ML14181A785

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Insp Rept 50-261/95-27 on 950917-1021.Violations Noted.Major Areas Inspected:Plant Operations,Maint Activities, Engineering Efforts & Plant Support Functions
ML14181A785
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 11/17/1995
From: William Orders, Shymlock M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A783 List:
References
50-261-95-27, NUDOCS 9512110103
Download: ML14181A785 (17)


See also: IR 05000261/1995027

Text

  • .pR REG&

UNITED STATES

0 oNUCLEAR

REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/95-27

Licensee:

Carolina Power & Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted:

September 17 - October 21, 1995

Lead Inspector:

__11-17-95

W. T. Orders,

0enior Revsident Inspector

Date Signed

Other Inspector:

J. Zeiler, Resident Inspector

Approved by:

O>L

11-17-95

Milton B. ShymocW, Chief

Date Signed

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

SCOPE:

This routine, resident inspection was conducted in the areas of plant

operations, maintenance activities, engineering efforts, and plant support

functions. As part of this effort, backshift inspections were conducted.

RESULTS:

In the Plant Operations area, one violation was identified involving an

inadequate clearance for removing the B Emergency Diesel Generator from

service. While implementing this clearance, the engine air start piping was

depressurized through the engine's air start distributor causing the engine to

unexpectedly start and run without normal engine support equipment properly

aligned (paragraph 3.a).

9512110103 951117

PDR

ADOCK 05000261

a

PDR

REPORT DETAILS

1.

PERSONS CONTACTED

Licensee Employees:

  • B. Baum, Director, Human Resources
  • M. Brown, Superintendent, Design Control
  • P. Cafarella, Superintendent, Mechanical Systems
  • G. Castleberry, Manager, Plant Electrical Engineering
  • B. Clark, Manager, Maintenance

T. Cleary, Manager, Mechanical Maintenance

  • D. Crook, Senior Specialist, Licensing/Regulatory Compliance

C. Gray, Manager, Materials and Contract Services

  • D. Gudger, Senior Specialist, Licensing/Regulatory Programs
  • M. Herrell, Manager, Training
  • C. Hinnant, Vice President, Robinson Nuclear Plant

P. Jenny, Manager, Emergency Preparedness

  • J. Keenan, Director, Site Operations
  • R. Krich, Manager, Regulatory Affairs

E. Martin, Manager, Document Services

  • B. Meyer, Manager, Operations
  • G. Miller, Manager, Robinson Engineering Support Services
  • H. Moyer, Manager, Nuclear Assessment Section

B. Steele, Manager, Shift Operations

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Manager, Plant Support Nuclear Assessment Section

  • D. Whitehead, Manager, Plant Support Services
  • T. Wilkerson, Manager, Environmental Control
  • D. Young, Plant General Manager

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Personnel:

  • W. Orders, Senior Resident Inspector
  • J. Zeiler, Resident Inspector
  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

PLANT STATUS AND ACTIVITIES

Operating Status

The unit operated at or near full power for the entire report period.

2

3.

OPERATIONS

a.

Plant Operations (NRC Inspection Procedure 71707)

The inspectors evaluated licensee activities to determine if the

facility was being operated safely and in conformance with

regulatory requirements. These activities were assessed through

direct observation of ongoing activities, facility tours,

discussions with licensee personnel, evaluation of equipment

status, and review of facility records. The inspectors evaluated

the operating staff to determine if they were knowledgeable of

plant conditions, responded properly to alarms, and adhered to

procedures and-applicable administrative controls. Selected shift

changes were observed to determine that system status continuity

was maintained and that proper control room staffing existed.

Routine plant tours were conducted to evaluate equipment

operability, assess the general condition of plant equipment, and

to verify that radiological controls, fire protection controls,

physical protection controls, and equipment tagging procedures

were properly implemented.

Emergency Diesel Generator B Unexpected Start During Tagout

On September 26, while operations personnel were in the process of

implementing LCTR 95-01384 for removing the B EDG from service for

scheduled maintenance, the engine started unexpectedly. The

engine ran for approximately 7 minutes until shutdown locally by

tripping the engine fuel racks.

