ML16148A700

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Insp Repts 50-269/92-24,50-270/92-24 & 50-287/92-24 on 920926-1103.Violation Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities Keowee Issues & LPSW Issues
ML16148A700
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 11/16/1992
From: Belisle G, Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A699 List:
References
50-269-92-24, 50-270-92-24, 50-287-92-24, NUDOCS 9212020066
Download: ML16148A700 (26)


See also: IR 05000269/1992024

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/92-24, 50-270/92-24 and 50-287/92-24

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Conducted:

September 26 -

November 3, 1992

Inspector:___

P. . Harmon ,enior

esident Inspector

Date/Si ed

B. . Desai, R ident InspectorSigned

W.K Pr

r

ient Inspector

W. K.eR-Dt'S

d

Approved b

G. A. Belisle, Section Chief

Date.Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, resident inspection was conducted in the

areas of plant operations, surveillance testing,

maintenance activities, Keowee issues, and Low Pressure

Service Water (LPSW) issues.

Results: One apparent violation was identified which is under

consideration for escalated enforcement action and

involves inadequate LPSW flow through the 3B Low

Pressure Injection (LPI) cooler (paragraph 6.d).

One

unresolved item with two parts was identified and

involved annual testing the MG-6 relay for the Keowee

overhead path in accordance with the Technical

Specification and taking corrective action for testing

of the Keowee overhead electrical path (paragraph 5.b).

Two other unresolved items were identified involving

submitting a TS change for Unit 3 LPSW (paragraph 6.d)

and submitting a TS change for the LPSW system

(paragraph 6.a),. Two inspector followup items were

identified related to the containment

pressure/temperature response during accident

conditions and NPSH requirements

(paragraphs 6.i and

6.j respectively).

9212020066 921116

PDR

ADOCK 05000269

G

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

S. Benesole, Safety Review

  • D. Coyle, Systems Engineering
  • J. Davis, Safety Assurance Manager

D. Deatherage, Operations Support Manager

  • B. Dolan, Manager, Mechanical/Nuclear Engineering (Design)

W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

  • 0. Kohler, Regulatory Compliance

C. Little, Superintendent, Instrument and Electrical (I&E)

  • M. Patrick, Performance Engineer
  • B. Peele, Engineering Manager

S. Perry, Regulatory Compliance

G. Rothenberger, Work Control Superintendent

R. Sweigert, Operations Superintendent

Other licensee employees contacted included technicians,

operators, mechanics, security force members, and staff

engineers.

NRC Resident Inspectors

  • P.

Harmon

  • W. Poertner
  • B. Desai
  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the

reporting period to verify conformance with regulatory

requirements, Technical Specifications (TS), and

administrative controls. Control room logs, shift

turnover records, the temporary modification log and

equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant

operations, maintenance, chemistry, health physics,

instrument & electrical (I&E), and performance

personnel.

Activities within the control rooms were monitored on

an almost daily basis. Inspections were conducted on

day and on night shifts, during weekdays and on

weekends. Some inspections were made during shift

2

change in order to evaluate shift turnover performance.

Actions observed were conducted as required by the

licensee's Administrative Procedures. The complement

of licensed personnel on each shift inspected met or

exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were

cognizant of plant conditions.

Plant tours were taken throughout the reporting period

on a routine basis. The areas toured included the

following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Equipment Rooms

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Station Yard Zone Within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation

control practices were observed.

Within the areas reviewed, licensee activities were

satisfactory.

b.

Plant Status

Unit 1

The Unit operated at power until October 3, 1992, when

the Unit experienced a reactor trip from 8 percent

power from an anticipatory loss of feed signal.

At

the time of the trip, 8:10 a.m., Unit 1 was critical at

8 percent power with the turbine generator off-line.

The licensee 'had reduced power from 100 percent power

to complete the testing and modifications on the Low

Pressure Service Water (LPSW) system as described in

paragraph 6. The cause of the trip was determined to

be a pressure swing that developed in the feed system

when a partially drained portion of the feed system was

realigned. The resultant pressure drop actuated the

Low Feedwater Discharge Pressure signal, which in turn

actuated the anticipatory Loss of Feedwater Reactor

Trip. Subsequent investigation revealed that a pump

vent valve did not function, resulting in the 1B

feedwater pump draining over a period of hours while

3

shut down. When operators began realigning the 1B

Pump, the void in the pump line caused a temporary low

pressure condition in the running pump's discharge

line.

Following the trip, the plant response was normal. The

vent valve was repaired and the unit was returned to

service on October 5, 1992.

Unit 2

The Unit operated at power until October 19, 1992 when

the Unit tripped due to a loss of offsite power. The

loss of offsite power event is discussed in NRC

Inspection Report Nos. 269, 270, 287J92-26. The Unit

was returned to service on October 26, 1992.

Unit 3

The Unit operated at power until September 29, 1992, at

9:16 a.m., when the Unit tripped from approximately 4

percent power. Just prior to the event, the Unit was

operating at 73 percent power and holding during

troubleshooting of the control rod drive (CRD) system.

When technicians opened a CRD breaker associated with

the 3A CRD power supply, the alternate 3B CRD power

supply should have provided power to the regulating

rods to keep them energized and withdrawn. Instead,

the control room operators observed that a single group

of regulating rods, group 5, had dropped. The

transient monitor later indicated that all three

regulating rod groups 5, 6, and 7 had dropped, but the

operators insisted that only the group 5 rods had

fallen.

With the dropped rods, a rapid power drop

occurred, and RCS pressure began dropping.

Approximately 13 seconds after the rods dropped, a

reactor trip was initiated by the RCS Low Pressure

signal.

The post trip response was normal, and the plant was

stabilized at Hot Shutdown conditions. The trip

investigation concluded that the probable cause of the

trip was a spurious failure of the 3B CRD power supply.

