"connoseal"

connections)

and from

detensioning

the head.

The licensee's

calculation, File 880311-0,

dated

March 11,

1988

showed that removal of the connoseal

head connections

would provide

2.5 square

inches of vent area for each of five connections

or 10.5

square

i'nches total.

The inspector

examined the connoseal

removal job in progress,

measured

the actual

gaps

between the thermocouple stalk and the head

penetration

and found the actual

values to be quite different than

those

used in the calculation.

The actual outer diameter

as measured

by the mechanics

at the

inspectors

request

was 2-5/8 inches

(2.625) whereas

the calculation

was based

on an erroneous

value of 2.09 inches.

The net result of

the error was that the

head vent area available

from the connoseal

work was 2.6 square

inches total vice the calculated

10.5 sq. in..

The design calculation, File 880311-0

had

been prepared

by one

engineer verified by another

and approved

a Senior

Nuclear

Generation

Engineer.

Subsequent

to the discovery of the error the licensee

revised the

sequence

of work to perform reactor vessel

stud removal prior to

installing the last hot leg nozzle

dam thus precluding the rapid

ejection of RCS inventory (if RHR cooling were lost).

The calculational error was caused

by the engineering

acceptance'of

informal information over the telephone for the critical dimensions

of the items involved in the calculation.

The dimensions

informally

provided were incorrect but neither the engineer performing the

calculation,

the verifier or the approver proper ly verified the

important input dimensions.

Pacific Gas

and Electric Company,

Engineering,

Nuclear,

Procedure

No.

3. 3 Revision

No.

9 dated 4/13/87,

"Design Calculations"

establishes

how Engineer ing will prepare,

check,

approve

and

document design calculations.

Paragraph

4. 1.2 states

in part

that..."All,design input data...shall

be documented

in the

calculation"

and "assumptions

requiring verification at a later

15

design

stage shall

be identified as 'Preliminary'ntil the

verification is completed...."

Paragraph

4.2 "Checking" states

in part "Checking of the

calculations

shall include...reviewing calculation inputs to verify

conformance with project conditions."

The fai lure to verify the dimensional

inputs received

over the

telephone

as preliminary assumptions

on the part of the preparer

checker

and approval

led to an erroneous

calculation which is an

apparent violation of 10 CFR 50 Appendix

B Criterion III Design

Control (Item 50-275/88-07-04).

Im ro er Cleanliness

Controls

During the observation of the connoseal

removal work on 3/21/88 the

inspector

observed that the opening to the reactor vessel

created

by

the work was left open at the completion of work.

Since the work left a 1/8 inch annular opening to the reactor

and

since cleanliness

had not been established

in the areas

above the

opening (i.e. the

head area cables,

the area

around the refueling

cavity or on the polar crane)

the inspector

was concerned for the

cleanliness

of the reactor since at a different reactor site

a 1/8

inch piece of foreign material

had caused

a stuck control rod.

The inspector identified his concern to the mechanics

and the

gC

inspector in attendance

in the refueling cavity.

On exiting the

cavity the inspector

informed the mechanic

foreman

and the outage

manager of his concern.

They stated

they agreed with the inspectors

concern

and would have the

head

openings protected.

The following day 3/22/88 the inspector

determined that the opening

had not been covered

and informed the plant manager

who agreed that

head openings

should

be covered

anti determined that

a nonconformance

report would be written to document the problem.

The next day 3/23/88 the inspector

determined that the

head vents

had not been covered

and informed the outage

manager

who

investigated

and determined that the order to cover the openings

had

been

countermanded

by a maintenance

general

foreman but that

he

would ensure

the openings

were covered.

The

gC Manager informed the

inspector that the requirements

to cover the

head opening were not

clear and therefore

a nonconformance

report was not warranted.

The openings

were covered late in the day on 3/23/88.

A nonconformance

report was written on 3/24/88

(DC1 88 MM-N027).

The problems

encountered

in this series

of events

are:

The mechanics

and

gC involved in the generation of the work

order

and the execution of work did not implement

a fundamental

cleanliness

precept which is to exclude foreign. material

from

16

the reactor vessel

by covering the opening or establishing

clean conditions

around

and above the opening.

The plants correction of the problem was not timely.

