ML14181A924

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Insp Rept 50-261/97-06 on 970323-0426.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML14181A924
Person / Time
Site: Robinson 
Issue date: 05/23/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A921 List:
References
50-261-97-06, 50-261-97-6, NUDOCS 9706050079
Download: ML14181A924 (19)


See also: IR 05000261/1997006

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/97-06

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

March 23 - April 26, 1997

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Resident.Inspector

G. Wiseman, Reactor Engineer, Region II

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9706050079 970523

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/97-06

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a five-week

period of resident inspection; in addition, it includes the results of an

inspection by one Region II based project engineer.

Operations

Conduct of operations was professional and safety-conscious

(Section 01.1).

Operators properly controlled a 50 percent downpower evolution to repair

a service water leak in the "A" Condensate Pump motor upper oil cooler.

In addition, operators adequately responded to and handled a heater

drain tank level control failure which resulted in a feedwater/

condensate transient. The transient was caused by troubleshooting

activities on the heater drain tank level controller and indicated a

weakness in contingency action planning and understanding of the

potential adverse impact of the activity on the plant (Section 01.2).

Several management changes were announced including Vice President and

Director of Site Operations (Section 06.1).

The Plant Nuclear Safety Committee and the Nuclear Assessment Section

provided strong oversight and safety focus of licensee activities

(Section 07.1).

Maintenance

Routine and emergent maintenance and surveillance activities were

performed satisfactorily. In general, good work control and

coordination was observed, however, several minor problems were

identified indicating a need for greater attention to detail by

maintenance personnel following work instructions and understanding the

work scope prior to implementation (Section M1.1).

A Violation was identified for inadequate Engineered Safeguards (ESF)

testing procedures, in that, they allowed ESF trains to be inoperable

for testing, without invoking a Technical Specification .action statement

(Section M3.1).

A Non-Cited Violation was identified for an inadequate Safety Injection

system check valve test procedure which allowed a testing configuration

that placed the Safety Injection system in a condition outside its

design basis. An Unresolved Item was identified to determine whether

the licensee needed to supplement a Licensee Event Report involving this

issue (Section M8.1).

Engineering

Efforts to strengthen the predictive maintenance program was determined

to be achieving the desired results. A critical self assessment was

performed by the licensee that identified areas of improvement. The

licensee is in the process of developing a program document

(Section E2.1).

Plant Support

A security Hand Geometry system equipment failure was being adequately

investigated. Security personnel failed to properly implement

compensatory measures resulting in an employee whose security badge was

not currently active being allowed to enter the Protected Area (Section

S2.1).

The performance by the fire brigade during a drill was satisfactory and

significantly improved from that observed in October 1996. The use of

additional fire drill props improved fire drill realism and aided the

fire brigade leader in assessing conditions. The fire brigade response

was aggressive and communication and guidance to the off-site fire

department personnel was good (Section F5).

Report Details

Summary of Plant Status

Unit 2 remained at power the entire inspection period. Power was reduced to

approximately 50 percent on April 14 to replace the upper oil cooler to the

"A"

Condensate Pump motor. Power was reduced to approximately 95 percent on

April 17 to assess root cause of minor feedwater oscillations.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspector conducted periodic control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspector attended daily operations turnover,

management review, and plan-of-the-day meetings to maintain awareness of

overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious. Good plant equipment material conditions and housekeeping

was noted throughout the report period. Specific events and noteworthy

observations are detailed in the sections below.

01.2 Downpower to Repair Condensate Pump Oil Cooler Leak (71707)

a. Inspection Scope

On April 14, 1997, at approximately 1:55 a.m., a downpower to 50 percent

power was initiated to repair a service water leak in the upper oil

cooler to the "A"

Condensate Pump motor.

b. Observations and Findings

The leak was identified by maintenance personnel through the routine oil

sampling program. In order to prevent a motor failure, the licensee

decided to reduce power to remove the pump from service and replace the

oil cooler. Operators properly controlled the downpower and stabilized

the plant at 50 percent power.

Following the downpower, the heater drain pumps were secured to support

troubleshooting of the Heater Drain Tank Level Controller, LC-1530,

which was not controlling level within the optimum range. During the

troubleshooting, the level control signal failed high causing a

feedwater/condensate transient. The operators used abnormal operating

2

procedures effectively to take manual control of heater drain tank and

condenser hotwell level in order to restore plant conditions to normal.