The actual root cause of the trip may not have been

positively determined. The licensee was also unable to

resolve the discrepancy between what the operators

observed as a single group of dropped rods, and what

the transient monitor identified as three dropped

regulating rod groups. Corrective actions included

replacing.a CRD programmer and revising troubleshooting

procedures to require checking the alternate

4

programmer's output prior to removing one programmer

from service.

After completing the post-trip review, permission to

restart was given by the plant manager at 8:15 p.m.,

11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> after the trip. The plant returned to'

criticality at 11:57 p.m., on September 29, 1992.

On October 1, Unit 3 was at 83 percent power and in the

process of pressurizing the electrical generator to 60

psig with hydrogen. At 3:00 p.m., generator alarms

began coming in which indicated that seal oil was

entering the generator.

The hydrogen addition was

stopped at approximately 58 psig, and a power reduction

initiated. The generator was taken off-line at 8:35

p.m.

Investigation into the event disclosed that

approximately 1600 gallons of seal oil had leaked past

seals on each end of the generator. The seal

assemblies were found to be cocked. The seals were

repaired and the generator inspected and cleaned. The

Unit was returned to service on October 14, 1992.

Within these areas, no violations or deviations were

identified.

3.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify

procedural and performance adequacy. The completed tests

reviewed were examined for necessary test prerequisites,

instructions,.acceptance criteria, technical content,

authorization to begin work, data collection, independent

verification where required, handling of deficiencies noted,

and review of completed work. The tests witnessed, in whole

or in part, were inspected to determine that approved

procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to

procedure, test results were acceptable and systems

restoration was completed.

Surveillances reviewed and witnessed in whole or in part:

TT/1/A/0251/21 Unit 1 and 2 LPSW System Flow Test

Within the areas reviewed licensee activities were

satisfactory.

No violations or deviations were identified.

4.

Maintenance Activities (62703)

5

Maintenance activities were observed and/or reviewed during

the reporting period to verify that work was performed by

qualified personnel and that approved procedures in use

adequately described work that was not within the skill of

the trade. Activities, procedures, and work requests were

examined to verify; proper.authorization to begin work,

provisions for fire, cleanliness, and exposure control,

proper return of equipment to service, and that limiting

conditions for operation were met.

Maintenance reviewed and witnessed in whole or in.part:

WR 92018790 Perform Diagnostic Test on 3FDW-316

WR 38156C

Investigate Why 3FDW-315 Indicates Open

WR 92046928 Repair Leak on Unit 2 EFDW Instrument Tap

Within the areas reviewed, licensee activities were

satisfactory.

No violations or deviations were identified.

5.

Keowee Issues

a.

General

The two Keowee hydro units provide two functions,

emergency power to the Oconee Nuclear Station (ONS)

through either the overhead or underground path and

commercial electrical power to the Duke system grid.

The electrical distribution and control circuitry is

designed so that one of the units will provide power

through the underground path and its respective

underground air circuit breakers (ACB) (ACB 3 for

Keowee Unit 1 and ACB 4 for Keowee Unit 2) through

transformer CT-4 to the standby buses. The other

Keowee unit provides emergency power through the

overhead path and its respective overhead ACB (ACB 1

and 2 for Keowee Units 1 and 2 respectively), the

Keowee main step up transformer, the 230 kv switchyard

and to each Oconee Units' startup transformer CT-1, 2,

or 3. The overhead path is also the path used when

using Keowee to generate power to the Duke Power

distribution grid via the 230 kv switchyard. The

overhead path is the preferred source of power because

unlike the underground path, it eliminates the need for

loadshed.

During an emergency, each Keowee unit could be either

running or in standby, and one units' underground ACB

would be closed. Upon receiving an emergency start

signal, both units will start if not already running,

and both overhead breakers (ACB 1 and 2) will open if

6

the units had been running and generating to the grid.

The overhead breaker for the unit aligned to the

overhead path will then close after certain criteria

are met. The criteria are:

1.

A four second time delay to enable Reactor Coolant

Pumps (RCPs) to trip and thus prevent overloading

a Keowee unit.

2.

Verification that the associated underground

feeder breaker is open to prevent energizing both

overhead and underground paths from the same unit.

3.

Verification that switchyard isolation has

occurred and a dedicated overhead path from Keowee

to Oconee has been established.

4.

Verification that the Keowee main step-up

transformer is deenergized.

After the above criteria are met, the Keowee unit would

then provide power to the main feeder busses either

through the overhead path or through the underground

path.

b.

Keowee Unit 2 Inoperable Due to Failure of MG-6 type

Undervoltage Relay

On September 29, 1992, at approximately 10:00 p.m.,

while performing a test concurrent with a post

modification test following installation of interlocks

on ACBs 1 and 2, ACB 2 did not close as expected per

the test procedure.

(The modification was initiated

because of a single failure vulnerability resulting in

two Keowee units tying to the overhead path, out of

phase, is discussed in NRC Inspection Report Nos. 50

269, 270, 287/92-23, URI 92-23-02).

Further

investigation revealed that relay 27T2X (Westinghouse

MG-6) had a one half inch contact gap instead of the

seven sixteenths inch gap specified by the

manufacturer. A technician tried to adjust the gap

between the contacts, and the plastic armature stop nut

broke apart. The relay was repaired by installing a

new armature stop nut and adjusting the contacts. The

test was reperformed and ACB 2 operated as required.

As a result of the failed MG-6 relay, the Keowee Unit 2

overhead path had been inoperable for an indeterminate

amount of time. One of the.prerequisites for the

overhead ACB (ACB 2) to close following an emergency

start is confirmation that the Keowee main step-up

transformer has deenergized. This is accomplished by

7

the MG-6 relay. With the relay failed, ACB 2 would not

have closed during an emergency start. Thus, the

overhead path when aligned to Keowee Unit 2, would not

have been available following an emergency start.

