ML16161A785

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Insp Repts 50-269/86-33,50-270/86-33 & 50-287/86-33 on 861015-1110.Violation Noted:Failure to Adequately Test Emergency Condenser Circulating Water Sys
ML16161A785
Person / Time
Site: Oconee  
Issue date: 11/28/1986
From: Bryant J, Peebles T, Sasser M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A784 List:
References
50-269-86-33, 50-270-86-33, 50-287-86-33, NUDOCS 8612100022
Download: ML16161A785 (14)


See also: IR 05000269/1986033

Text

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q.,UNITED

STATES

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NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos: 50-269/86-33, 50-270/86-33, and 50-287/86-33

Licensee:

Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Facility Name:

Oconee Nuclear Station

Docket Nos.: 50-269, 50-270, and 50-287

License Nos.: DPR-38, DPR-47, and DPR-55

Inspection Conducted: October 15 - November 10, 1986

Inspectors:

7,10A Z

J. C. Bryant

Date Signed

M.-(. Sasstr

Date Signed

Approved by:

T. Peeblef, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved resident inspection on-site

in the areas of operations, surveillance, maintenance, verification of engineered

safety features lineups, followup of events, followup items of non-compliance,

and performance indicators.

Results: Of the seven areas inspected, no violations or deviations were identi

fied in six areas.

One item of violation was identified in one area; Failure to

test the ECCW system adequately.

This violation is being considered for escalated enforcement:

Technical Specification 4.0 requires that surveillances be performed to

assure that the quality of systems is maintained and that operation is

within the safety limits and limiting conditions for operation.

The ECCW

system test frequency is given in Table 4.1.2.

Contrary to the above, as discovered during a test conducted on October 1,

1986, the ECCW had never been tested in a manner adequate to reveal that the

ECCW would not perform its required function during station blackout with

Lake Keowee level nine feet below full pond. Although the system has been

tested according to procedure at the required frequency, the test procedure

was inadequate to reveal system deficiencies.

The violation was identified

by the licensee. The resident inspectors also were present.

8612100022 861201

PDR ADOCK 05000269

G

PDR

REPORT DETAILS

1. Licensee Employees Contacted

  • M. S. Tuckman, Station Manager

T. B. Owen, Maintenance Superintendent

R. L. Sweigart, Operations Superintendent

J. M. Davis, Technical Services Superintendent

  • C. L. Harlin, Compliance Engineer
  • F. E. Owens, Assistant Engineer, Compliance

N. A. Rutherford, System Engineer, Licensing

Other licensee employees

contacted included technicians,

operators,

mechanics, security force members, and staff engineers.

Resident Inspectors:

  • J. C. Bryant
  • M. K. Sasser

.

  • Attended exit interview.

2. Exit Interview

The inspection scope and findings were summarized on November 13, 1986, with

those persons indicated in paragraph 1 above.

The licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

3.

Licensee Action on Previous Enforcement Matters

VIO 270/85-10-01

(Closed)

Control

Rod Position Limits Exceeded.

The

inspectors have reviewed the procedural revisions, additional training, and

other corrective actions and consider them satisfactory to prevent recurr

ence of this type of violation.

VIO 270/85-41-01 (Closed) Delayed Shutdown With RCS Leakage Greater Than 1

GPM. The inspectors have reviewed the implementation of a revised reactor

coolant system leakage calculation procedure and have verified that adequate

acceptance criteria exist to prevent similar problems in the future.

VIO 269/84-25-04, 270/84-24-04, 287/84-27-04 (Closed) Failure to Dissemi

nate Information on Operating Experience to Mechanical and I&E Personnel.

The inspectors reviewed revised Maintenance Directive II.3 which implements

the program for providing operating experience information to all levels of

Maintenance personnel.

The implementing procedures and training records

were also reviewed to ensure that plant personnel are being appropriately

trained on pertinent information and that this information is documented.

2

The program as implemented provides assurance for compliance with TMI Action

Item I.C.5, Establishment of Procedures for Feedback of Operating Experience

to Plant Staff.

4. Unresolved Items

No unresolved items were identified during this inspections.

5. Licensee Event Reports

The inspectors reviewed nonroutine event reports to verify the report

details met license requirements,

identified the cause of the event,

described corrective actions appropriate for the identified cause,

and

adequately addressed the event and any generic implications.

