ML15224A658

From kanterella
Jump to navigation Jump to search
Insp Repts 50-269/90-08,50-270/90-08 & 50-287/90-08 on 900218-0324.Violations Noted.Major Areas Inspected: Operations,Surveillance Testing,Maint Activities,Review of Lpdr & Insp of Open Items
ML15224A658
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/10/1990
From: Binoy Desai, Shymlock M, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A656 List:
References
50-269-90-08, 50-269-90-8, 50-270-90-08, 50-270-90-8, 50-287-90-08, 50-287-90-8, NUDOCS 9004250083
Download: ML15224A658 (13)


See also: IR 05000269/1990008

Text

t REQg

UNITED STATES

So

NUCLEAR REGULATORY COMMISSION

REGION II

0

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos:

50-269/90-08, 50-270/90-08, 50-287/90-08

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.:

DPR-38, DPR-47, DPR-55

Facility Name: Oconee Nuclear Station Units 1, 2, and 3

Inspection Conducted:

February 18 - March 24, 1990

Inspectors:

r4 aes

/

/0 ?a

P. H. Skinner,Senior Resident Inspector

Date Signed

L. D. Wdft, Resident Inspector

Date Signed

B. B. De.di, Resident Inspector

Date Signed

Approved by:

____A0

. B. Shymlo~

Section Ch

fDate

Signed

Division of eactor Projec s

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in the

areas of operations, surveillance testing, maintenance activities,

degraded grid voltage issues, review of local public document room

and inspection of open items.

Results: A violation associated with failure to take adequate corrective

action associated with Reactor Building Cooling Unit surveillance was

identified (paragraph 3.b).

A strength was noted in the licensees continuing indepth engineering

review associated with Design Basis Documentation (paragraph 5).

900425003 90411

FDR

ADCK:'.: 0500026 9

0

.

PDC

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • B. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

  • T. Curtis, Compliance Manager
  • J.

Davis, Technical Services Superintendent

D. Deatherage, Operations Support Manager

B. Dolan, Design Engineering Manager, Oconee Site Office

W. Foster, Maintenance Superintendent

D. Hubbard, Performance Engineer

  • E. LeGette, Compliance Engineer

H. Lowery, Chairman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

D. Powell, Station Services Superintendent

  • G. Rothenberger, Integrated Scheduling Superintendent

R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P.

Skinner

  • L. Wert

B. Desai

  • Attended exit interview.

2. Plant Operations (71707)(71710)

a. The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records, temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and on night shifts, during

weekdays and on weekends. Some inspections were made during shift

change in order to evaluate shift turnover performance. Actions

observed were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

2

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1, 2 and 3 Spent Fuel Pool Rooms

Keowee Hydro Station

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and-radiation control practices were observed.

Unit 1 operated at 100% power for the entire reporting period.

Unit 2 operated at 100% power until March 5 when Reactor Coolant Pump

2B2 experienced a low oil pot level on the motor. This resulted in

a power reduction and the pump being secured. An oil leak was

identified on a pipe flange. The licensee overtorqued the flange as

justified by an engineering evaluation, to correct the leakage

problem. Oil was added to the motor, the pump restarted and the unit

returned to 100% power on March 6. The unit continued to operate at

that condition for the remainder of this reporting period.

Unit 3 operated at 100% power until the reactor tripped due to high

Reactor Coolant System pressure on March 7 (See paragraph 2.b).

The

unit was returned to power on March 8 and remained at that level

through the remainder of the report period.

b. Unit 3 Reactor Trip

At approximately 2:06 p.m. on March 7, 1990, Unit 3 tripped from 100

percent power. The automatic trip was caused by high Reactor Coolant

System (RCS) pressure. The high RCS pressure occurred due to a

partial loss of main feedwater flow to the 'A' Once Through Steam

Generator (OTSG).

All safety systems performed as expected following

the trip.