As previously stated, the MG-6 relay and consequently

the Keowee overhead path were inoperable for an

indeterminate amount of time. The time is

indeterminate for the following two reasons.

1.

The overhead path through ACB 2 was inoperable

only when Keowee Unit 2 was aligned to the

overhead path. Swapping of Keowee Units between

overhead and underground paths is done routinely.

2.

Neither the particular MG-6 relay nor the Keowee

overhead path had ever been tested according to

the licensee. The relay could have been bad and

thus the overhead path could have been inoperable

since initial installation. Periodic testing of

either the relay or the overhead path would have

identified the problem.

The inspectors had discussed the issue regarding the

lack of direct testing of the overhead path with the

licensee on several occasions. The licensee had

acknowledged the inspectors concern and had maintained

the position that they were in the process of.

coordinating a test to prove that the overhead path

would work if called upon. The licensee's current

test, as required by TS 4.6.5, is limited to testing

the External Grid Trouble Protection System logic.

This test is a continuity test and does not directly

test the Keowee overhead function.

In addition Oconee Technical Specification 4.6.2.a

requires that the Keowee Hydro units will be started

annually using the emergency start circuits in each

control room. This is to verify that each hydro unit

and associated equipment is available to carry load

within 25 seconds of a simulated requirement for

engineered safety features. The licensee conforms to

this requirement by performing PT/O/A/0620/16, Keowee

Hydro Emergency Start Test. This performance test

verifies operability of the Keowee emergency start

circuitry, and demonstrates that both Keowee units can

supply 25 MW of power within 23 seconds of emergency

start initiation. It does not verify operability of

the MG-6 feature of ACB 2 which is part of the

"associated equipment" referred to in TS 4.6.2.a. The

licensee has stated that they do not agree with the

inspectors position on the intent of the TS.

In

8

effect, the licensee has never tested the actual path

emergency power must take from Keowee to the Oconee

emergency buses. Until this issue of testing the MG-6

relay feature of the Keowee overhead path can be

resolved, this is identified as one part of Unresolved

Item 50-269, 270, 287/92-24-01: Testing the MG-6 Relay

Function Of The Keowee Overhead Path

The licensee performed a test, concurrent with the post

modification test, on September 29.

This test directly

challenged a portion of the overhead emergency path.

It was during this test that the failed relay was

identified.

The licensee issued LER 269 92-14 which described this

event. The licensee.stated in the LER that as part of

planned corrective action, they intend to develop and

implement an appropriate preventive maintenance program

for the MG-6 relays. The LER also states that the

licensee intends to test the overhead path. No time

frame for the completion of these actions is mentioned.

In view of the on-going efforts related to Keowee by

the AIT, the adequacy of corrective action following

the identification of the lack of testing of the

overhead path is identified as the second part of

Unresolved Item 50-269, 270, 287/92-24-01, Corrective

Action For Testing The Keowee Overhead Path.

c.

Single Failure That Could Result in Both Keowee

Emergency Power Sources Becoming Inoperable.

On October 12, 1992, at approximately 6:00 p.m., the

licensee identified a potential single failure which

could result in the loss of both overhead and

underground emergency power paths. The single failure

was a postulated fault on the overhead breaker ACB 1 or

2 for the Keowee Unit tied to the underground path. A

fault on the ACB in an overlap region between Keowee

generator zone differential current and main

transformer zone differential current transformers

would result in tripping the Keowee unit tied to the

underground power path as well as isolate the overhead

power path for both Keowee units thus rendering them

inoperable.

As an immediate fix, the licensee opened the

disconnects for ACB 2 to preclude the potential single

failure from occurring. This removed the capability of

the Keowee unit to generate to the grid. With ACB 4

closed, Keowee unit 2 was aligned to the underground

path, thus retaining both the overhead and underground

paths.

The issue is still under review and will be

9

tracked as part of the review of the LER which will be

issued on this item.

6.

Low Pressure Service Water (LPSW) Issues

a.

Unit 1 and 2 LPSW Technical Specification Deficiency

The inspectors identified that the TS associated with

the LPSW system for the shared Unit 1 and 2 LPSW system

was inadequate when a single failure of an LPSW pump

was considered. TS 3.3.7, Low Pressure Service Water,

requires that two of the three LPSW pumps for the

shared Unit 1 and 2 LPSW system be operable when the

reactor coolant system (RCS) is in a condition with

pressure equal to or greater than 350 psig or

temperature equal to or greater than 250 degrees F.

The inspectors determined that the ability of one LPSW

pump to supply accident loads on one unit and shutdown

loads on the other unit was questionable after review

of the licensee's flow model calculation for the shared

Unit 1 and 2 LPSW system. The inspectors discussed the

potential inadequacy of the TS with the plant manager

and the operations superintendent, and were told that

the calculation was only a preliminary calculation.

The inspectors responded that the calculation had been

completed and reviewed prior to review by the

inspectors and that the calculation did not appear to

support operation of Units 1 and 2 with only two LPSW

pumps operable as required by the TS.

The licensee reviewed the inspectors concerns and

concluded that three LPSW pumps were required to

support continued operation of Units 1 and 2.

Additional flow model calculations would also be

required to determine if LPSW flows to safety related

components would be acceptable assuming that both units

were operating at power if a design basis event

occurred. The licensee made a four hour non-emergency

notification to the NRC at 7:17 p.m., September 2,

1992, identifying that a single failure of one of the

required two LPSW pumps could result in the inability

of the LPSW system to maintain adequate flow to all

safety related components. The licensee initiated a TS

interpretation to require that all three LPSW pumps in

the shared Unit 1 and 2 LPSW system be operable to

consider the LPSW system operable. The licensee will

also be submitting a TS change to reflect this

interpretation and until this TS change is submitted,

this is identified as Unresolved Item (URI) 269, 270,

287/92-24-05: TS Change For LPSW System.

