ML15224A691

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Insp Repts 50-269/90-12,50-270/90-12 & 50-287/90-12 on 900422-0519.Violations Noted.Major Areas Inspected: Operations,Degraded Grid Voltage,Surveillance Testing,Maint Activities,Seismic Monitoring & Outage Activities
ML15224A691
Person / Time
Site: Oconee  
Issue date: 06/19/1990
From: Binoy Desai, Shymlock M, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A689 List:
References
50-269-90-12, 50-270-90-12, 50-287-90-12, NUDOCS 9006290229
Download: ML15224A691 (17)


See also: IR 05000269/1990012

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos:

50-269/90-12, 50-270/90-12, 50-287/90-12

Licensee: Duke Power Company

P.O. Box 1007

Charlotte, N.C. 28201-1007

Docket Nos.:

50-269, 50-270, 50-287

License Nos.:

DPR-38, DPR-47, DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducted: A ril 22 - May 19, 1990

Inspectors

,

P.

Skinner, Senior esi ent Inspector

Date

L. D. Wert, Residen Inspector

Date Signed

B. B. Desai, Resident Inspector

Date Signed

Approved by:

_

__

___/

M. B. Shymigck, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in

the areas of operations including degraded grid voltage issues,

surveillance testing, maintenance activities, seismic monitoring,

outage activities, Notice of Unusual Event for a chemical spill and

inspection of open items.

Results:

One Violation was cited during this report period:

-

One violation addressed a failure to incorporate design basis

information involving degraded voltage protection

into

electrical relay procedures (paragraph 2.c).

-

Another violation addressed two examples of failure to follow

procedure.

These

examples

involved inadequate component

verification which resulted in incorrect component removal

(paragraph 4.c).

They are additional examples of a failure to

follow

procedures

addressed

in Inspection

Report

50-269,270,287/90-16.

The licensee's outage management continues to be very aggressive.

However, this aggressiveness may in part have contributed to some of

the activities which created the concerns discussed in this report.

The controls exhibited by all of the plant staff during the spill

from the spent fuel pool was expeditious and effective.

..*

  • j

.,

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • B. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

T. Curtis, Compliance Manager

  • J. Davis, Technical Services Superintendent

D. Deatherage, Operations Support Manager

R. Dobson, Electrical Engineering Manager

  • B. Dolan, Design Engineering Manager, Oconee Site Office

W. Foster, Maintenance Superintendent

D. Hubbard, Performance Engineer

D. Jamil, Electrical Systems Engineering Supervisor

  • E. LeGette, Compliance Engineer

H. Lowery, Ch-airman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

  • 0. Powell, Station Services Superintendent
  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees

contacted included technicians,

operators,

0

mechanics, security force memblers, and staff engineers.

NRC Resident Inspectors:

  • P. Skinner
  • L. Wert

B. Desai

  • Attended exit interview.

2.

Plant Operations (71707)

a. The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls.

Control room logs,

shift turnover records, temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and on night shifts, during

weekdays and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

observed were conducted as required by the Licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

2

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1, 2 and 3 Spent Fuel Pool Rooms

Keowee Hydro Station

Unit 1 Reactor Building

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 operated at 100 percent full power from the beginning of this

report period until April 26 when the unit was taken off-line to

begin the end of cycle 12 refueling outage.

The unit was in the

outage for the remainder of the reporting period.

Unit 2 and 3 operated at 100 percent for the duration of this report

period.

b.

Reduced Inventory Activities (71707)

The inspectors completed the actions required by the Midloop/Reduced

Inventory Activities checklist (promulgated by L. Reyes on April 11,

1990).

Generic Letter (GL) 88-17,

the licensee's responses and

Inspection Reports 269,270,287/89-17 and 89-25 which documented the

inspection required by TI 2525/101,

were reviewed.

The inspectors

observed that operators displayed a high level of attention and

focused on meticulous procedural compliance when proceeding to and

operating in midloop conditions.

OP/1/A/1103/11: Draining and

Nitrogen Purging of the Reactor Coolant System (RCS) contains most of

the administrative controls committed to in the GL 88-17 response.

This procedure specifically provides guidance for containment closure

capability, RCS temperature and level indications, inventory addition

paths and alternate power supplies as required by the checklist. The

inspectors noted that in addition to Oconee's installed reactor

vessel level instrument (LT-5),

two temporary ultrasonic level

detectors had been installed and provided a limited range of RCS

level indication in the control room.

One of these detectors was

mounted on an RCS cold leg, the other on a hot leg.

Information

3

provided by these indicators was very useful to the operators during

the draindown evolution.

Additionally, these level indications,

along-with information from the Reactor Vessel Level Indicating

System (RVLIS)

helped resolve a long standing problem involving

inadequate RCS venting during draining.