Prior to the start, normal engine support equipment such as pre

lube and cooling water had been isolated in accordance with the

clearance. Due to this, the licensee performed an evaluation to

ensure that no engine damage had occurred during the event. This

evaluation was conducted with assistance from the engine

manufacturer. The inspectors reviewed the results of this

evaluation and discussed details with the EDG system engineer.

The engine manufacturer identified one area of concern involving

the engine lube oil system. Since the lube oil strainer drain

valve was open when the engine started, the manufacturer indicated

that the lube oil filters could have deformed under the increased

oil system flow condition. Subsequent inspection of these filters

revealed that there was no damage; however, as a preventative

measure, they were replaced. Following the completion of

maintenance and inspection, the engine was tested successfully and

returned to service without further complications. The inspectors

determined that the licensee's evaluation and testing was

adequate, although, greater consideration should have been given

for the potential damage to the air start distributor. During the

event, air was not automatically isolated to the distributor

shortly after startup as would occur on a normal start.

Increased

wear and potential damage to the internal valves and springs in

3

the distributor can occur if air is continuously admitted to

distributor. Subsequently, the licensee evaluated in greater

detail the potential for this to occur. The results of this

evaluation determined that there was not sufficient air volume

admitted during the event to damage the distributor.

The inspectors reviewed the initial operator responses to the

event. Upon hearing the engine start, an Auxiliary Operator who

was outside the EDG room contacted the control room and was

instructed to close the manual air start isolation-valves (to

prevent any further chance of air entering the engine) and then to

shutdown the engine from the local control panel.

The Auxiliary

Operator closed the air start valves, but was unsuccessful in

shutting the engine down from the local control panel.

This

should have been expected since prior steps in the clearance had

de-energized electrical power to the control panel, thus,

disabling the normal shutdown capability. In a subsequent call to

the control room, the Auxiliary Operator was instructed to close

the fuel racks, which was successful in stopping the engine. The

inspectors determined that shutdown of the engine could have been

accomplished sooner if the control room operators had been more

familiar with details of the clearance. However, since the engine

did not experience any damage during the event, the inspectors

concluded that the extra time involved did not adversely impact

the engine during this event.

The inspectors reviewed LCTR 95-01384, the sequence of events for

the unexpected engine start, and discussed the event with the

operators involved. The clearance was developed to remove the

engine from service in order to conduct an annual inspection and

general engine work. One of these work items included the

replacement of valve, DA18B, located in the engine's air start

system piping. DA18B is the upstream manual isolation valve to

one of the two parallel air start solenoid valves (DA19B) that

open on an engine start signal and allow the admission of

compressed air into the air start distributor which starts the

engine. The individual preparing the clearance selected upstream

air start valves DA14B and DA28 as the isolation boundary for

DA18B. This boundary configuration allowed a 65 foot section of 2

and 2.5 inch air start piping to remain pressurized directly

upstream of the air start solenoid valve DA19B. When DA19B was

deenergized in accordance with the clearance, it failed open

allowing the residual compressed air that was contained within the

isolation boundary to be admitted into the engine's air start

distributor. The clearance preparer indicated that he understood

that deenergizing the air start solenoid valves would vent air

trapped in the air start piping through the air start distributor.

A decision was made when the clearance was being prepared that

there was not enough isolated air volume to start the engine. The

inspectors noted that this decision was not based on a clear

understanding of the actual length of piping or volume involved

and a walkdown of the piping had not been performed.

4

The inspectors also reviewed procedure OMM-05, Clearance and Test

Request, which provides the requirements for properly isolating

equipment that is being removed from service. Section 5.1 of this

procedure requires that systems which normally operate at

temperatures and pressures above ambient condition shall be vented

and drained if necessary for the work to be performed. Further,

the procedure requires that vent and drain valves used to

depressurize a system should be tagged in the open position. The

inspectors determined that this procedure was not followed, in

that, proper provisions for depressurizing the air start piping,

such as opening a high point vent valve within the isolation

boundary, or loosening an existing flange in the piping, was not

considered or utilized in the clearance.

TS 6.5.1.1, Procedures, Tests, and Experiments, requires in part,

that written procedures be established, implemented, and

maintained, covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev. 2, 1978, including procedures for

controlling the clearance of safety-related equipment.