10

b.

Unit 1 and 2 LPSW Flow Calculation

The inspectors reviewed calculation OSC-4672, Unit 1

and 2 LPSW System Response To A Large Break LOCA With

Single Failure Using a Benchmarked Hydraulic Computer

Model. The inspectors questioned the adequacy of the

LPSW systems prior to reviewing the calculation and had

been informed by the licensee that the flow model

calculation had been completed on all three units and

that the calculation showed that flows to safety

related components were acceptable. .The calculation

assumed that one unit was shutdown and that the other

unit was operating at power and that the accident

occurred on the operating unit. The calculation was

then divided into separate scenarios:

The first scenario assumed all system flow path

valves wide open, all three LPSW pumps running

with loss of instrument air, no single failure and

both LPI coolers on the shutdown unit in service.

In this scenario, the calculation predicted that

LPSW flow to the Reactor Building Cooling Units

(RBCUs) would range from 1169 gpm to 1235 gpm and

that LPSW flow to the LPI coolers would range from

5447-gpm to 5944 gpm.

The 2nd scenario assumed a LOCA on Unit 1 and Unit

2 in a refueling outage with only one LPI cooler

in

service. The scenario assumed a loss of

instrument air, a single failure of an electrical

bus resulting in the loss of an LPSW pump and the

failure of an LPSW block valve to an LPI cooler to

open. This scenario also assumed that LPSW flow to

one RBCU was isolated and two LPSW pumps started.

In this condition, LPSW flow to the RBCUs on the

accident unit were predicted to be 1389 gpm and

1336 gpm and flow to the LPI cooler was predicted

to be 5810 gpm.

-

The 3rd scenario assumed a LOCA on Unit 2 and Unit

1 in a refueling outage with one LPI cooler in

service. In this condition, LPSW flow to the

RBCUs on the accident unit were predicted to be

1318 gpm and 1371 gpm and flow to the LPI cooler

was predicted to be 6120 gpm.

The inspectors questioned design engineering: (a) about

the assumption that two LPSW pumps would be available

on the combined Unit 1 and 2 LPSW system assuming a

pumps be operable for the LPSW system to be considered

11

operable; (b) the assumption that only one LPI cooler

would be in service on the shutdown unit; (c) the flow

to the RBCUs since past operability of the RBCUs had

been based on achieving 1400 gpm through the cooling

units under accident conditions; (d) the assumption

that LPSW flow to one RBCU was isolated since the RBCUs

are normally in service with LPSW flow established

through them; (e) the assumption that LPSW flow to the

RBCUs on the non-accident unit was throttled; and (f)

the assumption that LPSW flow to the reactor coolant

pumps on the non-accident unit would be isolated.

The inspectors-were told that the calculation was based

on the system capabilities, not the TSs and that

operator action could be expected to occur to throttle

LPSW flow to the LPI coolers to increase LPSW flow to

the RBCUs. The inspectors stated that the calculation

did not assume that only one LPSW pump would be

available under single failure conditions and informed

the design engineer that indication of flow to the

RBCUs would not be available under a loss of instrument

air conditions because the RBCU flow instruments are

air operated flow instruments and would lose indication

with a loss of instrument air. Therefore, the operator

would not have any indication that flow was less than

1400 gpm to the RBCUs. The inspectors also expressed

concern that credit was taken for operator action to

throttle LPSW flow to the LPI coolers since this

evolution could not be accomplished from the control

room and no guidance was available to the operators in

the control room on when or how to accomplish this

task.

The inspectors determined that calculation OSC-4672 had

been completed on June 19, 1992, and that the approval

of the calculation had been completed on July 30, 1992.

Based on the licensee's additional review and

discussion with the residents, the licensee determined

that the LPSW system required that three pumps be

operable and made a report to the NRC on September 2,

1992, as discussed in paragraph 6.a.

c.

Unit 3 LPSW Flow Calculation

The inspectors reviewed Calculation OSC-4489, Predicted

LPSW System Response To A Large Break LOCA With A

Single Failure Using a Benchmarked Hydraulic Computer

Model. The calculation assumed that the worst case

single failure was a loss of a 4160 volt switchgear

which would result in the loss of an LPSW pump, a low

pressure injection (LPI) pump and LPI cooler LPSW inlet

valve, and a reactor building cooling unit (RBCU).

12

The inspectors questioned the adequacy of the

licensee's assumptions in determining predicted flow to

the safety-related components. The calculation

reviewed by the inspectors assumed that all non

essential (non-safety) loads were isolated during a

LOCA event and that when a component was lost due to a

single failure, flow through that component was

isolated. The inspectors questioned the assumption

that all non-safety loads would isolate and that LPSW

flow to the inoperable RBCU would be zero. Unit 3 was

in a scheduled refueling outage when the inspectors

reviewed the calculation and the LPSW system was not

required to be operable per the TS.

The inspectors' concerns were discussed with licensee

management. The licensee's response was that flow

testing was not required. After further discussion,

the licensee agreed to perform an LPSW flow

verification test on Unit 3 prior to returning the unit

to service from the refueling outage. The inspectors

met with licensee management to express concerns that

the flow model did not accurately reflect the LPSW

system. The inspectors were initially told that the

Unit 3 flow model would be verified by the flow test

and that the adequacy of the Unit 1 and 2 flow model

would be evaluated based on the results of the Unit 3

testing, since flow testing on Units 1 and 2 could not

be performed conveniently with the units at power.

d.