Apparently the venting

problem is caused by a particular type of valve (Kerotest) installed

in the vent flowpaths.

These valves will be changed to another type

of valve during this outage.

Procedure changes will be made to

ensure adequate vent paths exist during draining.

The inspectors

verified portions of the alternate inventory addition flowpaths and

insured that no work was in progress which knowingly could lead to

perturbations to the RCS or to systems necessary to keep the RCS

stable.

Particular attention was given to electrical system lineups

and evolutions.

During the report period the licensee identified one instance of an

apparent failure to meet a GL 88-17 response commitment.

The

licensee committed to maintaining two makeup paths available (during

reduced inventory operations)

in addition to the Low Pressure

Injection pumps.

Since one of the required available alternate

makeup flowpaths is gravity flow from the Borated Water Storage Tank

(BWST)

via valves 1LP-21 or 1LP-22, a minimum level of 46 feet is

required to

be maintained in the

BWST.

Enclosure 4.7 of

OP/1/A/1103/11: Draining and Nitrogen Purging of the RCS, lists these

requirements as prerequisites to lowering Reactor Vessel (RV)

level

to less than 50 inches on LT-5. These conditions had been met prior

to entering reduced inventory conditions. During filling of the Fuel

Transfer Canal (FTC) from the BWST on May 3, the level was allowed to

decrease to less than 46 feet.

PT/1/A/0600/01:

Periodic Instrument

Surveillance requires verification of this level once per shift when

in reduced inventory conditions. A Problem Investigation Report was

generated to address this issue.

The 46 feet level is the level

required by TS 3.3.4 for normal operations. BWST level of less than

46 feet may not make the BWST makeup path inoperable. It should be

noted that AP/1/A/1700/07:

Loss of Low Pressure Injection System

lists this path to be utilized only if the primary alternate path is

not operable (Bleed Holdup Tank path).

Additionally, Unit 1 was

maintaining one additional alternate LPI pump suction path available

at this time.

The inspectors will follow the licensee's actions on

this issue. Once resolution of a minimum BWST level is determined it

is expected that training and more stringent procedural controls will

be utilized to ensure BWST level is maintained as required.

c. Degraded Grid Issues (71707)

Inspection Reports 50-269,270,287/90-10 and

11 discuss an issue

regarding degraded grid protection which was initially identified in

March 1990 by Design Engineering (DE) as part of the ongoing Design

Basis Documentation

(DBD)

program.

That issue involved past TS

violations and a potential single failure vulnerability in degraded

grid voltage conditions due to the startup transformer breakers (the

4

"E" breakers)

opening on undervoltage

(UV).

At that time the

licensee stated that the plant was protected from degraded grid

voltage by this undervoltage feature.

On April 23,

1990,

the

inspectors were informed by the licensee that the undervoltage

setting on the breakers was not properly set.

Due to a 3 percent

tolerance in the sensing relays and a nonconservative setpoint, even

if switchyard voltage decreased to approximately 207 KV, the breakers

may not have opened.

The minimum acceptable grid voltage level to

insure all safety related loads would be supplied with adequate

voltage under Loss of Coolant Accident (LOCA) conditions is 219 KV.

(The

208 V level safety-related valves are the limiting loads,

information on their performance under degraded voltage conditions is

limited.)

The inspectors questioned if this issue had been reviewed

for reportability in accordance with 10 CFR 50.72 since this is

potentially a more significant issue than the previously identified

problem. With the existing UV setting, if a degraded grid condition

existed and a LOCA occurred (inrush of Emergency Safeguard (ES) loads

actuating), inadequate voltages could be applied to the ES loads. On

April 24,

1990, it was determined that the problem was reportable in

accordance with 10 CFR 50.72(b)(2)(iii)(D) and notification was made.

The interim corrective actions for the previous problem (see

Inspection Report 50-269,270,287/90-11) appear sufficient to ensure

that continued plant operation under degraded grid conditions will

require initiation of extensive actions.

The licensee is continuing

progress on the urgent Nuclear Station Modification

(NSM)

as

described in Inspection Report 50-269,270,287/90-11.

A separate

10 CFR 50.73 report will be submitted concerning this latest issue.

In further review of this issue, the inspectors reviewed the past ten

years of procedure RTP/0/A/4980/27A:

Routine Test Procedure:

Westinghouse

Type

CV-7

Relay.

This procedure is used by

Transmissions department personnel to periodically verify the proper

operation of the UV relays involved in this issue.

These relays

sense the voltage which is available from the switchyard.

Their

function is to open the normal

(N) or emergency (E) breakers and

block closure of the breakers if voltage is too low.

The following

information was noted:

-

The original procedure (1976) required the UV relays to be set

at approximately 68 percent of 4160V (2829V).