Contrary to the above, LCTR 95-01384 was inadequate in that, it

did not provide adequate instructions for ensuring that the ai.r

start system piping associated with the B EDG was properly

isolated and depressurized. This issue is considered a violation

of the requirements of TS 6.5.1.1 and is identified as Violation

50-261/95-27-01:

Inadequate Clearance Results in Unexpected

Emergency Diesel Start.

During review of this event, the inspectors recalled a similar

event involving an inadequate clearance that occurred on April 17,

1995, during maintenance on valve V1-18A, steam supply valve. The

clearance boundary for this work failed to properly isolate the

steam supply to the Steam Driven Auxiliary Feedwater Pump

resulting in it inadvertently starting. This issue was one of

three examples of Violation 95-19-01, addressed in NRC Inspection

Report 50-261/9519, dated July 17, 1995. The inspectors reviewed

CR 95-00961 which addressed this event. Corrective actions

included counseling the clearance preparer and enhancing the model

clearances for future work on valve VI-18B. The inspectors noted

that this CR had been classified as "Non-Significant," therefore,

a formal root cause evaluation was not performed. The inspectors

considered the effectiveness of corrective actions for this event

to have been questionable as result of the similarity to the

clearance problems identified with the unexpected EDG start. Both

of these issues involved improper clearance assumptions. The

licensee indicated that the root cause evaluation for the EDG

start event would address the corrective action for the clearance

program.

5

Control Room Instruments Affected by Radio Usage

The inspectors noted on several occasions during routine control

room tours, that hand held radio transmissions, seemed to be

having an adverse effect on the trace of the unit electrical

output chart recorder. When the inspectors asked the operators

about these observations, they were told that indeed the radios

did have an effect on the chart recorder, but to their knowledge,

no other control room equipment seemed to experience interference

from the radios. The inspectors also identified to operations

management that a sign which had been previously posted on the

door leading from the control room to the adjoining protection

electronics equipment (Hagan) room, warning that radios were not

to used inside, had been removed. This was identified to the

operations management.

The inspectors discussed this issue with the engineering staff to

determine if there was a formal program in place to address radio

frequency interference. The licensee informed the inspectors that

there was no formal program, and initiated a condition report to

facilitate an evaluation of the problem. At the end of this

report period, the licensee's efforts to address this issue are

incomplete, and will be addressed in the next report.

Housekeeping Discrepancies with Potential Seismic Impact

During a walkdown of the Hagan Room, the inspectors noted that

electrical test equipment and furniture (e.g., chair, file

cabinet, table, and ladder) were in close proximity to the reactor

protection system cabinets. The inspectors questioned engineering

personnel whether this unsecured material had been evaluated with

regards to its potential seismic interaction with the reactor

protection cabinets. They recalled performing seismic evaluations

for the furniture in the past, but were unable to provide this

documentation. Licensee engineering personnel conducted a

walkdown of the Hagan room. Several of the unsecured items were

removed or relocated, including the electrical test equipment.

The licensee initiated CR 95-02419 to address the improper storage

of this equipment. They determined that none of the items had

been close enough to be a significant interaction threat to the

reactor protection cabinets. The inspectors agreed with this

assessment, but, concluded that general housekeeping control of

electrical test equipment could be improved in this area. Based

on these observations and discussions with I&C personnel who

perform protection system testing in the Hagan room, there was not

a good understanding of the potential seismic impact when

storing/placing equipment or material near safety-related

equipment.

The inspectors reviewed procedures AP-02, Plant Conduct of

Operations, and, AP-10, Housekeeping Instructions, which describe

the plant housekeeping requirements for controlling work

6

activities, conditions, and environments. While these procedures

require that all employees properly store loose work items, it did

not provide guidance for evaluating the seismic acceptability of

storing/locating unsecured tools/material near safety-related

equipment. The inspectors discussed these observations with plant

management and reviewed the planned corrective actions for CR 95

02419. Specific corrective actions included the following: 1)

perform plant walkdowns to identify material which may represent a

seismic concern, 2) provide instructions for evaluating the

placement of unsecured equipment around safety-related equipment,

3) establishing storage areas for unsecured equipment, and, 4)

providing training to all plant personnel on the new guidance.

