ML14188A414

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Forwards Monthly Operating Rept for Jan 1981
ML14188A414
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/10/1981
From: Starkey R
CAROLINA POWER & LIGHT CO.
To: Stello V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
Shared Package
ML14188A416 List:
References
RSEP-81-225, NUDOCS 8102170066
Download: ML14188A414 (5)


Text

ACCESSION NBR:8102170066 DOC.DATE: 81/02/10 NOTARIZED: NO DOCKET #

FACIL:50-?b1 H. 8, Robinson Plant, Unit 2, Carolina Power and Ligh 05000261 AUTH.NAME AUTHOR AFFILIATION STARKEYRB. Carolina Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION STELLOV. Director's Office, Office of Inspection and Enforcement

SUBJECT:

Forwards monthly operating rept for Jan 1981, DISTRIBUTION CODE: A0088 COPIES RECEIVED:LTR ENCL j- SIZE:4,. JY....

TITLE: Annual, Semi-Annual & Monthly Operating Reports (OL Stage)

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL ACTION: VARGAS. 04 7 7 INTERNAL: D/DIRHUM FACO7 1 1 DIRDIV OF LIC 1 1 I&E 06 2 2 MPA 13 2 2 NRC PDR 04 1 1 OP E L BR09 1 1 OR ASSESS BR 10 1 1 FIL 01 1 1 EXTERNAL: ACRS 11 1 1 BROOKHAVEN 12 1 1 LP)R 03 1 1 NSIC 05 1 1 TOTAL NUMBER OF COPIES REUUIRED: LTTR 21 ENCL 21

CP&L

- Carolina Power & Light Company H. B. ROBINSON STEAM ELECTRIC PLANT POST OFFICE BOX 790 HARTSVILLE, SOUTH CAROLINA 29550 FEB 1 1981 Robinson File No: 2-0-4-a-8 SERIAL: RSEP/81-225 Mr. Victor Stello, Jr., Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, DC 20555 H. B. ROBINSON STEAM ELECTRIC PLANT, UNIT NO.,2 DOCKET NO. 50-261 LICENSE NO. DPR-23 MONTHLY OPERATIONS REPORT

Dear Mr. Stello:

In accordance with Technical Specifications 6.9.1.c for the H. k binson Steam Electric Plant, Unit No. 2, Carolina Power and Light Compan erewith submits the report of operating statistics and shutdown experience for the month of January, 1981.

P44.

Very truly yours, R. B. Starkey, r.

General Manager H. B. Robinson S.E. Plant MLW/gbm Enclosures cc: R. A. Hartfield (2)

J. P. O'Reilly (1)

Poo P10 c- -7 06/

Enclosure to Serial: RSEP/81-225 yage 1 of 3 OPERATING DATA REPORT DOCKET NO: DPR-23 DATE: 810203 COMPLETED BY: M. L. Watford TELEPHONE: (803) 383-4524 OPERATING STATUS OPERAING SATUSNotes: There are presently 113

1. Unit Name: H. B. Robinson Two spent fuel assemblies
2. Reporting Period: 810101,0000/810131,2400
3. Licensed Thermal Power (MWt): 2300
4. Nameplate Rating (Gross M'e): 739
5. Design Electrical Rating. (Net MWe): . 700
6. Maximum Dependable Capacity (Gross MWe): 700
7. Maximum Dependable Capacity (Net MWe): 665
8. If Changes Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report, Give Reasons: No change
9. Power Level to Which Restricted, If Any (Net MWe): None
10. Reasons For Restrictions, If Any: N/A This Month Yr.-to-Date Cumulative
11. Hours in Reporting Period 744 744 86,910
12. Number of Hours Reactor Was Critical 669.07 669.07 66,434.35
13. Reactor Reserve Shutdown Hours 74.93 74.93 1,052.81
14. Hours Generator On-Line 661.40 661.40 64,820.22
15. Unit Reserve Shutdown Hours 0.00 0.00 23.20
16. Gross Thermal Energy Generated (MWH) 1,458,329 1,458,329 132,670,703
17. Gross Electrical Energy Generated (MWH) 479,925 479,925 42,818,692
18. Net Electrical Energy Generated (MWH) 456,022 456,022 40,572.474
19. Unit Service Factor 88.90 88.90 74.58
20. Unit Availability Factor 88.90 88.90 74.61
21. Unit Capacity Factor (Using MDC Net) 92.17 92.17 70.20
22. Unit Capacity Factor (Using DER Net) 87.56 87.56 66.69
23. Unit Forced Outage Rate 11.10 11.10 13.84
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Steam Generator Inspection, April - May, 1981, 3 weeks

25. If Shut Down At End of Report Period, Estimated Date of Startup: February 4, 1981
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION --

(9/77) sg

Enclosure to Serial: RSEP/81-225 Page 2 of 3 UNTSHUTDOWNS AND POWER REDUCTIONS DOCKET NO. DPR-23 UNITNAME H. B. Robinson Two, DATE 810203 COMNLETED IY M. L. Watford REPORT MONTi nuary TELEPH ONE (803)_ 383-4524,

~..~ .~

1ociltig

£vcntPrevent Re) repa&Correclty Action i Recurrence zinCasumaoeLa capacitorssee 01-02 810110 F A 4 ----- HH VALVEX "A" Feedwater Reg. Valve (FWRV) oscillating, replaced faulty capacitors in summator (Load (oaReduction) 01-02 810123 B 4 HH PTPEXX "A" Main Feedwater Pp recirc.

I I Iline elbow leaking, elbow replaced (Load Reduction)01-03j 810124 F 17.42 B 3 I --- HH RTEXCR "6B' FW Htr. tube leaks, leaks weld repaired 01-04 810129 F 65.18 A 3 ----- XX PUMPXX E.H. Oil Pump(s) Failure - One was replaced due to seal problems and the other had a crack repaired on the discharge unloader piping 2 3 4 F: Forced Reason: Method: Exhibit G Instructions S: Schedu!Cd A-Eq uipmCnt Failure (Explain) I -M inual for Preparation of Data' IT-Maintenance or 2-Manual Scram . Entry Sheels fIor Licensee C-Refueling 3-Automuatic Scram. Event Repot (E) File (NUREG D-PegLatory Restrict ion 4-0ther (Explain) 0161 E-Operator Training & License Examination F-Athni nist ra :ive ..

G-Operational L r (Explain) Exhibit I - Same Source (9/77) l-(thec Hixphin)

Enclosure to Serial: RSEP/81-225 Tage 3 of 3 .A AGE DILY UNITPOWER LEVEL DOCKETNO. DPR-23 UNIT H. B. Robinson Two DATE 810203 COMPLETE ) BY M. L. Watford TELEPHONE (803) 383-4524 MONTH January, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net)

] 722 17 724 2 722 I8 708 722 724 3 _ _ _ _ _ _ _ _ _ _ _ _ _ _19 ._ _ _ _ _ _ __ _ _ _ _ _ _

4 698 20 723 5 720 . 21 722 723 722 22 724 661 7 ________ _______23

8. 723 24 321 9 723 25 42 10 589 . 26 714 11 721 27 689 12 722 28 722 13 722 29 168 14 723 30 -19 15 723 31 -19 16 724 INSTRUCTIONS On this format. list (hc average daily unit power level in MWe-Net for each day in the reportingi month. Compute to the nearest whole megawatt.

(9/77)