In addition,

as appropriate, the inspectors examined operating and maintenance logs, and

records and internal investigation reports.

Personnel were interviewed to verify that the report accurately reflected

the circumstances of the event, that the corrective action had been taken or

responsibility assigned to assure completion,

and that the event was

reviewed by the licensee, as stipulated in the Technical Specifications.

The following event reports were reviewed:

LER 269/86-01 (Closed) Generator/Reactor Trip Due To Failure Of PCB-20

In 230 KV Switchyard.

Corrective actions taken by the licensee have

been reviewed and are acceptable.

LER 269/86-03 (Closed)

Missed Grab Sample When The #3 Chemical

Treatment Pond Liquid Effluent Sampler Was Inoperable. Procedures have

been revised to improve shift turnover to ensure personnel are aware of

inoperable instruments and resulting required actions.

LER 269/86-04 (Closed)

Fuel Movement In Progress While NI-1 Inoper

able. Corrective actions taken by the licensee have been reviewed and

determined to be satisfactory.

LER 269/86-07 (Closed) Two Reactor Protection System Channels Inoper

able At The Same Time.

I&E Maintenance procedures have been revised to

require tagging of an

RPS channel

any time a dummy bistable is

installed or when the channel is inoperable due to a failed instrument.

Tagging of the bypass key alerts personnel of the condition to ensure

that two channels are not bypassed at the same time.

LER 270/86-02 (Closed)

Reactor Trip Due To Personnel Error During

On-Line Control

Rod Drive Breaker Testing.

The inspectors have

reviewed the corrective actions and consider them appropriate to

prevent recurrence of this type of event.

LER 270/86-04 (Closed) Reactor Trip From High Steam Generator Level.

LER 270/86-05

(Closed) Reactor Trip From High Steam Generator Level.

3

LER 269/85-07 (Closed) Unit 1 Trip On Loss Of Main Feedwater Following

Failure of Static Inverter. All corrective actions have been completed

and are satisfactory.

LER 269/84-07 (Closed) Unit 1 Trip Upon Loss of Main Feedwater Pumps.

Shaft oil pump was disassembled and inspected with no problems found.

Check valve on auxiliary oil pumps was found stuck open, preventing

shaft pump from maintaining sufficient pressure.

6. IE Bulletins and Inspector Followup Items

BU 83-03 (Closed)

Check Valve Failures in Raw Water Cooling Systems of

Diesel Generators (DG's).

The inspectors reviewed the licensee's response

dated June 20, 1983.

At that time there were no DG's in use at Oconee.

Since that time, the standby shutdown facility (SSF) was completed and was

declared operational in October 1985.

The SSF utilizes a DG. The inspec

tors reviewed tests of flows and back leakage performed on valve CCW-284.

The system is tested under PT/O/A/0400/04, Diesel Engine Service Water Pump

Test, which is performed quarterly.

Tests performed on 7/30/85, 1/8/86,

6/3/86, and 9/3/86 gave satisfactory results with little or no back leakage.

The test of 4/8/86 revealed considerable back leakage.

The inspectors

reviewed Work Request (WR) 91067C, dated 4/8/86 and performed on 6/8/86,

under which valve CCW-284 was disassembled, inspected, cleaned and blue

checked. No problem was found other than crud in the system. The valve was

tested subsequently and performed with no back leakage.

IFI 269/84-25-05,

270/84-24-05,

287/84-27-05

(Closed)

Deficiencies in

General Employee Training (GET).

The inspectors reviewed the licensee's

upgraded training program to determine if upgrades had been effected in

those areas where deficiencies were found to exist. The licensee was found

to have appropriately upgraded training in security, QA, emergency response,

independent verification, adherence to procedures, and health physics, both

in the video presentations and the material included in the GET handbook.

These revisions were a direct response to the inspectors' earlier findings

and the licensee's normal program for review and upgrade of training

programs.

IFI

269, 270, 287/86-10-01

(Closed)

End of Cycle Moderator Temperature

Coefficient

(MTC)

Measurements.

Additional measurements of MTC were

completed on Unit 3. The results were acceptable and verified the revised

Final Safety Analysis Report calculations.

IFI 270/85-37-02

(Closed)

Mispositioned Containment Isolation Valve.

Immediate corrective actions were taken to ensure that containment integrity

was maintained.

