ML16161A983

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Insp Repts 50-269/88-12,50-270/88-12 & 50-287/88-12 on 880419-0516.No Violations Noted.Major Areas Inspected: Operations,Surveillance,Maint,Physical Security,Radiation Protection,Esfs Lineups & Nonroutine Reporting
ML16161A983
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/01/1988
From: Peebles T, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A984 List:
References
50-269-88-12, 50-270-88-12, 50-287-88-12, NUDOCS 8806200208
Download: ML16161A983 (13)


See also: IR 05000269/1988012

Text

R REG

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.V.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/88-12, 50-270/88-12, 50-287/88-12

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.:

DPR-38, DPR-47, DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducted:

April 19 - May 16, 1988

Inspectors: _

_

_

__(_

_

)/__/_f

P. H.-Skinne , genior Resident Inspector

Date Signed

L. D. Wert, Resident Inspector

Date Signed

Approved by:__

__

__

__

__

__

_

/

T. A. Peebles,'Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine inspection involved resident inspection on-site in the

areas of operations, surveillance, maintenance,

physical security, radiation

protection, engineered safeguards features lineups, nonroutine reporting, and

B&W Owners Group Plant Reassessment Program.

Results:

Of the eight areas inspected,

no violations or deviations were

identified.

8806200208 SS0602

PDR

ADOCK 05000269

Q

DCD

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • M. Tuckman, Station Manager

J. Davis, Technical Services Superintendent

W. Foster, Maintenance Superintendent

T. Glenn, Instrument and Electrical Support Engineer

  • C. Harlin, Compliance Engineer

D. Hubbard, Performance Engineer

J. McIntosh, Administrative Services Superintendent

  • B. Millsaps, Maintenance Service Engineer
  • F. Owens, Assistant Engineer, Compliance

P. Street, Mechanical Technical Support Engineer

  • R. Sweigart, Operations Superintendent

L. Wilkie, Integrated Scheduling Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

  • P. H. Skinner

L. D. Wert

  • Attended exit interview.

2.

Exit Interview

The inspection scope and findings were summarized on May 16,

1988, with

those persons indicated in paragraph 1 above.

The inspectors described the areas inspected and discussed in detail the

inspection findings listed below. Dissenting comments were not received

from the licensee.

Proprietary information is not contained in this

report.

Item Number

Status

Description/Reference Paragraph

269/85-21-01

Closed

Violation for Failure to Follow

Procedure

269,270,287/85-21-03

Closed

Violation for Failure to Provide

an Adequate Procedure

2

269,270,287/88-12-01

Closed

Licensee

Identified

Violation

Potential Loss of All AC Power Due

to Switchyard Modification

269,270,287/88-12-02

Open

Inspector

Followup

Item:

Corrective Actions to

Preclude

Late Submittal of Reports

270/88-12-03

Open

Inspector

Followup

Item:

Management

review

of

Communications

Interface Between

Performance and Operations During

Testing

LER 269/87-02

Closed

Appendix R Review With Respect to

Valve Operability

LER 270/82-10

Closed

Stuck Suction Relief Valve on Main

Feedwater

Pump After a Reactor

Trip

LER 270/87-06

Closed

TS 3.3.6

Violation

Due

to

Management Deficiency

3.

Licensee Action on Previous Enforcement Matters

a.

(Closed) Violation (50-269/85-21-01):

Failure to Follow Procedure on

Classification of Work Requests.

The licensee responded to this

violation in correspondence dated October 11,

1985.

The inspector

has reviewed this information and the corrective actions addressed

and based on this review, this item is closed.

b.

(Closed) Violation

(50-269,270,287/85-21-03):

Inadequacies

in

Development

and

Implementation

of

Procedure

MP/O/A/2001/4,

CRD

Breaker Inspection and Maintenance.

The licensee addressed this

violation in correspondence dated October 11,

1985.

Based on this

action, this item is closed.

4.

Plant Operations (71707)

a.

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

technical

specifications (TS), and administrative controls. Control room logs,

shift turnover records, Unitf2 refueling log and equipment removal

and restoration records were reviewed routinely.

Discussions were

conducted with plant operations,

maintenance,

chemistry,

health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted during the day,

night shifts,

and on

weekends.

Some

inspections were made during

shift

3

change in order to evaluate shift turnover performance.

Actions

observed were conducted as required by the Licensee's Administrative

Procedures.

The complement of licensed personnel

on

each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1, 2, and 3 Electrical Equipment Rooms

Units 1, 2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1, 2, and 3 Penetration Rooms

Unit 2 Containment

Condenser Circulating Water Intake Structure

During the plant tours,

ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 -

Unit 1 has continuously operated during this reporting

period at 100% power. As of May 16, the unit has operated

continuously for 185 days without a shutdown.

