ML16154A807

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Insp Repts 50-269/95-11,50-270/95-11 & 50-287/95-11 on 950528-0624.Violations Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Testing,Onsite Engineering & Plant Support
ML16154A807
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 07/12/1995
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A806 List:
References
50-269-95-11, 50-270-95-11, 50-287-95-11, NUDOCS 9507200034
Download: ML16154A807 (17)


See also: IR 05000269/1995011

Text

SREGj

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-269/95-11, 50-270/95-11 and 50-287/95-11

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.: DPR-38, DPR-47 and DPR-55

Facility Name: Oconee Units 1, 2 and 3

Inspection Conducte

ay 28 - J e 24, 1995

Inspectors * A ,Z

q

E. 'HarmsSenior R ident Inspector

ate Signed

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. G.

phrey, Re ide

t Inspector

Approved by:

WFV. Crle r

f

Date Signed

Reactor Projects Branc 3

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, maintenance and surveillance testing, onsite

engineering, and plant support. It included an inspection of open

items and licensee event reports.

Results:

One violation, one inspector followup item, and one programmatic

strength were identified. In addition, a weakness in designating

the proper Quality Assurance (QA) classification was identified in

the licensee's work control system.

In the operations area, Unit 3 mid-loop activities were conducted

safely. The licensee's program, which included redundant

instrumentation, containment controls and contingency plans, was

well implemented, paragraph 2.c.

In the area of maintenance, a weakness in designating the proper

QA classification was identified in the licensee's work control

system, paragraph 3.a.(5). An inspector followup item was

identified regarding the QA level assigned to Condenser

ENCLOSURE 2

9507200034 950712

PDR ADOCK 05000269

PDR

2

Circulating Water (CCW) pump breaker maintenance activities,

paragraph 3.a.(7).

In the area of engineering, a violation was identified involving

the failure to initiate the Problem Investigation Process (PIP) in

a timely manner for a problem with containment isolation valves,

paragraph 4.a.

In the area of plant support, licensee management's support of

efforts to reduce Unit 3 outage dose was considered a strength,

paragraph 5.c.

ENCLOSURE 2

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

B. Peele, Station Manager

  • E. Burchfield, Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

  • W. Foster, Safety Assurance Manager
  • J. Hampton, Vice President, Oconee Site
  • D. Hubbard, Maintenance Superintendent
  • B. Jones, Training Manager

C. Little, Electrical Systems/Equipment Manager

  • J. Smith, Regulatory Compliance
  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends. Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

ENCLOSURE 2

2

housekeeping, security, equipment status, and radiation control

practices were observed.

b.

Plant Status

Unit 1 operated at full power throughout the reporting period.

Unit 2 operated at full power throughout the reporting period.

Unit 3 operated at full power until June 6, 1995, when the unit

began a scheduled 35-day end of cycle refueling outage.

c.

Mid-Loop/Reduced Inventory Activities

During the Unit 3 End Of Cycle 15 Refueling Outage (U3EOC15), the

licensee reduced Reactor Coolant System (RCS) inventory and

reached the mid-loop operations level on June 12, 1995. This was

done for the purpose of installing nozzle dams in the steam

generators. The inspectors reviewed the licensee's program prior

to the reduction of RCS inventory and verified that the

requirements were met while operating at the reduced inventory

levels as specified in Operations Procedure OP/3/A/1103/11,

Draining And Nitrogen Purging Of RC System, Enclosure 3.6,

Requirements For Reducing RXV Level To < 50" On LT-5. This

procedure stipulated the sequence and steps required for reduction

of RCS inventory and mid-loop operation. It further specified the

precautions and limitations to be adhered to while in mid-loop.

Step 1 of Enclosure 3.6 specifically addressed the ability to

establish containment closure. The licensee implemented a

Shutdown Protection Plan for the outage which required containment

closure to be maintained except as necessary to bring materials

and tools in and out of the reactor building. The Plan further

required that penetrations be closed, except for those with

temporary cables installed, as necessary for outage activities

such as steam generator tube testing and maintenance.