Supplemental actions were taken to provide added assurance

that the valves in question will remain in the required position in the

  • k

future.

4

7.

Plant Operations

The inspectors reviewed plant operations throughout the reporting period to

verify conformance with regulatory requirements,

technical specifications

(TS), and administrative controls.

Control

room logs, shift turnover

records,

and equipment removal

and restoration records were reviewed

routinely.

Interviews were conducted with plant operations, maintenance,

chemistry, health physics and performance personnel.

Activities within the control rooms were monitored on an almost daily basis.

Inspections were conducted on day and on night shifts, during week days and

on weekends.

Some inspections were made during shift change in order to

evaluate shift turnover performance.

Actions observed were conducted as

required by Operations Management Procedure 2-1. The complement of licensed

personnel on each shift inspected met or exceeded the requirements of TS.

Operators were responsive to plant annunciator alarms and were cognizant of

plant conditions.

Plant tours were taken throughout the reporting period on a routine basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1 and 2 Penetration Rooms

Units 1,2, and 3 Electrical Equipment Rooms

Units 1,2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Condenser Circulating Water Intake Structure

During the plant tours,

ongoing activities, housekeeping,

security,

equipment status, and radiation control practices were observed.

Unit 1 began the report in cold shutdown,

having shut down during the

previous report period due to inoperability of the Emergency Condenser

Circulating Water (ECCW)

system (see report 86-26).

Following repairs to

and successful testing of the ECCW system, the unit was taken critical on

10/19 at 10:09 p.m.

The turbine generator was placed in service the

following day.

Power was increased to approximately 99% and remained there

for the duration of the report period. The unit is limited to 99% power due

to a high level in the B Once Through Steam Generator (OTSG).

Unit 2 began the report period in a refueling and maintenance outage, with a

delayed startup date due to ECCW inoperability. On 10/17 the reactor was

taken critical for performance of zero power physics testing (ZPPT).

Later

the same day, after completion of ZPPT,

power was increased to 15% for

additional Low Power Physics Testing.

On 10/18 the generator was place in

service and power was increased to succeeding higher levels for power

escalation testing.

5

Unit 2 reached 92%,

limited to that power level due to high level in the B

OTSG.

Both OTSGs had undergone water slap and sludge lance cleaning

processes during the outage, with levels in the A OTSG improving while the B

OTSG appeared to have gotten worse.

On 10/23, at 2:37 p.m. the reactor

tripped when high OTSG level caused a turbine trip. The high level trip was

reached during a secondary feedwater swing initiated by problems in the

integrated control system (see paragraph 10).

The reactor was returned

critical at 7:17 the same day.

Power was increased to approximately 95%

where it has remained for the duration of the report period.

Unit 3 began the report period in cold shutdown due to ECCW inoperability.

On 10/22 at 2:11 a.m. the reactor was taken critical and power ascension

began. At 8% reactor power control room alarms indicated a low oil level in

the 3B1 Reactor Coolant Pump (RCP).

The pump was secured and the reactor

taken subcritical at 7:50 a.m. in order to make a reactor building entry to

add oil to the RCP.

Following addition of oil the reactor was critical at

2:13 a.m.

On 10/23,

the turbine generator was placed on line and power

increased to 100%.

On 10/24 the Statalarm for low oil level on 3B1 RCP was again received in

the control room. Power was reduced to less than 75%, the RCP was secured

and shutdown of the Unit was initiated for repair of the oil leak.

The

reactor was shutdown at 1:02 a.m.

on 10/25 and subsequently taken to cold

shutdown conditions.

Following a four day outage the reactor was again

critical at 9:19 a.m. on 10/29.

Power was increased to 96% when, on 10/30,

the 3B1 motor frame vibration increased and alarms on the Unit 3 Loose Parts

Monitor indicated problems with the RCP. Power was reduced to less than 75%

and the pump was secured.

See paragraph 17 for details surrounding the

problems found with the RCP and analysis thereof. The Unit has continued in

a 3 RCP operating mode at 72% as limited by Technical Specifications. The

licensee plans to operate in this mode for the duration of this cycle, with

a refueling outage scheduled in March 1987.

No violations or deviations were identified.

8.

Surveillance Testing

The surveillance tests listed below were reviewed and/or witnessed by the

inspectors to verify procedural and performance adequacy.

