Letter Sequence Approval |
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MONTHYEARML15040A7202015-03-12012 March 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15083A5592015-03-24024 March 2015 Extended Power Uprate: Response to Replacement Steam Dryer Requests for Additional Information Project stage: Other ML15033A4892015-03-27027 March 2015 NRC Staff Review of Replacement Steam Dryer Re-Benchmarking to Support Extended Power Uprate Power Ascension Project stage: Approval ML15086A3332015-03-27027 March 2015 Request for Additional Information Regarding Replacement Steam Dryer Analysis, Exelon Generation Company, Llc. Peach Bottom Atomic Power Station - Unit 2 Project stage: RAI ML15096A0082015-04-0505 April 2015 Extended Power Uprate: Response to Replacement Steam Dryer Requests for Additional Information Project stage: Other ML15084A3422015-04-0606 April 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15099A7482015-04-0909 April 2015 Power Ascension Hold at 104% of 3514 Mwt Project stage: Other ML15110A0982015-04-10010 April 2015 E-Mail Peach Bottom Unit 2 - Power Ascension Hold at 104% of 3514 Mwt Project stage: Other ML15091A1342015-04-16016 April 2015 Summary of Closed Meeting Held on March 26, 2015, with Exelon Generation Company, LLC to Discuss Steam Dryer Analysis for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Meeting ML15125A1682015-04-25025 April 2015 Power Ascension - 108% Hold Point Decision Project stage: Other ML15127A5182015-05-0505 May 2015 Draft Request for Additional Information (Tac No. MF4792) Project stage: Draft RAI ML15127A5262015-05-0505 May 2015 Draft Request for Additional Information (Attachment 2) Project stage: Draft RAI ML15110A0852015-05-12012 May 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15135A4372015-05-15015 May 2015 Approval of Steam Dryer Methodology and Resumption of EPU Power Ascension Project stage: Other ML15135A4022015-05-15015 May 2015 Extended Power Uprate: Response to Replacement Steam Dryer Request for Additional Information Project stage: Request ML15127A2082015-05-19019 May 2015 Approval of Revision to Methodology for Establishing Replacement Steam Dryer Strain Limits Project stage: Other ML15196A6372015-07-15015 July 2015 Error Identified in Letter from Exelon to NRC Re Predicted Strain Ratios Provided in Response to Request for Additional Information (RAI-11) Project stage: Response to RAI 2015-04-05
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Category:Letter
MONTHYEARIR 05000277/20240032024-11-0404 November 2024 Integrated Inspection Report 05000277/2024003 and 05000278/2024003 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification 05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 IR 05000277/20240022024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) ML24061A2642024-03-0101 March 2024 Revision of Two Procedures That Implement the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) Commissioners ML24060A1192024-02-29029 February 2024 Notification of Conduct of a Fire Protection Team Inspection 2024-09-06
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML24197A0162024-07-12012 July 2024 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC - Fleet Request - License Amendment Request to Adopt TSTF-591 ML24185A1772024-07-0303 July 2024 Request for Additional Information IR 05000277/20244012023-10-0505 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000277/2024401 and 05000278/2024401 ML23264A7992023-09-21021 September 2023 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC – Fleet Request – License Amendment Request to Adopt TSTF-580, Revision 1 ML22118A3312022-04-28028 April 2022 NRR E-mail Capture - Peach Bottom - Formal RAI for Proposed Alternative I5R-14, Revision 1 ML22041B5362022-02-10010 February 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Request for Additional Information Regarding Fleet License Amendment Request to Adopt TSTF-541 IR 05000277/20224032022-01-21021 January 2022 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000277/2022403 and 05000278/2022403 ML22020A0642022-01-13013 January 2022 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21256A1902021-09-10010 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21144A2132021-05-24024 May 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21062A0652021-03-0101 March 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative to Documentation Requirements for Pressure Retaining Bolting ML21049A2572021-02-18018 February 2021 Request for Additional Information Byron/Dresden Proposed Changes to Site Emergency Plans to Support Post-Shutdown and Permanently Defueled Conditions (EPID-2020-LLA-0240 & EPID-2020-LLA-0237) ML21035A2222021-02-0404 February 2021 Notification of Conduct of a Fire Protection Team Inspection ML21091A1782021-02-0202 February 2021 Ti 2515/194 Inspection Documentation Request ML21012A1302021-01-12012 January 2021 Request for Additional Information - TSTF-505 ML20357A0972020-12-21021 December 2020 Request for Additional Information - TSTF-505 ML20296A3342020-10-21021 October 2020 ISI Remote Inspection - Supplemental Request for Information ML20239A7982020-08-25025 August 2020 NRR E-mail Capture - Exelon