Unit 2 -

Unit 2 commenced this reporting period at approximately 30%

power recovering from a generator runback caused

by

a

faulty temperature sensing device. The device was repaired

and the unit reached 100% on April 19 and has remained

there except for a 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period on April 26 to correct a

feedwater heater tube leak on 2A2 heater, for the remainder

of the reporting period.

Unit 3 -

Unit 3 commenced the report period in an outage caused by a

steam generator tube leak. Steam generator tube leakage

repairs were completed May 2 and return to power operations

commenced. On May 4, a primary leak occurred which forced

the plant to return to a cold condition to make repairs

(see

paragraph 4.c.).

The plant returned to normal

operating

pressure

and

temperature

on

May 8, but

experienced problems with the electrical system on the main

generator. On May 10, the plant had been returned to 100%

power.

b.

Unusual Event On Unit 3 Due To SG Tube Leak

On April 17,

1988,

at approximately 3:15 p.m.,

the condenser air

ejector exhaust radiation monitor (RIA-40)

began increasing steadily

from about 280,000 cpm. Investigation identified that a primary to

4

secondary leak of approximately 1.3 gpm in the steam generators had

developed. By 10:00 p.m.,

RIA-40 had increased to 900,000 cpm and

operators began shutting down the unit. At 1:15 a.m. on April 18, an

Unusual

Event was declared and a cooldown of the unit to cold

shutdown conditions was commenced to isolate the leak and perform

effective repairs. The leak was localized to the 'A' steam generator

and the cooldown was conducted using the 'B' steam generator.

Upon

obtaining cold shutdown conditions at 4:40 p.m. the Unusual Event was

terminated. The licensee performed an extensive inspection of the

steam generator tubes in both steam generators as discussed in TS 4.17.4.d. A total of 3974 tubes were inspected in the 'A'

SG and

3740 tubes inspected in the

'B'

SG.

Two

leaking tubes

were

identified in the 'A' SG and none in the 'B' SG. As a result of the

eddy current testing, a total of 27 tubes in the 'A' steam generator

were plugged and 23 tubes plugged in the 'B'

generator.

Steam

generator work was completed on May 2 and the unit commenced recovery

from the outage.

c.

Unusual Event On Unit 3 Due To Seal Injection Leak

On May 4, with the plant at 2200 psig and 480 degrees F, the licensee

was conducting PT/0/A/200/46,

Reactor Coolant System

Leak Test.

During the visual inspection a leak was reported on

the

seal

injection piping to the mechanical seal on reactor coolant pump 3B1.

After further investigation, the leak appeared to be on the seal 'C'

(1st stage) which is in an unisolable section of piping.

Based on

this observation an Unusual Event was declared on May 5 at 0008 and

the required notifications were made.

Rough calculations performed

during the cooldown to cold conditions indicated a leak on the order

of 0.1 gpm. The licensee decided to attempt to stop the leak using

the weld overlay method developed by NUTECH and used in early 1987 on

Units 2 and 3 to repair leaks in the reactor vessel level indicating

system. This method was attempted but did not work due to the

pressure build up in the system piping in the area of the weld

repair. When the personnel went into the area to make the repair,

they identified that the leak was actually on the line associated

with the 2nd stage seal.

The initial investigation had identified

the incorrect pipe due to the large quantity of pipes in this area.

Had the location initially been correctly identified, the plant would

probably not have declared a Unusual

Event.

As a result of the

inability to stop the leak using the overlay method with pressure in

the piping, the unit was cooled down,

depressurized and placed in

decay heat removal cooling mode. The Unusual Event was terminated on

May 6 at 0745. The leak was repaired on May 6 at 0300 and the unit

returned to critical operation on May.8 at 3:20 p.m.

d.

A recent review by the licensee identified that 10 of the last 17

reports required by TS 4.17.6.a and 4.17.6.b were not submitted

within the time requirements specified by TS. In addition the report

required by TS 4.4.2 concerning tendon surveillance dated March 29,

1988, was also submitted after the required due date specified. The

licensee has

identified both of these problems in problem

investigation reports 4-088-0009 and 3-088-0083 respectively.

The

licensee has investigated this area and developed corrective action

to correct this problem.

The inspector is identifying this as an

Inspector Followup Item 269,270,287/88-12-02: Corrective Actions to

Preclude

Late

Submittal

of

Required

TS

Reports,

pending

implementation and subsequent review of future submittals.

No violations or deviations were identified.

5.

Surveillance Testing (61726)

a.

