ML16161A935

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Insp Repts 50-269/87-49,50-270/87-49 & 50-287/87-49 on 871120-1207.Violations Noted.Major Areas Inspected: Containment Integrity During Refueling Operations
ML16161A935
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 12/23/1987
From: Bryant J, Peebles T, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A933 List:
References
50-269-87-49, 50-270-87-49, 50-287-87-49, NUDOCS 8801110415
Download: ML16161A935 (5)


See also: IR 05000269/1987049

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

REGION II

-<

101 MARIETTA STREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-269/87-49, 50-270/87-49, and 50-287/87-49

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242

Docket Nos.: 50-269, 50-270,

License Nos.: DPR-38, DPR-47, and

and 50-287

DPR-55

Facility Name:

Oconee 1, 2, and 3

Inspection Conducted: N vember 20 -

December 7, 1987

Inspectors:

Approved by: ____________,__________________

2

T. A. Peebles, Section ChiefDteSgd

r an

ate/Signed

H.

kinnDate

S igned

Division of Reactor Projects

SUMMARY

Scope:

This special,

unannounced inspection involved resident inspector

inspection in the area of containment integrity during refueling operations.

Results:

In the area inspected, one violation was identified.

9t801110415 971229

FPtR

ADOCK 05000269

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REPORT DETAILS

1.

Licensee Employees Contacted:

  • M. S. Tuckman, Station Manager

R. L. Sweigart, Operations Superintendent

C. L. Harlin, Compliance Engineer

  • F. E. Owens, Assistant Engineer, Compliance

Other licensee employees contacted included technicians, mechanics and

staff engineers.

Resident Inspectors

  • J. C. Bryant

P. H. Skinner

L. D. Wert

  • Attended exit interview.

2. Exit Interview

The inspection scope and findings were summarized on December 7, 1987,

with those persons indicated in paragraph 1 above.

The licensee did not

identify as proprietary any of the materials provided to or reviewed by

the inspectors during this inspection.

The following new item was

identified:

Violation

269,270,287/87-49-01:

Failure

to

Maintain

Containment Integrity During Refueling Operations.

3.

Licensee Action on Previous Enforcement Matters

Not inspected.

4.

Unresolved Items

Not inspected.

5.

Loss of Containment Integrity During Refueling Operations

On October 12,

1987, during reinsertion of fuel into the Unit 1 reactor,

the licensee notified the resident inspectors that air inleakage had been

detected at the containment emergency hatch through, installed temporary

seals.

Refueling operations had been stopped until the situation was

corrected. An investigation of the event was begun by the licensee and

findings of the investigation are provided in detail in Licensee Event

Report 50-269/87-08 which was issued November 25, 1987.

2

Oconee Nuclear Station (ONS)

Technical Specification (TS)

3.8.6 requires

that during the handling of irradiated fuel in the reactor building, at

least one door on the personnel and emergency hatches shall be closed.

The purpose of TS 3.8.6 is to prevent spread of contamination outside

containment in the event an irradiated fuel element is dropped during

handling.

At times,

due to ongoing work being performed in containment during

outages, it is necessary to have both of the emergency air lock hatches

open in order to permit piping and electrical connections from temporary

equipment

outside containment to

equipment being

serviced inside

containment, to pass through the hatches.

Examples of work requiring

this adjustment are sludge lance

and water slap cleaning of steam

generators and,

during the recent Unit 1 outage, chemical cleaning of

the steam generators.

Due to outage time considerations,

it

is very

beneficial to provide temporary sealing of the emergency lock hatches

to avoid extension of the refueling outage by several weeks.

During

refueling, TS Interpretation 3.8 permits sealing the emergency hatch to

prevent airflow by methods other than having one hatch closed, when it is

necessary to permit ongoing work to continue.

Description of Physical Layout

The emergency lock is 5 feet in diameter and 12 1/2 feet long overall.

Ith a hatchway 2 1/2 feet in diameter toward each end of the lock.

Both hatches open inward toward containment. Both hatches are operated

by a common shaft which is geared to provide sequential opening and

closing. The shaft is so geared that it is impossible to have one hatch

open unless the other is closed. Also, as the locking dogs are released

when either hatch is opened, an equalizing valve is cammed open to relieve

differential pressure.

When

it

is necessary to

have both hatches open while maintaining

containment isolation during refueling operations,

it

is necessary to

,physically disconnect the operating -

interlocking mechanism.

A steel

closure plate is then installed inside the lock to replace the inner

hatch.

The closure plate

has penetrations with welded-in

sleeves

protruding toward containment.