The inspectors concluded that these corrective actions were

comprehensive toward heightening plant personnel and management

awareness to the adverse impact of unsecured material in areas

containing safety-related equipment.

Onsite Follow-up Of Written Reports Of Non-Routine Events

The following Licensee Event Reports were reviewed to assess the

safety significance of the issue, the corrective actions proposed

or taken by the licensee, the licensee's compliance with the

applicable reporting requirements, and the validity of the

licensee's review and evaluation of the subject of the report:

LER 93-001

TS 3.0 Implementation Due To Excessive PPS

Leakage

LER 93-004

Unusual Event Caused By Reactor Coolant

System Leakage

LER 93-005

Apparent Temperature Violation Of The

Boric Acid Storage Tank

LER 93-006

Inadequate EDG Ventilation System Due To

Bypassed Air

LER 93-007

Ventilation System Outside Design Basis

Due To Positive Pressure Condition

LER 93-007-01

Ventilation System Outside Design Basis

Due To Positive Pressure Condition

LER 93-009

TS 3.0 Entry For Service Water Pump

Operability Testing

LER 93-012

Engineered Safety Feature Actuation

LER 93-013

TS Specification 3.10.1.3 Implementation

Due To Exceeding Rod Insertion Limits

LER 93-014

Surveillance Tests Exceeded Technical

Specification Test Intervals

7

After having reviewed the licensee's corrective actions proposed

or taken, the licensee's compliance with the applicable reporting

requirements, and the validity of the licensee's review and

evaluation of the issues addressed by these reports, these LER's

are closed.

b.

Effectiveness of Licensee Control in Identifying, Resolving, and

Preventing Problems (NRC Inspection Procedure 40500)

NAS Identified Clearance Deficiencies and Resulting Site Stand

Down

On September 6, NAS personnel were witnessing work activities

associated with WR/JO 95-ADTI1 for troubleshooting degraded

service water flow through the Primary Air Compressor. During

this activity, NAS observed a maintenance individual manipulate a

valve that was incorrectly believed to be within the valve

clearance boundary established for the work. In accordance with

OMM-005, Clearance and Test Request, only operations personnel are

allowed to manipulate valves or components within clearance

boundaries. The only exception is components on which maintenance

is actually being performed. Based on these observations, NAS

determined that the maintenance personnel did not have a clear

understanding of the clearance boundaries or the requirements of

OMM-005 regarding manipulation of components within clearance

boundaries. NAS ordered the work to be stopped until the problems

were corrected. The inspectors reviewed the assessment results

performed by NAS and considered them to be an example of good

performance based assessment capability. The actions to stop work

and correct the deficiencies were representative of a good safety

focus.

On September 13, licensee management initiated a work "stand-down"

to address the clearance problems identified. The following

actions were taken associated with this stand-down:

-

all section and unit managers met with their personnel and

discussed details of the event, management expectations that

personnel verify and understand clearance boundaries prior

to beginning work, and, expectations that personnel

understand and comply with the requirements of OMM-005,

-

this event was to be included in refueling outage training

for contract personnel,

and,

-

an analysis was to performed within 60 days to determine if

additional training on other site programs was warranted.

The inspectors reviewed these actions and determined that they

were comprehensive toward preventing recurrence. The inspectors

noted that licensee management was sensitive to the seriousness of

8

the potential consequences involved with this issue and was

supportive of NAS efforts to correct the weaknesses identified.

No violations or deviations were identified. Based on the

information obtained during the inspection, the area/program was

adequately implemented.

C.

Followup - Operations (NRC Inspection Procedure 92901)

(Closed) IFI 50-261/93-21-06: Vital Battery Terminal Fractures

This IFI documented observations of deformed and cracked vital

battery terminal posts.

Both vital batteries were replaced during Refueling Outage 16.

Procedure PM-411, Disassembly, Cleaning, Assembly, And Testing Of

A and B Station Battery Cell Connections, has been revised to

incorporate appropriate torque valves.

Engineering Evaluation 93-134 was performed to verify that the B

battery was operable with the degraded terminal posts until it was

replaced. This item is closed.