Unit 3 LPSW Flow Testing

The inspectors reviewed and witnessed the Unit 3 LPSW

system flow testing which commenced on September 14,

1992.

During review of the initial procedure, the

inspectors identified that the test did not fail all

the air operated valves in the system to their failed

condition. The air operated flow control valves to the

air handling units in the auxiliary building were left

in their normal alignment. These valves fail open on a

loss of air. The inspectors discussed this item with

the licensee and were told that the flow through these

lines would be insignificant even with the air operated

valves failed open and that failing'the valves open

would only increase the time required to perform the

flow test and would not affect the outcome of the test.

During the flow test, the licensee was unable to

achieve greater than 5200 gpm flow through the 3B LPI

cooler with the 3A LPI cooler isolated and the main

turbine oil cooler isolated. The licensee's emergency

operating procedures require that LPSW flow be

increased to 5200 gpm on the operable LPI cooler after

13

swap over to the containment sump if both trains of LPI

are not available. The licensee determined that manual

isolation valve, 3LPSW-78, downstream of the cooler

flow control valve was not fully open due to an

actuator problem. The valve is a butterfly valve and

the pin connecting the actuator to the stem had

dislodged. This resulted in the valve being in a

throttled position when the handwheel indicated full

open.

The inspectors expressed doubts to the licensee about

the ability to achieve 5200 gpm through the 3B LPI

cooler prior to the unit shutting down for the

scheduled refueling outage. The inspectors had

reviewed a performance of procedure PT/3/0150/22A,

Operational Valve Stroke Test, on June 9, 1992, while

Unit 3 was operating at full power. The LPSW portion

of this PT requires that a flowrate of 5200 gpm be

achieved through the LPI coolers. During the

performance of the test, 5200 gpm could not be achieved

through the 3B LPI cooler with only one LPSW pump

running, so the operators in the control room started

the second LPSW pump to achieve the required 5200 gpm.

The inspectors questioned the operators in the control

room, operations staff and performance engineering,

about the adequacy of the testing conducted and were

told that the status of the LPSW pumps was not a

requirement for performing the test and that under

accident conditions, 5200 gpm could be achieved through

the cooler due to isolation of nonessential loads. The

inspectors were also told that the 3B LPI cooler had

always exhibited lower flow than the 3A LPI cooler and

that starting the second LPSW pump to achieve the

required flow was normally done for the test and not

unexpected. The inspectors expressed concern about the

apparent flow imbalance between the two LPI coolers to

licensee management and requested that flow testing of

the LPSW system be considered during the refueling

outage. The inspectors consider the licensee's actions

inadequate with respect to identifying and correcting

the degraded LPSW flow path to the 3B LPI cooler and

identify this item as apparent Violation 269, 270,

287/92-24-02: Inadequate Corrective Action.

After valve 3LPSW-78 was repaired, the licensee

recommenced the LPSW flow test. The inspectors

witnessed the performance of the test and observed that

during the performance of the test, the licensee could

not achieve 1400 gpm flow through the RBCUs with only

one LPSW pump running, unless flow through both LPI

coolers was secured. The licensee has experienced

fouling of the RBCUs in the past and implemented an

14

RBCU testing program to ensure operability of the

RBCUs.

The operability determinations assumed that the LPSW

flow to the RBCUs would exceed 1400 gpm. The TS also

requires that 1400 gpm-LPSW flow be achievable for RBCU

operability. TS 4.5.2.1.2, Reactor Building Cooling

System, requires that a system test be conducted each

refueling outage to demonstrate proper operation of the

system. The test is considered satisfactory if control

board indication verifies that all components responded

to the actuation signal properly, the appropriate pump

breakers completed their travel, fans are running at

half speed, LPSW flow through each cooler exceeds 1400

gpm and air flow through each fan exceeds 40,000 CFM.

The licensee took the position that 1400 gpm was not a

requirement with only one LPSW pump operating, and that

as long as the heat inside containment could be removed

with the reduced flow rate provided by one LPSW pump,

restart of Unit' 3 could proceed. The licensee stated

that the requirements of the TS could be met by

operating two LPSW pumps. The inspectors did not agree

with the licensee's interpretation of the TS

requirement and a meeting was held between NRR, Region

II and the licensee. The meeting determined that

restart of Unit 3 with LPSW flows less than 1400 gpm to

the RBCUs, with one LPSW pump operating, was acceptable

provided an analysis was performed to verify that

reactor building heat removal requirements could still

be met with the reduced LPSW flow available, and 1400

gpm could be achieved with two LPSW pumps operating.

The licensee would also submit a TS amendment to revise

the operability requirements for the LPSW system. The

inspectors will review the corrective action as stated

in the LER to verify that a TS change is submitted for

this item. Until the licensee submits this TS change,

this is identified as Unresolved Item (URI) 269, 270,

287/92-24-04: TS Change For Unit 3 LPSW.

The licensee performed a temporary test to verify that

1400 gpm could be achieved through the RBCUs with two

LPSW pumps operating and LPSW flow to the LPI coolers

throttled to 3000 gpm. The temporary test also

established maximum flow through one LPI cooler with

two LPSW pumps operating to verify that LPSW flow

through the cooler would not exceed 7500 gpm. The

design flow rate for the LPI coolers was originally

6000 gpm; however, the cooler manufacturer was

contacted and stated that the cooler was designed for

7500 gpm continuous service. During the performance of

the test the flow rate to the RBCUs was greater than

15

1400 gpm with two LPSW pumps operating. However, when

the flow control valve to the 1A LPI cooler was failed

open, flow exceeded 7500 gpm. The 1A LPI cooler flow

indicated 7900 gpm when the control valve was failed

open. The inspectors questioned the performance

engineer prior to the test about the expected flow to

the cooler when the control valve was failed open. The

performance engineer stated that design engineering had

calculated that LPSW flow to the cooler would not

exceed approximately 6500 gpm if the valve was failed

open and the other LPI cooler was isolated. The

procedure required that 5800 gpm be established through

both LPI coolers prior to failing the 1A cooler outlet

valve open. This was to ensure that excessive flow

would not be experienced through the cooler with the

failed open control valve. When the valve was failed

open, the control valve to the main turbine oil cooler

was in automatic and approximately 75 percent open.