Because of periodic spiking on Nuclear Instrument (NI) number 9, the

normal input to the Integrated Control System (ICS), NI 5 (an

available alternate NI channel) was being used to provide nuclear

power level input to the ICS.

NI 5 also provides a signal to the

RPS.

Instrument and Electrical (I&E) technicians were performing

routine online RPS testing. Part of this required manipulation of

the NI 5 signal.

In preparation for this testing, the control room

3

operators had placed certain portions of the ICS into the 'hand' mode

so that the testing would not affect the ICS.

(With these ICS

stations in 'hand', the ICS does not process the incoming signals and

will not automatically control the plant.) The operators were

manually controlling plant parameters.

During the testing, NI 5 continued to provide a signal to the main

feedwater block valve interlock circuitry. At low power conditions

(less than 25 percent power) if the startup feedwater control valves

are open, this interlock functions to shut the main feedwater block

valve. The limit switch assembly on the startup valves associated

with this interlock feature on the 'A' OTSG had previously

malfunctioned and the main feedwater block valve was receiving an

erroneous signal indicating that the startup valve was open. As a

result, when the I&E technicians decreased the NI signal to less than

25 percent, the main feedwater block valve went shut. Operators were

unable to increase the feedwater flow rapidly enough to prevent an

increase in RCS pressure and the trip occurred.

Following the trip the operators reduced turbine header pres.sure to

about 975 psi to reseat one main steam relief valve. The valves are

required to reseat within a tolerance of 93 percent of their lifting

setpoint. Post trip review verified that this valve had reseated

within the acceptance band. There were also indications of

overheating at the discharge of the condensate booster pumps (CBP)

after the trip. This had been noted during a previous Unit 3 trip.

Apparently one of the CBPs has a slightly lower discharge pressure

causing its discharge check valves to remain shut limiting

recirculation flow through the pump. The minimum recirculation

valves open on a flow signal from the discharge header of all three

pumps. It is believed that the discharge flow remained above the

recirculation valve open setpoint. Operators have been informed of

this potential problem and available corrective actions.

Also,

during the post trip review process, one reactor trip breaker was

identified as exceeding the maximum opening time interval specified

by the post trip review procedure by 28 milliseconds and was replaced

prior to startup.

The broken limit switch assembly on the 3A startup control valve was

repaired and its correct function verified. While the limit switch

had been documented as broken in December 1989, it was widely

believed that the only function of the switch was for position

indicating lights.

Its role in the main feedwater block valve

interlock had been previously overlooked and maintenance personnel

had been directed to delay its repair. The unit was returned to

criticality at 9:40 p.m. on March 7 and reached 100 percent power at

11:13 a.m. on March 8, 1990.

No violations or deviations were identified.

4

3. Surveillance Testing (61726)

a. Surveillance tests were reviewed by the inspectors to verify

procedural and performance adequacy. The completed tests reviewed

were examined for necessary test prerequisites, instructions,

acceptance criteria, technical content, authorization to begin work,

data collection, independent verification where required, handling of

deficiencies noted, and review of completed work. The tests

witnessed, in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable and systems restoration was completed.

Surveillances reviewed and witnessed in whole or in part:

PT/1/A/0257/O1

Performance Testing of Unit 1/2 Low Pressure

Service Water Pumps

PT/O/A/0170/05

Penetration Room Ventilation System Monthly

Performance Test dated 5/6/88 (Unit 3)

PT/1/A/0600/13A Performance Testing of the '2B' Motor Driven

Emergency Feedwater Pump dated 3/2/90

PT/3/A/0204/07

Reactor Building Spray Performance Test

dated 9/13/88

PT/2/A/0400/07

SSF RC Makeup Pump Performance Test

dated 12/16/88

b. Thermal Performance of Unit 3 Reactor Building Cooling Units (RBCU)

Degraded Due To Fouling (61726)

On February 19, 1990, as a result of observed Reactor Building (RB)

