Letter Sequence Approval |
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MONTHYEARML15040A7202015-03-12012 March 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15083A5592015-03-24024 March 2015 Extended Power Uprate: Response to Replacement Steam Dryer Requests for Additional Information Project stage: Other ML15033A4892015-03-27027 March 2015 NRC Staff Review of Replacement Steam Dryer Re-Benchmarking to Support Extended Power Uprate Power Ascension Project stage: Approval ML15086A3332015-03-27027 March 2015 Request for Additional Information Regarding Replacement Steam Dryer Analysis, Exelon Generation Company, Llc. Peach Bottom Atomic Power Station - Unit 2 Project stage: RAI ML15096A0082015-04-0505 April 2015 Extended Power Uprate: Response to Replacement Steam Dryer Requests for Additional Information Project stage: Other ML15084A3422015-04-0606 April 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15099A7482015-04-0909 April 2015 Power Ascension Hold at 104% of 3514 Mwt Project stage: Other ML15110A0982015-04-10010 April 2015 E-Mail Peach Bottom Unit 2 - Power Ascension Hold at 104% of 3514 Mwt Project stage: Other ML15091A1342015-04-16016 April 2015 Summary of Closed Meeting Held on March 26, 2015, with Exelon Generation Company, LLC to Discuss Steam Dryer Analysis for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Meeting ML15125A1682015-04-25025 April 2015 Power Ascension - 108% Hold Point Decision Project stage: Other ML15127A5182015-05-0505 May 2015 Draft Request for Additional Information (Tac No. MF4792) Project stage: Draft RAI ML15127A5262015-05-0505 May 2015 Draft Request for Additional Information (Attachment 2) Project stage: Draft RAI ML15110A0852015-05-12012 May 2015 Request for Withholding Information from Public Disclosure for Peach Bottom Atomic Power Station, Unit No. 2 Project stage: Withholding Request Acceptance ML15135A4372015-05-15015 May 2015 Approval of Steam Dryer Methodology and Resumption of EPU Power Ascension Project stage: Other ML15135A4022015-05-15015 May 2015 Extended Power Uprate: Response to Replacement Steam Dryer Request for Additional Information Project stage: Request ML15127A2082015-05-19019 May 2015 Approval of Revision to Methodology for Establishing Replacement Steam Dryer Strain Limits Project stage: Other ML15196A6372015-07-15015 July 2015 Error Identified in Letter from Exelon to NRC Re Predicted Strain Ratios Provided in Response to Request for Additional Information (RAI-11) Project stage: Response to RAI 2015-04-05
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Category:Letter
MONTHYEARML24022A2262024-01-22022 January 2024 (PBAPS) Unit 3 - Submittal of the Inservice Inspection (ISI) Owner'S Activity Report (OAR) for the 24th Refueling Outage for Unit 3 ML23346A2412024-01-17017 January 2024 Staff Assessment of Updated Seismic Hazards Following the NRC Process for the Ongoing Assessment of Natural Hazards Information (EPID L-2019-PMP-0061) - Letter IR 05000277/20234022024-01-11011 January 2024 Security Baseline Inspection Report 05000277/2023402 and 05000278/2023402 and Independent Spent Fuel Storage Installation Security Inspection 07200029/2023401 ML23354A1922024-01-0505 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) ML23355A0622023-12-18018 December 2023 Independent Spent Fuel Storage Installation (Isfsi), Security Plan, Training and Qualification Plan, and Safeguards Contingency Plan ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 ML23334A2502023-11-30030 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23270C0072023-11-29029 November 2023 Notice of Proposed Amendment to Decommissioning Trust Agreement ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums ML23305A3472023-11-0101 November 2023 Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) IR 05000277/20230032023-10-30030 October 2023 Integrated Inspection Report 05000277/2023003 and 05000278/2023003 and Exercise of Enforcement Discretion ML23286A0012023-10-13013 October 2023 Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2023010-01 RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans ML23271A1342023-10-11011 October 2023 Dtf Analysis Letter IR 05000277/20244012023-10-0505 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000277/2024401 and 05000278/2024401 ML23265A1502023-09-22022 September 2023 License Amendment Request Revise a License Condition and Certain Technical Specifications to Remove Restrictions in Support of Decommissioning Activities ML23264A8682023-09-21021 September 2023 Independent Spent Fuel Storage Installation Registration of Dry Storage Canister WC-EOS-37PTH-008-B4L, WC-EOS-37PTH-007-B4L, and WC-EOS-37PTH-002-B4L IR 05000277/20230102023-09-15015 September 2023 Biennial Problem Identification and Resolution Inspection Report 05000277/2023010 and 05000278/2023010 and Notice of Violation ML23251A2022023-09-11011 September 2023 Cover Letter W/Report LR-N23-0045, and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement IR 05000277/20230052023-08-31031 August 2023 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2023005 and 05000278/2023005) ML23158A1952023-08-30030 August 2023 R. E. Ginna - Issuance of Amendments to Adopt TSTF-273-A, Revision 2, Safety Function Determination Program Clarifications ML23232A0012023-08-19019 August 2023 Revision of One Procedure That Implements the Radiological Emergency Response Plan (Rerp). Includes EPP 06-009, Rev. 13 IR 05000277/20230112023-08-15015 August 2023 Comprehensive Engineering Team Inspection Report 05000277/2023011 and 05000278/2023011 ML23226A1112023-08-14014 August 2023 10 CFR 50.46 Annual Report IR 05000277/20230022023-08-0808 August 2023 Integrated Inspection Report 05000277/2023002 and 05000278/2023002 RS-23-087, Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor2023-08-0404 August 2023 Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor IR 05000277/20230402023-07-17017 July 2023 95001 Inspection Supplemental Report 05000277/2023040 and Follow-Up Assessment Letter ML23188A0532023-07-0707 July 2023 Registration of Use of Independent Spent Fuel Storage Installation (ISFSI) Casks ML23186A1272023-07-0606 July 2023 Response to Disputed Non-Cited Violation Documented in Peach Bottom Atomic Power Station, Units 2 and 3, Inspection Report 05000277/2022004 and 05000278/2022004 ML23178A0352023-06-27027 June 2023 Senior Reactor and Reactor Operator Initial License Examinations RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23151A4162023-05-31031 May 2023 Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) ML23150A2052023-05-30030 May 2023 Independent Spent Fuel Storage Installation (Isfsi), Annual Radiological Environmental Operating Report 80 January 1, 2022 Through December 31, 2022 RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling ML23142A1602023-05-23023 May 2023 Summary of April 11, 2023, Public Observation Meeting with Constellation Energy Generation, LLC Re Proposed Exemption Request from Work Hour Requirements ML23132A1582023-05-18018 May 2023 Correction to Technical Specification 3.4.7 (Page 3.4-16) Issued in Amendment No. 337 ML23132A1532023-05-12012 May 2023 Transmittal of 2022 Annual Financial Reports WM 23-0009, Financial Assurance Requirements for Decommissioning Nuclear Power Reactors 10 CFR 50.75(f)(1)2023-05-10010 May 2023 Financial Assurance Requirements for Decommissioning Nuclear Power Reactors 10 CFR 50.75(f)(1) IR 05000277/20230012023-05-0808 May 2023 Integrated Inspection Report 05000277/2023001 and 05000278/2023001 ML23114A2522023-04-28028 April 2023 Request to Use a Provision of a Later Edition of the ASME Boiler & Pressure Vessel Code, Section XI 2024-01-05