Even with the extra flowpaths established, the flow to

the 1A LPI cooler exceeded the 7500 gpm requirement.

The licensee reduced the flow through the 1A LPI cooler

to less than 7500 gpm by securing an LPSW pump and

returned the control valve to normal.

The licensee contacted the cooler manufacturer and

obtained an engineering evaluation that 7900 gpm flow

would not have caused degradation of the cooler and

obtained an evaluation that LPSW flow through the

cooler could be sustained at 8800 gpm for two hours

without resulting in catastrophic failure of the

cooler. The licensee performed another temporary test

to determine if flow through an LPI cooler could be

throttled to less than 7500 gpm assuming two LPSW pumps

operating and still achieve greater than 5200 gpm with

one LPSW pump operating. The purpose of the temporary

test was to determine if travel stops could be

installed on the flow--control valves to prevent

excessive flow through the cooler and still achieve the

required flow rate during worst case low flow

conditions. The test determined that travel stops

could be installed. The licensee installed travel

stops on the LPI LPSW flow control valves while

increasing plant temperature and pressure in

preparation for restarting the Unit. The travel stops

were installed and tested prior to exceeding 250

degrees F or 350 psig in the RCS. No additional flow

model testing was conducted after installation of the

travel stops.

16

e.

Unit 1 and 2 LPSW System

Throughout the reporting period the inspectors

questioned the licensee about the adequacy of the Unit

1 and 2 flow model calculation. The inspectors were

informed that the Unit 1 and 2 flow model calculation

had been revised to reflect the worst case low flow

condition assuming both units were operating and that

the model showed that adequate flows would be achieved

through the safety-related loads but that flow to the

RBCUs would be less than 1400 gpm on the accident Unit.

The licensee performed an operability evaluation that

determined that LPSW flows as low as 800 gpm would be

acceptable to the RBCUs under accident conditions. The

flow model calculation predicted that LPSW flow to the

RBCUs would be greater than 1000 gpm. -The licensee

also performed a flow model calculation to determine

predicted high flow conditions through the LPI coolers

assuming only one cooler was in service and a loss of

instrument air occurred. The calculation determined

that with three LPSW pumps operating, LPSW flow to one

LPI cooler would not exceed 8800 gpm and that with two

LPSW pumps operating LPSW flow would not exceed 7500

gpm. The licensee had obtained an evaluation from the

cooler manufacturer that a flow rate of 8800 gpm could

be sustained for two hours and failure of the cooler

would not occur. Based on the predicted flow rate, the

licensee modified the emergency operating procedures to

require that one LPSW pump be secured following an

accident if all three LPSW pumps in the shared Unit 1

and 2 system automatically started.

The inspectors still had concerns with the adequacy of

the Unit 1 and 2 flow model and requested that the

licensee evaluate the possibility of performing limited

flow testing of the Unit 1 and 2 LPSW system to

determine if the flow model calculation could be

bounded or verified by actual flow or pressure

measurements. The licensee's position was that the

Unit 1 and 2 flow model calculation supported the

continued operation of Units 1 and 2 and that further

review of the issue would be conducted.

f.

Unit 1 and 2 Waiver of Compliance

On September 29, 1992, the licensee determined that the

LPSW pump performance curves assumed in the Unit 1 and

2 LPSW system flow model calculation were

nonconservative. The licensee initially used generic

pump performance curves provided by the pump

manufacturer and included a five percent margin in the

17

flow model calculation to account for actual pump

performance. On September 29, 1992, the licensee

performed a test to determine the actual head curve

generated by the LPSW pumps. The actual LPSW pump head

curve exceeded the generic head curve used in the flow

model calculation. Based on the information obtained

from the LPSW pump testing, the licensee determined.

that the predicted flow rate could exceed the allowable

maximum continuous flow rate allowed by the cooler

manufacturer. The licensee also determined that pump

runout problems could potentially exist under certain

conditions. The licensee reported the condition to the

NRC via the requirements of 10 CFR 50.72 and entered a

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Limiting Condition for Operation (LCO).

On September 30, 1992, the licensee requested a

temporary waiver of compliance to allow Units 1 and 2

to remain at less than 10 percent power for 84 hours9.722222e-4 days <br />0.0233 hours <br />1.388889e-4 weeks <br />3.1962e-5 months <br /> to

permit testing and modification of the LPSW and LPI

systems. Units 1 and 2 commenced a power reduction and

power levels were stabilized at approximately 8 percent

on October 1, 1992, at approximately-2:30 a.m. to allow

testing and modification.

On October 4, 1992, testing and modifications of the

shared Unit 1 and 2 LPSW system were completed. The

licensee installed travel stops on the LPI cooler LPSW

flow control valves to prevent excessive flow through

the coolers under worst case conditions. During the

testing process, the licensee determined that with the

travel stops installed and two LPSW pumps operating,

the required LPSW flow to the LPI cooler on the

accident Unit might not be achievable if LPSW flow to

both LPI coolers on the non-accident Unit was

established. The licensee agreed that simultaneous

LPSW flow through the LPI coolers would not be

established and also stated that both Units would be

shutdown if one Unit was required to shutdown to cold

shutdown conditions until resolution of the issue.

Based on these conditions, concurrence was obtained to

exit the LCO and return the Units to power.

g.