(Closed) IFI 50-261/93-33-03:

Need For Verification Of CV Spray

And Turbine Auto Stop Circuitry Continuity Following Routine

Testing

This IFI documented deficiencies in routine testing of the

containment spray system and turbine auto stop circuitry. The

deficiencies were associated with continuity testing of circuitry

following routine testing.

The procedures involved, OST-351, CV Spray and MST-11, Turbine

Autostop Testing, were revised to incorporate continuity tests.

This item is closed.

(Closed) VIO 50-261/93-28-04:

Three Examples Of Inadequate Or

Failure To Follow Procedure

This violation involved the following three issues:

1.

A situation on September 13, 1993, in which the licensee

failed to follow procedure, MMM-006, Calibration Program,

for documenting an engineering evaluation or other

appropriate justification to support using a dead weight

tester for the calibration of a pressurizer pressure

transmitter;

2.

An occurrence on November 8, 1993, in which Maintenance

Procedure CM-121, Pressurizer Spray Valve Maintenance, PCV

455A/B was inadequate to facilitate maintenance on valve

9

PCV-455B in that it did not represent the valve as

installed;

3.

An incident on September 16, 1993, in which, procedure CM

704, Service Water Pump Motor Maintenance, was inadequate to

facilitate maintenance on the D service water pump in that

it provided erroneous guidance for setting the pump impeller

clearance.

The corrective steps that have been taken included the following:

1.

Plant personnel have reviewed the calibration records

associated with the dead weight testers used to calibrate

the Pressurizer pressure transmitters. They determined that

the accuracy of calibration of the transmitters exceeds the

0.25% of reading stated in MMM-006, Calibration Program.

MMM-020, Control Of Portable Measuring And Test Equipment,

will be changed to reflect an allowed accuracy of 0.06% of

reading. This will provide an accuracy of reading that

exceeds the accuracy of the pressurizer pressure

transmitters. The Pressurizer Pressure Protection

Transmitters,1[6XPT-455?T-456, and PT-457 were recalibrated.

2.

Procedure CM-121, Pressurizer Spray Valve Maintenance, PCV

455A/B, has been revised to require verification of match

marks prior to proceeding with valve disassembly and

reassembly during maintenance. Also, the procedure now

reflects the "as installed" orientation of the actuator on

the valve body.

3.

A revision to CM-704, Service Water Pump Motor Maintenance,

has been completed to correct the deficiencies noted

pertaining, in part, with impeller clearance.

This item is closed.

(Closed) VIO 50-261/93-11-01:

Failure to Make a Timely

Notification to the NRC of a Notification to State Authorities

This issue involved the licensee's failure to make a timely 4-hour

non-emergency notification to the NRC after contacting the State

of South Carolina regarding an NPDES permit limit violation. In

accordance with 10 CFR 50.72(b)(2)(vi), notifications to other

government agencies, regarding among other topics, protection of

the environment, require a 4-hour non-emergency NRC notification.

to be made.

The licensee responded to this violation by letter dated August 2,

1993.

The root cause was attributed to the failure to understand

the specific reporting requirements of 10 CFR 50.72(b)(2)(vi).

Licensee personnel had historically interpreted this criteria to

apply to the communications involving offsite radiological

10

releases or plant deaths. The inspectors reviewed procedure AP

30, NRC Reporting Requirements. The procedure was revised to

include clarification of the NRC reporting requirements. Specific

plant examples were provided for each of the notification

requirement categories. One of the examples added to the 4-hour

notification category included notifications made as a result of

exceeding NPDES permit requirements. In addition, formal training

was provided for operations and regulatory affairs personnel on

the lessons learned from this issue and clarifications of the NRC

reporting requirements. The inspectors determined that licensee

corrective actions for this issue was adequate and had been

properly implemented. Based on this review, this violation is

closed.

(Closed) VIO 50-261/93-18-01:

Operations Failure to Follow

Procedures, Three Examples

This issue involved three separate examples where operations

personnel failed to follow plant procedures. The first issue

involved three valves that were found improperly locked using

chain link. The second issue involved an ERFIS alarm for control

rod position deviation that went undetected and not acted upon by

the control room reactor operator for several hours. The third

issue involved a reactor operator who flashed the field of the

emergency diesel generator at the wrong engine speed.

The licensee responded to this violation by letter dated October

11, 1993.