The inspector verified that the requirement for two independent

trains of RCS level monitoring was met while at reduced inventory.

This was accomplished by the use of two permanently installed

instruments (LT-5A and LT-5B) and two temporary ultrasonic

instruments. Level indications were displayed in the control room

on the LT-5A and LT-5B indicators, the Inadequate Core Cooling

Monitor, and on the Operations Aid Computer.

The inspector verified that two trains of core exit thermocouples

were available and utilized while at reduced inventory, as well as

the two sources of inventory makeup and cooling were available for

operation. The inspector reviewed the licensee's contingency

ENCLOURE 2

3

plans to repower vital busses from available alternate electrical

power supplies in the event of a loss of the primary source.

The licensee was at reduced inventory for approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />.

During the time that Unit 3 was in a reduced inventory status, the

licensee implemented and maintained the requirements specified by

procedure, and the operation at reduced inventory was accomplished

without incident. The inspector concluded that this reduced

inventory evolution was well coordinated and controlled.

Within the areas reviewed, licensee activities were satisfactory.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures and work orders (WO) were examined to verify that

proper authorization and clearance to begin work was given,

cleanliness was maintained, exposure was controlled, equipment was

properly returned to service, and limiting conditions for

operation were met.

Maintenance activities observed or reviewed in whole or in part

are as follows:

(1) Replace RCS High Point Vents, WO 95005775

The inspector witnessed part of a modification (NSM-32927)

that added a dedicated shutdown vent line to the Unit 3

quench tank from the existing Unit 3 High Point Vent (HPV)

system. The activity observed was the replacement of

existing HPV valves 3RC-19 and 3RC-38 with new class "A"

Anderson Greenwood 1-inch manual globe valves. In addition

to observing portions of the work in the field, the

inspector reviewed the licensee's 10CFR5O.59 evaluation for

the modification, reviewed the work order, verified that the

manufacturer's certificate of conformance for these valves

matched the specifications called for in the licensee's

purchase order, and verified that the control room drawings

reflected the new piping configuration. All activities

observed, and all documentation reviewed, were satisfactory.

(2) Perform Bench Test on 3BS-2, WO 94089245

The inspector observed the post maintenance test conducted

on Unit 3 building spray valve 3BS-2. The test was

conducted in accordance with procedure IP/O/A/3001/11F,

Limitorque Actuator Testing Using KALSI Engineering Test

ENCLOSURE 2

4

Bench. This test measured the developed torque by the valve

operator at various voltages. For the test conducted at 75%

voltage, the developed torque was 718 ft-lbs in the open

direction and 728 ft-lbs in the close direction. Both

measured values were below the calculated value of 754 ft

lbs. The licensee initiated a Problem Investigation Process

(PIP) for this discrepancy. This PIP concluded that the

developed torque was adequate for this motor operated valve

to meet all design basis requirements. As of the end of the

inspection period the licensee was still trying to resolve

the difference between the predicted and actual torque

values. The inspector concluded that the test was conducted

in accordance with the procedure and that actions taken to

resolve test deficiencies were appropriate.

(3) Replace 3HP-410 With Item No. DMV-1023, WO 94093641

The inspector observed replacement of Unit 3 High Pressure

Injection valve 3HP-410 on June 16, 1995. The effort

involved cutting out the existing valve and installing the

new one. The inspector noted that the work was performed in

accordance with Minor Modification OE-7089. The inspector

reviewed the hot work permit for the welding process that

was included as part of the work package. All work observed

was determined to meet acceptable standards.

(4) Repair 3BS-1 Seat Leak, WO 95019948

The inspector observed repair of Unit 3 building spray valve

3BS-1 on June 16, 1995. The valve bonnet was being re

installed on the valve body. The effort was in accordance

with MP/0/A/1200/002A, Valve - Globe - Pressure Seal and

Bolting Bonnet Disassembly, Repair, and Reassembly.