The completed tests reviewed were examined for necessary test prerequisites,

instructions, acceptance criteria, technical content, authorization to begin

work, data collection, independent verification where required, handling of

deficiencies noted, and review of completed work.

The tests witnessed, in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated, prere

quisites were met, tests were conducted according to procedure, test results

were acceptable and systems restoration was completed.

6

Surveillances witnessed in whole or part:

TT/2/A/0711/09 Unit 2 Cycle 9 ZPPT

TT/2/A/0811/09 Unit 2 Cycle 9 Power Escalation Test

No violations or deviations were identified.

9. Maintenance Activities

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within the

skill of the trade.

Activities, procedures and work requests were examined

to verify proper authorization to begin work, provisions for fire, clean

liness, and exposure control,

proper return of equipment to service, and

that limiting conditions for operation were met.

Maintenance witnessed in whole or in part:

WR 91457C Repair Gov. Valve on 2 TDEFWP

WR 40501C Troubleshoot ICS to find source of feedwater swings,

turbine header pressure swings.

No violations or deviations were identified.

10.

Unit 2 Trip

At 2:37 p.m. on 10/23 Unit 2 tripped from 92% power following a turbine trip

on high steam generator (OTSG) level.

Prior to the trip the reactor was

restricted to 92% power by high OTSG levels (90% in B OTSG)

despite the

OTSGs having been water slap and sludge lance cleaned during the recently

completed refueling outage.

The initiating cause of the transient was the failure of an Integrated

Control System (ICS)

module responsible for control of the turbine steam

header pressure.

Upon failure of the instrument the turbine control valves

stepped open resulting in rapid decrease of the turbine header pressure.

The sudden decrease in steam pressure caused a rapid overfeed of feedwater

to the OTSG's.

Since the OTSG's were already operating with high levels,

the high level trip setpoint (96%)

was exceeded all most immediately,

preventing recovery from or corrective actions by the reactor operators.

The OTSG high level trip caused the main turbine and main feedwater pumps to

trip, resulting in an anticipatory reactor trip.

Both motor driven emergency feedwater pumps (MDEFWP)

actuated to control

OTSG levels.

At the time of the transient the turbine driven emergency

feedwater pump (TDEFWP) was out of service for maintenance. There was no

Engineered Safety Feature Actuation.

All systems responded normally.

Following a post trip review, replacement of the ICS instrument module, and

return to service of the TDEFWP,

the reactor was returned critical at 7:37

pm with the generator on line at 12:30 a.m., 10/24.

7

This type of transient is expected to occur more frequently than in the past

as the reactors continue to operate with higher than normal OTSG levels.

The licensee is pursuing additional methods for cleaning the OTSGs,

including chemical cleaning which will be tried in a future refueling

outage.

No violations or deviations were identified.

11.

Unusual Event:

Hydrazine Spill

An Unusual Event was declared at the Oconee site at 9:10 p.m. on October 21,

1986 due to a hydrazine spill of approximately two gallons in the turbine

building. The Unusual Event was declared due to the release of a toxic gas,

although there was no detectable gas at site boundaries.

There were no

injuries due to the release.

Hydrazine is used at Oconee for oxygen scavenging in the secondary system.

The spill was caused by a deionized water mixing valve leaking through and

causing the mix tank, located in the turbine building, to overflow.

The

spill was detected by an operator who smelled ammonia and tracked down the

source. A site assembly was held in order to account for all personnel.

The leakage was stopped, the spilled area cleaned, and the Unusual Event

terminated at 11:25 p.m. on October 21, 1986.

No violations or deviations were identified.

12.

Electrical Inoperability of Limitorque Valve - Unit 2

Prior to start up of Unit 2 following refueling shutdown,

the licensee

discovered damage to Limitorque operated valve 2CF-1.

Valve 2CF-1 is the

isolation valve from 2A core flood tank, which normally is in the open

position with breaker open and locked during reactor operation. Valve 2CF-1

is not on the licensee's list of valves for immediate rework as given in the

response to IE Bulletin 85-03 dated May 16,

1986.

However,

the valve

operator will be refurbished and MOVATS tested in the program presented to

Region II on August 1, 1986. The description of the event as given below is

essentially verbatim from a licensee internal report.

