ML14191A972
| ML14191A972 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 03/07/1989 |
| From: | Julian C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML14191A973 | List: |
| References | |
| 50-261-89-01, 50-261-89-1, NUDOCS 8903240153 | |
| Download: ML14191A972 (2) | |
Text
ENCLOSURE 1 NOTICE OF VIOLATION Carolina Power and Light Company Docket No. 50-261 H. B. Robinson License No. DPR-23 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 9 -
13, 1989, a violation of NRC requirements was identified.
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (19),
the violation is listed below:
10 CFR 50.55a.(g).(4).(ii), states that inservice examinations of components and inservice tests to verify operational readiness of pumps and valves whose function is required for safety shall comply with the requirements of the code (ASME Section XI).
ASME Boiler and Pressure Vessel Code-1977,Section XI, Paragraph IWV3413(c),
states that if an increase in stroke time of 25 percent or more from the previous test for valves with stroke times greater than ten seconds or 50 percent or more for valves with stroke times less than or equal to ten seconds is observed, test frequency shall be increased to once each month until corrective action is taken, at which time the original test frequency shall be resumed. In any case, any abnormality or erratic action shall be reported.
Contrary to the above, test records indicate that during the September 1988 outage, the stroke time for cold shutdown valve PCV-1716 increased by more than the Section XI limit of 50 percent and corrective action was not taken nor was the test frequency increased to once each month.
This is a Severity Level IV violation (Supplement I).
Pursuant to the provisions of 10 CFR 2.201, Carolina Power and Light Company is hereby required to submit a written statement or explanation to the Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC
- 20555, with a copy to the Regional Administrator, Region.II, and a copy to the NRC Resident Inspector, within 30 days of the date of the letter transmitting this Notice.
This reply should be clearly marked as a "Reply to a Notice of 8903240153 890307 PDR ADOCK 05000261 G
A PNU
Carolina.Power and Light Company 2
Docket No. 50-261 H. B. Robinson License No. DPR-23 Violation" and should include [for each violation]:
(1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when, full compliance will be achieved.
Where good cause is shown, consideration will be given to extending the response time.
If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken.
Security or safeguards information should be submitted as an enclosure to facilitate withholding it from public disclosure as required by 10 CFR 2.790(d) or 10 CFR 73.21.
FOR THE NUCLEAR REGULATORY COMMISSION Caudle A. Julian, Chief Engineering Branch Division of Reactor Safety ODated at Atlanta, Georgia this q4 day of March 1989 0II