-

In 1977,

as a result of a DE evaluation, the settings were

increased to approximately 88 percent (3660V) to "ensure minimum

voltage required for continued operation of non-safety and

safety related equipment" (degraded voltage protection).

This

88 percent setpoint corresponds to approximately 212 KV in

switchyard voltage (conversion includes tap setting

and

transformer loss approximations).

-

In June of 1980 the settings were decreased to about 77 percent

3203V) to comply with a DE study concerning degraded voltage

5

operation of unit auxiliaries.

This was done to prevent the

opening of the "E" breakers on UV in certain scenarios if two

Oconee units were sharing a single startup transformer.

A commitment was made in correspondence dated February 5, 1982,

to the NRC to return the setpoints to 88 percent since that was

the minimum analyzed value.

A TS change was also made which

prohibited connection of two units to one startup transformer

except for short periods of time.

However,

the inspectors

identified that the UV setting actually remained at 77 percent

until 1985 when it was returned to 88 percent for an unrelated

reason.

This discovery was immediately discussed with both DE

and station management.

Further review of this issue was conducted including review of

portions of the licensee's response to and correspondence relating to

a Generic Letter issued in June 1977 addressing degraded grid

protection. The following observations were noted;

-

Oconee does not meet all of the recommended actions of Branch

Technical Position PSB-1:

Adequacy of Station Electrical

Distribution System Voltages.

The proposed modification being

initiated for this problem will not result in Oconee being in

full compliance with PSB-1 since with a degraded grid a

subsequent occurrence of an ES signal will not automatically

separate the class

1E

system from the offsite system.

Additionally,

no TS requirements for the degraded voltage

protection system exist.

While the External Grid Trouble

Protection System (EGTPS) (designed to actuate on a loss of the

grid )is not specifically addressed in TS,

the switchyard

isolation circuitry is an inherent support system of the Keowee

overhead path and, therefore, its operability is required by TS.

-

The formal response to the GL did not specifically list the UV

feature of the E breakers as degraded grid protection for

Oconee, however, other related correspondence did.

-

The role of these UV relays in degraded grid protection has not

been sufficiently acknowledged in the past.

-

The setting of the relays was not properly controlled and they

were set well below both the value specified by DE and the value

required to accomplish their safety function. Although lack of

formal control of relay settings in general has been previously

recognized by the licensee as a weakness, the formal setpoint

documentation is still being developed. Longterm intentions are

to review each vital relay setting to ensure the relay is

properly set after the setpoint document is developed.

The

inspectors were concerned that since the E and N breaker UV

settings, were.in error, other critical relay settings may also

be in error.

6

The recently completed Emergency Power Switching Logic (EPSL)

Self Initiated Technical Audit (SITA)

reviewed the historical

relay test data sheets on these CV-7 UV relays, but the improper

settings were not noted.

The SITA team did make an observation

concerning the CV-7 relays tendency to drift from setpoint and

to be vibration sensitive. Since the DBD review of EPSL had not

yet been completed, it

would have been difficult for the SITA

team to discover the incorrect settings.

On April 26,

1990, discussions were held with NRR and the licensee

regarding both of the two recently identified degraded voltage issues

and the proposed modification to correct the problems.

On May 2,

1990, the

inspectors met with station management and DE

representatives to further discuss the improperly set relay issue.

The following key points were included;

With the UV relays set at their current value (87.5 percent of

rated bus voltage which is about 209 KV switchyard voltage), if

the relay had actuated 3 percent below the setting under

conservative assumptions and simultaneous ES actuation occurred,

then voltage supplied to the 208 V safety-related valve motors

may not have been adequate.

This could result from the 3

percent tolerance and the nonconservative setpoint of the

relays.

DE stated that the 4160V and 600V ES loads would have

sufficient voltage to operate under these conditions.

Additionally DE representatives verified that there would be no

problem with normally running loads if grid voltage decreased to

these existing settings.

-

In order to provide absolute certainty that all ES loads under

the most conservative assumptions

would receive adequate

voltage, the existing UV relays would have to be set above 92

percent of 4160V rated bus voltage.

This corresponds to about

219 KV switchyard voltage.

-

With the relays set at 77 percent (1980 to 1985 settings) the

plant was not protected from degraded grid voltage conditions.

The 77 percent setpoint corresponds to about 195 KV in the

switchyard.

If this voltage was supplied to the main feeder

busses under LOCA conditions, many ES loads would not start and

even could be damaged. There may also be some concern regarding

normally running loads if grid voltage actually decreased to the

77 percent setpoint.

-

The lowest value of degraded grid voltage recorded at Oconee was

a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> period at 208 KV on the yellow bus in 1982. Other than

that period, switchyard voltage has been above 219 KV.