Previous LPSW Calculations

The inspectors reviewed some earlier calculations

performed by the licensee concerning LPSW flow

predictions. The calculations reviewed by the

inspectors all used the same basic assumptions

contained in the calculation reviewed by the inspectors

on September 2, 1992.

The calculations reviewed by the

inspectors were performed as early as 1988 and

concluded that the LPSW systems were acceptable as is.

18

The inspectors reviewed Calculation OSC-4017,

Evaluation of the LPSW System Flow Models Under Single

Failure Scenario, completed October 4, 1990. The

purpose of the calculation was to run the hydraulic

models assuming a single failure and a loss of offsite

power. The calculation assumed only one LPI cooler was

operable on the accident unit and that one LPI cooler

was out for maintenance on the outage unit. The

calculation assumed that one RBCU was out of service on

the accident unit and that flow was throttled to the

RBCUs on the nonaccident unit. The calculation assumed

that LPSW flow to the reactor coolant pump motors had

been isolated. The calculation determined that flow to

the two operable RBCUs on the accident unit would be

less than 1400 gpm for both Units 1 and 2 with two LPSW

pumps operating. The calculation concluded that LPSW

flow to the two operable RBCUs on Unit 3 would be

greater than 1400 gpm. The calculation stated that

flow is marginally inadequate to the RBCUs on Units 1

and 2, that in both cases flows are no greater than 10

percent less than the required flows and that given the

accuracy of the computer program, the flows were

acceptable. The calculation goes on to state that the

LPSW system is adequate as designed to provide the

required flowrates to all safety related components.

These calculations are additional examples like those

discussed in paragraph 6.b. The resolution of the

operation of the LPSW system is discussed in paragraph

6.a.

h.

Self Initiated Technical Audit (SITA) Findings.

The licensee performed a technical audit of the LPSW

system in 1987. This audit identified numerous

deficiencies and unresolved items. It also identified

that calculations which demonstrated acceptable flow to

all safety-related LPSW loads during accident

conditions were not documented and the current test

program was inadequate to verify acceptable flow. The

licensee response stated that recognition that normal

flows exceed emergency flow demand rendered this

calculation unnecessary; however, the licensee agreed

to generate a hydraulic flow model. The calculation

documenting the results of the model would be completed

by August 20, 1988, and the calculation would verify

that the LPSW system is sufficient to supply all

required needs. The licensee had the opportunity to

identify LPSW performance problems based on the results

of the flow model calculations.

The SITA identified that the LPSW control valves to the

LPI coolers fail open on a loss of air and that the LPI

19

coolers are susceptible to damage caused by excessive

flow. The licensee responded that the concern that the

LPI coolers are susceptible to damage caused by

excessive flow was not founded. Calculation OSC-859

determined that the maximum cooler flow that can be

obtained on the LPSW shell side is 7500 gpm. The

licensee also responded that performance tests also

support that an LPSW flow rate of over 7500 gpm through

the LPI cooler is not obtainable.

The inspectors reviewed calculation OSC-859, Decay Heat

Coolers Overflow Protection. The calculation states

that test data was obtained in the field with one LPSW

pump in operation and service water flow to all normal

LPSW requirements. The calculation records a flow

through the "A" LPI cooler of 5500 gpm with the outlet

flow control valve 60 percent open. The calculation

goes on to generate a flow versus head curve and

concludes that 7500 gpm is the maximum cooler flow if

approximately 10,500 gpm is assumed going to other LPSW

requirements. The assumption that 10,500 gpm goes to

other components is not supported.

The inspector's review concluded that the calculation

did not support the conclusion that LPSW flow through

the LPI cooler would not exceed 7500 gpm. The

inspectors also concluded that the performance testing

conducted on the LPSW system did not support the

conclusion that an LPSW flow rate of over 7500 gpm was

not obtainable through the cooler. LPSW flow through

the LPI coolers is discussed in paragraph 6.d under

item 92-24-02: Inadequate Corrective Action.

i.

Containment Heat Removal Requirements

The licensee performed a benchmark flow test on the

Unit 3 LPSW system in May of 1991. The licensee

performed a benchmark flow test of the shared Unit 1

and 2 LPSW system in January of 1992.

The purpose of

the tests was to record pressure and flow measurements

at various key points throughout the LPSW system. The

data obtained from the benchmark tests was used to

"calibrate" the LPSW flow model calculation originally

performed in 1988.

The inspectors reviewed the Benchmark test conducted on

the Unit 3 LPSW system and determined that the

benchmark test did not establish flow through all LPSW

loads simultaneously to establish a baseline condition.

The benchmark test established 3200 gpm flow through

the 3A LPI cooler, isolated the 3B RBCU, and throttled

LPSW flow to the 3A and 3B RBCUs to 1400-1450 gpm. The

20

inspectors questioned the usefulness of the data

obtained from the benchmark test since the system

resistance had been artificially induced by throttling

all the flowpaths. The inspectors questioned the

decision not to establish flow through the 3B RBCU and

the 3A LPI cooler. The inspectors were told that the

test had been performed when Unit 3 was operating at

power and that the normal accident alignment could not

be achieved because the nonaccident loads could not be

isolated. The inspectors reviewed the past operating

history of Unit 3 and determined that the Unit had been

shutdown for a scheduled refueling outage from February

13, 1991 to March 30, 1991. The benchmark test could

have been performed during the refueling outage and the

unit could have been configured in any test

configuration required to support the acquisition of

useful data. The inspectors believe that an adequate

benchmark test would have identified that the

performance of the LPSW system was questionable.

The inspectors reviewed the benchmark test performed on

the shared Unit 1 and 2 LPSW. The inspectors noted

that during the benchmark test the licensee was unable

to obtain greater than 1400 gpm through the Unit 2

RBCUs even though the 1B and 2B RBCUs were isolated.