Surveillance tests were

reviewed

by

the inspectors to verify

procedural

and performance adequacy.

The completed tests reviewed

were examined for necessary test prerequisites,

instructions,

acceptance criteria, technical content, authorization to begin work,

data collection, independent verification where required, handling of

deficiencies noted, and review of completed work.

The tests

witnessed, in whole or in part,

were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable and systems restoration was completed.

Surveillances reviewed and/or witnessed in whole or in part:

PT/3/A/0600/12

Turbine Driven Emergency

Feedwater Pump

Performance Test

PT/0/A/0400/11

Safe

Shutdown

Facility

(SSF)

Diesel

Generator Performance Test

PT/0/A/600/23

SSF Fuel Oil Inventory

b.

Condenser Discharge Valve (2CCW-21)

During the most recent refueling outage on Unit 2, the inspectors

observed portions of PT/2/A/0261/006

(Condenser

Circulating Water

(CCW) System Gravity and Recirculation Flow Test).

During the test

one of the condenser discharge valves (2CCW-21)

failed to

shut

automatically as required by the test. Additionally, an operator was

unable to shut the valve from a remote station above the valve.

Testing was stopped, a work request written (WR 14246C) and the valve

was repaired.

Subsequently

the CCW gravity

flow test was

satisfactorily completed and

2CCW-21

functioned

as required.

A

review of the completed work request indicated that components were

replaced only in the "open" circuit of the valve and these components

would have no effect on the valves ability to shut. 2CCW-21 is a air

operated,

78 inch diameter butterfly valve located in the condenser

discharge piping between the condenser outlet and the concrete floor

of the turbine building. At certain lake elevations (greater than

approximately 791 feet) the failure of this valve to shut on a CCW

piping rupture could cause flooding of the turbine building through

backflow of the lakewater. Although various modifications have been

6

completed to lessen the severity of this casualty should it

occur,

(for example;

a drain out of the turbine building basement

and

watertight doors between the auxiliary building and the basement) the

Oconee Probabilistic Risk Assessment still considers flooding of the

turbine building from CCW system a very significant contribution to

core melt frequency.

After the inspector discussed his finding an initial investigation by

Instrument and Electrical (I&E)

Engineers supported the inspectors

concerns that the maintenance performed on the valve as detailed in

the work request would not address the valve's failure to

automatically shut. Automatic and remote cycling of the valve is

accomplished by operation of dual solenoid valves which act to port

air to/from the piston of the valve.

At the CCW valve itself, the

air system can be manually operated to shut the valve but in the case

of a ruptured

CCW pipe this option may

not be available.

The

inspectors requested that the licensee look into the repairs of

2CCW-21

and also examine

the history of all of the condenser

discharge valves for other instances of failure to automatically

shut.

Additional investigation by I&E personnel identified that the limit

switch replaced was the "open" limit switch which is in the close

circuit rather than the limit switch in the open circuit.

Further

review by I&E indicated no history of failure of this valve and other

condenser discharge valves.

Operator and Performance Engineer Interface During Conduct of Test

During observation of portions of PT/3/A/0600/12 (Turbine Driven

Emergency Feedwater Pump (TDEFWP)

Performance Testing) the inspector

observed that the testing was not completed with strict adherence to

the procedure.

Specifically, a precaution which stated that a

Nuclear Equipment Operator (NEO)

should be stationed at the pump to

"continuously monitor the TDEFWP while it

is running and ensure

adequate suction pressure is maintained to the pump at all times" was

not followed.

While the NEO did continuously monitor the TDEFWP

while it

was operating,

he was not aware of the requirement to

monitor suction pressure.

He did not know the location of the

suction pressure gage and was unsure what suction pressure values

were "adequate". The NED stated he had not reviewed the performance

procedure. There is no indication of pump suction pressure in the

control room. The inspector informed the NEO of the suction pressure

gage location and the requirement to monitor suction pressure.

A

specific requirement for a minimum suction pressure is provided in

the procedure.

A performance engineer, responsible for the test

coordination,

was

aware of the gage location and the pressure

specified in the procedure since he maintained the controlled copy of

the test. However, the engineer was not in the immediate vicinity of

the pump as it

was operated.

The operating requirements of the

performance test was not communicated to the NED by the performance

7

engineer nor by the onshift reactor operator.

The unit supervisor

was made aware of this problem and also this problem was discussed

with other licensee management. The licensee is going to review this

interface area to determine if a communication problem exists and if

NEO's are being provided adequate guidance when performing equipment

operation in support of the performance engineering effort.

