ML16148A599

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Insp Repts 50-269/91-35,50-270/91-35 & 50-287/91-35 on 911124-920104.Violations Noted.Major Areas Inspected: Operations,Surveillance Testing,Maint Activities & Insp of Open Items
ML16148A599
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/29/1992
From: Belisle G, Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A597 List:
References
50-269-91-35, 50-270-91-35, 50-287-91-35, NUDOCS 9202140115
Download: ML16148A599 (10)


See also: IR 05000269/1991035

Text

Vs

REGU4

UNITED STATES

NUCLEAR REGULATORY COMMISSION

10

.REGION

II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/91-35, 50-270/91-35 and 50-287/91-35

Licensee:

Duke Power-Company

P. 0. Box 1007

Charlotte, NC 28201-1007

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility.Name: Oconee Nuclear Station

Inspection Conductedi November 24, 1991 - January 4, 1992

Inspector:

nz ,

lr

sident Inspector

Date Si ned

aiB-.De1,

as-tdent'Inspector

Dae Signed

W. K. Poert er,

esi ent Inspector

Date Si ned

Approved by:

.Z/

G. A. Belisle, Sectiii'>hief

Date

gned

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in

the areas of operations, surveillance testing, maintenance activities

and inspection of open items.

Results: One violation with two examples for failure to follow procedures was

identified.

Both examples involved controlled and configured valves

being found in the wrong position.

In one instance, the licensee

generated a LER because the valve found out of position was a

containment isolation valve. In the other instance, an inadvertent

dilution of a concentrated boric acid storage tank occurred over a

period of several days.

These two examples indicate a problem in the

configuration control area.

9202140115 920129

PDR ADOCK 05000269

PDR

REPORT DETAILS

1. Persons Contacted

Licensee Employees,

  • H.. Barron, Station Manager
  • J. Davis, Quality Assurance Manager

D. Deatherage, Operations Support Manager

  • W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

.0. Kohler, Compliance Engineer

C. Little, Superintendent, Instrument and Electrical (I&E)

  • M. Patrick, Compliance Manager
  • S. Perry, Assistant Licensing Coordinator

G. Ridgeway, Shift Operations Manager

G. Rothenberger, Superintendent, Integrated Scheduling

  • R. Sweigart, Superintendent, Operations

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P Harmon
  • W Poertner
  • B Desai
  • Attended exit interview.

2. Plant Operations (71707)

a. General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records,

temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and on night shifts, during

weekdays and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

observed were conducted as required by the licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

2

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and.3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station.

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Within the areas reviewed, licensee activities were satisfactory.

b.

Plant Status

Unit 1 operated at power for the entire reporting.period.

Unit 2 operated at power for the entire reporting period.

Unit 3 remained in a shutdown condition the entire reporting period

as a result of an unisolable reactor-coolant system (RCS) leak from a

failed instrument fitting.

During the subsequent startup after

repairs and equipment, inspections,

a dropped control. rod on

December 8. forced a return to cold shutdown for repairs to several.

rod drive mechanisms.

On December 15,

during plant heatup and

pressurization, a through-wall crack in the RCS decay heat removal

dropline was discqvered.

The unit was again shut down and

depressurized to repair the leak.

At the end of the reporting

period, the unit was in the process of returning to power.

c. Mispositioned Containment Isolation Valve

On December 9, the Operations Manager informed the resident staff of

a Unit .3 containment isolation valve that had been found out of

position. The val-ve, 31A-91, is a 3 inch containment isolation valve

for the Instrument Air System.

The valve is a manually operated

valve located inside containment, and is required to be closed to

meet containment isolation criteria.

Technical Specification (TS)

3.6.1 requires containment integrity to be established when RCS

temperature is greater than 200 degrees, pressure is above 300 psig,

3

and fuel is in the reactor vessel.

Valve position is controlled by

Enclosures 13.1 and 13.2 of procedure PT/3/A/115/08, Inside Reactor

Building Manual Isolation Valve Checklist Verification.

The last

documented manipulation of 31A-91 occurred on March 27,

1991, when

the unit was being prepared for startup after a refueling outage.

Several entries into containment were performed after that.date, but

there had been no documented position change of the valve.

On November 30,

1991, a non-licensed operator entered the reactor

building to perform valve lineups, including opening valve 31A-91.

The NLO found the valve *in the open position and notified the Unit 3

supervisor.

Several individuals had made containment entries since

the November 23 shutdown, but none questioned admitted operating the

valve.

The valve is not in a high traffic area in containment, and

is not subject to inadvertent operation. A Shift Incident Report

(SIR)

was initiated on December 1, 1991,

but an LER was not

immediately initiated. . An LER was initiated on December 9.