Dome and RBCU inlet temperature increases, an entry was made into the

Unit 3 RB to conduct an investigation. Extensive boron deposits were

observed on the surfaces of the Auxiliary Cooling Units. Thermal

Performance testing was promptly conducted on the 'A' and 'C' RBCUs

on February 20, 1990. The results indicated that the 'A' cooler was

operating at about 26% capacity and the 'C' cooler at 23%. The 'B'

cooler had not been operated since unit startup in late December

1989. Available information measured during startup indicated that

it would perform at approximately 71% capacity. Design Engineering

(DE) determined that a combined performance of 82% capacity (two

worst RBCUs) was required. At 2:50 p.m. on February 20, the 'C'

cooler was declared inoperable and a 7 day LCO was entered in

accordance with TS 3.3.5. The auxiliary coolers and then the 'C'

RBCU were cleaned. The licensee has concluded that it is possible

that the 'A' and 'C' cooler combination had been inoperable for some

time in excess of 7 days before the testing and will be submitting a

voluntary 10 CFR 50.73 report.

5

Degradation in the thermal performance of the RBCUs (particularly

Unit 3) due to fouling has been a continuing problem. As early as

1986, Oconee has been investigating heat exchanger fouling problems.

Although some indications of fouled heat exchangers had been noted

during 1985/1986, it was not until early 1987 that thermal

performance testing and calculation methodology improvements

identified that some heat exchangers were fouled beyond acceptable

design values. LER 269/87-04 addressed this issue.

Operability

evaluations later revealed that all 3 Oconee units had degraded

coolers and operation at 100% power could not be supported. The NRC

issued a confirmatory order on April 10, 1987 which limited Unit 1

and Unit 2 operation with degraded cooler capability. (Unit 3 was in

an outage and cleaned the coolers prior to startup.) Meetings were

held with Region II and NRR personnel to discuss cooler fouling in

mid 1987.

In August 1988 testing indicated that the Unit 3 RBCUs were again

fouled. The licensee's operability evaluation indicated that the

coolers had degraded over operating cycle 10 to a point at which

operation at 100% power could not be supported. Testing indicated

that while some degradation had occurred on Units 1 and 2, they were

still fully operable. At this time temperature trending was being

utilized as a rough indicator of degradation with approximately

monthly testing. Based on projections utilizing conservative fouling

rates, testing frequency was shifted to preclude inoperability. Also

there was still a question if air or water side fouling was the

primary problem. Calculational and operability evaluation

methodology was actively being improved. In October 1988 an

Enforcement Conference was held concerning the Unit 3 issue. The

meeting concluded that all information indicated that the licensee's

analysis was conservative. It was acknowledged that difficulties

were present in both measurement of heat transfer in air-to-water

heat exchangers and in correlating the testing conditions to LOCA

conditions. The licensee's commitment for increased frequency of

testing to assure component operability and to perform additional

data collection was also acknowledged.

The licensee continued thermal performance testing and analysis on

the RBCUs on all three units.

As of December 1988, testing was being

performed quarterly and, in addition, at intervals determined by

previous operability assessments and conservative fouling

projections.

Improvements in testing and calculational methodology

were still being identified. In January 1989, the Unit 3 coolers

again became fouled (see LER 287/89-01). A unit shutdown and

subsequent cooler cleaning were necessary. This was attributed to

lack of information and fouling unpredictability. Also in January

1989, a task force of licensee general office and Oconee site

6

representatives was formed to address and resolve the overall RBCU

fouling issue. The resident inspectors have been closely monitoring

these efforts, by attending meetings and detailed reviews of

calculational and testing results. The licensee has expended

extensive resources in efforts to:

-

refine the calculational methodology involved

-

develop improved cleaning methods for the fouled coolers

-

determine whether air side or water side fouling is the primary

problem

-

install on-line monitoring capability, at least on Unit 3 which

has been identified as the unit most susceptible to fouling

-

determine the effect of operation of the Auxiliary cooling units

on the RBCU's

-

develop some "rough" onsite analysis capability, possibly with

data acquisition capabilities.