The transient demonstrated, however,,a weakness in contingency action

planning and understanding of the potential adverse impact of the

troubleshooting activity.

c. Conclusions

The inspector concluded that plant operators appropriately controlled

the downpower evolution and adequately responded to the feedwater/

condensate transient. The transient was caused by troubleshooting

activities on the.heater drain tank level controller and indicated a

weakness in contingency action planning and understanding of the

potential adverse impact of the activity on the plant.

06

Operations Organization and Administration

06.1 Management Changes (71707)

a. Inspection Scope

The licensee announced several management changes during this report

period.

b. Observations and Findings

The management changes announced by the licensee included:

John S. Keenan who was promoted to Site Vice President upon departure of

Scotty Hinnant to Brunswick; Dale Young was promoted to be the Director

of Site Operations, and John Boska was selected as the Operations

Manager due to the departure of Bruce Meyer to assume a position at

Harris Nuclear Plant. The licensee plans to name the new Plant Manager

in the near future. Additionally, Talmage Clements replaced John Boska

as the Superintendent for Design Control, and Jim Hendrickson was

promoted to Supervisor for Reactor Systems within the Robinson

Engineering Support Section (RESS).

c. Conclusions

The inspector will followup and update upon the announcement of the new

PlantManager.

07

Quality Assurance In Operations

07.1. Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

(40500)

a. Inspection Scope

The inspector evaluated certain activities of the Plant Nuclear Safety.

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

3

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed

understanding of the issues and potential risks. Further, the inspector

reviewed NAS audits and concluded that they were appropriately focused

to identify and enhance safety.

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meeting topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

08

Miscellaneous Operations Issues (92901)

08.1 (CLOSED) Licensee Event Report (LER) 50-261/96-003-00, Condition

Prohibited by Technical Specifications Due to Failure to Maintain Shift

Compliment: This LER promulgated the condition described in Non-Cited

Violation (5-261/96-10-01), documented in NRC Inspection Reports 50

261/96-10 and 50-261/96-11, in which a licensed Senior Reactor Operator

stood seven shifts without a current biannual medical examination.

In response to the event, the licensee initiated and committed to

the following corrective actions: revise operations procedures

OMM-001-1, Operations Unit Organization and Administration, and

OMM-001-5, Training and Qualifications, to require monitoring and

reporting of the medical status of all operators and personnel

assigned to the fire brigade in the Operator Hours Tracking Log.

The inspector reviewed the Operator Hours Tracking Log and

verified that the medical qualifications of the April 1997

operations personnel was up-to-date. The inspector reviewed these

completed corrective actions and determined that they were

completed satisfactory. This item is closed.

08.2 (CLOSED) LER 50-261/96-004-00, Manual Initiation of Reactor Protection

System (RPS) due to Turbine Governor Valve Failure: This LER described

the manual reactor trip that occurred on-September 7, 1996. This event

was discussed previously in section 01.4 of NRC Inspection Report

50-261/96-11. The inspector determined that the licensee had adequately

determined the root cause of the trip and corrected the equipment

related failure.

4

The inspector reviewed the licensee's corrective actions which included

the addition of angle mounts and weather covers to the turbine governor

valve actuators to eliminate looseness and broken bolts, soldering and

covering the wire terminations with heat shrink protective shields, and

revisions to relevant maintenance work instructions to caution workers

of the fragile wires in the valves. The inspector determined that

adequate corrective actions were completed. This item is closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments (61726 and 62707)

a. Inspection Scope

The inspector observed all or portions of the following maintenance

related Work Requests/Job Orders (WRs/JOs) and surveillances and

reviewed the associated documentation:

WR/JO 97-ABFZ1

Repair Pressurizer Pressure Control

Station,

WR/JO 97-ABKM1

Implement Modification.ESR 97-00198 to

Provide Alternate Reactor Containment Sump

Discharge Flowpath,

WR/JO 97-ABII1

Investigate Tripping of "B"

Control Rod

Drive Motor Generator Breaker,

WR/JO 97-ABGH1/2

Repair Leak on Emergency.Diesel Generator

A Standby Circulating Coolant Pump,

WR/JO 97-ACIR1

Auxiliary Feedwater to "C" Steam Generator

Transmitter FT-1425C Calibration,

OST-902

Containment Fan Coolers Component Test,

Revision 24, and.