-

The inspectors expressed concern that other relay settings

throughout Oconee's electrical systems may be different than DE

setpoints. The licensees longterm corrective action involving a

7

formal relay setpoint document and subsequent verification of

each setting may not be adequate if

other critical relay

settings are presently set incorrectly. The licensee committed

to comparing some transmissions procedure relay setpoints to

those specified/assumed in DE documentation.

A total of 44

safety significant overcurrent relays were checked and no

discrepancies found.

The differential current relay settings on

the Main Feeder Busses (considered an important protective

feature) have also been verified as current. Apparently this is

a time consuming process with the major effort required to

determine the DE documented setpoints.

The issue of the 3 percent tolerance band and nonconservatively set

UV relays was identified by the licensee as a result of the DBD

effort.

While the significance of the issue and the discovery of

relay settings lower than the DE values were the results of the

inspectors interactions,

the inspectors would probably not have

examined this area if

not prompted by the licensee's previous

discoveries.

The temporary corrective actions listed in Inspection

Report 50-269,270,287/90-11 appear to be adequate to address the

degraded grid issue sufficiently until the proposed modification is

installed. The issue of improper control of relay settings remains a

concern.

Incorporating design basis requirements into implementing

  • procedures

is essential to safe plant operation and is required by

Criterion III of 10 CFR 50, Appendix B. The failure of the licensee

to incorporate design basis requirements into implementing procedures

is identified as Violation 50-269,270,287/90-12-01:

Failure to

Incorporate Design Basis

Information

Into Electrical Relay

Procedures.

d. Unit 1 Reactor Protection System Actuation

At 7:32 p.m. on April 26, 1990, Oconee Unit 1 experienced a Reactor

Protection System (RPS) actuation.

RPS channels A, C, and D tripped

on number of Reactor Coolant Pumps (RCPs)/flux signal.

The unit was

in hot shutdown conditions cooling down to cold shutdown. Group one

rods were at fifty percent withdrawn (as required by procedure) to

ensure the availability to add negative reactivity during the

cooldown. In accordance with step 2.1 of Enclosure 4.2, Hot Shutdown

Conditions to 250 degrees F/350 PSI conditions, of OP/1/A/1102/10:

Controlling Procedure for Unit Shutdown, dated 2/10/89, the operators

secured 2 of the 4 running RCPs (1 in each loop).

The resultant 2

RCPs running condition initiated the RPS actuation.

Group One rods

.tripped and dropped into the core.

On December 29,

1989,

TS 2.3 (Limiting Safety System Settings,

Protective Instrumentation) had been amended to prohibit operation

above zero percent reactor power with 2 or less running RCP's.

Accordingly, Instrument and Electrical (I&E) procedures were revised

and the RPS setpoints were changed to ensure compliance with the

requirement (See Inspection Report 269,270,287/89-40).

Apparently

8

small fluctuations in the Nuclear Instrumentation circuitry caused

the RPS to receive a reactor power signal greater than zero. (Actual

power level was 200 cpm on source range).

As expected, with a

reactor power signal greater than zero and only 2 RCPs running, the

RPS was actuated. OP/1/A/1102/10 was revised to permit three RCP

operation until RCS pressure was reduced to 1700 psi where shutdown

bypass could be actuated which blocks this trip. Group One rods were

withdrawn and the cooldown continued.

I&E is investigating the issue

and will be proposing permanent action to resolve the issue.

e. Overflow of the Unit 1 and 2 Spent Fuel Pool

At-approximately 9:15 a.m. on May 17, 1990, the licensee informed the

resident inspectors that the Spent Fuel Pool

(SFP)

had overflowed

resulting in contamination of various areas in the plant including an

area in the Unit 1 and 2 combined control room.

It was determined

that the spill resulted from performing steps out of sequence in

OP/1/A/1102/15, Filling and Draining of the Transfer Canal.

Performing the steps out of sequence resulted in shutting the

isolation valves between the SFP and the transfer canal with the SFP

pump still taking a suction from the transfer canal and discharging

into the SFP.

The details associated with this spill and review by

the NRC are contained in Inspection Report 50-269,270,287/90-16.

3. Surveillance Testing (61726)

a. Surveillance tests were reviewed by the inspectors to verify

procedural and performance adequacy.

The completed tests reviewed

were

examined for necessary test prerequisites,

instructions,

acceptance criteria, technical content, authorization to begin work,

data collection, independent verification where required, handling of

deficiencies noted,

and review of completed work.

The tests

witnessed, in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable and systems restoration was completed.