Additional procedures were provided with the work package

which included MP/O/A/1200/001D, Valves - NRC - 89-10

Replacing and Adjusting Packing, and MP/0/A/1210/007,

Operator - Limitorque SMB/SB Series - Removal and

Replacement. The work effort reviewed was in accordance

with plant procedures and documentation was updated to the

current work status.

(5) Inspect and Clean The A HPSW Pump Strainer, WO 95029083

The inspector reviewed activities performed to inspect and

clean the strainer at the suction of the High Pressure

Service Water (HPSW) pump. Maintenance procedure,

MP/0/A/1800/003, Flanges - Torquing, was attached as part of

the work package which listed the torquing values and

tightening sequence for the replacement of the strainer

flange. However, the procedure torque values were not

ENCLOSURE 2

S

5

utilized since the gasket was rubber. The values were

changed by the system engineer from 581 psi to 100 psi.

The inspector noted that the work package was designated as

non-QA. The inspector questioned the appropriateness of

work on the HPSW system to non-QA standards. As a result,

the licensee evaluated the classification and determined

that it should have been classified as QA level III.

Since

the standards were essentially the same for QA level III

classification work and non-safety work, the inspector

concluded that there was no safety impact. The inspector

concluded that the failure to appropriately classify this

work constituted a weakness in the licensee's work control

system.

(6) Replacement of NI-2 and NI-4, WO 93052259

The inspector observed portions of the replacement of Unit 3

nuclear instrumentation NI-2 and NI-4. The inspector

concluded the work activity was in accordance with Nuclear

Station Modification NSM-32909, which provided the guidance

for the replacement of a source range (NI-2) and

intermediate range (NI-4) detector with Gamma-Metrics system

full scale operating range detectors. The inspector

concluded that the work activity was performed to acceptable

standards.

(7) Replace Broken Fuse Block in 3TC-4, WO 95032254

The inspector observed corrective maintenance activities

associated with the replacement of a broken fuse block in

4160 volt switchgear 3TC. During the maintenance activity

the original installed fuses did not fit the replacement

fuse block. The original fuses were type K fuses and the

replacement fuse block required type R fuses. The

replacement fuse block was supplied by the vendor as a

direct replacement for the existing fuse block. The

maintenance personnel reinstalled the old fuse block (with

original fuses) and initiated a PIP to determine the

appropriate replacement fuses and the means of documenting

appropriate replacement fuses on drawings.

The PIP also

identified that no documentation existed to control the

replacement of fuses for the safety-related switchgear. The

fuse replacement program is essentially a like-for-like

process. When a different type fuse is required, design

information specifying the original fuse is frequently

unavailable or inadequate. This substantially complicates

the process for specifying a new fuse.

ENCLOSURE 2

6

While reviewing the work order the inspector questioned the

Quality Assurance (QA) level identified on the work order.

The work order stated that the work activity was non-QA.

The broken fuse block was associated with the control power

for the 3A Condenser Circulating Water (CCW) pump and the

fuse block is part of the feeder breaker for this pump.

This breaker is required to open during a load shed

condition. Subsequent discussions with the licensee

determined that the replacement parts were QA parts.

The licensee had originally considered the breaker

non-QA, but had committed to the NRC to maintain and test

the breaker to QA requirements as a result of a violation

(50-269,270,287/93-02-01) issued during the Electrical

Distribution System Functional Inspection (NRC Inspection

Report 50-269,270,287/93-02). The licensee stated that the

non-QA specification on the work order was based on the

initial QA classification, but that the work activity was

identified as being conducted to QA requirements based on

the NRC commitment. Pending completion of the licensee PIP

evaluation and review of control power QA requirements by

the inspectors, this item is identified as Inspector

Followup Item 50-269,270,287/95-11-01:

QA Level for CCW

Pump Breaker Activities.

b.