Licensee corrective actions for these issues were part

of broader actions to address weaknesses in personnel procedure

adherence and attention to detail.

Specific corrective actions

for the first issue included re-verifying that all valves in the

locked valve program were properly secured using chain devices.

The inspectors reviewed completed valve lineup documentation and

verified that this action was completed. Licensee corrective

actions to address the second violation example included adding

administrative controls for providing increased observation and

monitoring of Control Room indications. The inspectors reviewed

OMM-23, Operator Logs and Rounds, which requires that the reactor

operator review important plant parameters via the ERFIS Group

Trend printout on an hourly basis. The inspectors verified that

the operators were completing these reviews. Specific licensee

corrective actions for the third issue involved counselling the

operator involved relative to management expectations of procedure

compliance. This emphasis on procedure compliance was also

discussed with all other licensed and non-licensed operators.

The inspector determined that licensee corrective actions for

these issues were adequate and had been properly implemented.

Based on this review, this violation is closed.

(Closed) VIO 50-261/93-18-03:

Failure to Maintain Design Control

of Reactor Auxiliary Building Ventilation System

This issue involved the failure to implement adequate measures to

maintain the integrity of the Reactor Auxiliary Building

Ventilation System design between January 1992 until July 1993.

The licensee had implemented modifications and performed

maintenance during this period which degraded the system and had

not adequately performed post maintenance testing to verify the

system's design requirement for maintaining a negative building

pressure. A negative building pressure ensures that the air flow

is directed into the building and not outward.

The licensee responded to this violation by letter dated

October 11, 1993. Corrective actions included rebalancing the RAB

ventilation system (flow balance test completed on June 9, 1994)

to ensure, among other design requirements, that the RAB was

maintained at a negative pressure. The inspectors reviewed the

flow balance test results verifying that the acceptance criteria

for negative pressure in the RAB was met. As part of the flow

balance evaluation, the number and location of existing pressure

gauges in the RAB were reviewed by the licensee and determined to

be adequate. As a backup to the existing building pressure

gauges, provisions were made for installing portable pressure

instrumentation at various locations in the building.. Provisions

for periodically monitoring the RAB negative air pressure were

also developed. The inspectors reviewed the Inside Auxiliary

Operator's Log which was revised to include a check of the RAB

pressure once per shift. The licensee also provided formal

training for design engineering personnel on the need to consider

the effect of modifications on the RAB ventilation system

capability to maintain its design requirements. This training was

completed for selected personnel on April 8, 1994.

The inspector determined that licensee corrective actions for

these issues were adequate and had been properly implemented.

Based on this review, this violation and LER are closed.

4.

MAINTENANCE

a.

Maintenance Observation (NRC Inspection Procedure 62703)

The inspectors observed safety-related maintenance activities on

systems and components to determine if the activities were

conducted in accordance with regulatory requirements, approved

procedures, and appropriate industry codes and standards. The

inspectors reviewed associated administrative, material, testing,

radiological, and fire prevention controls requirements to

determine licensee compliance. In particular, the inspectors

observed/reviewed the following maintenance activities detailed

below:

12

WR/JO ABIL-001:

Calibration of Spray Additive Flow

Instruments FI-949 and FIT-949

WR/JO ABBW-001:

Calibration of Containment Spray Pump A

Pressure Gauge PI-945

WR/JO 95-AMNL1:

Investigate Problem with Boric Acid Bypass

Meter Flow Indication

Troubleshooting of Unexplained Turbine Governor Valve Movement

On October 3, the control room reactor operator noticed that the

number 2 turbine governor valve was slowly closing as indicated by

valve position on the RTGB. The operator placed the turbine

controls in manual which stopped the valve movement. During this

time period, the Net Megawatt recorder indicated that turbine load

had decreased by 5 Megawatts (electric). Following the event, I&C

was instructed to investigate this problem by checking for any

electrical problems with the turbine Electro-Hydraulic Controller

which controls the movement of the governor valves. These efforts

included taking voltage measurements in the controller panel with

the turbine in both automatic and manual mode to verify that the

governor valve demand signals were proper. The test results

confirmed that the valves were operating properly. The licensee

later determined that the problem may have been related to higher

than expected moisture in the turbine EHC oil and was continuing

with this investigation at the end of the report period.