During the visual inspection of 2CF-1 for functional verification after

maintenance it was discovered that the limitorque operator had some sheared

bolts on the operator cap flange. When attempting to replace the bolts it

was further discovered that the cap flange bolting surface on the operator

housing has cracks around the bolt holes.

This portion of the operator

contains the stem c'ollar and bushing, stem nut and a locking nut. The lock

nut threads were found to be stripped and as a result the stem collar and

stem nut were forced up against the cap flange upon stem movement.

This

overstressed the cap flange retaining bolts causing the bolts to shear and

bolt holes to crack.

8

The licensee determined that the torque switch on the operator was not

functioning properly, causing the operator to overtorque, stripping the lock

nut. Temporary repairs were made which replaced the lock nut and cap flange

bolts.

Permanent repair of the operator would require removal from the

valve and subsequent valve stroking upon replacement to set up the limit and

torque switches. A Performance stroke test is also required after operator

repair. This repair, at the present time with RCS system pressure

800

psig, would require direct violation of Technical Specification 3.3.3 upon

stroking the valve closed.

The temporary repair will allow the valve to be operated manually if needed.

However, there is no guarantee that the valve will operate electrically.

Presently the valve is in its normal position, open, with the breaker white

tagged and locked open.

This allows the 2A Core Flood Tank to operate as

designed during an accident situation (i.e. largeLOCA).

During a normal

plant shutdown, when isolating the Core Flood Tanks, the 2A tank will have

to be isolated by manually closing 2CF-1.

Emergency Operating Procedure EP/2/A/1800/01 directs the operators to close

the Core Flood Tank isolation valves in 3 different situations:

Cooldown

Following a Large LOCA; Steam Generator Cooldown with a Saturated RCS; and

HPI Cooling Cooldown. The licensee determined that the inability to isolate

the core flood tank after dumping following a large break LOCA is not a

concern since the nitrogen entering the system would exit out the break. In

the other two situations, isolation of the Core Flood Tanks is performed to

aid in cooldown when the following conditions exist, RCS pressure § 1000

psig and core subcooling margin

0 degrees Fahrenheit.

Attempting to

isolate 2A Core Flood Tank by electrically operating 2CF-1 should only be

done in these 2 situations if absolutely necessary and with approval of the

Operations Duty Engineer.

Control of 2CF-1 will be handled in the following way until the next

available time for repair (RCS

system § 800 psig).

The control switch will

be white tagged and an additional white tag will be put on the valve breaker

with instructions to operate electrically only with the approval of the

Operations Duty Engineer. A copy of this letter will be put in the Unit 2

Operational Guide Book and this information will be noted on the RO turnover

sheet and the Unit 2 Supervisors turnover sheet.

The inspectors will follow up on repairs to 2CF-1.

This is listed as an

inspector followup item;

IFI 86-33-01, Repairs to Valve 2CF-1.

13. Operability of Rotork Valve Actuators

On Friday, 10/24, the Oconee staff was notified by the Duke General Office

(GO)

that valve actuator testing conducted at the Catawba Nuclear Station

had determined that the torque switch settings on Rotork actuators are not

linear as previously assumed by the vendors and licensee. The non-linearity

was found in the non-conservative direction such that the torque switch

setting of installed valves may not allow adequate torque development for

operation of the valves under all conditions.

9

While the licensee's McGuire and Catawba Nuclear Stations utilize Rotork

actuated valves in numerous applications, their use at Oconee is limited to

30 valves in 12 different applications. Limitorque actuators are used more

frequently at Oconee.

The licensee's Oconee and GO staff reviewed the

applications of the 30 safety related Rotorks to determine if

the oper

ability of the valves is in question. Based on the current switch settings,

the design conditions that each valve must meet to accomplish its safety

function, and actual testing on the valves, each has been determined to be

fully operable at the present time. The licensee's findings are as follows:

1. 3LP1,

3LP2 - Suction valves to decay heat cooling pumps from the

reactor coolant system.

A calibration curve is on file for each of these valves and the

torque switch settings have been field verified.

2.

1,2,3LP103 - Post LOCA boron dilution valves

1,2,3LP104 - Post LOCA boron dilution valves

1LP105

- Alternate flowpath for post LOCA boron dilution

for Unit 1 only

1,2,3HP398 - RCP seal injection from Standby Shutdown Facility

reactor coolant makeup pump

1,2,3LPSW565 - Low pressure service water isolation to the

reactor building auxiliary cooling units.