The inspectors observed surveillance activities to ensure they

were conducted with approved procedures and in accordance with

site directives. The inspectors reviewed surveillance

performance, as well as system alignments and restorations. The

inspectors assessed the licensee's disposition of any

discrepancies which were identified during the surveillance.

Surveillance activities observed or reviewed in whole or in part

are as follows:

(1) High Pressure Injection Pump Test, PT/2/A/0202/11

The inspector observed performance testing of the Unit 2

high pressure injection pumps and associated check valves on

June 14, 1995. The purpose of the test was to demonstrate

operability of the equipment required to meet Technical

Specification requirements. The inspector concluded that

testing activities were performed according to the procedure

and acceptance criteria were met.

(2) Motor Driven Emergency Feedwater Pump Test, PT/1/A/0600/13

The inspector observed surveillance activities associated

with the 1A Motor Driven Emergency Feedwater pump. The

performance test implements the requirements of ASME Section

XI. The inspector concluded that the testing activities

ENCLOSURE 2

7

were performed in accordance with the procedure and the

procedure acceptance criteria were met.

(3) Unit 3 Mainfeeder Bus 1 Lockout Test, TT/3/A/0610/013

The inspector observed a test of the Unit 3 Mainfeeder Bus

  1. 1 (MFB1) lockout relays. These relays were energized by

manually operating initiating relays (current and

differential). All activities observed were satisfactory.

The inspector concluded that this test verified that the

Unit 3 MFB1 lockout relays operated properly.

Within the areas reviewed, the failure to provide the appropriate QA

category to a HPSW work activity was identified as a weakness in the

licensee's work control system, paragraph 3.a.(5). An Inspector

Followup Item was identified regarding the QA level assigned to CCW pump

breaker maintenance activities, paragraph 3.a.(7).

4.

Onsite Engineering (37551)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

a.

Failure To Initiate Problem Investigation Process (PIP) In A

Timely Manner

On May 23, 1995, Revision 2 of Oconee Calculation OSC-2061, Oconee

Unit 3 Voltage and Load Study, was signed as an approved

engineering document. Section 4.0 of this calculation indicated

that with the 230 KV switchyard supplying Unit 3 via Startup

Transformer CT3, coincident with a Loss Of Coolant Accident

(LOCA), the computed minimum voltages at the motor terminals for

motor-operated valves (MOVs) 3HP-3, 3HP-4, and 3HP-20 were below

the computed minimum operating voltages previously analyzed.

These three valves are part of the High Pressure Injection system

which receive an Engineered Safeguards (ES) signal to close

following an accident requiring containment isolation.

The licensee's vehicle for resolving operability questions or

conditions adverse to quality is the PIP. Nuclear System

Directive 208, Problem Investigation Process (PIP), is the

controlling document for the PIP. NSD 208, Appendix E, indicates

that the discovery of a condition which calls into question the

current or past operability of a system or component, required to

be operable by TS, requires the initiation of a PIP. Therefore,

the fact that the operability of these containment isolation

valves was in question should have resulted in the immediate

initiation of a PIP. In fact, Section 4.0, "Conclusions And

ENCLOSURE 2

8

Recommendations," of OSC-2061 states in part that "A PIP item must

be generated on the new minimum voltages for the three above-named

MOVs..."

However, a PIP for this issue was not initiated until

June 6, 1995 (PIP 3-095-0663). The licensee subsequently

completed an analysis which showed that the three MOVs in question

had been operable at the new minimum starting voltage. However,

due to the lack of margin for 3HP-20 (less than 10 percent), the

licensee replaced 315 feet of motor feeder cable with cable of

less resistance (#6 AWG versus #10 AWG).