SP-1388

Containment Isolation Valves Leakage Test

for WD-1722, Revision 0.

b. Observations and Findings

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks. Work

and surveillance procedures were present at the work location and being

adhered to. Procedures provided sufficient detail and guidance for the

intended activities. Detailed plans were developed with good support

from engineering for troubleshooting activities associated with the

pressurizer pressure control malfunction and control rod drive motor

5

generator trip. Activities were properly authorized and coordinated

with operations prior to start. Test equipment in use was calibrated,

procedure prerequisites were met, system restoration was completed, and

surveillance acceptance criteria were met. Specific observations and

details for several of these activities included the following:

WR/JO 97-ABKM1: This activity was associated with the implementation of

a temporary modification to provide an alternate flowpath from the

reactor containment sump pumps to the Waste Holdup Tanks. The alternate

flowpath involved connecting a pressure rated fire hose from the

discharge vent on the sump pumps to a vent valve in the reactor coolant

drain tank pump suction line which also discharged to the Waste Holdup

Tanks. The inspector observed a minor problem when maintenance

personnel tied off the hose to the incorrect line. A different line for

this purpose had been seismically evaluated and was specified in the

modification implementing procedure. The inspector alerted the engineer

who was monitoring the activity and the discrepancy was corrected.

Since the problem was corrected prior to the actual signoff and

completion of the job, the inspector determined that a procedural

violation had not occurred. The inspector concluded that this problem

was an example of lack of attention to detail on the part of maintenance

personnel in following the work instructions and poor engineering

personnel overview of the activity which allowed the condition to go

uncorrected until questioned by the inspector.

WR/JO 97-ABGH1/2: While mechanical maintenance personnel were

completing the installation of a new circulating water coolant pump and

motor assembly on the "A"

Emergency Diesel Generator, the inspector

noted that the instructions in WR/JO 97-ABGH2 required that

Instrumentation and Control (I&C) perform an electrical resistance check

of the motor following installation. The WR package, however, did not

include a copy of the procedure for performing the motor check and the

I&C technician who was about to start electrical connection of the motor

was not aware that the test was prescribed in the WR instructions.

Following discussions with hi.s supervisor, the I&C technician obtained

the procedure and completed the test. The inspector concluded that this

minor problem demonstrated a need for better understanding of the work

scope by the I&C personnel involved.

c. Conclusions

The inspector concluded that maintenance and surveillance activities

were performed satisfactorily. In general, good work control and

coordination was observed, however, several minor problems were

identified indicating a need for greater attention to detail in

following work instructions and understanding the work scope prior to

implementation.

6

M3

Maintenance Procedures and Documentation

M3.1 Engineered Safeguards Periodic Surveillance (71707, 61726)

a. Inspection Scope

The inspector observed portions of maintenance surveillance test (MST)

procedure MST-23, Safeguards Relay Rack Train "B" (Monthly). MST-23 and

MST-22, Safeguards Relay Rack Train "A" (Monthly) implement the Robinson

TS, Section 4.1, Operational Safety Review, Table 4.1-1, Item 27

requirements to monthly test the Engineered Safeguards Features (ESF)

logic circuitry.

  • b. Observation and Findings

The inspector noted that during the performance of MST-22 and MST-23, no

TS action statement was considered applicable by the control room

operating crew. During the performance of MST-22, portions of the

automatic actuation capability associated with ESF Train "A"

was

sequentially bypassed to accommodate logic testing, thus precluding

starting the respective ESF Train "A"

components. The performance of

MST-23 had a similar effect on Train "B".

Upon further discussion, the

inspector was informed that Robinson TS did not specifically prescribe

an action statement during ESF logic testing, and consequently, an

action statement had never been considered to be in effect.

The inspector reviewed the standard Westinghouse TS and confirmed that

it prescribed a very restrictive action statement of two hours to bypass

each ESF train during testing. The restrictive action statement was

based on one train of multiple ESF components being out-of-service

simultaneously. The inspector discussed this with the licensee.