The

station Compliance Manager informed the inspectors that this LER

would not be complete within the required 30 days from discovery of

the event, primarily due to the relatively late start on preparing

the LER and the intervening Christmas holidays.

The licensee sent a

memo to AEOD stating that the LER would be late.

The inspectors discussed with site management the lack of timeliness

in the licensee':s investigation into the circumstances of this event.

In addition, the fact that 9 days passed before the resident

inspector staff was notified of the event is not acceptable.

Failure to meet the requirements of procedure PT/3/A/115/08 resulted

in a mispositioned valve and a lack of configuration control for a

containment isolation valve.

This item is identified as Violation

50-287/91-35-01: Inadequate Configuration Control.

d. Unit 3 Loss of Feedwater

On December 7,. 1991, *at approximately 3:45 p.m., with the reactor

coolant system at 1230 psig and 519 degrees F, the operating Hotwell

pump (3A) tripped followed by the operating condensate booster pump

(3A) and the operating main feedwater pump (3A) resulting in a loss

of feedwater to the steam generators.

At the time of the event the

unit was subcritical and in the process of heating up in preparation

of returning the unit to service.

A hotwell pump and condensate

booster pump were restarted and the 3A main feedwater pump was reset

and feedwater was reestablished to the steam generators at

approximately 3:48 p.m.

The lowest level reached in. the steam

generators was 19 inches on the startup range level instruments. The

inspectors were in the control room during the event and monitored

the operators actions to restore feedwater.

4

The licensee determined that the trip signal was generated by an

erroneous low hotwell level signal from level, switch 3LS-28.

The

level switch was checked and no problems could be .found with its,

operation or setpoint..

The licensee theorized that relay chatter

associated with the feedwater pump low discharge pressure relay that

is physically located approximately four inches above the hotwell low

level relay may have caused the low level relay to actuate.

To.

prevent an inadvertent trip signal from being received with the unit

at power, the hotwell low level trip signal was removed from service.

'The licensee based this decision on the fact that the trip signal is

for pump protection only and a plant modification package had been

requested previously to delete the low hotwell level trip signal.

e. Unit 3 Water Hammer

On December 9, 1991, at approximately 5:30 a.m., a water hammer event

occurred on Unit 3 when the operators in the control room attempted

to place steam generator hot blowdown in service.

The inspectors

were in the turbine building at the time of the event and heard the

water hammer occur. The inspectors toured the turbine building and

observed piping insulation on the floor around the Unit 3 emergency

switchgears and several pipe supports that had been ripped from the

wall.

The inspectors proceeded to the control room and determined

that the water hammer had resulted when valves 3FDW-103 and 3FDW-104

had been opened to reestablish hot blowdown.

Hot blowdownhad been

secured during the Unit 3 startup.

However, the startup had been

stopped due to a dropped rod and the unit was returning to cold

shutdown to replace the control rod drive stator of the rod that had

dropped.

At the time of the event steam generator pressure was

approximately 850 psig.

The licensee walked down the piping,

evaluated the damage resulting from the water hammer and repaired the

broken hangers. * At the conclusion of the inspection period the

licensee was evaluating potential procedure changes to prevent a

recurrence of this event.

f. Erroneous Estimated Critical Position (ECP).Calculation

On December 8, 1991,

an ECP calculation was performed by the night

shift operations crew in preparation for the Unit 3 startup and

approach to criticality. The

ECP calculation determined that

criticality would be achieved at 19% withdrawn on group 6 based on.a

reactor coolant system (RCS)

boron concentration. of 1304 ppm.

The

calculation was performed per Enclosure 13.2 of PT/3/A/1103/15 and

had been independently verified as correct.

Subsequent to shift

turnover, the oncoming shift questioned the adequacy of the ECP

calculation based on the RCS boron concentration prior to the unit

shutting down.

The oncoming shift performed another ECP calculation

per PT/3/A/1103/15 and did not obtain the same results as the

previous shift had achieved.

The previous ECP calculation was

5

reviewed and it was determined that the error was a result of not

reversing the reactivity coefficient sign in step 13.2.6 of the

procedure as specified in the procedure. Review of the incorrect ECP

calculationdetermined that both the person performing the ECP. and

the independent verifier had made the same error when performing .the

calculation.

The error introduced into the ECP calculation was in a

conservative direction such that criticality would not have been

achieved early in the rod withdrawal

sequence.