Pending

completion of this review and action taken, if required, this item is

identified as an Inspector Followup Item (IFI) 269,270,287/88-12-03:

Management

Review of Communications Interface Between Performance

Engineering and Operation During Performance of Testing.

No violations or deviations were identified.

6.

Maintenance Activities (62703)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

procedures

and

work

requests were

examined to verify proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control,

proper return of equipment to service,

and that

limiting conditions for operation were met.

Maintenance reviewed and/or witnessed in whole or in part:

WR 15094C

Investigate Torque Switch Setting LP-20

WR 14246C 2CCW-21 Repairs

WR 51629G 2CF-1 Limitorque Repairs

b.

Emergency Power Switching Logic Malfunctions

In late 1987,

Duke Power Company decided that due to increases in

present generation capacity and for future increases due to projects

in progress, modifications to the 230kv switchyard were required.

Nuclear Station Modification (NSM) ON-22637, 230kv Switchyard Circuit

Breaker Replacement,

was developed to replace the power circuit

breakers (PCB)

and various associated relaying with larger capacity

PCB's. This NSM is in the process of being performed at this time.

Since the PCB's

have a higher interrupting capability,

larger

capacitance is provided to suppress the voltage gradient across the

contacts during breaker operation.

On March 28, 1988, while

performing a surveillance test on the Keowee Emergency Start System

per

PT/2/A/0610/01J,

the

unit

experienced

a CT-2

(Startup

Transformer)

lock-out from a transformer differential phase relay.

The cause of the lockout could not be determined and an investigation

was performed with the assistance of the design engineering group.

On April 4, the design engineering group met with the operations

staff and identified that due to the higher value of capacitance on

the new PCBs an induced resonance circuit had developed on the CT-2

circuit which under certain breaker alignments.could result in a CT-2

8

lockout condition.

The

design personnel also provided recommen

dations for operations under these specific circumstances if

they

occurred. Design was requested at this time to do further studies on

this problem.

On April

26, design engineering as a result of

additional studies, identified that Unit 2 could experience a failure

where emergency power would not be automatically provided to the Unit

2 loads as described in the

FSAR.

The licensee immediately took

action to place Unit 2 on Unit 3's startup transformer since Unit 3

was already shut down to cold conditions, and placed Unit 3 power on

the Lee Station 100kv power source.

The licensee also made notifi

cations as required by 10 CFR 50.72. At approximately 1:30 p.m.

on

April 27,

a conference call was held between

NRR (Helen Pastis,

Carl Shulton, Dave Matthews), Region II (Brian Bonser), DPC Corporate

Engineering (Bob Dobson, Jim Stoner, Paul Guill),

Oconee station

Management and the resident inspector to discuss facts associated

with this event.

Duke provided NRC a draft memo detailing the

information discussed in this conference call dated April 28,

1988.

The licensee identified that as a result of the resonance problem the

voltage induced on the low voltage side of the startup transformer is

of a sufficient magnitude to exceed the pickup setting of the

Emergency Power Switching Logic (EPSL)

voltage sensing relay.

This

would result in the EPSL system falsely sensing that the transformer

is available for use and would prevent the automatic transfer to the

standby power source which would be available for use if an emergency

were to occur. The only situations in which this condition would

exist would be if

the PCB's are open and all disconnect switches

associated with the startup transformer and the PCB's are closed or

when

a transformer differential

lockout existed that was not a

sustained fault to ground or was spurious in nature coincident with a

loss of off-site power to that unit. This item is being identified

as a Licensee Identified Violation (LIV)

270/88-12-01:

Potential

Complete Loss of All AC Power Due to 230kv Switchyard Modifications.

This is identified as a LIV as discussed in 10 CFR 2, Appendix C due

to the facts that it meets all the following criteria:

(1) it was identified by the licensee

(2) it

fits a Severity Level

IV or V violation category because

of

the

low

probability

of

all

conditions

occurring

simultaneously

(3) it was reported, as required

(4) it

has been corrected and measures to prevent recurrence are

being taken

(5) it

was not a violation that could reasonably be expected to

have

been

prevented by the licensee's corrective action to

a previous violation.

No violations or deviations were identified.

9

7.

Resident Inspector Safeguards Inspection (71881)

In the course of the monthly activities, the Resident Inspectors included

review of portions of the licensee's physical security activities.

The

performance of various shifts of the security force was observed in the

conduct of daily activities which included; protected and vital areas

access controls, searching of personnel,

packages and vehicles, badge

issuance and retrieval, escorting of visitors, patrols and compensatory

posts.

In addition, the inspectors observed protected area lighting and

protected

and vital areas barrier integrity,

and verified interfaces

between the security organization and operations or maintenance.

No violations or deviations were identified.