The licensee reviewed the issue and deliberated whether to enter TS 3.0

during the future performance of MST-22 and MST-23. The licensee then

made a decision that TS 3.6.3.d associated with automatic containment

isolation valves would be more appropriate. This TS prescribes a four

hour action statement and was the most restrictive.action statement

affecting ESF components. This effectively allowed four hours to bypass

each ESF trains for testing. A Night Order related to this issue was

issued, in addition to a condition report. The inspector noted that

during the TS conversion to the new improved standard TS this item was

not identified.

c. Conclusions

The inspector concluded that procedures MST-22 and MST-23 were

inadequate, in that, they allowed ESF trains to be inoperable for

testing, without invoking a TS action statement. -The problem

constituted a violation of TS 6.5.1.1.1, Procedures, Tests, and

Experiments. This issue will be documented as Violation (VIO)

50-261/97-06-01: Inadequate Safeguards Procedures that Allowed ESF Train

Being Out-of-Service Without Invoking a TS Action Statement.

7

M8

Miscellaneous Maintenance Issues (92902)

M8.1 (CLOSED) LER 50-261/95-01-00, Safety Iniection Pump Testing Requires TS 3.0 Entry: The licensee identified that the past test configuration for

ASME Section XI Inservice surveillance testing of Safety Injection (SI)

system pump discharge check valves potentially rendered the SI system

inoperable. During partial forward flow testing of the SI pump

discharge check valves (SI-879A B, and C) in accordance with Operations

Surveillance Test (OST) procedure OST-151. Safety Injection System

Components Test, the procedure aligned the normally closed SI test line

to the SI pump discharge header. In this configuration, adequate SI

system flow to the reactor core could not be assured during all design

bases accidents since a portion of the flow would be diverted to the

Refueling Water Storage Tank through the SI test line. As an interim

measure until the issue could be resolved, the licensee entered the

action statement of TS 3.0 on three occasions to complete quarterly

scheduled testing of each of the three SI pump discharge check valves.

The licensee's corrective actions included evaluating the test

configuration to determine if the SI system was actually inoperable with

the SI test line open. The inspector reviewed engineering calculation

RNP-M/MECH-1556, Revision 1, dated April 25, 1995. The results of this

calculation indicated that design SI flow rates would still be

maintained to the Reactor Coolant System (RCS), even with the SI test

line open. However, with a single SI pump in operation, and RCS

pressure near atmospheric conditions, the.increased flow rate would

result in the pump exceeding its runout flow rate. Based on this, the

licensee determined that there was adequate justification for changing

the check valve test frequency from quarterly to a Cold Shutdown and

Refueling Outage interval. The inspector reviewed Technical Management

Manual (TMM) procedure TMM-004, Inservice Inspection Testing, Revision

14, and verified that the change to the testing frequency was properly

documented. In addition, the inspector verified via completed check

valve test data and startup procedures that the valves were being tested

at refueling outage intervals and were scheduled for testing during cold

shutdown conditions. This LER is closed.

The inspector determined that, prior to the licensee recognizing the

adverse test configuration, procedure OST-151 was not appropriate to the

circumstances, constituting a violation of 10 CFR 50, Appendix B,

Criterion V, Procedures. This licensee-identified and corrected

violation is being treated as a Non-Cited Violation (NCV), consistent

with Section VII.B.1 of the NRC Enforcement Policy. This issue will be

documented as NCV 50-261/97-06-02: Inadequate SI Pump Discharge Check

Valve Testing Procedure.

During review of this LER, the inspector noted that a supplement to the

existing LER had not been submitted to the NRC in order to report the

results of the SI operability determination. The past operability

evaluation had concluded that the SI system would have operated at

runout conditions resulting in the inoperability of the system. The

inspector believed that a supplement to the LER, reporting the

8

inoperability, had been required. At the end of the report period, the

licensee had not completed their review to determine whether an LER

supplement was warranted. This issue was identified as Unresolved Item

(URI) 50-261/97-06-03: Review Licensee Assessment of Need to Supplement

LER 50-261/95-001-00.

M8.2 (CLOSED) LER 50-261/96-007-00, Automatic Initiation of RPS Due to Steam

Generator Feedwater Level Control System Failure: On October 20, 1996,

an automatic reactor trip occurred from 20 percent power during startup

from Refueling Outage 17. The reactor trip occurred on Steam Generator

high water level after the "B"

feedwater regulating valve

automatic/manual control station failed to properly control steam

generator level.

During the previous inspection report period covering

the date of this trip, the inspector reviewed the licensee's post-trip

report and plant data 'to ensure that plant equipment operated properly

in response to the trip. With the exception of several minor operator

training enhancements, no problems were identified.