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARIR 05000277/20244012023-10-0505 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000277/2024401 and 05000278/2024401 ML23264A7992023-09-21021 September 2023 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC Fleet Request License Amendment Request to Adopt TSTF-580, Revision 1 ML22118A3312022-04-28028 April 2022 NRR E-mail Capture - Peach Bottom - Formal RAI for Proposed Alternative I5R-14, Revision 1 ML22041B5362022-02-10010 February 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Request for Additional Information Regarding Fleet License Amendment Request to Adopt TSTF-541 ML22021A5692022-01-21021 January 2022 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000277/2022403 and 05000278/2022403 ML22020A0642022-01-13013 January 2022 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21256A1902021-09-10010 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21144A2132021-05-24024 May 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21062A0652021-03-0101 March 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative to Documentation Requirements for Pressure Retaining Bolting ML21049A2572021-02-18018 February 2021 Request for Additional Information Byron/Dresden Proposed Changes to Site Emergency Plans to Support Post-Shutdown and Permanently Defueled Conditions (EPID-2020-LLA-0240 & EPID-2020-LLA-0237) ML21035A2222021-02-0404 February 2021 Notification of Conduct of a Fire Protection Team Inspection ML21091A1782021-02-0202 February 2021 Ti 2515/194 Inspection Documentation Request ML21012A1302021-01-12012 January 2021 Request for Additional Information - TSTF-505 ML20357A0972020-12-21021 December 2020 Request for Additional Information - TSTF-505 ML20296A3342020-10-21021 October 2020 ISI Remote Inspection - Supplemental Request for Information ML20239A7982020-08-25025 August 2020 NRR E-mail Capture - Exelon Generation Company, LLC - Fleet License Amendment Request to Adopt TSTF-568, Revision 2 ML20153A7042020-06-0101 June 2020 NRR E-mail Capture - Preliminary RAI for Fleet Request to Use Alternative OMN-26 ML20135H1972020-05-14014 May 2020 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Request to Extend Safety Relief Valve Test Interval ML20070R2282020-03-10010 March 2020 Request for Additional Information - RR ML19303D1662019-10-31031 October 2019 Requests for Additional Information for the Environmental Review of the Peach Bottom Subsequent License Renewal Application - Set 2 (EPID No. L-2018-RNW-0013)- RAIs ML19232A1752019-08-20020 August 2019 Request for Additional Information - TSTF-500 Implementation LAR ML19140A2832019-05-15015 May 2019 Email - Peach Bottom Atomic Power Station, Units 2 and 3 Second Round RAI Request - Set 1 ML19140A2822019-05-15015 May 2019 027 Pb FU RAI Subsequent to Clarification Call - Cu Greater than 15 Zn Holston (Jg) ML19253D2932019-05-0707 May 2019 002 Attachment 4D Confirmation Water Chemistry Chereskin Revised (002) ML19249C7252019-05-0303 May 2019 SLRA Requests for Additional Information - Set 2 May 3, 2019 ML19108A4282019-04-10010 April 2019 RAIs SLRA Set 1_ERO(Rev 1) ML19079A0232019-03-19019 March 2019 Licensed Operator Positive Fitness-For-Duty Test ML19058A2902019-02-27027 February 2019 Request for Additional Information - High Pressure Service Water One Time TS Change ML19037A4832019-02-0606 February 2019 NRR E-mail Capture - Clarification Questions Associated with Staff Assessment of Peach Bottom Seismic Probabilistic Risk Assessment Report Dated August 28, 2018 ML19028A0062019-01-25025 January 2019 Secondary Containment LAR Requests for Additional Information ML19017A0472019-01-16016 January 2019 Request for Additional Information - High Pressure Service Water One Time TS Change ML18348B0292018-12-13013 December 2018 Subsequent License Renewal Severe Accident Mitigation Alternatives Requests for Additional Information ML19010A3832018-12-0707 December 2018 Additional Documents Needed for Peach Bottom SLR Environmental Review ML18324A6742018-11-15015 November 2018 Request for Additional Information (FINAL)- LAR to Allow 2SRV/SVs OOS at High Pressure ML18312A4072018-11-0808 November 2018 Request for Additional Information (Public) - LAR to Allow 2SRV/SVs OOS at High Pressure ML18276A0202018-10-0202 October 2018 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Amendment Request to Revise Emergency Plan for Limerick and Peach Bottom ML18240A1742018-08-28028 