Surveillances reviewed and witnessed in whole or in part:

PT/1/A/600/22 Motor Driven Emergency Feedwater Pump Suction Check

Valve Test

IP/2/A/305/3C RPS Channel 'C' On-Line Test

PT/2/A/115/08 Rx Building Containment Isolation and Verification

b. Unit 1 ES Actuation During Nuclear Station Modification (NSM) Testing

On May 16, 1990 at 2:18 p.m., an inadvertent automatic actuation of

the Engineered Safeguards

(ES)

channels 1 through 6 occurred on

Unit 1. The unit was in a refueling outage with fuel loading in

progress.

A low pressure injection (LPI)

pump,

both Keowee hydro

units,

and several

ES valves actuated as expected.

Refueling

9

operations were immediately stopped by the Refueling Senior Reactor

Operator.

The cause of the ES actuation was a procedure deficiency.

NSM

Procedure

TN/1/A/2682/OO/AK1,

Replacement of Existing

Reactor

Building Pressure Switches was being performed.

The ES system is

designed such that the three analog channels receive signals from

various Reactor Coolant System pressure transmitters and Reactor

Building pressure transmitters.

When the measured parameter reaches

a certain setpoint it

trips the associated analog channel.

If

2-out-of-3 analog channels trip, the digital ES channel is tripped.

As per the procedure, the trips associated with replaced pressure

switches (PS)

21 and 23 were blocked to accommodate testing, which

prevented digital channels 7 and 8 from actuating.

However, the

procedure did not block the signal from the pressure transmitters

associated with digital channels 1 through 6 from actuating during

testing.

When pressure was introduced to test PS 21,

"B" analog

channel tripped.

This trip was not reset by the operators.

Later

when PS 23 was tested, "C" analog channel tripped.

This fulfilled

the required 2-out-of-3 trip logic for the ditigal channels and

actuated ES digital channels 1 through-6.

Coincident with this testing,

I&E personnel were performing ES

calibration on the other ES circuits.

Analog channel "B" was not

reset by the control room operator since the trip condition was

attributed to the ongoing calibration.

The licensee notified the resident inspectors immediately and

reported this occurrence to the NRC duty officer pursuant to the

requirement of 10 CFR 50.72(b)(2)ii.

The licensee reset the trip and

returned components to their required conditions.

The licensee is

investigating the circumstances associated with this problem.

Fuel

movement was also restarted after the investigation was completed.

4. Maintenance Activities (62703)

a. Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

procedures,

and work requests were examined to verify; proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control,

proper return of equipment to service, and that

limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 58734

Replacement of Inner Tier Connector Cables On

Keowee Unit 2 Battery

WR 571130 Perform P.M. On Main Steam Emergency Feedwater Pump

Turbine

10

WR 545731

Perform Votes Testing On Valve 1C 391

WR 545181

P.M. Motor Driven EFW Pump 'lB' Breaker

WR 57865A Visual Inspection and Test lB LPI Pump Motor

WR 51883J CT-1 Transformer 4160V Bus Maintenance

WR 27982C

Investigate BKR Feeder On 3X5F "Alternate Feeder For

1XSF"

WR 64789C Repack 1LP22

WR 50868J Repairs to 1C-391

Additionally, various portions of the activities listed in paragraph 7 of

this report were periodically observed by the inspectors.

b. Near-Miss Accident Involving Work In Energized Switchgear

On May 8, 1990, at approximately 10:30 a.m. a near-miss accident

occurred during preventive maintenance work on selected Motor Control

Center

(MCC)

panels.

While no injuries actually occurred the

accident had the potential for causing serious injury or death to

personnel involved.

The incident, which involved maintenance on the

shutdown unit, resulted in conditions which could have had adverse

effects on the operations of Unit 3 which was operating at 100

percent power.

A safety investigation was performed by the

licensee's safety group.

Two Instrument and Electrical

(I&E)

specialists were assigned to perform work involving torquing of

electrical connections inside the cabinet for 208V MCC 1XSF located

in the Safe Shutdown Facility (SSF).

208V MCC

1XSF is normally

powered from 600V MCC 1XSF but contains a Kirk Key interlock feature

to allow it to be fed from 208V MCC 3XSF.

600V MCC 1XSF had been

deenergized with both its supplies (600V Load Center OXSF and 600V

Load Center 1X8) tagged out. Apparently, due to some communications

problems between the I&E specialists and the Unit 1 Operations

Supervisor, the specialists did not realize the line side of the

Kirk Key enclosure on 1XSF was being supplied with 208 volts from

3XSF.

Although the specialist did check for voltage present on the

bus prior to work he didn't detect any, apparently, because he did

not make good contact with the test leads.

The cabinet involved is

very small and confined.

Protective gloves were being worn during

the work in accordance with the procedure. At the conclusion of the

work his screwdriver touched the Kirk Key housing and caused an

electrical arc.