The inspectors first became aware of the issue on June 7, 1995,

upon reading PIP 3-095-0663. The inspectors recalled that the

subject calculation (OSC-2061) was part of a group of Emergency

Power Upgrade Project calculations that were completed several

weeks earlier, and therefore questioned the timeliness of this

PIP. In response to the inspector's inquiry, licensee management

stated that they were unaware that this issue was several weeks

old. The inspectors noted that the applicable Technical

Specification action statement (TS 3.6) time frame for containment

isolation valves was 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors concluded that the

15 days taken by the licensee to initiate the PIP for this problem

did not meet the requirements of NSD 208, and was not commensurate

with the safety significance of containment isolation valves. The

licensee agreed that their PIP initiation for this problem was not

timely, and indicated that it was their expectation that a problem

that brought into question the operability of a safety-related

system or component would result in the immediate initiation of a

PIP. As of the end of the inspection period, the licensee was

still investigating the failure to initiate a PIP in a timely

manner. This matter is identified as Violation 287/95-11-02:

Failure to Initiate a PIP in a Timely Manner.

b.

Emergency Power Upgrade Project Items

Keowee Hydro Station was designed, constructed, and maintained to

hydroelectric standards. The hydro station was not originally

under the Nuclear Generation Department management, and

documentation and programmatic controls have not been consistent

with nuclear industry standards. Over the years several events

and internal/external assessments resulted in a growing list of

commitment items. These included the May 15, 1992, Self-Initiated

Technical Audit (SITA), October 1992 loss of offsite power event,

Electrical Distribution System Functional Inspection (EDSFI), and

the Design Basis Document (DBD) review program. In order to

manage the list of commitment items, the licensee initiated the

Oconee Emergency Power Upgrade Project.

This upgrade project provides for the engineering analyses,

procedure upgrades, maintenance program development, and

configuration documentation/upgrade for the Keowee Hydro Station

ENCLOSURE 2

III9

and the Emergency Power Path of Oconee Nuclear Station. The

licensee stated that this project will fully incorporate Keowee

into the Oconee nuclear maintenance program and satisfy all open

commitment items. The project contains approximately 160

individual items.

During this inspection period the inspectors reviewed the

following project items:

(1) Investigate Need For MG-6 Relay Covers (Item #32)

This item was the result of two MG-6 relay failures during

September 1992 that were attributed to dirty contacts. The

licensee subsequently determined that relay covers would not

prevent the type of contact fouling which occurred in these

two instances; therefore, they decided not to install relay

covers. The inspector noted that there have been over 500

Keowee Hydro Unit starts since September 1992 without

further MG-6 relay problems. The inspector concluded that

the licensee's decision not to install relay covers was

acceptable.

(2) Inspect Westinghouse Electromechanical Relays for Stress

Cracks (Item #43)

A Westinghouse vendor notice (VIL-W 89-25) documented that

the moving contact holder in certain Westinghouse

electromechanical relays had developed stress cracks.

Westinghouse stated in their notice that the relays subject

to this stress cracking were probably manufactured during

the years 1981-1983. Keowee Hydro Station relaying systems

were installed during the period from 1970 through 1972.

Although no problems were anticipated, the licensee

inspected the contact holders for Westinghouse relays. No

problems were identified as a result of the licensee's

inspection. The inspector concluded that the licensee's

actions were adequate.

(3) Revise Loss of Power Abnormal Procedure, AP/1/A/1700/11,

(Item #31)

The 1992 electrical distribution SITA identified an

inconsistency within AP/1/A/1700/11 regarding the amount of

time required to establish RCS makeup and primary to

secondary heat transfer, in order to prevent core damage.

The licensee subsequently revised the procedure. The

inspector reviewed the latest revision of the procedure and

concluded that the changes effectively eliminated the SITA

concern.

ENCLOSURE 2

10

(4) Development of Alarm Indications for Loss of Control Power

to Keowee Air Circuit Breakers (Item #64)

In response to problems with loss of control power to Keowee

Air Circuit Breakers (ACBs) going undetected for a prolonged

period of time, the licensee developed Nuclear Station

Modification (NSM) ON-52944. This NSM will, when

implemented, provide Operations the ability to diagnose

control power failures on ACB-5,6,7 & 8 in a timely manner.