August 2018 Request for Additional Information (Final) - Adopt TSTF-500 Battery TS Changes LAR ML18239A1322018-08-27027 August 2018 Request for Additional Information Final - Relief Request I5R-04 ML18228A6762018-08-14014 August 2018 Request for Additional Information - Adopt TSTF-500 Battery TS Changes LAR ML18226A2012018-08-14014 August 2018 Request for Additional Information - Relief Request I5R-05 ML18214A2812018-08-0202 August 2018 Request for Additional Information Draft - Relief Request I5R-02 ML18200A2742018-07-17017 July 2018 Request for Additional Information 2nd Round (Final) - Adopt 50.69 License Amendment ML18192A1192018-07-10010 July 2018 Request for Additional Information 2nd Round (Final) - Adopt 50.69 License Amendment ML18178A4772018-06-27027 June 2018 Request for Additional Information 2nd Round - Adopt 50.69 License Amendment ML18096B5062018-04-0606 April 2018 Request for Additional Information Exelon Generation Company, LLC Requested Amendment to Adopt 10 CFR 50.69 for Risk-informed Categorization and Treatment of Structures, Systems and Components ML18094B0832018-04-0505 April 2018 Enclosurequest for Additional Information (Letter to P. Duke RAI Regarding Entergy Operations, Inc.'S Decommissioning Funding Plan Update for Salem and Hope Creek, and Peach Bottom ISFSIs Docket Nos. 72-48 and 72-29) ML18067A1482018-03-0808 March 2018 Enclosurequest for Additional Information (Letter to P. R. Simpson Request for Additional Information Regarding Exelon Generating Company, Llc'S Decommissioning Funding Plan Update for Independent Spent Fuel Storage Installation) ML17317B5502017-11-0909 November 2017 Licensed Operator Positive Fitness-For-Duty Test ML17240A0062017-08-24024 August 2017 Request for Additional Information Regarding License Amendment Request for Measurement Uncertainty Recapture Power Uprate ML17222A0962017-08-10010 August 2017 Request for Additional Information - Amendment Request Regarding Safety Relief Valve and Safety Valce Operability for Cycle 22 2023-09-21
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OFFICIAL USE ONlY PROPRIETARY INFORMATION UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 March 27, 2015 Mr. Bryan C. Hanson President and Chief Nuclear Officer Exelon Nuclear 4300 Winfield Road Warrenville, IL 60555
SUBJECT:
PEACH BOTTOM ATOMIC POWER STATION, UNIT 2 - NRC STAFF REVIEW OF REQUEST FOR APPROVAL OF REVISION TO METHODOLGY FOR ESTABLISHING REPLACEMENT STEAM DRYER STRAIN LIMITS (TAC NO. MF4792)
Dear Mr. Hanson:
On August 25, 2014, the Nuclear Regulatory Commission (NRC) issued Amendment Nos. 293 and 296 to Renewed Facility Operating License Nos. DPR-44 and DPR-56 for Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML14133A046). These amendments authorized an increase in the maximum licensed thermal power level for PBAPS, Units 2 and 3, from 3514 megawatts thermal (MWt) to 3951 MWt, which is an increase of approximately 12.4%. This change in power level is considered an extended power uprate (EPU).
The NRC staff approval of the EPU was based, in part, on the capability for Exelon Generation Company, LLC (Exelon, the licensee) to monitor, evaluate, and take prompt action in response to potential adverse flow effects as a result of EPU operation on plant structures, systems, and components (including verifying the continued structural integrity of the replacement steam dryer (RSD)). License condition 2.C(15) was added to the facility operating license for each unit, as part of the EPU amendment, to provide the necessary requirements associated with potential adverse flow effects. This license condition requires, in part, that the licensee benchmark the RSD stress analysis methodology using data collected at or near 3514 MWt.
This benchmarking effort establishes the PBAPS Unit 2 RSD strain limits that will be used as acceptance criteria for power ascension above 3514 MWt. The license condition also requires that the methodology for establishing the RSD strain limits not be made less restrictive without prior NRC approval.