The inspectors witnessed I&C technicians troubleshooting the

turbine Electro-Hydraulic Controller under WR/JO 95-AMDH1.

Overall, the conduct of this troubleshooting was satisfactory.

Noteworthy was the continuous I&C supervision and engineering

support provided during the activity. However, the inspectors did

note one item that was not indicative of good maintenance

practice. This involved the I&C technician's use of turbine

control system training material to reference voltage test points

as opposed to using controlled, technical information. When this

was brought to the attention of the I&C supervisor, who was

present during the activity, the inspectors were informed that he

had already instructed the technician to not use this information

during the field activity work.

b.

Surveillance Observation (NRC Inspection Procedure 61726)

The inspectors evaluated certain safety-related surveillance

activities to determine if these activities were conducted in

accordance with license requirements. For the surveillance test.

procedures listed below, the inspectors determined that

precautions and LCOs were adhered to, the required administrative

approvals and tagouts were obtained prior to test initiation,

testing was accomplished by qualified personnel in accordance with

an approved test procedure, test instrumentation was properly

calibrated, the tests were completed at the required frequency,

and that the tests conformed to TS requirements. Upon test

13

completion, the inspectors verified the recorded test data was

complete, accurate, and met TS requirements, test discrepancies

were properly documented and rectified, and that the systems were

properly returned to service. Specifically, the inspectors

witnessed and/or reviewed portions of the following test activity:

MST-003

T-Average and Delta-Temperature Protection

Channel Testing

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

5.

ENGINEERING

a.

Engineering Support Activities (NRC Inspection Procedure 37551)

Throughout the inspection period, engineering evaluations of

problems and incidents were reviewed and discussions were held

with engineering personnel to assess the effectiveness of the

licensee's controls for identifying, resolving, and preventing

problems. Based on these inspections, the engineering staff was

effective and timely in responding to plant problems and

interfacing with operations.

b.

Engineering Followup (NRC Inspection Procedure 92703)

(Closed) URI 50-261/95-23-01:

Inadequate Justification for Plant

Operation With One Pressurizer Spray Valve Inoperable

This issue involved the adequacy of the licensee's operability

justification that the pressurizer pressure control system was

operable with one of the two pressurizer spray valves (PCV-455A)

out of service. Spray valve PCV-455A was removed from service and

isolated on August 8, 1995, after experiencing erratic position

indication. During the previous inspection, the inspectors

reviewed Expert Operability Analysis For OD 95-015, dated

August 7, 1995, which documented the licensee's evaluation of the

impact with the inoperable spray valve. It was determined that

the evaluation did not fully justify operation with only one spray

valve. Specifically, it did not adequately address design basis

information that implied that both spray valves were necessary for

controlling pressure during a 10 percent step load reduction, as

well as the need for redundant emergency power requirements for

the spray valves.

During this report period, the inspectors reviewed revisions 1 and

2 to Expert Operability Analysis For OD 95-015, dated August 11

and September 1, respectively. The inspectors determined that

these evaluations provided adequate justification for continued

operability of the pressurizer pressure control system with one

valve unavailable. This was based primarily on the licensee's

14

review of Chapter 15 of the Final Safety Analysis Report, which,

determined that there were no accidents that the plant was

designed for that took credit for the spray valves to help

mitigate. While the second spray valve is required to accommodate

step load changes between 5 and 10 percent without challenging the

Pressurizer Power Operated Relief valves, this loading or

unloading rate is considered to be initiated by planned operator

actions. The inspectors verified that limitations existed to

restrict operator loading and unloading to 5 percent. With regard

to emergency electrical power, the licensee determined that there

was no design requirement for the valves to receive redundant

electrical power. The inspectors discussed the licensee's

position and evaluation results with NRC personnel in the

department of Nuclear Reactor Regulation, who agreed with these

conclusions. The inspectors considered this URI closed.

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

6.

PLANT SUPPORT (NRC Inspection Procedures 71707 and 71750)

Throughout the inspection period, facility tours were conducted to

observe personnel activities as they relate to radiation protection and

security. The tours included entries into the protected areas and the

radiologically controlled areas of the plant and included assessment of

radiological postings and work practices. During these inspections,

discussions were held with radiation protection and security personnel.