This modification will add an alarm relay (1 each) to the

close coil control circuit of ACB-5,6,7, & 8 to indicate

loss of 125 VDC control power. The inspector verified that

the new relays will be safety-related and will provide

isolation between the safety power supply and the non-safety

alarm outputs. The inspector reviewed the final scope

document for this NSM and concluded that it was adequate.

This NSM is scheduled for implementation during October

1995.

Within the areas reviewed, a violation was identified regarding the

failure to initiate the Problem Investigation Process in a timely manner

for a problem which called into question the operability of containment

isolation valves, paragraph 4.a.

5.

Plant Support (71750, 40500, and 64704)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the following areas were reviewed:

a.

Fire Protection

The inspectors reviewed the Oconee Nuclear Station Fire

Protection/Prevention Program. The review included Site Directive

(SD) 3.2.7, Control Of Combustible Materials; SD 3.2.8, Fire

Brigade Organization And Training; SD 3.2.9, Reporting Of Fire

Protection Impairment; and SD 3.2.10, Hot Work Permit

Authorization Directive. Program operability requirements were

specified in Section 16.9, Auxiliary Systems - Fire Protection

Systems, of the Selected Licensee Commitment (SLC) Manual which

specified the surveillance requirements and compensatory measures

for impaired equipment and fire barriers.

The inspector routinely observed housekeeping throughout the plant

during the inspection period. The areas observed were kept clean

and the use of fire hazard materials appeared to be minimized.

The inspector noted that fire extinguishers and hose stations were

inspected by the licensee within the allowable inspection time

period. Hot work permits reviewed by the inspector were adequate.

The inspector witnessed a fire drill on May 16, 1995, that

ENCLOSURE 2

simulated a fire in the basement of the Unit 3 turbine building.

All documents reviewed, and activities observed were satisfactory.

The inspector reviewed a fire protection audit, SA-95-24(ON)(RA),

dated May 8, 1995 through June 8, 1995. The audit utilized the

services of a consultant fire protection engineer. The audit

identified several strengths and weaknesses. The inspector

verified that the audit concerns were documented in the licensee's

PIP for resolution. The inspector concluded that this audit was

adequate and represented good self-assessment in the area of fire

protection.

The inspector concluded that the licensee's fire protection

program was adequate, and that in general, the implementation of

the program was in accordance with the program requirements.

b.

Unit 3 Failed Fuel

During cycle 15, Unit 3 had high reactor coolant system.(RCS)

activity. Based on the cycle 15 radiochemistry the licensee

estimated that there were 3 to 4 failed fuel pins with likely

secondary hydride failures. During this inspection period Unit 3

began a scheduled refueling outage (3EOC15), in which the entire

core underwent an ultrasonic examination. The ultrasonic test

(UT) revealed that 22 fuel pins had failures. These 22 pins were

located in 16 different fuel assemblies. Of these 16 assemblies,

13 were first burn assemblies (19 fuel pins), 3 second burn

assemblies (2 fuel pins), and 1 third burn assembly (1 fuel pin).

The majority of the failed fuel pins (19 of 22) were replaced with

new uranium dioxide rods using standard fuel reconstitution

techniques. Two of the pins had such extensive damage that a

complete recaging of their associated fuel assemblies was

required. The failed pin in the third burn assembly was not

replaced since that assembly was not being returned to the core.

Based on the nature of the failures the licensee concluded that

they were not debris induced.

The inspectors witnessed portions of the UT and reconstitution

effort and concluded that the activities observed were

satisfactory. As of the end of the inspection period the licensee

was still evaluating why their estimate for the number of failed

pins was greatly underestimated and what was the cause of the

failed fuel.

c.