In February 1989, Unit 3 had remote flow and humidity monitoring

instruments installed on RB cooler ductwork. By this time Unit 3 had

been observed to undergo fouling behavior which often did not

parallel the fouling of Units 1 and 2. The reason for this

difference has not been determined. A total of 14 thermal

performance tests were conducted on Unit 3 in 1989. In April the

remote monitoring instruments for measuring relative humidity failed,

apparently due to the harsh conditions in the RB. Replacement

instrumentation was recently received and prepared for installation

but has not been installed.

Since this fouling issue was initially identified, the NRC's primary

concern and emphasis has been that the licensee closely monitor

performance to ensure operability. The licensee, through several

LER's and during meetings with the NRC, repeatedly committed to

testing as necessary to prevent operation of a unit with coolers

degraded beyond required performance levels. Projections have been

made based on conservative fouling rates and extensive resources have

remained dedicated to testing of the coolers.

As an interim measure, while additional data was being collected, two

parameters available to Control Room operators were being monitored.

These were RBCU air inlet temperature and the difference between RBCU

inlet temperature and condenser circulating water inlet temperature.

These parameters had specific limits placed on them above which

additional testing would be initiated. As additional data was

gathered and improvements were made in the testing process, these

limits were no longer used. Thermal performance testing was

completed quarterly and at intervals based on conservative fouling

rates determined by previous testing. Performance engineers, on a

7

daily basis, reviewed computer printouts of specific temperature

data.

DE had established a limit of 116 degrees F on RBCU air inlet

temperature based on a related concern. On February 20, 1990,

Performance personnel noted that the RBCU air inlet temperature was

approaching this limit and initiated the RB entry. The coolers,

however, had already degraded to inoperable levels.

Investigation by

the licensee and the resident inspectors has resulted in the

following observations:

-

The coolers had been tested in November 1989, just prior to

shutdown for a refueling outage. Based on the results, DE

projected the coolers would remain operable through at least

November of 1990. As a conservative measure, cleaning of all

the RBCUs was conducted during the outage.

Following startup

the coolers were tested again on January 9, 1990. The results

of this test indicated that the coolers had undergone

significant degradation despite their previous high capacities

and the recent cleaning. The results were attributed to

relatively low RB temperatures during the testing and the fact

that the RBCU fusible dropout plates had been reinstall-ed. It

was felt that both of these factors may have significantly

affected the testing data. A projection of operability based on

this test was not transmitted to onsite personnel.

-

No reason for the increased fouling has been identified. The

source of the boron has not been identified. RCS leakage rates

and RB sump rates have not indicated any excessive RCS leakage.

While Unit 3 underwent a trip in early January 1990, no

correlation between the increased fouling rate and the trip has

been noted.

-

While both Performance and Operations staff personnel have been

aware of steadily increasing Unit 3 RBCU inlet and RB dome

temperatures, this data along with other information which

should have alerted personnel to a potential excessive fouling

problem apparently was not adequately trended or monitored.

-

Since the susceptibility of Unit 3's RBCUs to foul has been

known for some time, a formal dedicated effort should have been

made to track all pertinent information. Apparently only an

RBCU inlet temperature limit of 116 degrees F and informal

monitoring by Performance Engineers were being utilized to

follow the RBCU concerns. Unit 3 temperatures steadily

increased for the six weeks following startup which was an

unexpected trend and, in retrospect, should have keyed personnel

to investigate closer.

The inspectors concluded that the licensees corrective actions to

prevent recurrence of fouling beyond operability limits were

inadequate. The program established to insure operability was not

sufficient in that it was not formally defined and controlled.

Additionally, the inspectors noted that the attention given to the

.program by management was less than expected since the RBCU's were

8

inoperable at the time of significant management involvement. This

is identified as Violation 50-269,270,287/90-08-01:

Inadequate

Corrective Actions to Prevent Reactor Building Cooling Unit

Inoperability Due to Fouling.

4. Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

the skill of the trade. Activities, procedures, and work requests were

examined to verify:

proper authorization to begin work, provisions for

fire, cleanliness, and exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 058879

Annual Inspection and Maintenance on Air Circuit

Breaker (ACB) Number 2

WR 55622B

Preventive Maintenance on Valve 3 PR-15

WR 55623B

Preventive Maintenance on Valve 3 PR-19

MP/0/A/2001/2

Inspection and Maintenance of Keowee ACB's and

Associated Disconnects and Bus

No violations or deviations were identified.

5. Degraded Grid Voltage Issue Identified During Switchyard Design Basis

Documentation Analysis Program (71707)

On March 1, 1990, DE identified a potential problem concerning Oconee's

offsite power supply and a degraded voltage situation. This issue was

identified during the licensee's Design Basis Documentation effort on the

230 KV switchyard system.

Normally one of the available sources of power to the Oconee Engineered

Safeguards Systems is the 230 KV transmission system through each unit's

startup transformer. This circuit is designed to be available within a

few seconds following a loss of coolant accident (LOCA). The onsite

backup source of auxiliary power (the 2 unit Keowee Hydrostation) is

available to provide power if the offsite source were to fail.

The Keowee

units can supply power to the engineered safeguards switchyard buses

through either the 230 KV switchyard isolated yellow bus, the unit's

startup transformer and its associated breakers (overhead path) or a

dedicated 13.8 KV underground circuit (underground path).

In the event

that the external transmission circuit is lost and a LOCA occurs

simultaneously, the switchyard isolation system will automatically isolate

(the under voltage setpoint is 70 percent of the 230 KV) the 230 KV safety

related yellow bus to permit one of the Keowee hydrostation units to

utilize the overhead path to provide power to the safeguards buses as

required. Additionally, the underground power path automatically becomes

9

energized as the other hydro unit is started. In summary, there are

essentially three sources of power normally available to supply power to

the engineered safeguards buses; the 230 KV transmission system via each

unit's startup transformer, the underground circuit from one Keowee hydro

unit, and the remaining Keowee unit via the switchyard yellow bus and the

startup transformer (overhead path).

The current concern is a scenario in which the external grid undergoes a

degradation which causes the voltage available at the startup transformer

to be low enough to prevent the startup transformer breakers (the "E"

breakers) from closing yet still above the Switchyard Isolation circuitry

setpoint. An undervoltage feature exists on the "E" breakers which is

intended to ensure that the engineered safeguards loads are not energized

by a source of voltage which is too low. The setpoint of this feature

corresponds to approximately 219 KV on the switchyard side of the startup

transformer when it is loaded. DE identified that if the switchyard

voltage degraded to a value of approximately 222 KV, in certain scenarios

the resultant effect of loading the transformer could result in the

E breakers not closing due to low voltage. (The plant is protected from

the degraded grid voltage in these situations since the undervoltage

feature on the E breakers will function).

But this means that the 230 KV

transmission system via the unit's startup transformer is not available at

a grid voltage of 222 KV or lower.

Technical Specification (TS) 3.7.2(i)2, states that if a startup

transformer becomes inoperable for unplanned reasons then one of the

Oconee units shall be in cold shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. It is important

to note that in the above situation, the startup transformer is inoperable

as a source from the 230 KV switchyard but it is not considered by the

licensee to be inoperable as part of the overhead path from the Keowee

hydro units. The justification for this interpretation is if the grid

degrades to the switchyard isolation circuitry setpoint, the Keowee unit

will then be able to provide power.

(TS 3.7.1(b)2 requires this overhead

path to be normally operable whenever a unit is above 200 degrees F.)

TS 3.7.2.(i)(1) requires that if a startup transformer is inoperable for

tests or maintenance, the underground feeder path must be verified

operable within one hour of the loss and every eight hours thereafter for

periods not exceeding 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

No verification of the underground path

is required by TS if the transformer is inoperable for unplanned reasons.