During the benchmark test both units were operating at

power and the nonaccident loads were not isolated.

The licensee performed an operability evaluation prior

to restart of Unit 3 to ensure that reduced LPSW flow

through the RBCUs would not adversely affect the

pressure/temperature response of thereactor building

after a design basis accident. This evaluation

determined that an LPSW flowrate of 800 gpm to the

RBCUs was acceptable to remove the required heat load

inside the reactor building. The inspectors requested

that the licensee provide the heat removal requirements

for the containment heat removal systems. The

inspectors were informed that the containment heat

removal requirements were predicated on not exceeding

59 psig peak containment pressure and the reactor

building equipment qualification (EQ) temperature

curve. The licensee stated that RBCU performance did

not affect peak containment pressure and that the

combined effect of the RBCUs and LPI maintained the

containment within the requirements of the EQ curve.

The FSAR states that a reactor building cooling unit

has a design heat removal capacity of 80 million BTU/HR

for a combined heat removal capability of 240 million

BTU/HR. The licensee, in the past, stated that the

combined heat removal capability of the two worst RBCUs

must meet or exceed 80 million BTU/HR to meet

21

containment heat removal requirements. A meeting was

held between the inspectors and the licensee on October

22, 1992, to discuss containment heat removal

requirements. The inspectors were provided a copy of

the licensees EQ curve superimposed on the reactor

building temperature response curves contained in the

FSAR (Figure 15-71).

Based on the curve provided, the

inspectors determined that containment heat removal

systems were not required to meet the EQ curve in the

first 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> of the accident. The inspectors asked

the licensee to verify this assumption and were told

that the RBCUs were required to remove 71.8 million

BTU/HR.until the LPI system was aligned to the

containment sump to maintain containment temperature

below the EQ curve. The inspectors stated that the

curves provided did not indicate that containment

temperature could exceed 286 degrees even with no RBCUs

operating and no building spray actuation. The

licensee again stated that based on analysis, the RBCUs

were required to remove 71.8 million BTU/HR until LPI

is aligned to the containment sump at which time they

are only required to remove 31 million BTU/HR to

maintain the containment within the requirements of the

EQ curve. The inspectors requested that the licensee

provide the original licensing basis of the containment

heat removal systems for review. Subsequent to the

meeting, the inspectors were informed that the 71.8

million BTU/HR requirement was based on a more

sophisticated computer code that the licensee is in the

process of submitting to the NRC for approval. The

FSAR curves are based on the present computer code and

show that containment temperature response stays below

the EQ envelope without RBCUs in operation for the

initial phase of the accident. The inspectors were

informed that the new computer code was scheduled to be

submitted to the NRC for approval in 1993.

The

inspectors identify this item as Inspector Followup

Item 269, 270, 287/92-24-03: Containment

Pressure/Temperature Response.

j*

Net Positive Suction Head (NPSH) Requirements

Subsequent to returning the Units to power operation,

the licensee determined that LPSW flow rates could

exceed the analyzed flow rate for pump operation of

15,000 gpm, with no Condenser Cooling Water (CCW) pumps

operating and a lake level of 780 feet. During the

LPSW flow testing conducted on the Unit 1 and 2 LPSW

system, the "C" LPSW pump indicated 19,200 gpm with

maximum flow through all four LPI coolers and one main

turbine oil cooler in service.

In this configuration,

one CCW pump was in operation supplying NPSH to the

22

LPSW pumps. The licensee was unable to determine the

developed flow rate from the other operating LPSW pump

due to the location of the flow instrument on the "B"

LPSW header.

The licensee performed Calculation OSC-5018,

Operability Evaluation for PIR 0--92-0535, dated

October 26, 1992, to evaluate the operability of the

LPSW system and ensure that NPSH available to the LPSW

pumps is greater than required NPSH. The licensee

determined that available NPSH would exceed required

NPSH if lake level was maintained at or above 795 feet

and LPSW flow was limited to 16,600 gpm per pump. The

licensee contacted the pump manufacturer and obtained

an evaluation that the pumps could withstand operation

with inadequate NPSH for short term operation of 30

minutes. Based on the information provided, the

licensee's operability statement required that LPSW

flow to one LPI cooler on the nonaccident Unit be

secured within 10 minutes and flow through a bypassed

Main turbine oil cooler be secured within 30 minutes to

ensure that LPSW flow would be less than 16,600 gpm.

The NPSH concern is applicable when one Unit is in a

refueling outage and an accident occurs on the other

Unit. Until the inspectors can review this item in

detail prior to the Unit 1 refueling outage scheduled

for December 1992, this is identified as IFI 269, 270,

287/92-24-06: NPSH Requirements.

Within these areas, one apparent violation, two unresolved

items and two inspector followup items were identified.

7.

Exit Interview (30703)

The inspection scope and findings were summarized on

November 3, 1992, with those persons indicated in paragraph

1 above. The inspectors described the areas inspected and

discussed in detail the inspection findings. The licensee

did not identify as proprietary any of the material provided

to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference

Paragraph

URI 269,270,287/92-24-01

Testing the MG-6 Relay And

Corrective Action For Keowee

Overhead Path (paragraph 5.b).

VIO 269,270,287/92-24-02

Inadequate Corrective

(Apparent)

Action For LPSW Low Flow

(paragraph 6.d).

23

Item Number (CONTINUED)

Description/Reference

Paragraph

IFI 269,270,287/92-24-03

Containment

Pressure/Temperature Response

(paragraph 6. i).

URI 269,270,287/92-24-04

TS Change For Unit 3 LPSW

(paragraph 6.d)

URI 269,270,287/92-24-05

TS Change For LPSW System

(paragraph 6.a).

IFI 269,270,287/92-24-06

NPSH Requirements

(paragraph 6.j).

ENCLOSUPE 2

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