Unit 3 Outage Dose Reduction Efforts

Due to operating the previous cycle with failed fuel there were

high fission product and activation inventories throughout systems

which came into contact with Unit 3 reactor coolant. The high

amount of activity associated with Unit 3 provided the likelihood

ENCLOSURE 2

  • II12

of high outage dose. In order to reduce outage dose the licensee

incorporated several shutdown chemistry practices designed to

maximize the cleanup of the RCS during cooldown. These shutdown

chemistry practices included the addition of temperature holds

during the cooldown process designed to maximize the chemical

reactions that take place during certain phases of the shutdown.

This was followed by hydrogen peroxide addition (crudburst) to

achieve acid oxidizing conditions which further dissolved

activation products from RCS piping. After hydrogen peroxide

addition, a 40 hour4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> purification was undertaken to remove these

activation products through the purification demineralizer system.

The acid oxidizing phase of the crudburst allowed the removal of

approximately 738 curies of cobalt from the RCS.

The cooldown temperature holds were incorporated into the Unit 3

outage schedule after a licensee review of elevated dose rate

events at Catawba and McGuire Nuclear Stations following

accelerated shutdowns. This review indicated that there was a

relationship between accelerated cooldowns and elevated shutdown

dose rates. Therefore, the licensee established: (1) a 6-hour

hold at hot shutdown; (2) a 6-hour hold at 350 degrees fahrenheit;

and (3) a 16-hour hold prior to the addition of hydrogen peroxide.

These holds prevented the formation of particulates which deposit

in the RCS and cause elevated dose rates. Approximately 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />

were added to the Unit 3 critical path activity due to these

chemistry holds and the prolonged purification evolution.

The inspectors observed that these chemistry holds resulted in

lower dose rates than that experienced during the previous outage

(3EOC14). This was significant considering the activity levels

going into this outage were much higher than the previous outage.

The inspectors concluded that the licensee's willingness to

substantially extend their outage critical path schedule in order

to reduce dose was an example of management commitment to their

ALARA program. Additionally, the inspectors concluded that the

licensee's incorporation of lessons learned from the Catawba and

McGuire outages to be an example of good self-assessment.

Within the areas reviewed, licensee activities were satisfactory. The

licensee's efforts to reduce Unit 3 outage dose was considered a

strength (paragraph 5.c).

ENCLOSURE 2

13

6.

Inspection of Open Items (92902, 92903 and 92904)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

a.

(Closed) Violation 287/93-31-03, Failure To Evaluate Materials For

Fire Loading

The inspectors had identified equipment and scaffolding in the

penetration rooms where flammable plastic had been used as wrap

for those items. The licensee was notified of the condition and

was responsive in the removal of the material. In addition, the

licensee reviewed the use of combustible materials in accordance

with Site Directive 3.2.7 with all groups of personnel involved

with the use of this material. The inspectors determined the

licensee's actions to be acceptable for correcting the issue and

preventing recurrence.

b.

(Closed) Violation 269,270,287/93-31-02, Inadequate 50.59

Evaluation

This violation identified that an inadequate 50.59 evaluation was

performed to implement a modification to the Keowee breaker

control logic to allow operation of both Keowee Hydro Units to the

electrical grid for power generation purposes. The 50.59

evaluation should have determined that a Technical Specification

(TS) change was required prior to implementation of the

modification. The corrective action associated with this

violation included revising Nuclear System Directive (NSD) 209,

10CFR 50.59 Evaluations, to clarify and emphasize the need to

consider new TS surveillances when performing safety evaluations.

The inspectors verified that NSD 209 had been revised.

c.

(Closed) Violation 269,270/93-23-01, Failure To Follow Procedures

To Maintain Configuration Control

This violation addressed the failure of Maintenance personnel to

properly control the configuration of lifted leads during

maintenance activities on a control power panelboard. When the

lifted leads were improperly reterminated, alternate power to the

panelboard was not available when the normal power supply was

tripped. This resulted in a reactor trip, which is described in

the closure evaluation of Licensee Event Report (LER) 269-93-08,

detailed in paragraph 7.b of this inspection report. The

inspector verified that the corrective actions for this violation

and the LER were implemented.