Enclosure 1 transmitted herewith contains sensitive unclassified information.
When separated from Enclosure 1, this document is decontrolled.
OFFICIAL USE ONlY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION B. Hanson Exelon implemented the EPU during the fall 2014 refueling outage for PBAPS Unit 2. Since about mid-December 2014, PBAPS Unit 2 has been holding at about 3514 MWt (89% of the current licensed power level of 3951 MWt, or 100% of the pre-EPU license power level) as part of the RSD benchmarking effort. As described in Exelon's letter dated February 3, 2015 (ADAMS Accession No. ML15034A573), RSD strain gauge measurements, collected near 3514 MWt, identified strain responses in the low frequency range that were not previously predicted.
As a result, the licensee developed an approach to quantify the magnitude of the unpredicted loads and integrate the results into the original methodology. In accordance with PBAPS Unit 2 license condition 2.C(15)(d)3, Exelon's letter requested NRC approval for this revision to the methodology for establishing the RSD strain limits. Exelon provided supplemental information in a letter dated March 24, 2015 (ADAMS Accession No. ML15083A559).
The NRC staff has reviewed the information provided in Exelon's letters dated February 3, 2015, and March 24, 2015. The revised methodology contains a certain degree of conservatism that provides reasonable assurance of the structural integrity of the RSD for power ascension up to 104% of 3514 MWt. Nonetheless, the technical approach involves approximations leading to uncertainties that preclude a finding of assurance, at this time, of satisfactorily maintaining the required American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code), Section Ill endurance limit of 13,600 pounds-force per square inch (psi) at the full EPU level.
Based on the above considerations, the NRC staff approves the resumption of power ascension for PBAPS Unit 2 to the next hold point specified in license condition 2.C(15) (i.e., 104% of 3514 MWt). Further power ascension of PBAPS Unit 2 beyond 104% of 3514 MWt will be contingent upon continued demonstration of the structural integrity of the RSD in accordance with the provisions in license condition 2.C(15). In addition, the staff has determined that additional information, as described in Enclosure 1, needs to be provided to help inform the staff's decision on the acceptability of power ascension beyond 104% of 3514 MWt. This request for additional information (RAI) was provided in draft form to Exelon on March 19, 2015.
In addition, the RAI was discussed during a meeting between Exelon and the NRC on March 26, 2015. Based on a discussion between the NRC staff (Mr. Richard Ennis) and Exelon (Mr. Ken Ainger) on March 27, 2015, Exelon agreed to provide the RAI response no later than the date that the steam dryer evaluation, performed based on data collected at 104% of 3514 MWt, is provided to the NRC in accordance with license condition 2.C(15).
The NRC staff has determined that Enclosure 1 contains proprietary information pursuant to 10 CFR 2.390. Accordingly, the staff has prepared a redacted, publicly available, non-proprietary version (i.e., Enclosure 2).
OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION B. Hanson If you have any questions regarding this matter, you may contact the PBAPS Project Manager, Mr. Richard Ennis, at 301-415-1420.
Sincerely, Michele G. Evans, Director Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-277
Enclosures:
- 1. Request for Additional Information (non-publicly available)
- 2. Request for Additional Information (publicly available) cc w/encl 2: Distribution via Listserv OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION REQUEST FOR ADDITIONAL INFORMATION REGARDING REPLACEMENT STEAM DRYER ANALYSIS EXELON GENERATION COMPANY. LLC PEACH BOTTOM ATOMIC POWER STATION- UNIT 2 DOCKET NO. 50-277 Proprietary information pursuant to Title 10 of the Code of Federal Regulations (10 CFR) Section 2.390 has been redacted from this document.
Redacted information is identified by blank space enclosed within double brackets as shown here (( )).