The licensee

initiated a shift incident report on this event and continued with

unit startup activities.

g. Valve 3CS-60 Mispositioned

On December

17,

1991, with the 3A bleed transfer pump taking a

suction on the. concentrated boric acid storage tank (CBAST) and

adding water to the letdown storage tank (LDST)

to increase the

reactor coolant system boron concentration, the expected increase in

system boron concentration was not achieved for the amount of boric

acid thathad been injected into the RCS. A water sample of the 3A

bleed transfer pump discharge was obtained with the pump running and

the results indicated 3317 ppm boron instead of the expected CBAST

concentration of 10550 ppm boron...' Investigation by the operators

determined that valve 3CS-60 was open approximately 5 turns instead

of in its required position of closed.

Valve 3CS-60 is the bleed

transfer pump suction crossconnect valve and with the valve open the

3A bleed transfer pump was taking. a suction on the CBAST and the 3B

bleed holdup tank simultaneously. The boron concentration in the 3B

bleed holdup tank was less than .10 ppm and resulted in 'the reduction

of the expected increase in boron concentration of the RCS.

Valve

3CS-60 in the open position also allowed water from the 3B bleed

holdup tank to enter and dilute the CBAST.

A boron sample of the

CBAST was taken and indicated a boron concentration of 5341 ppm in

the CBAST as opposed to the expected 10550 ppm.

The licensee could not determine when 3CS-60 had been opened. Review

of the completed procedure files determined that the valve had been

opened on .December 9, 1991, to borate the RCS from the' CBAST using

the 3B bleed transfer pump; however, the procedure returns the valve

to the shut position and requires that the valve be independently

verified as shut after the boron addition and the system is flushed.

The inspectors consider this item 'not only a configuration control

problem but also a reactivity management issue.

The failure to

maintain configuration control of valve 3CS-60 is identified as .a

second example of violation 50-287/91-35-01 discussed in paragraph

2.c.

Within the areas reviewed, one violation with two examples was identified.

6

3.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, authorization to begin work,

data collection, independent

verification where required, handling of deficiencies noted, and review of

completed work. The tests witnessed, in whole or in part, were inspected

to determine that approved procedures were available, test equipment was

calibrated, prerequisites were met, tests were conducted according to

procedure, test results were acceptable and system restoration was

completed.

Surveillances reviewed and witnessed in whole or in part:

PT/0/A/115/07

Reactor Building Spray Valve Verification.

PT/0/A/305/01

Reactor Manual Trip Test.

PT/0/A/201/04

PORV Operability Test.

Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

4. Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

the skill of the trade. Activities, procedures, and work requests were

examined to verify; proper authorization to begin work, provisions for

fire, cleanliness, and exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 36230C

Investigate and repair RPS Channel A Hot Leg Temperature

Indication

WR 35864C

Repair 1CCW-304

Unit 3 CRDM Stator Checkout/Replacement

Unit 3 Decay Heat Removal Dropline. Pipe Replacement

.Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

0

7

5.

Unit 3 Forced Outage

Unit 3 experienced a Reactor Coolant System (RCS) leak greater than 50 gpm

on November 23, 1991, and subsequently had to be shutdown. The leak was

caused when an improperly installed compression fitting failed.

Details

of the event are discussed in NRC Inspection Report (IR) 50-287/91-34.

The unit was still shutdown for repairs at the end of the inspection

period for IR 50-287/91-34 and all the activities conducted during the

outage. were not captured in the special inspection report. The following

items occurred during the Unit 3 forced outage and were not addressed in

IR 50-287/91-34..

a. Control Rod Drive Mechanism Problems

Following the RCS leak, various components in the reactor building

were inspected by the licensee for possible moisture intrusion.

Included in the components inspected were the Control Rod Drive (CRD)

.

mechanisms.

Due to airborne contamination in the reactor building,

the CRD stators were initially tested from the cable spreading room

on November 26, 1991.

Specifically, testing involved meggering to

measure resistance to ground values.

The resistance values found

from the cable spreading room were below the acceptance criteria of

200 megohms or more.

Low resistance values indicate that there may

be a problem.With the stator or the insulation.

Since all of the

readings taken from the cable spreading room were low, the licensee

decided to remegger the stators from within the reactor building.

The licensee chose eighteen stators and obtained megger readings from

the bulkhead (side wall of the refueling canal where the cables from

all stators are centrally located) to the stator.

All eighteen

stators meggered above the value of 200 megohms.

The licensee

concluded that the readings from the cable spreading room were in

error and that all the CRD mechanisms were free of any moisture

instrusion.

On December 8, 1991 during Unit 3 startup, CRD group 5, rod 6 dropped

into the core.

Startup was halted and investigation by the licensee

indicated that two phases of the stator had shorted together causing

the rod to drop into the core.

The unit was cooled down to repair

the stator and a decision was made to megger all sixty nine stators.

The stator for the dropped rod meggered above the acceptance

criteria; however, the connector was found to have moisture in it.

When meggering on all sixty nine stators was completed, there were

twenty nine stators that did not meet the designated acceptance

criteria. Consequently, they had to be removed from the vessel head

and dried.