ENCLOSURE 2

14

7.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs are closed:

a.

(Closed) LER 269/93-04, A Postulated Single Failure During a

LOCA/LOOP May Result In The Loss Of Post Accident Cooling Due to A

Design Deficiency

On April 5, 1993, the inspectors identified that the control logic

associated with the condenser circulating water (CCW) pump

discharge valves was not single failure proof. Loss of the CCW

system would isolate the primary suction flow path for the low

pressure service water (LPSW) pumps.

This issue was discussed in NRC Inspection Report 269,270,

287/93-13. To correct the immediate single failure vulnerability,

the licensee opened the CCW cross connect valves to align multiple

water supplies to the LPSW pumps. Subsequent corrective actions

included performing a single failure analysis on the CCW supply to

the LPSW system, modification of the CCW pump discharge valve

control circuitry to eliminate the single failure vulnerability,

and implementing administrative controls on Keowee lake levels.

The inspector verified that the above actions had been completed.

b.

(Closed) LER 269-93-08, Inappropriate Actions Result In Loss Of

Vital Power Panelboard And A Reactor Trip

Unit 1 tripped from 100% power on August 23, 1993, when power to a

Unit 1 AC and DC control power panelboard was lost. The power

loss occurred when technicians attempted to switch the

panelboard's power to the alternate source for routine

surveillance. The panelboard's alternate power supply electrical

leads were later found to have been reversed or rolled during

previous maintenance activities. This configuration control error

resulted in the alternate supply's diode arrangement blocking

current flow to the panelboard.

The licensee determined that maintenance technicians had

incorrectly relanded leads during a May 18, 1993, maintenance

activity. Since they were not required to perform continuity

checks or other post-maintenance verifications, the problem went

undetected until the time of the event.

ENCLOSURE 2

15

Corrective actions included revising Maintenance Directive 4.4.13,

I&E Configuration Control Work Practices on November 20, 1993, to

provide specific guidance for marking leads and termination points

during lifted lead evolutions. In addition, a Quality Steering

Team (QST) was formed to review the Post Maintenance Testing

program. As a result of the QST recommendations, a new Nuclear

Station Directive NSD 208, Testing, was issued to provide guidance

for Post Maintenance Testing.

The inspector verified the changes were incorporated into the

Oconee Maintenance program. This item is closed.

8.

Exit Interview

The inspection scope and findings were summarized on June 28, 1995, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings. No

dissenting comments were received from the licensee. The licensee did

not identify as proprietary any of the material provided to or reviewed

by the inspectors during this inspection.

Item Number

Status

Description/Reference Paragraph

Inspector Followup Item

Open

QA Level for CCW Pump Breaker

269,270,287/95-11-01

Activities (paragraph 3.a.(7))

Violation 287/95-11-02

Open

Failure to Initiate a PIP in a

Timely Manner (paragraph 4.a)

Violation 287/93-31-03

Closed

Failure To Evaluate Materials For

Fire Loading (paragraph 6.a)

Violation

Closed

Inadequate 50.59 Evaluation

269,270,287/93-31-02

(paragraph 6.b)

Violation

Closed

Failure To Follow Procedures To

269,270/93-23-01

Maintain Configuration Control

(paragraph 6.c)

LER 269/93-04

Closed

A Postulated Single Failure During a

LOCA/LOOP May Result In The Loss Of

Post Accident Cooling Due to A

Design Deficiency (paragraph 7.a)

LER 269-93-08

Closed

Inappropriate Actions Result In Loss

Of Vital Power Panelboard And A

Reactor Trip (paragraph 7.b)

ENCLOSURE 2