The licensee was unable to determine the exact cause of the controller

failure and concluded that the most likely failure mechanism was

controller aging. The "B"

feedwater automatic/manual control station

was replaced and no further problems were experienced. As part of the

licensee corrective actions, the event was reviewed with all licensed

operators during subsequent routine operator training. Preventive

maintenance procedures were implemented to perform periodic diagnostic

testing of automatic/manual control stations to detect potentially

degrading controllers. The inspector determined that adequate

corrective actions were completed. This LER is closed.

III. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1 Predictive Maintenance (37551)

a. Inspection Scope

The inspector reviewed licensee activities relating to the predictive

maintenance program.

b. Observations and Findings

During this report period, as a result of the predictive maintenance

program, the licensee identified several components that were showing

degradation. Oil analysis from the "A"

Safety Injection pump's outboard

bearing indicated an increasing trend in iron and wear particles. The

pump bearing was replaced. Additionally, the "B"

Spent .Fuel Cooling

Pump was refurbished based on vibration and oil analysis indicating a

negative trend.

9

The licensee has recently employed a supervisor/engineer whose is also

responsible for the coordination of the predictive maintenance program.

Efforts are also under way to develop a predictive maintenance program

guidance/procedure to better coordinate future activities.

c. Conclusions

The inspector concluded that efforts are under way to further strengthen

the predictive maintenance program. A critical self assessment was

performed by the licensee that identified areas for improvement. The

licensee is in the process of developing a program document.

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspection

discussed in this report, the inspector reviewed selected portions of

the UFSAR that related to the areas inspected. The inspector verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues (92903)

E8.1 (CLOSED) Violation 50-261/96-10-01, Inadequate Corrective Actions for

Solenoid Operated Valve (SOV) Design Discrepancies: This violation

involved inadequate licensee corrective actions to address configuration

control problems associated with air-operated SOVs being overpressurized

beyond their design limits. In 1988, the licensee failed to adequately

evaluate whether problems existed at Robinson after being alerted to the

potential problem via NRC Information Notice 88-24, Failures of Air

Operated Valves Affecting Safety-Related Systems. Following a

subsequent review of the Information Notice in 1995, the licensee again

failed to adequately evaluate the extent of condition, or determine the

operability impact of 14 safety-related SOVs that were identified with

operating pressure exceeding their design limits.

The licensee responded to the violation by letter dated October 13,

1996. The root cause was attributed to personnel failure to follow

operating experience and corrective action procedures after conditions

adverse to quality were identified. The inspector reviewed these

procedures and determined that they had been enhanced to provide more

specific guidance to plant personnel if potential operability concerns

are identified. In addition, engineering personnel were provided real

time training to emphasize management expectations in this area.

The licensee conducted an evaluation of all safety-related and non

safety-related SOVs to identify and evaluate any SOVs in applications

10

where their design pressure limits were exceeded. The inspector

reviewed the results of this evaluation and determined that it was

comprehensive and detailed. Discrepancies identified by the licensee

were being adequately resolved. This item is closed.

E8.2 (CLOSED) Inspector Followup Item (IFI) 50-261/96-12-03, Review Licensee

Justification for not Completing Non-Validated DBD and GID Evaluations:

This issue was raised during a review of licensee corrective actions for

Violation 50-261/94-23-01 involving the failure to properly revise plant

documents based on the results of a non-validated Containment Isolation

Generic Issue Document (GID) evaluation. Initial licensee corrective

actions for this violation had been to implement a procedure to ensure

that plant personnel perform formal reviews of non-validated GIDs and

Design Basis Documents (DBDs) to .ensure that there were no other plant

documents that needed revision. However, only one non-validated DBD

involving the Main Steam System was.formally reviewed. Since the

results of this review did not identify any documents that needed

revision, the licensee believed it unlikely that there were any other

problems with the other 14 non-validated GIDs and DBDs. Based on this,

the licensee decided not to perform a formal review of the remaining

documents.