This.caused the 100 amp breaker between 600V MCC

3XSF and 208V MCC 3XSF to trip, deenergizing 208V MCC 3XSF and 208V

MCC 3XSF-1. This deenergized several Unit 3 valves:

3HP-3,4

Letdown Cooler Outlet Valves

SSF-3HP-20

Reactor Coolant Pump Seal Return Isolation Valve

SSF-3RC-5,6

Pressurizer Water and Steam Space Isolation

Valves

SSF-3SF-97

SSF Reactor Coolant Makeup (RCMU) Pump Supply

Valve

SSF-3HP-428

SSF RCMU Pump Return and Letdown Valve

11

Indications of the valves being deenergized were received in the

Unit 3 Control Room and personnel in the SSF Control Room called the

Unit 3 Control Room and informed them of alarms received. No valves

shifted position.

The loss of power to the valves did not result in

any immediate operational concerns or transients since either the

valves were already in the required safety position or another valve,

operable from the control

room,

was available in the flowpath

involved.

The proposed Limiting Conditions for Operation (LCO)

Action Statements of TS 3.18 (Standby Shutdown Facility) and TS 3.6

(Reactor Building) for containment isolation valves out of service

were both entered. Approximately 15 minutes after the loss of power

to the 3XSF panels they were reenergized by shutting the tripped

breaker.

Security was initially informed to take the measures

required if the SSF is degraded. Due to an apparent misunderstanding

by some of the security personnel involved, no security measures were

taken.

The licensee's safety investigation concluded that the I&E personnel

were complying with their procedures but failed to verify all

alternate power sources deenergized despite review of an electrical

diagram.

Additionally,

poor communications

between

the I&E

specialists and the Unit 1 Operations Shift Supervisor along with a

personnel error while checking for voltage prior to work, resulted in

personnel working on energized gear without realizing it

was

energized.

The inspectors also noted that the 100 amp breaker between 600V MCC

3XSF and 208V

MCC 3XSF tripped on the fault prior to the 50 amp

breaker between 208V MCC's 3XSF and 1XSF.

This is under

investigation by the licensee.

C. Activities Being Performed on Wrong Unit

On May 10, 1990, the licensee informed the inspectors that a valve on

Unit 2 had been inadvertently cut out of an operating system. This

mistake did not result in the loss of any safety-related function.

On May 9, two mechanical technicians were directed to cut out

1LWD498,

a drain valve on a Unit 1 Low Pressure Injection pump,

in

room 62 of the Auxiliary Building. This valve is in a portion of the

system that is isolated except during draining operations. Instead,

the technician cut out valve 2LWD498.

Unit 1 and Unit 2 components

are located in room 62 and are adequately labeled.

The technicians

were experienced and qualified to perform this function.

The work

which was to be performed was documented on work request (WR) 541261

which also contains a sign-off and a verification sign-off to assure

the craft conducting the WR are performing the desired work on the

correct component. The area was well lighted and no reasons could be

identified, other than personnel error, for this occurrence.

The

mistake was made late in the shift on May 9 and was recognized by the

technicians on May 10 and reported to their supervision.

The valve

was immediately re-welded into the system, as required.

12

A second occurrence of work being performed on the wrong unit

occurred on May 17,

1990.

Two I&E Technicians were assigned to

replace a solenoid valve in the operating system to 1PR4. This valve

was to be replaced in accordance with WR 546111.

This valve is

normally shut during operation with power removed so there was no

affect on unit operation. The valve is located in the Unit 1 purge

room adjacent to the combined Unit 1 and 2 purge room, which was

poorly lighted.

Working with a flashlight as the source of light,

the technicians removed the solenoid valve.

Upon exiting the area,

they noted that the valve was labeled as a Unit 2 valve and not

Unit 1. Their immediate action was to reinstall the valve, to leave

the electrical splices exposed for QA verification, and to notify

their supervision.

The work request for this activity also included

sign-offs for verification that work was being performed on the

correct component.

Oconee Nuclear Station Directive 2.2.2,

Independent Verification

dated 1/24/90, defines how this process is to be performed to assure

that activities are conducted to reduce human errors.

TS 6.4.1

requires the licensee to have adequate procedures and specifies that

these procedures will be adhered to.

The failure to adhere to

SD 2.2.2 is a violation of TS 6.4.1 and is identified as violation

50-269,270,287/90-12-02.

These examples of failure to follow

procedures are another example of the violation identified in

Inspection Report 50-269,270,287/90-16 and will not be cited

separately.

d.

Grounding Strap Inadvertently Left On 1B2 RCP Switchgear

On May 16, 1990, at 5:46 p.m., when control room (CR) operators were

attempting to run a test on the 1B2

RCP motor with the pump

uncoupled, an electrical flash occurred in the 1B2 Reactor Coolant

Pump (RCP) motor switchgear (designated 1TB) followed by smoke coming

out of the switchgear compartment. Additionally, the rear panel had

blown clear of the compartment.