1,2,3LPSW566 - Low pressure service water isolation to the B

reactor building cooling unit.

1.2.3PR59 -

Reactor building purge system isolation to

hydrogen analyzer

1,2,3PR60 -

Reactor building purge system isolation to

hydrogen analyzer

The above listed valves are tested (ASME

XI cycled) during normal

plant operations at conditions which approximate those conditions

which would occur when each has to perform its safety function.

Each has operated satisfactorily during normal testing, therefore

each is considered operable with the current settings.

HP398 is

required only during an SSF event.

3. 1,2,3FDW347 - SSF auxiliary service water pump supply to B

OTSG.

1,2,3CCW269 - SSF auxiliary service water pump supply to A

OTSG.

Comparison of the factory torque settings with the field installed

settings verified that the actuators were installed as received.

Those settings used will allow the valves to perform their safety

functions.

FDW 347 is required to be open during plant opera

tions.

CCW269 is required only during an SSF event.

Based on the above evaluations, these valves have been determined to be

fully operable. The licensee will adjust torque settings to their optimum

value during a future outage as part of the program to upgrade motor

operated valves through a program of signature analysis, rebuilding, and

testing (as defined by IE Bulletin 85-03).

14.

Followup on General Electric Service Information Letter (SIL) 445

Region II correspondence to the residents dated 10/20 requested followup on

SIL 445 entitled, "Intermediate Range Monitor (IRM)

Fuse Failure", dated

7/26/86. While the SIL involved specific equipment installed only at GE

Boiling Water Reactors,

the residents reviewed the intermediate range

channel equipment installed at Oconee to determine if similar problems could

exist.

In the GE IRM system, multiple fuse failures had occurred in the positive

and negative 24 Vdc power supplies to the system. Fuses for the +24Vdc were

replaced and the system appeared to be working properly.

However, it was

later discovered that there were still blown fuses in the -24Vdc power which

prevented signal processing in the system, with the ultimate result that IRM

initiated scrams provided by the Reactor Protection System (RPS)

may not

have occurred if needed.

O At Oconee the RPS uses a +15Vdc and -15Vdc

power supply system.

If any

power supply fails (blown fuse, open breaker, etc.) the respective RPS

channel will trip providing control room statalarms and a channel tripped

indication to the other RPS channels. Therefore,

any failure places the

system in a conservative configuration.

The power supplies for the source, intermediate, and power range detectors

are all separate. If any fail, the flux signal from the respective detector

fails low. Once again, control room statalarms provide indication of failed

channels.

15.

Emergency Condenser Circulating Water (ECCW)

IE Report No. 50-269, 270 and 287/86-26 discusses in detail the licensee's

finding of the plants inability to sustain ECCW gravity flow, the rapid

response in shutting down the two operating units, the determination of the

cause and the corrective action taken. Though the resident inspectors were

witnessing this test, the licensee also promptly reported the events and

developments to Region II.

Three Unresolved Items were identified in report 86-26.

One of these

concerned inadequate procedures and testing to verify gravity flow, in that

gravity flow probably could never have been maintained when Lake Keowee was

approximately nine feet below full pond.

The lake was in that condition in

the early 1980's and had been in that condition most of the preceding year

when the deficiency was identified in October 1986.

Condenser Circulating

Water System Gravity Flow Test, PT/1,2,3/A/261/06, is performed on each

refueling outage with the purpose of, as related to gravity flow, to test

that following simulated loss of power to the CCW pumps, cooling water flow

is maintained by gravity and siphon effect to the Keowee tail race.

The

acceptance criteria are that all valves assume their proper position to

establish and sustain gravity .....

flow as specified in the procedure; and,

gravity flow is verified by visual observation.

No required time of flow

was specified.

In a letter to the Region II Administrator, the licensee described the

manner in which the test will be performed in the future. This states that

flow will be maintained a minimum of four hours and that an acceptable

minimum CCW

pump discharge vacuum shall be maintained for at least four

hours.

Technical Specification 4.0 requires functional tests to demonstrate

capability of systems to perform design functions, though the ECCW system

has been tested at required frequency and met the acceptance conditions, it

is apparent that the tests performed were not capable of demonstrating that

the system met design intent.