After continued investigation and further analysis, on March 8, 1990, it

was determined that corrective actions would be necessary. The licensee

promptly initiated specific monitoring procedures and issued guidance to

operators as interim compensatory actions concerning this issue. Guidance

was provided to the control room operators on this issue in the form of a

March 8, 1990, letter which states;

-

If voltage in the 230 KV switchyard is less that 222 KV, the startup

transformer must be considered inoperable, the appropriate limiting

condition for operation entered, and the underground path verified

operable within one hour.

10

-

A restricted change to PT/1/A/0600/01: Periodic Instrument

Surveillance has been implemented to require monitoring switchyard

voltage every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> until further analysis or modifications are

completed.

The inspectors reviewed this guidance, the required actions and the

applicable TS requirements. It appears that the licensee's immediate

actions are conservative and adequate.

The licensee has determined that on several occasions during the past 8-10

years,' Oconee has seen voltages in the 230 KV switchyard degrade to less

than 222 KV. These situations were all of short duration and the

underground power path was not inoperable at those times.

The licensee

currently intends to submit information to NRR supplementing earlier

(1979) documentation discussing Oconee's degraded grid voltage protection.

The inspectors will continue to follow the licensee's actions and are

presently discussing this issue and its implications with the licensee.

No violations or deviations were identified.

6. Public Document Room Review

The inspectors visited the Public Document Room, (PDR) for Oconee Nuclear

Station located in the Oconee County Library in Walhalla, South Carolina.

The inspectors met with the PDR librarian and discussed recent utilization

of the document room, any potential problems with maintenance of the PDR,

and current status of the PDR. The inspectors reviewed the types of

material maintained in the facility. Using the PDR indexing system,

several samples of information were located and reviewed. A random check

of numerous documents was conducted. The facility appears to be

maintained in a very organized and efficient manner in accordance with PDR

directives.

It was noted that some material dated prior to 1986 has been

relocated to the basement of the library due to spacing limitations. The

librarian stated that this material is organized and accessible if an

individual requested any of the material.

The PDR custodian appeared very

knowledgeable of her duties and highly capable of maintaining the PDR.

7.

Inspection of Open Items (92700)(90712)(92701)

The following open items were reviewed using licensee reports, inspection,

record review, and discussions with licensee personnel, as appropriate:

a.

(Closed) Violation 50-269,270,287/89-17-01: Electrical Distribution

TS Violations Due To Inadequate Procedures. The response to this

violation was contained in correspondence dated August 16, 1989.

This response included a commitment to establish a specific procedure

to address emergency power system removal and restoration by

December 1, 1989. The Operations group developed OP/O/A/1107/11,

Removal and Restoration of Auxiliary Electrical Systems, which was

reviewed by the Design Engineering electrical group, and issued

November 21, 1989. It was used during the most recent outage on

Unit 3. Based on this review, this item is closed.

11

b.

(Closed) Violation 50-287/89-36-04:

Inadequate Control of Polar

Crane Operation During Unit 3 Refueling. This violation was

addressed by the licensee in correspondence dated February 7, 1990,

and is also the subject of LER 287/89-06 dated December 27, 1989.

The corrective actions for this violation are also contained as

corrective actions in the LER. To eliminate duplicate review

efforts, the violation is being closed and licensee's actions will be

assessed during review of the LER.

c. (Closed) Inspector Followup Item 50-269,270,287/88-15-01:

Retraining

of Personnel on EPSL Operation. The licensee has conducted Emergency

Power Switching Logic (EPSL) training for the operations shift

personnel and the operations staff. The training included EPSL

logic, related LER's, the electrical TS and its interpretations, and

revised operating and performance procedures. The training was

completed on October 31, 1989.

Based on this action, this item is

closed.

d.