Plant managements

direction to correct the problem was

countermanded

at lower levels without feedback to management.

Plant procedures

do not adequately

prescribe cleanliness

requirements

of ANSI 45.2. 1.

Once the problem was recognized,

plant staff did not inform

craft and

gC personnel

of the problem (to preclude repetition)

in a timely way.

The inspectors will followup the licensee's

corrective actions to

the above

problems through the licensee's

NCR process.

The licensee

committed to implement Regulatory Guide 1.37 and ANSI

N 45 2. 1.,

1973 in the

FSAR Table 17.2.

ANSI

N 45.2. 1 "Cleaning of Fluid Systems

and Associated

Components

of Water Cooled Nuclear

Power Plants" is applicable "during the

operation

phase".

ANSI

N 45.2. 1. paragraph

3. 1.2 describes

"Class

B" cleanliness

as

applicable to reactor coolant systems.

The standard

provides

guidance

in the flushing criteria as to the

maximum size of foreign

material

allowed specifically "there shall

be

no particles larger

than 1/32 inch in any direction".

The standard

gives further guidance in paragraph

6 "Maintenance of

Installation Cleannes" (sic) that "seals

must. be installed" or

"prior to opening surrounding

should

be cleaned.

It is noted that the licensee's

cleanliness

implementing procedures

NPAP-C-10 "Housekeeping

General"

an NPAP-D-6 Cleanliness

Controls

for Corrosion Resistant

Alloys do not address

many details of ANSI

N45.2. 1Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2. 1" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. nor do they invoke the basic definitions of cleanliness

classes

"A" "B" "C" and "D".

Procedure

NPAP 0-6 (for corrosion

resistant alloys only) does

invoke ANSI N45.2. 1.

by reference,

but

the lack of understanding

experienced with the mechanics,

gC

inspectors

and higher levels of plant staff indicate the procedures

and training dealing with cleanliness

are not adequate.

The implementation of ANSI N45.2. 1 into plant procedures

and the

emphasis

to plant workers of the fundamental

precepts

of cleanliness

around the reactor coolant system should

be addressed

by the

licensee

in response

to the apparent violation described

in Section

4.e. of this report.

Revisions to the Action Re uest

Pro

ram

The inspector

reviewed the licensee's

ongoing program to address

Action Request

(AR) program deficiencies

and backlog.

In July 1987

a task force concluded

by providing management

suggested

enhancements

to the Action Request

program.

Examples of proposed

changes

include the

use of component

ID should

be implemented

by the

Work Planning Center

and not the initiator as is currently required.

In the past, initiators not familiar with the comprehensive

component

I.D. system

have attributed problems to the wrong

component.

Concurrent with implementing

AR formal changes,

the licensee

plans

to implement

a revised prioritization program.

The program,

based

on one established

at Florida Power and Light's Turkey Point,

provides

a priority number

and required completion time.

As an

example,

a priority 1A would describes

work required to ensure

personnel

safety or prevent license violations within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The

licensee is confident that implementation of this program will

better categorize

work activities.

The revisions to the

AR program,

at the

end of this report period,

were

up for Plant Safety

Review

Committee

and Plant Manager review.

The inspector also reviewed the licensee's

AR and Work Order backlog

tracking system.

As of March 31,

1988 the licensee

had 1279

corrective maintenance

Action Requests

open excluding lowest

priority, "nice-to-do", work.

In the previous quarter the licensee

had completed

1,082 corrective maintenance

work orders.

Over the

last six months the licensee

has

improved its method of categorizing

and understanding its work backlog.

The inspector will monitor the implementation of AR program

revisions in a future inspection.

One violation and

no deviations

were identified.

12.

Instrumentation

and Controls

De artment Activities

Inspections

were conducted for two weeks

by a contractor to the

NRC,

INEL.

The area

examined

was Instrumentation

and Controls.

The results

will be reported in a future inspection.

13.

Inservice Ins ection

ISI

73753

In accordance

with the NRC's ISI work observation

procedure,

the

inspector

examined

ASME Code replacement activities

on the reactor vessel

head.

These activities included cutting leaking spare control rod drive

mechanism

head penetrations

and welding caps

on the cut ends.

Details of

the inspector's

examination

are provided in section 4.e. of this report.

14.

Exit

30703

On April 8,

1988 an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.