8.

Inspection of Open Items (92701)

The following open items are being closed based on review of licensee

reports,

inspection,

record review, and discussions with licensee

personnel, as appropriate:

(Closed)

LER 269/87-02:

Appendix R Review With Respect to Valve

Operability.

The

licensee has completed all corrective actions

specified in this report.

The inspector verified the action to be

complete and that it

met the commitment identified in the report.

Based on this review, this item is closed.

(Closed) LER 270/82-10: Stuck Suction Valve On The 2B MFP After A

Reactor Trip. Nuclear Station Modification 1584 has been completed

on all Units. Based on this action, this item is closed.

(Closed)

LER 270/87-06:

TS 3.3.6 Violation

Due To A Management

Deficiency. The licensee's program in response to IE Bulletin (IEB)

85-03 covers the problem areas addressed in this LER.

The program

for IEB 85-03 is implemented and has not identified similar problems

of this nature.

Based on this review this item is closed.

9.

Babcock and Wilcox Owners Group Plant Reassessment Program

In January 1986, NRR requested the Babcock and Wilcox Owners Group (BWOG)

to assume a leadership role in accomplishing key aspects of the overall

effort required for the reassessment of all

B&W

plants.

The BWOG

committed to take the lead in a planned effort to define concerns relative

to reducing the frequency of reactor trips and the complexity of post-trip

response in B&W plants.

The BWOG issued BAW-1919,

"Trip Reduction and

Transient Response Improvements Program" including 5 revisions as of July

1987.

The NRC has reviewed BAW-1919 and its revisions and has issued a

Safety Evaluation Report (SER) (NUREG-1231) and

Supplement 1 to

NUREG-1231. Table 12.1 of the NUREG list 207 recommendations that were

developed by the BWOG for implementation considerations at each of the B&W

10

utilities. These recommendations comprise the BWOG Safety and Performance

Improvement Program (SPIP)

which has goals by the end of 1990,

to reduce

the average trip frequency per plant to less than two per year ,and also

that the number of complex transients will be reduced to 0.1 per plant per

year based on a moving 3-year average. Attachment 1 to this report shows

the actions taken on various of these recommendations.

See inspection

report 269,270,287/87-55 for additional actions taken to date.

Attachment:

Safety and Performance Improvement

Program Recommendations

ATTACHMENT

SAFETY AND PERFORMANCE IMPROVEMENT PROGRAM RECOMMENDATIONS

Recommendation

Number

Subject

Remarks

TR-009-ICS

Improvements in ICS tune

Complete

control circuit

TR-040-ADM

Use the TA Committee's Trip

Complete

Investigation Root Cause

Determination Program

TR-112-PES

Review Switchyard maintenance

Complete

procedures to ensure there is no

mechanism for loss of offsite power

TR-113-PES

Review breaker control power

Complete

distribution to determine effects

of a loss of battery bus

TR-116-PES

Review DC charging system and

Complete

ensure the charging voltage does

not exceed plant equipment

voltage ratings

TR-117-PES

Modify inverter overcurrent

Complete

protection to ensure the

breakers/fuses open on

overcurrent before inverter fail

TR-118-PES

Evaluate loadings on AC and DC

Complete

.vital buses to ensure adequate

margins exist without trip of

equipment

TR-184-ICS

Provide separate fuses for hand

  • Not

stations that use AC power

Applicable

TR-185-ICS

Power feedwater flow recorders

  • Not

directly from NNI

Applicable

TR-188-ICS

Maintain DC power supply current

  • Not

balance and perform a periodic

Applicable

full load test for each power

supply

TR-189-ICS

Set selector switches to select

  • Not

maximum NNI dependence

Applicable

Attachment

2

TR-190-ICS

Develop backup controls for

  • Not

pressurizer level and pressure

Applicable

control

TR-193-ICS

Review/test pressurizer heater

  • Not

low -

low level interlock logic

Applicable

TR-194-ICS

Buffer hand powered indicators

Rejected

and recorder inputs from

automatic power signals

TR-195-ICS

Supply hand and automatic

Rejected

powered circuit from separate

panels

TR-196-ICS

Set pressurizer level signal

Rejected

select relays to automatic

powered transmitters

TR-197-ICS

Provide automatic power transfer

Rejected

for the modulating pressurizer

heater converters

TR-198-ICS

Automatic selection of auto

Rejected

powered sensor on loss of

hand power

TR-203-PES

Establish preventive maintenance

Complete

to increase reliability of

inverters

TR-204-ICS

Eliminate or reduce automatic

Rejected

ICS runback rate on asymmetric

rod conditions

  • per DPC analysis