Generation Company, LLC - Fleet License Amendment Request to Adopt TSTF-568, Revision 2 ML20153A7042020-06-0101 June 2020 NRR E-mail Capture - Preliminary RAI for Fleet Request to Use Alternative OMN-26 ML20135H1972020-05-14014 May 2020 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Request to Extend Safety Relief Valve Test Interval ML20070R2282020-03-10010 March 2020 Request for Additional Information - RR ML19303D1662019-10-31031 October 2019 Requests for Additional Information for the Environmental Review of the Peach Bottom Subsequent License Renewal Application - Set 2 (EPID No. L-2018-RNW-0013)- RAIs ML19232A1752019-08-20020 August 2019 Request for Additional Information - TSTF-500 Implementation LAR ML19140A2832019-05-15015 May 2019 Email - Peach Bottom Atomic Power Station, Units 2 and 3 Second Round RAI Request - Set 1 ML19140A2822019-05-15015 May 2019 027 Pb FU RAI Subsequent to Clarification Call - Cu Greater than 15 Zn Holston (Jg) ML19253D2932019-05-0707 May 2019 002 Attachment 4D Confirmation Water Chemistry Chereskin Revised (002) ML19249C7252019-05-0303 May 2019 SLRA Requests for Additional Information - Set 2 May 3, 2019 ML19108A4282019-04-10010 April 2019 RAIs SLRA Set 1_ERO(Rev 1) ML19079A0232019-03-19019 March 2019 Licensed Operator Positive Fitness-For-Duty Test ML19058A2902019-02-27027 February 2019 Request for Additional Information - High Pressure Service Water One Time TS Change ML19037A4832019-02-0606 February 2019 NRR E-mail Capture - Clarification Questions Associated with Staff Assessment of Peach Bottom Seismic Probabilistic Risk Assessment Report Dated August 28, 2018 ML19028A0062019-01-25025 January 2019 Secondary Containment LAR Requests for Additional Information ML19017A0472019-01-16016 January 2019 Request for Additional Information - High Pressure Service Water One Time TS Change ML18348B0292018-12-13013 December 2018 Subsequent License Renewal Severe Accident Mitigation Alternatives Requests for Additional Information ML19010A3832018-12-0707 December 2018 Additional Documents Needed for Peach Bottom SLR Environmental Review ML18324A6742018-11-15015 November 2018 Request for Additional Information (FINAL)- LAR to Allow 2SRV/SVs OOS at High Pressure ML18312A4072018-11-0808 November 2018 Request for Additional Information (Public) - LAR to Allow 2SRV/SVs OOS at High Pressure ML18276A0202018-10-0202 October 2018 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Amendment Request to Revise Emergency Plan for Limerick and Peach Bottom ML18240A1742018-08-28028 August 2018 Request for Additional Information (Final) - Adopt TSTF-500 Battery TS Changes LAR ML18239A1322018-08-27027 August 2018 Request for Additional Information Final - Relief Request I5R-04 ML18228A6762018-08-14014 August 2018 Request for Additional Information - Adopt TSTF-500 Battery TS Changes LAR ML18226A2012018-08-14014 August 2018 Request for Additional Information - Relief Request I5R-05 ML18214A2812018-08-0202 August 2018 Request for Additional Information Draft - Relief Request I5R-02 ML18200A2742018-07-17017 July 2018 Request for Additional Information 2nd Round (Final) - Adopt 50.69 License Amendment ML18192A1192018-07-10010 July 2018 Request for Additional Information 2nd Round (Final) - Adopt 50.69 License Amendment ML18178A4772018-06-27027 June 2018 Request for Additional Information 2nd Round - Adopt 50.69 License Amendment ML18096B5062018-04-0606 April 2018 Request for Additional Information Exelon Generation Company, LLC Requested Amendment to Adopt 10 CFR 50.69 for Risk-informed Categorization and Treatment of Structures, Systems and Components ML18094B0832018-04-0505 April 2018 Enclosurequest for Additional Information (Letter to P. Duke RAI Regarding Entergy Operations, Inc.'S Decommissioning Funding Plan Update for Salem and Hope Creek, and Peach Bottom ISFSIs Docket Nos. 72-48 and 72-29) ML18067A1482018-03-0808 March 2018 Enclosurequest for Additional Information (Letter to P. R. Simpson Request for Additional Information Regarding Exelon Generating Company, Llc'S Decommissioning Funding Plan Update for Independent Spent Fuel Storage Installation) ML17317B5502017-11-0909 November 2017 Licensed Operator Positive Fitness-For-Duty Test 2024-07-03
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OFFICIAL USE ONlY PROPRIETARY INFORMATION UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 March 27, 2015 Mr. Bryan C. Hanson President and Chief Nuclear Officer Exelon Nuclear 4300 Winfield Road Warrenville, IL 60555
SUBJECT:
PEACH BOTTOM ATOMIC POWER STATION, UNIT 2 - NRC STAFF REVIEW OF REQUEST FOR APPROVAL OF REVISION TO METHODOLGY FOR ESTABLISHING REPLACEMENT STEAM DRYER STRAIN LIMITS (TAC NO. MF4792)
Dear Mr. Hanson:
On August 25, 2014, the Nuclear Regulatory Commission (NRC) issued Amendment Nos. 293 and 296 to Renewed Facility Operating License Nos. DPR-44 and DPR-56 for Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML14133A046). These amendments authorized an increase in the maximum licensed thermal power level for PBAPS, Units 2 and 3, from 3514 megawatts thermal (MWt) to 3951 MWt, which is an increase of approximately 12.4%. This change in power level is considered an extended power uprate (EPU).