In not analyzing the system adequately to

determine that flow would exist for a time due to draining of the system,

with or without a siphon being established, the acceptance criteria led

observers into thinking siphon flow had been established as soon as flow

appeared at the tailrace.

Though the licensee's actions meet the criteria of 10 CFR Part 2, Appendix C, for licensee identified violations, in the inspector's opinion,

adequate review of the procedure should have determined much earlier that

the performance test was not adequate to demonstrate proper operation of the

system.

Therefore,

UNR 50-269,270,287/86-26-04 will be changed to a

Violation, (Violation 50-269.270,287/86-33-02,

Inadequate Testing of ECCW

System).

The unresolved item will be cancelled.

The referenced report also listed two other Unresolved Items concerning the

ECCW event.

These were UNR 50-269,270,287/86-03, Questionable Design of

ECCW system and UNR 50-269,270,287/86-05, Inoperable High Point Vent Vacuum

Lines, concerning blind flanges in the vacuum lines of Unit 2. While these

events were as described, they will not be cited as violations since they

occurred over thirteen years ago, and failure to detect them earlier would

fall under inadequate testing cited earlier in this paragraph.

16.

U-3 Steam Generator Tube Leak

At the time Unit 3 was shut down on October 2 for ECCW system modification,

it had demonstrated a possible steam generator tube leak.

At the time of

shut down,

the suspected leak was too small to make identification of a

leaking tube certain.

During the shutdown for the ECCW system, the steam

generator was examined and four tubes which exhibited small leaks were

plugged along with an additional three tubes in the same area.

12

17.

Unit 3 - Reduced Power Due to Reactor Coolant Pump Problem

At 5:10 a.m. on October 30, 1986, Unit 3 was reduced in power from 96% to

65% and reactor coolant pump (RCP) 3B1 was shut down due to reduced perfor

mance and other symptoms of degraded pump operation.

Anomalies noted prior

to, during, and following pump shut down were as described below.

10/28;

6:00 p.m.

Primary chemistry detected a possible crud burst

in the RCS

and a high suspended solid concentration.

Activation product concentration using Mn 56 as an indicator

reached 2.1 uCi/ml prior to pump shutdown.

Concentration

reached 0.119 uCi/ml 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> after RCP shut down.

10/29;

7:15 p.m. Slight FDW re-ratio along with a 1-2% increase in

total RCS flow.

10/29;

11:27 p.m.

Computer alarm on RPS flow low with 6% drop in

RCS total flow indicated.

Loose parts monitor alarm for

reactor vessel, cleared upon acknowledgement.

10/30;

12:01 a.m. RCP 3B1 motor input power dropped from 6.1 to 5.1

mw.

Stattor temperature dropped 12 degrees Fahrenheit.

Motor vibration began increasing.

10/30;

4:44 a.m. RCP 3B1 motor frame vibration had increased to 2.1

mils.

10/30;

5:10 a.m. RCP 3B1 was shut down after reactor power had been

reduced to 65%.

Analysis by the licensee resulted in the evaluation that there had been no

core damage; that the noise monitor reflected normal pump shut down noise;

that there probably was a failure in the pump wear ring or intake vanes; and

that continued operation, without any starting or stopping of RCP's, should

not result in the relocation of or generation of any loose parts.

Following an evaluation to justify continued operation,

the licensee

increased power to 72% with RCP 3B1 shut down,

as permitted by Technical

Specifications.

It is planned to complete the current cycle at that power.

Unit 3 is scheduled for refueling shutdown about March 1, 1987.

18. Licensee Identified Violations

LIV86-01 (Closed) Time Limit Exceeded in Emergency Response Requalification

Training.

In a letter to Region II dated October 7, 1986,

the licensee

reported that,

due to a change in the schedule for annual

requalification of Operations Emergency Response personnel,

the

requalification training period exceeded the stated one year + 3

13

months period for certain personnel.

The licensee has taken

adequate corrective action to update training and to prevent

recurrence. This item is closed.

LIV86-02 (Closed) RIA-54, Isolation of Turbine Building Sump Discharge on

High Activity found bypassed on October 28, 1986.

All releases from the sump had been sampled daily with no high

activity noted; also, RIA-54 Statalarm in control room would have

alarmed on high activity even though there would have been no

automatic isolation.

Adequate corrective action was taken to

prevent recurrence. This item is closed.