The inspector did not consider this adequate justification for not

completing the original scope of the corrective actions for Violation

50-261/94-23-01. During subsequent discussions with the licensee

concerning this matter, the licensee committed to complete the review of

all other non-validated GIDs and DBDs. The inspector reviewed CP&L

letter dated February 11, 1997, which provided the licensee's response

to the NRC's request pursuant to 10 CFR 50.54(f) regarding the adequacy

and availability of design bases information at CP&L nuclear plants. As

part of their enhancements to provide additional assurance that the

plant's design bases had been incorporated into the design, operation,

and maintenance of the plant, the licensee committed to complete the

review of all other non-validated GIDs and DBDs by October 15, 1998.

Based on this commitment, the inspector concluded that this IFI was

closed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls (71750)

R1.1 Tours of the Radiological Control Area (RCA)

The inspector periodically toured the RCA during the inspection period.

Radiological control practices were observed and discussed with

radiological control personnel including RCA entry and exit, survey

postings, locked high radiation areas, and radiological area material

conditions. The inspector concluded that radiation control practices

were proper.

Si

Conduct of Security and Safeguards Activities (71750)

51.1 General Comments

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion or

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

S2

Status of Security Facilities and Equipment

S2.1 Plant Access Control Equipment Problem and Compensatory Measure

Deficiency (71750)

a. Inspection Scope

The inspector reviewed licensee actions to resolve an operability

problem with the security Hand Geometry system. The inspector also

reviewed the licensee's preliminary investigation into an employee being

allowed to enter the Protected Area (PA) with an inactive security badge

while compensatory measures were being implemented for inoperable hand

geometry equipment.

b. Observations and Findings

On April 6, 1997, the security Hand Geometry system malfunctioned

resulting in the licensee declaring the system inoperable. Compensatory

measures were implemented for controlling personnel entry into the PA.

These measures included assignment of two security personnel at the PA

entry point with post orders to check two forms of personnel

identification for each individual seeking entry into the PA and

verifying each individual was on the authorized access list.

On April 8, while these compensatory measures were still active, an

employee whose security badge was not currently active was allowed to

enter the PA. The employee's badge had been terminated by mistake on

March 27, while the employee was on sick leave. Upon entering the PA,

the employee contacted the Fitness For Duty organization to determine

whether any testing was necessary for returning to work. At this time,

Fitness For Duty personnel identified that the employee's badge had been

terminated. After contacting security, the employee was located and

escorted out of the PA. The employee had been in the PA for

approximately twelve minutes unescorted.

The licensee initiated an investigation of the incident and checked the

access authorization status of all other personnel granted plant access

since implementing the compensatory measures to ensure that no other

12

instances of this type had occurred. No further instances were

identified. The licensee determined that the two security personnel

assigned at the PA entry point failed to verify the individual's access

levels prior to allowing the individual access to the PA. Each of the

two security persons involved in the incident had assumed that the other

person had performed the required access verification indicating a lack

of clear assignment of task responsibility. Following the incident, the

licensee revised the post orders to include specific assignment of the

tasks between security personnel assigned to this post. The inspector

periodically observed implementation of the revised post orders to

verify adequate security personnel performance. No other problems were

identified. The licensee plans to submit an LER for the unauthorized

entry. The inspector will review completion of the licensee's

investigation and corrective actions during review of the LER.

The malfunction in the Hand Geometry system involved an intermittent

problem with the transfer of employee.hand profile data between the

turnstyle hand readers and the main security computer. On April 17, the

problem was temporarily corrected and the system was placed back in

service. The inspector determined that the problem did not involve the

potential for an unauthorized individual to gain access due to hand

geometry reading errors. At the end of the report period, the licensee

was continuing troubleshooting and discussions with the vendor to fully

understand and prevent any future data transfer problems.

c. Conclusions

The inspector concluded that the licensee was adequately investigating

the cause of the Hand Geometry system failure. Security personnel

failed to properly implement compensatory measures for the inoperable

equipment resulting in an employee whose.security badge was not

currently active being allowed to enter the Protected Area. Further

review and enforcement disposition of this incident is planned during

followup of the LER.

F5

Fire Protection Staff Training and Qualification (71750)

F5.1 Fire Drill (71750)

a. Inspection Scope

On April 15, 1997, at 8:00 p.m., the inspector witnessed an announced

backshift fire brigade drill (Fire Drill Number 97-2Q-01-SHIFT-2) with

assistance of the local off-site fire department located in Hartsville,

South Carolina.

b. Observations and Findings

The fire drill simulated a lubricating oil spill of approximately 150

gallons with a fire involving two levels of the Unit 2 Turbine Building

(Plant Fire-Area "G" - Fire Zone 25). The simulated fire involved the

Unit 2 turbine lubricating oil reservoir and filter pumps.