The NRC staff approval of the EPU was based, in part, on the capability for Exelon Generation Company, LLC (Exelon, the licensee) to monitor, evaluate, and take prompt action in response to potential adverse flow effects as a result of EPU operation on plant structures, systems, and components (including verifying the continued structural integrity of the replacement steam dryer (RSD)). License condition 2.C(15) was added to the facility operating license for each unit, as part of the EPU amendment, to provide the necessary requirements associated with potential adverse flow effects. This license condition requires, in part, that the licensee benchmark the RSD stress analysis methodology using data collected at or near 3514 MWt.
This benchmarking effort establishes the PBAPS Unit 2 RSD strain limits that will be used as acceptance criteria for power ascension above 3514 MWt. The license condition also requires that the methodology for establishing the RSD strain limits not be made less restrictive without prior NRC approval.
Enclosure 1 transmitted herewith contains sensitive unclassified information.
When separated from Enclosure 1, this document is decontrolled.
OFFICIAL USE ONlY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION B. Hanson Exelon implemented the EPU during the fall 2014 refueling outage for PBAPS Unit 2. Since about mid-December 2014, PBAPS Unit 2 has been holding at about 3514 MWt (89% of the current licensed power level of 3951 MWt, or 100% of the pre-EPU license power level) as part of the RSD benchmarking effort. As described in Exelon's letter dated February 3, 2015 (ADAMS Accession No. ML15034A573), RSD strain gauge measurements, collected near 3514 MWt, identified strain responses in the low frequency range that were not previously predicted.
As a result, the licensee developed an approach to quantify the magnitude of the unpredicted loads and integrate the results into the original methodology. In accordance with PBAPS Unit 2 license condition 2.C(15)(d)3, Exelon's letter requested NRC approval for this revision to the methodology for establishing the RSD strain limits. Exelon provided supplemental information in a letter dated March 24, 2015 (ADAMS Accession No. ML15083A559).
The NRC staff has reviewed the information provided in Exelon's letters dated February 3, 2015, and March 24, 2015. The revised methodology contains a certain degree of conservatism that provides reasonable assurance of the structural integrity of the RSD for power ascension up to 104% of 3514 MWt. Nonetheless, the technical approach involves approximations leading to uncertainties that preclude a finding of assurance, at this time, of satisfactorily maintaining the required American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code), Section Ill endurance limit of 13,600 pounds-force per square inch (psi) at the full EPU level.
Based on the above considerations, the NRC staff approves the resumption of power ascension for PBAPS Unit 2 to the next hold point specified in license condition 2.C(15) (i.e., 104% of 3514 MWt). Further power ascension of PBAPS Unit 2 beyond 104% of 3514 MWt will be contingent upon continued demonstration of the structural integrity of the RSD in accordance with the provisions in license condition 2.C(15). In addition, the staff has determined that additional information, as described in Enclosure 1, needs to be provided to help inform the staff's decision on the acceptability of power ascension beyond 104% of 3514 MWt. This request for additional information (RAI) was provided in draft form to Exelon on March 19, 2015.
In addition, the RAI was discussed during a meeting between Exelon and the NRC on March 26, 2015. Based on a discussion between the NRC staff (Mr. Richard Ennis) and Exelon (Mr. Ken Ainger) on March 27, 2015, Exelon agreed to provide the RAI response no later than the date that the steam dryer evaluation, performed based on data collected at 104% of 3514 MWt, is provided to the NRC in accordance with license condition 2.C(15).
The NRC staff has determined that Enclosure 1 contains proprietary information pursuant to 10 CFR 2.390. Accordingly, the staff has prepared a redacted, publicly available, non-proprietary version (i.e., Enclosure 2).
OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION B. Hanson If you have any questions regarding this matter, you may contact the PBAPS Project Manager, Mr. Richard Ennis, at 301-415-1420.