Drying involved nitrogen purging and then, if needed,

electrical drying of the stators.

After drying, the twenty- nine

stators were remeggered and.at this time three stators did not meet

the acceptance criteria. The licensee decided to replace the three

stators with new stators.

In addition, one more stator had to be

replaced due to physical damage experienced when that stator was

dropped during handling.

The licensee also replaced twenty four

connector inserts with a new type of insert that is thought to be a

better quality insert. After reinstalling the twenty stators and the

connector inserts, the licensee remeggered all the stators and all

but one meggered within the acceptance criteria.

This stator was

redried and subsequently meggered greater than 200 megohms. With all

sixty nine stators meggering above the acceptance criteria, the

licensee .decided to proceed with unit startup.

On January 3, with RCS temperature at 240 degrees F, the stators were

again meggered.

At this time four stators did not meet the

acceptance criteria of at least 200 megohms. The licensee decided to

proceed with the startup.

This decision was based on industry

experience and the fact that the 200 megohm guideline set by B&W was

for new stators.

The stators in question were not newly installed

and due to some wear, the licensee postulated that megger readings

could be expected to be a lower value and the stator would still be

reliable. The licensee, at RCS temperature of 410 degrees F, again

meggered the four stators that had meggered below 200 megohms at RCS

temperature of 210 degrees. The results showed that meggering values

for stator readings had dropped slightly and two had risen

substantiality. Apparently, moisture from the leak had collected in

the stator at the bottom of the stator conduit and therefore the

initial reading at shutdown was not affected.

However, as heatup

began, moisture began to evaporate up the stator tube where it cooled

and condensed and then traveled back down the tube where it was

cooled.

This moisture trapped inside served to lower the megger

readings obtained during the subsequent checkout.

b. Through-Wall Crack in the Decay Heat Removal Dropline

At 8:30 a.m.,

on December 15,

1991,

during a tour of the reactor

building, the licensee noticed a small leak coming from the decay

heat dropline.

The exact location of the leak could not be

identified due to insulation. However, the leak was in the vicinity

of the decay heat drop line isolation valve 3LP-2. At this time the

unit was at 130 degrees F, 30 psig, with a pressurizer bubble

established and Low Pressure Injection (LPI)

aligned in the decay

heat removal mode.

The leak was later identified as coming from a

crack on. the decay heat dropline where a 3/4 inch piping relief

valve, 3LP-25, connects to the dropline.

The licensee determined

that the piping could possibly fail during further RCS pressuri

zation.

A decision was made on December 15 to depressurize and

cooldown to accommodate replacement of the portion of piping with the

crack. Additionally, the dropline had to be isolated to enable pipe

replacement. To remove decay heat, the licensee developed a special

procedure which involved aligning the spent fuel pool pumps to force

circulation through the core.

With the refueling canal full, vessel

head removed,

decay heat dropline isolated, the spent fuel pool pump

9

would take suction from a low point in the refueling canal and force

water through the core via the LPI'headers. The spent fuel cooler as

well as the LPI coolers were available heat sinks.

The licensee encountered some problems during filling.the refueling

canal.

The canal seal plate was. not leak tight during the initial

fill. *The canal had to be drained and portions of the rubber gasket

had to be shimmed to make the canal seal plate completely leak tight.

The licensee did not encounter any problems controlling core

temperature at approximately 90 degrees F during the time that they

were in the special spent fuel pump alignment.

The portion of the pipe with the crack was cut out and sent out to.

Babcock and Wilcox (B&W) for analysis. A replacement pipe was welded

on the decay heat dropline.

Preliminary analysis done by B&W

indicated that the failure mode for the decay heat dropline pipe was

high cycle, low amplitude load fatigue. There were no indications of

corrosion contributing to- the failure.

An NRC special materials

inspector closely followed the licensee's actions pertaining to the

crack and pipe replacement. Details of this issue will be documented

in NRC Inspection Report No. 50-287/91-37.

No violations or deviations were identified..

6.

Inspection of Open Items (92701)

The following open item was reviewed using licensee reports, inspection,

record review, and discussions with licensee personnel, as appropriate:

(Closed) Inspector Followup Item 56-269,270,287/90-34-01: Corrective

Actions Associated with LPSW Pilot and Solenoid Operated Valves for MDEFW

Pumps.

The licensee replaced the valve operator for the valves in

question with a different design of operator that does not use air as the

motive force to open the valve.

7. Exit Interview (30703)

The inspection scope and findings were summarized on January 10,

1992,

with those persons indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings.

The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

VIO 50-287/91-35-01

Inadequate

Configuration

Control

(paragraphs 2.c and 2.g)