(Closed) Inspector Followup Item 50-269,270,287/89-05-03:

Cable

Separation Issues. This item addressed a situation of improper

routing of safety related cables. The problem was discovered during

repair work on cables following the January 3, 1989 fire in the ITA

switchgear. An operability evaluation had concluded that.the cables

in question were operable despite not being routed in accordance with

FSAR criteria. The licensee committed to rerouting these particular

cables to correct the problem and also to conduct a detailed survey

of safety related cables selected at random to ensure that the above

identified cables are an isolated case. This survey was completed in

February 1989. Of 116 cables inspected six discrepancies were found.

All were minor problems with the exception of 2 cables utilizing the

same cable room penetration (a Unit 2 Main Feeder Bus 1 cable and a

Unit 1 Main Feeder Bus 2 cable). An operability evaluation was

completed which concluded that these 2 cables are not mutually

redundant in function and simultaneous failures will not

significantly impact any Engineered Safety or Reactor Protection

System functions. A Station Problem Report (SPR-2726) has been

initiated to reroute one of the cables.

The original cable separation issue was the subject of LER 269/89-04:

Deviation From FSAR Cable Separation Criteria Due to Design

Deficiency. This LER contains several extensive, long-term

corrective actions and will be utilized to follow the licensee's

progress on this issue.

Based on this information, this item closed.

e.

(Closed) LER 269/89-01:

Reactor Trip Due to Personnel Error. This

LER was submitted to the NRC in correspondence dated February 1,

1989. The inspectors have reviewed the corrective action taken.

Modification NSM 2804, which corrected switching discrepancies of the

Main Feedwater Block Valves, was completed on February 17, June 29,

and December 17, 1989 for Units 1, 2 and 3 respectively. Based on

this review, this item is closed.

12

f.

(Closed) LER 269/89-05:

Emergency Steam Air Ejector Inoperable Due

to Defective Procedure. This LER was submitted by licensee

correspondence dated March 27, 1989. The planned corrective action

for this report was to do a random comparison of valve checklists on

selected systems for missing valves. This comparison was completed

on January 30, 1990. Several missing valves were identified and

procedures corrected as a result. These valves were all vent and

drain valves. Based on this review, this item is closed.

g.

(Closed) LER 269/89-10, Revision 2:

Central Switchyard Was Used As

An Unacceptable Offsite Power Source As A Result Of A Management

Deficiency. This LER was submitted by correspondence dated July 10,

and revised on August 9, and August 15, 1989. The inspectors

reviewed the actions taken by the licensee. Procedure changes have

been made to the specific procedure involved. In addition, a

specific procedure (OP/0/A/1107/11, Removal and Restoration of

Auxiliary Electrical Systems) has been generated, reviewed by Design

Engineering and approved by station management to preclude recurrence

of this specific problem. Based on this review, this item is closed.

h. (Closed) LER 269/89-11, Revision 1:

Technical Specification 3.7 Was

Violated as a Result of a Defective Procedure. This LER was

submitted in correspondence dated July 28, 1989. Corrective action

included a review and revision of the defective procedure and review

of other procedures associated with Emergency Power Switching Logic

(EPSL).

In addition, new procedures and revisions to existing

procedures associated with EPSL receive a review by the Design

Engineering group. Based on this action, this item is closed.

i. (Closed) LER 270/89-07: Design Oversight Results in a Potential for

Operating in an Unanalyzed Condition During a Dropped Rod Event

Concurrent With Large Tilt and Imbalance. This was a voluntary LER

submitted on January 12, 1990. The concern of this item was the

potential for operating in an unanalyzed condition during a dropped

rod event. Upon further analysis by the Design Engineering group and

discussions with Babcock & Wilcox, a determination was made that

conservatism did exist in the TS limit and the unit had not been

operating in an unanalyzed condition as previously thought. Based on

this analysis, this item is closed.

6. Exit Interview (30703)

The inspection scope and findings were summarized on March 26, 1990, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings. The

licensee did not identify as proprietary any of the material provided to

or reviewed by the inspectors during this inspection.