Enclosure 2 OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION On August 25, 2014, the Nuclear Regulatory Commission (NRC) issued Amendment Nos. 293 and 296 to Renewed Facility Operating License Nos. DPR-44 and DPR-56 for Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML14133A046). These amendments authorized an increase in the maximum licensed thermal power level for PBAPS, Units 2 and 3, from 3514 megawatts thermal (MWt) to 3951 MWt, which is an increase of approximately 12.4%. This change in power level is considered an extended power uprate (EPU).
By letter dated February 3, 2015, as supplemented by letters dated March 24, 2015 (ADAMS Accession Nos. ML15034A573 and ML15083A559, respectively), Exelon Generation Company, LLC (Exelon, the licensee) requested NRC approval of a revision to the methodology, previously approved during the EPU review, for establishing the PBAPS Unit 2 replacement steam dryer (RSD) strain limits. Exelon's request was submitted to support the continuation of EPU power ascension above 3514 MWt.
The NRC staff has reviewed the information the licensee provided in Exelon's letters dated February 3, 2015, and March 24, 2015, and has determined that there is reasonable assurance that the PBAPS Unit 2 RSD will maintain its structural integrity for continued power ascension to the next hold point specified in license condition 2.C(15) (i.e., 104% of 3514 MWt). However, the staff has determined that additional information, as described below, needs to be provided to help inform the staff's decision on the acceptability of power ascension beyond 104% of 3514 MWt.
Request for Additional Information (RAI) questions 1 through 9, regarding the revision to the methodology, were addressed in Exelon's letter dated March 24, 2015. As such, this RAI is designated as RAl-10.
RAl-10 The NRC staff has the following observations on the information submitted so far:
- Using (( )) to infer the alternating stress state in a steam dryer is, in principle, acceptable.
- Statistical studies of the peak measured strains on the dryer hood and skirt by the licensee appear to show that ((
)) is consistent with guidelines in NUREG 0484. The licensee indicated that cumulative distribution function (CDF) curves were developed, ((
)) To further validate the licensee's findings from its analysis, the NRC staff requests that the CDF curves for SG4 and SG20 be provided for review.
)) does not have a sound technical basis. Therefore, this raises concerns regarding the stress analysis of the PBAPS Unit 2 steam dryer. All ((
))) do not seem to be included in the current analysis, raising the concern that the (( )) may not be an appropriate upper bound. Also, the ((
OFFICIAL USE ONLY PROPRIETARY INFORMATION
OFFICIAL USE ONLY PROPRIETARY INFORMATION
)) These problems with the approach used to date lead to ((
)) adding further uncertainty to the accuracy of the current calculations.
The general methodology as submitted by the licensee is reasonable, but the ((
)) must be complete and representative of (( ))
strains and stresses in all major dryer components (outer hoods, inner and middle hoods, and skirt), and the approach used to determine the (( )) in the analysis must be revised as follows:
a) Due to possible inaccuracies in the ((
)), a frequency shift of at least +/-10% must be considered to ensure that all (( )) are included in the analyses.
b) (( )) used in the analysis should be submitted, and demonstrated to be reasonable for use on the outer hood, middle/inner hood, and skirt, regardless of whether the ((
))
c) The (( )) should be based on attempting to match as closely as possible
(( ))1 d) The simulated (( )) should bound the measured ones.
e) Simulated (( )) should be reasonably consistent with those measured.
f) The (( )) must be used to estimate the top 5 maximum stresses and their locations on the upper and lower dryer.
g) For each of the (( )), please provide ((
)) at each of the strain gage locations on the hood.
h) Please confirm whether the outer hood, middle hood and inner hood are dynamically coupled.
))
OFFICIAL USE ONLY PROPRIETARY INFORMATION
Package: ML15086A310 Letter: ML15033A489 (publicly available) : ML15086A328 (non-publicly available) : ML15086A333 publicly available) *via e-mail OFFICE LPL 1-2/PM LPL 1-2/LA* LPL 1-2/BC(A) EMCB/BC(A) DE/SLA DE/D DORL/D KManoly MEvans (LLund NAME REnnis ABaxter CSanders YLi JLubinski for)
DATE 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015 3/27/2015