Necessary piping and cables are passed

through the sleeves. The sleeves are then sealed from inside the airlock

with a tough sealant foam to make the penetrations air tight.

Problems Experienced With Hatch Sealing

During the Unit 1 EOC 10 refueling outage, several things went wrong with

the job control process which resulted in defeating the sealing of the

emergency hatch. Also, the licensee's investigation determined that the

hatch probably had not been properly sealed on three earlier refueling

3

outages when temporary seals were used on emergency hatches, since the

procedure did not require sealing the 1" diameter equalization lines.

The events, as identified by the licensee, were as described below:

a.

The temporary modification designer did not realize that when the

emergency hatches were opened equalization valves were cammed open.

With both doors open,

equalization valve outlets would need to be

sealed to avoid providing a path from containment

to outside

atmosphere. There was no provision in the plan for sealing these

openings. The designer had used portions of a previous job plan in

preparing his job plan.

That job plan did not require sealing the

equalizing line. This led the licensee to suspect that the previous

temporary modifications might have failed to seal the line also.

b. After all items had been installed-through the closure plate, foaming

of the plate was assigned to a Construction and Maintenance Division

(CMD) crew. The Planning and Scheduling Coordinator (P&SC) informed

the CMD supervisor that the work should be done under a specific job

plan, and furnished an incorrect job plan number. The supervisor was

not informed that the work was safety related and, therefore,

a

procedure was required and a procedure was available for the work.

c.

The CMD lead man who was to perform the work was not sure of the

proper place to install the foam.

He made several phone calls to

CMD and ONS management but those he contacted could not answer his

questions. He was then advised by the P&SC,

who provided somewhat

ambiguous directions. The lead man then had the work performed by

building two dams about six inches apart inside the outer hatch of

the emergency lock, then foaming between the dams.

The work was

completed on September 22, 1987.

d.

On September 24, ONS Operations signed off a refueling procedure step

which verified that the temporary door had been installed in the

emergency hatch; defueling of the reactor began and was completed on

September 28. Sealing of containment was not required again until

October 10 when refueling began.

e.

On October 12 at 1:30 p.m. the reactor building coordinator (RBC) was

informed that air was coming through the closure plate and light

could be observed through the opening. The RBC verified the air flow

but did not notify Outage and Operations management until about

3:10 p.m. Fuel movement was then secured until the seal had been

repaired.

The licensee's investigation also determined that the

equalization valve was not sealed. This also was corrected.

Discussions With Personnel Involved

In the inspectors' discussions with the modification designer, who was on

emergency leave when the seals were installed, the P&SC and the CMD lead

man who performed the job, it became evident that there was considerable

lack of understanding and confusion between the principals. In the past,

4

the sleeves had been foamed from inside the airlock throuch the inner

hatch toward the inside of the containment building.

To do this, the

workmen had to crawl through the 30 inch diameter outer hatch and around

the cables and piping passing through it.

The designer recognized that during this particular outage with the

addition of two large pipes for chemical cleaning, it would be impossible

for the workmen to crawl through the outer opening to reach the inner

hatch. His intent was that the foaming be done into the sleeves from

inside the containment building. He had taken pictures of the seal plate

with sleeves and labeled them as taken from inside the reactor building

to indicate how the foam should be introduced. He was not aware that CMD

preferred to avoid taking the foam machine into a contaminated area.

The

P&SC was

aware that the

foam machine would not be taken into

containment, but was not aware that, with the additional piping, workers

could not enter the air lock from the yard area in order to foam in the

same manner as in the past.

The CMD

lead man believed he should not take the foam machine inside

containment, was told to foam from the outside, and did it

in the only

manner he saw possible.

Reaching into the lock through the outer hatch,

he constructed two

forms

around the cables

and

pipes

and

foamed

inbetween.

The work was done with the general foaming procedure,

but

without the work package and procedure on hand;

however,

the general

procedure was of little value for this particular job.

Results of Loss of Containment Integrity

There was no release of activity to -the environment .

A purge normally

is maintained during refueling activities, which maintains a slight

negative pressure in containment.

Also, there wa.s no dropped fuel or

other occurrence which released unusual activity during any of the four

periods mentioned when integrity was not maintained.

LER 50-269/87-08

,describes the FSAR analysis of fuel handling accidents.

This analysis

shows that had a fuel

handling accident occurred at the time,

the

consequences would be bounded by the analysis and that doses at the site

boundary would have remained below the limits of 10 CFR 100.

This is

Violation

269,270,287/87-49-01:

Failure

to -Maintain

Containment

Integrity During Refueling Operations.