The smoke cleared immediately and

there was no indication of any fire.

At the time a non-licensed

operator in the area of the breaker saw some smoke coming out of the

corpartment and notified the CR.

When the CR operator attempted to

start the 1B2 RCP motor he received indications that the breaker had

not closed and immediately opened the incoming supply breakers for

the 6.9 KV 1 TB switchgear.

The licensee's investigation revealed that this incident occurred as

a result of a personnel error. Due to the error the grounding straps

were inadvertently left connected to the load side of the 6.9 KV

breaker supply to the 1B2 RCP motor.

Grounding straps had been

installed earlier in the outage to protect equipment and personnel in

case of inadvertent closing of the breaker. When the operator tried

to close the breakers,

current was shorted to ground. through the

straps.

The breaker opened on an overcurrent condition.

The test

was run successfully at a later date.

A high-potential test was

performed on the 1B2 RCP motor cables and gas pressure in the cable

13

penetration was checked.

No damage to the pump motor or cables was

identified. Minimal damage to the breaker occurred.

The CX transformer, which serves as a backup power supply to the

auxiliary loads of the Keowee hydro units, was also locked out by

actuation of its differential current relay. As a result, the plant

entered a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO in accordance with TS 3.7.2.a.3. The licensee

is continuing their investigation to determine why this occurred.

The transformer was declared operable after a ratio test was

performed and the LCO was exited.

The primary source of auxiliary

power to the Keowee unit transformers lX and 2X were operable at all

times during this event.

The inspector reviewed this event. This event was due in part to the

lack of a formal mechanism for controlling the installation and

removal of grounding straps on the non-safety 6.9 KV breakers. This

is considered by the licensee to be within the skills of the craft.

The licensee is evaluating this process- as part of their

investigation of this incident.

5. Seismic Monitoring Instrumentation

During this report period the inspectors reviewed the installation and

testing of the five peak accelerometer recorders in the Unit 1 Reactor

Building (RB).

Deviation 50-269/86-20-02:

Discrepancies Between the FSAR

and Installed Seismic Instrumentation addressed an earlier situation in

which the five peak recording accelerometers listed in Section 3.7.4.1 of

the FSAR were not operable.

This item was closed in Inspection Report

50-269,270,287/89-22 after a Nuclear Station Modification and several

Exempt Changes were utilized to replace the old degraded detectors with 2G

Peak Accelerometer Recorder model PRA-400. These detectors are made by

Engdahl Enterprises and are rated for the temperature and other conditions

present in the RB.

These are self contained devices requiring no external

power.

Essentially each device consists of 3 metal plates which are

etched with a scribe upon seismic activity.

On a tour of the RB the

inspectors examined each of the five recorder locations.

The detectors

had been removed for calibration. The following observations were made;

-

Three of the recorders are mounted on components which experience

high temperatures during operation and thus are attached to thermal

mounts specifically designed for this purpose. The thermal mount for

the recorder attached to a pressurizer. support was loose and its

attachment blocks were broken.

Subsequent discussion with the

Instrument & Electrical (I&E)

technicians who removed the detector

for calibration confirmed that little useful information would have

been attainable from this instrument.

-

All of the recorder mounts with the exception of the one mounted on a

line hanger are aligned in a North-South location (the latter is

aligned East-West due to interference).

While the manufacturer's

data sheet indicates that the recorder should be mounted within 1

14

degree of North, the licensee's- installation procedures did not call

for such precision.

The inspectors reviewed the safety evaluation

addressing the alignment steps of the procedure and discussed this

issue with the responsible onsite engineer.

He stated that Design

Engineering had contacted the manufacturer (Engdahl) who indicated it

was not necessary to align the detectors within 1 degree North for

them to operate properly.

The inspectors discussed the calibration procedure and walked through

several steps of the procedure (IP/1/B/125/2A:

2G Peak Recording

Accelerometer Calibration) with several I&E technicians who perform the

calibrations.

The equipment required to interpret the plate indications,

was readily available and operable. The technicians were knowledgeable of

the monitors and how to interpret the indications. The plates, which had

been removed for calibration, were examined.

Several of the plates had

indications of motion,

some as high as 2G.

The technicians and the

engineer involved indicated that these had been caused by mounting the

recorders in areas of high vibration.

These indications could mask the

desired information in the case of an actual earthquake.

DE is currently

assessing this issue and considering mounting the recorders in more rigid

locations such as the RB floor or walls during the next outage.

Since

Section 3.7.4.1 of the FSAR specifically lists the locations of the

recorders a change will be required if

the detectors are moved in the

future.

The licensee intends to remount detectors in their present

locations before the end of the current outage.

The licensee performed

an operability evaluation on the recorders in their current- locations and

determined them to be operable.