Sincerely, Michele G. Evans, Director Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-277
Enclosures:
- 1. Request for Additional Information (non-publicly available)
- 2. Request for Additional Information (publicly available) cc w/encl 2: Distribution via Listserv OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION REQUEST FOR ADDITIONAL INFORMATION REGARDING REPLACEMENT STEAM DRYER ANALYSIS EXELON GENERATION COMPANY. LLC PEACH BOTTOM ATOMIC POWER STATION- UNIT 2 DOCKET NO. 50-277 Proprietary information pursuant to Title 10 of the Code of Federal Regulations (10 CFR) Section 2.390 has been redacted from this document.
Redacted information is identified by blank space enclosed within double brackets as shown here (( )).
Enclosure 2 OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION On August 25, 2014, the Nuclear Regulatory Commission (NRC) issued Amendment Nos. 293 and 296 to Renewed Facility Operating License Nos. DPR-44 and DPR-56 for Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML14133A046). These amendments authorized an increase in the maximum licensed thermal power level for PBAPS, Units 2 and 3, from 3514 megawatts thermal (MWt) to 3951 MWt, which is an increase of approximately 12.4%. This change in power level is considered an extended power uprate (EPU).
By letter dated February 3, 2015, as supplemented by letters dated March 24, 2015 (ADAMS Accession Nos. ML15034A573 and ML15083A559, respectively), Exelon Generation Company, LLC (Exelon, the licensee) requested NRC approval of a revision to the methodology, previously approved during the EPU review, for establishing the PBAPS Unit 2 replacement steam dryer (RSD) strain limits. Exelon's request was submitted to support the continuation of EPU power ascension above 3514 MWt.
The NRC staff has reviewed the information the licensee provided in Exelon's letters dated February 3, 2015, and March 24, 2015, and has determined that there is reasonable assurance that the PBAPS Unit 2 RSD will maintain its structural integrity for continued power ascension to the next hold point specified in license condition 2.C(15) (i.e., 104% of 3514 MWt). However, the staff has determined that additional information, as described below, needs to be provided to help inform the staff's decision on the acceptability of power ascension beyond 104% of 3514 MWt.
Request for Additional Information (RAI) questions 1 through 9, regarding the revision to the methodology, were addressed in Exelon's letter dated March 24, 2015. As such, this RAI is designated as RAl-10.
RAl-10 The NRC staff has the following observations on the information submitted so far:
- Using (( )) to infer the alternating stress state in a steam dryer is, in principle, acceptable.
- Statistical studies of the peak measured strains on the dryer hood and skirt by the licensee appear to show that ((
)) is consistent with guidelines in NUREG 0484. The licensee indicated that cumulative distribution function (CDF) curves were developed, ((
)) To further validate the licensee's findings from its analysis, the NRC staff requests that the CDF curves for SG4 and SG20 be provided for review.
)) does not have a sound technical basis. Therefore, this raises concerns regarding the stress analysis of the PBAPS Unit 2 steam dryer. All ((
))) do not seem to be included in the current analysis, raising the concern that the (( )) may not be an appropriate upper bound. Also, the ((
OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION
)) These problems with the approach used to date lead to ((
)) adding further uncertainty to the accuracy of the current calculations.
The general methodology as submitted by the licensee is reasonable, but the ((
)) must be complete and representative of (( ))
strains and stresses in all major dryer components (outer hoods, inner and middle hoods, and skirt), and the approach used to determine the (( )) in the analysis must be revised as follows:
a) Due to possible inaccuracies in the ((
)), a frequency shift of at least +/-10% must be considered to ensure that all (( )) are included in the analyses.
b) (( )) used in the analysis should be submitted, and demonstrated to be reasonable for use on the outer hood, middle/inner hood, and skirt, regardless of whether the ((
))
c) The (( )) should be based on attempting to match as closely as possible
(( ))1 d) The simulated (( )) should bound the measured ones.
e) Simulated (( )) should be reasonably consistent with those measured.
f) The (( )) must be used to estimate the top 5 maximum stresses and their locations on the upper and lower dryer.
g) For each of the (( )), please provide ((
)) at each of the strain gage locations on the hood.
h) Please confirm whether the outer hood, middle hood and inner hood are dynamically coupled.
))
OFFICIAL USE ONLY PROPRIETARY INFORMATION
Package: ML15086A310 Letter: ML15033A489 (publicly available) : ML15086A328 (non-publicly available) : ML15086A333 publicly available) *via e-mail OFFICE LPL 1-2/PM LPL 1-2/LA* LPL 1-2/BC(A) EMCB/BC(A) DE/SLA DE/D DORL/D KManoly MEvans (LLund NAME REnnis ABaxter CSanders YLi JLubinski for)
DATE 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015