The inspections confirmed the licensee's compliance with 10 CFR,

Technical Specifications, License Conditions, and Administrative

Procedures.

The inspectors considered noteworthy the good radiation controls

observed while witnessing maintenance personnel check the calibration of

the A Containment Spray Pump discharge pressure associated with WR/JO

ABBW-001. This activity was continuously controlled and monitored by

radiation control personnel to ensure that there was no contamination

spread during the maintenance activity.

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

7.

EXIT INTERVIEW

The inspectors met with licensee representatives (denoted in paragraph

1) at the conclusion of the inspection on October 26. During this

meeting, the inspectors summarized the scope and findings of the

inspection as they are detailed in this report. The licensee

representatives acknowledged the inspector's comments and did not

identify as proprietary any of the materials provided to or reviewed by

15.

the inspectors during this inspection.

No dissenting comments from the

licensee were received

Item Number

STATUS

Description/Reference Paragraph

VIO 95-27-01

Opened

Inadequate Clearance Results in Unexpected

Emergency Diesel Start (paragraph 3.a)

LER 93-001

Closed

TS 3.0 Implementation Due To Excessive PPS

Leakage (paragraph 3.a)

LER 93-004

Closed

Unusual Event Caused By Reactor Coolant

System Leakage (paragraph 3.a)

LER 93-005

Closed

Apparent Temperature Violation Of The

Boric Acid Storage Tank (paragraph 3.a)

LER 93-006

Closed

Inadequate EDG Ventilation System Due To

Bypassed Air (paragraph 3.a)

LER 93-007

Closed

Ventilation System Outside Design Basis

Due To Positive Pressure Condition

(paragraph 3.a)

LER 93-00-01

Closed

Ventilation System Outside Design Basis

Due To Positive Pressure Condition

(paragraph 3.a)

LER 93-009

Closed

TS 3.0 Entry For Service Water Pump

Operability Testing (paragraph 3.a)

LER 93-012

Closed

Engineered Safety Feature Actuation

(paragraph 3.a)

LER 93-013

Closed

T.S. Specification 3.10.1.3 Implementation

Due To Exceeding Rod Insertion Limits

(paragraph 3.a)

LER 93-014

Closed

Surveillance Tests Exceeded Technical

Specification Test Intervals (paragraph

3. a)

IFI 93-021-06

Closed

Vital Battery Terminal Fractures

(paragraph 3.c)

IFI 93-33-03

Closed

Need For Verification Of CV Spray And

Turbine Auto Stop Circuitry Continuity

Following Routine Testing (paragraph 3.c)

VIO 93-28-04

Closed

Three Examples Of Inadequate Or Failure To

Follow Procedure (paragraph 3.c)

16

VIO 93-11-01

Closed

Failure to Make a Timely Notification to

the NRC of a Notification to State

Authorities (paragraph 3.c)

VIO 93-18-01

Closed

Operations Failure to Follow Procedures,

Three Examples (paragraph 3.c)

VIO 93-18-03

Closed

Failure to Maintain Design Control of

Reactor Auxiliary Building Ventilation

System (paragraph 3.c)

URI 95-23-01

Closed

Inadequate Justification for Plant

Operation With One Pressurizer Spray Valve

Inoperable (paragraph 5.)

8.

ACRONYMS AND INITIALISMS

AP

Administrative Procedure

CFR

Code of Federal Regulation

CR

Condition Report

CV

Containment Vessel

EDG

Emergency Diesel Generator

EHC

Electro-Hydraulic Control

ERFIS

Emergency Response Facility Information System

I&C

Instrumentation And Control

IFI

Inspector Followup Item

LCTR

Local Clearance and Test Request

LER

Licensee Event Report

MMM

Maintenance Management Manual

MST

Maintenance Surveillance Test

NAS

Nuclear Assessment Section

NPDES

National Pollutant Discharge Elimination System

OMM

Operations Management Manual

PM

Preventative Maintenance

PPS

Penetration Pressurization System

RAB

Reactor Auxiliary Building

RTGB

Reactor Turbine Gauge Board

TS

Technical Specifications

URI

Unresolved Item

VIO

Violation

WR/JO

Work Request/Job Order