No violations or deviations were identified.

6. Notification Of Unusual Event Due To Chemical Spill

On April 26,

1990, at 1:10 p.m. an Unusual Event was declared due to a 16

gallon spill of hazardous chemicals in a pipeyard. The pipeyard is inside

the protected area but is not in an enclosed area.

The source of the

spill was a 55 gallon drum which had rusted through.

The spill was

stopped by uprighting the drum. The chemical involved was "M and S Safety

Solvent" which contains Tetrachlorethylene and Methylene chloride. The 16

gallons were spilled into soil under the drum. No personnel were injured

or exposed to the chemical.

RP/O/B/1000/01:

Emergency Classification requires that an Unusual Event

be declared if a spill of a chemical equal to or greater than ten times

the Reportable Quantity (RQ)

per RP/O/B/1000/17:

Hazardous Substance

Release, occurs.

Enclosure 4.2 of RP/O/B/1000/17 states that a spill of

greater than

.33 gallons of M&S Safety Solvent (30 percent

Tetrachloroethylene, 30 percent Methylene Chloride) is reportable. Local

agencies, South Carolina's Department of Health and Environmental Controls

(DHEC), and the National Response Center were all informed as required. A

report to the NRC in accordance with 10 CFR 50.72(a)(3) was made.

The inspector toured the pipeyard and examined the remaining barrels of

chemicals.

Several corroded barrels containing chemicals were noted.

15

This was brought to the licensee's attention.

Additional corrective

actions are being.considered by the licensee.

No violations or deviations were identified.

7.

Unit 1 Refueling Outage (71707)

Unit 1 commenced the end of cycle 12 refueling outage on April 26.

The

outage is presently scheduled for 41 days.

Major maintenance activities

during this period have been:

'B' Low Pressure (LP) Turbine Inspection

Refurbish 'B' LP turbine intercept valves (6)

Hi-Pot Test all 4160V breakers

PM all 600V breakers

Eddy Current Test Steam Generators

ISI inspections on Reactor Vessel Closure

Head Weld and Head to Flange Weld

Major PM on 1B2 RCP Motor

Approximately 400 Valve and valve actuator overhauls

Local Leak Rate Testing and Integrated Leak Rate Testing

preparations

The inspectors have monitored various activities including the initial

shutdown and subsequent cooldown/draindown.

The schedule at present

indicates the unit should be returned to operation about June 6, 1990.

8.

Inspection of Open Items (92700)(90712)(92701)

The following open items were reviewed using licensee reports, inspection,

record review, and discussions with licensee personnel, as appropriate:

a.

(Closed)

P2189-18:

Limitorque Corporation Reported Failures of

Melamine Torque Switches on SMB-000 and SMB-00 Operators.

In

November of 1988, the Limitorque Corporation identified a common mode

failure of melamine torque switches installed in SMB-000 and SMB-00

actuators.

This information was transmitted to Duke Power Company in

correspondence dated November 3, 1989.

Problem Investigation Report

4-088-0250, was issued to determine if the problem existed at Oconee

and the corrective actions to be taken if the problem was identified.

The licensee identified 34 valves as needing inspection.

Of this

group 22 were identified as safety-related and 12 non safety-related.

Of these operators,

27

have been repaired or replaced,

16

safety-related and 11 non safety-related.

There are 3 left to be

corrected on Unit 1, all safety-related, which are scheduled to be

corrected during the outage presently in progress. The remaining 4

are on Unit 2 and are scheduled to be corrected in upcoming outage.

Based on this action, this item is closed.

b.

(Closed)

P2190-01:

PT 21 Associated With Findings and Potential

Concerns Based on ECOTECH/RAM-Q Source Verification and Performance

16

Based Audit of the Rockbestos Company. This item was discussed with

the Design Engineering (DE)

section.

DE stated no safety-related

applications of this material has been used at Oconee. In addition,

DE informed the inspector that Rockbestos had recently been audited

by the

NRC

and

no unsatisfactory findings were identified.

Rockbestos Co., is providing written documentation to Duke that the

wire which was the subject of this concern, is satisfactory to be

used in safety-related applications. Based on this information, this

item is closed.

9. Exit Interview (30703)

The inspection scope and findings were summarized on May 21,

1990, with

those persons indicated in paragraph 1 above.

The inspectors described

the areas inspected and discussed in detail the inspection findings. The

licensee did not identify as proprietary any of the material provided to

or reviewed by the inspectors during this inspection.

Item Number

Description and Reference

VIO 269,270,287/90-12-01

Failure

to

Incorporate Design

Basis

Information Into Electrical Relay Procedures

(paragraph 2.c)

VIO 269,270,287/90-12-02

Failure to Follow Procedures Resulting in

Incorrect Component Maintenance

0II