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The inspector observed the drill controllers at the site directing the

fire drill.

The drill was conducted using fire drill planning guide

FBS-01R. The licensee used fire drill props such as tape to simulate

the oil spill area, strobe lights to identify the involved fire areas of

both the lower and second level turbine decks, computer generated

pictures to define the fire status and a device that produced fog for

simulation of smoke.

The control room sounded the plant fire alarm within two minutes of the

report of the simulated fire. The Unit 2 fire brigade team leader and

four fire brigade members responded promptly in full protective clothing

with appropriate fire fighting equipment. Additional personnel from

Unit 2 operations, security and the Hartsville Fire Department, who were

pre-staged onsite, also responded to the drill.

An offensive fire

attack was mounted utilizing two 1/2-inch attack foam fire hose lines

from opposite sides of the fire on the lower level turbine deck,

followed by additional 1/2-inch foam lines extended to the second level

turbine deck. The fire brigade leader properly deployed the fire

brigade personnel, established a command post and effectively used radio

communications. The control room properly used the fire protection Pre

Plans, OMM-003, and simulated tripping the plant due to potential fire

damage. A drill critique was conducted with the fire brigade members

following the drill to discuss the drill, participants performance and

recommendations for improvements. The drill objectives were met.

c. Conclusions

The inspector concluded the drill was performed in a controlled manner

and provided realistic training for the fire brigade. The drill

scenario was challenging. Fire brigade performance has improved.

During observation of a fire drill, the brigade exhibited good command

and control, fire ground tactics, and recovery operations.

V. Management Meetings

X1

Exit Meeting Summary

The inspector presented the inspection results to members of licensee

management at the conclusion of the inspection on May 1, 1997. The

inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information

was identified.

X3

Management Meeting Sumary

On March 25, 1997, the licensee was presented the results of the NRC

Systematic Assessment of Licensee Performance (SALP) results by the

Region II

Regional Administrator, Luis A. Reyes. The presentation was

open to the public, as well as local officials. The licensee received a

SALP 1 rating in Operations and Plant Support and a SALP 2 rating in

Engineering and Maintenance.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

H. Chernoff, Supervisor, Licensing/Regulatory Programs

J. Clements, Manager, Site Support Services

D. Crook, Senior Specialist, Licensing/Regulatory Compliance

J. Keenan, Vice President, Robinson Nuclear Plant

D. Winters, Acting Manager, Operations

G. Miller, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director, Site Operations

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

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INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened.

Ijye Item Number Status

Description and Reference

VIO

50-261/97-06-01

Open

Inadequate Safeguards Procedures that

Allowed ESF Train Being Out-of-Service

Without Invoking a TS Action Statement

(Section M3.1)

NCV

50-261/97-06-02

Open

Inadequate SI Pump Discharge Check Valve

Testing Procedure (Section M8.1)

URI

50-261/97-06-03

Open

Review Licensee Assessment of Need to

Supplement LER 50-261/95-001-00 (Section

M8.1)

Closed

lype

Item Number Status

Description and Reference

LER

50-261/96-003-00 Closed

Condition Prohibited by Technical

Specifications Due to Failure to Maintain

Shift Compliment (Section 08.1)

LER

50-261/96-004-00 Closed

Manual Initiation of Reactor Protection

System (RPS) due to Turbine Governor Valve

Failure (Section 08.2)

LER

50-261/95-001-00 Closed

Safety Injection Pump Testing Requires TS 3.0 Entry (Section M8.1)

NCV

50-261/97-06-02

Closed

Inadequate SI Pump Discharge Check Valve

Testing Procedure (Section M8.1)

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LER

50-261/96-007-00 Closed

Automatic Initiation of RPS Due to Steam

Generator Feedwater Level Control System

Failure (Section M8.2)

VIO

50-261/96-10-01

Closed

Inadequate Corrective Actions for Solenoid

Operated Valve (SOV) Design Discrepancies

(Section E8.1)

IFI

50-261/96-12-03

Closed

Review Licensee Justification for not

Completing Non-Validated DBD and GID

Evaluations (Section E8.2)

Discussed

Type Item Number

Status

Description and Reference

None