ML14178A401

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Insp Rept 50-261/93-21 on 930912-1016.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Followup of Previously Identified Items & Routine Followup
ML14178A401
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 11/08/1993
From: Christensen H, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A399 List:
References
50-261-93-21, NUDOCS 9311160127
Download: ML14178A401 (20)


See also: IR 05000261/1993021

Text

NR REG4

UNITED STATES

Co

NUCLEAR REGULATORY COMMISSION

REGION II

o

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/93-21

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: September 12 - October 16, 1993

Lead Inspector:

-

t.sn

P-'-

///5 95$

W. T. Orders, Seni

Resident Inspector

Date Signed

Other Inspector:

C. R. Ogle, Resident Inspector

C. W. Rapp, Regional Inspector

N. Merriweather, Regional Inspector

Approved by:

_

7

_ _ __ _

_________

_73

)' 0. C ristensen, Chief

Date Signed

Reactor Projects Section lA

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, maintenance observation, followup of previously

identified items, and routine followup

Results:

One violation was identified which involved two examples of personnel failing

to follow procedures. The issues concerned an operator opening the incorrect

electrical breaker, and the failure to control a sludge lance vent path.

(paragraph 3)

A second violation was identified which concerned a failure to establish

containment integrity before commencing refueling operations. (paragraph 3)

Two non cited violations were identified involving an STA who departed the

site before the end of his shift and an area fire watch who vacated his post

before being relieved of his duties. (paragraph 3)

9311160127 931108

PDR ADOCK 05000261

G

PDR

2

Two inspector followup items were identified involving a loose part in a fuel

assembly, and fractures in the terminal posts of the vital batteries.

(paragraphs 3 and 4)

REPORT DETAILS

1.

Persons Contacted

R. Barnett, Manager, Project Management

J. Benjamin, Shift Outage Manager, Outages and Modifications

S. Billings, Technical Aide, Regulatory Compliance

B. Clark, Manager, Maintenance

  • T. Cleary, Manager, Technical Support
  • D. Crook, Senior Specialist, Regulatory Compliance
  • C. Dietz, Vice President, Robinson Nuclear Project

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

G. Elam, Program Manager, EGS Corporation

S. Farmer, Manager, Engineering Programs, Technical Support

R. Femal, Shift Supervisor, Operations

  • W. Flanagan Jr., Operations Manager

R. Hardy, Test Director, Wyle Laboratories

B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

D. Labelle, Project Engineer, Nuclear Assessment Department Site Unit

A. McCauley, Manager, Electrical Systems, Technical Support

R. Moore, Shift Supervisor, Operations

D. Morrison, Shift Supervisor, Operations

  • T. Niemi, Project Engineer, Nuclear Assessment Department

D. Nelson, Shift Outage Manager, Outages and Modifications

A. Padgett, Manager, Environmental and Radiation Control

H. Patel, EQ Engineer, CP&L

  • M. Pearson, Plant General Manager

D. Seagle, Shift Supervisor, Operations

M. Scott, Manager, Reactor Systems, Technical Support

  • E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

  • A. Wallace, Manager, Shift Operations, Operations

D. Waters, Manager Regulatory Affairs

  • D. Whitehead, Manager, Plant Support Services

D. Winters, Shift Supervisor, Operations

P. Yandow, EQ Coordinator, CP&L

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Managements Visits

H. Christensen, Chief, Projects Section lA, Division of Reactor

Projects, visited the site on October 15, 1993. Mr. Christensen toured

the facility with the residents and attended the exit meeting on

October 15, 1993. He also met with members of the licensee's management

organization.

  • Attended exit interview on October 15, 1993.

2

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

Refueling Outage 15 continued during the report period with fuel

assembly reload ongoing at the end of the inspection period. The outage

is currently scheduled to end on November 3, 1993.

3. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operation's records, data sheets, instrument

traces, and records of equipment malfunctions. Through work

observations and discussions with Operations staff members, the

inspectors verified the staff was knowledgeable of plant conditions,

responded properly to alarms, adhered to procedures and applicable

administrative controls, cognizant of in-progress surveillance and

maintenance activities, and aware of inoperable equipment status. The

inspectors performed channel verifications and reviewed component status

and safety-related parameters to verify conformance with TS. Shift

changes were routinely observed, verifying that system status continuity

was maintained and that proper control room staffing existed. Access to

the control room was controlled and operations personnel carried out

their assigned duties in an effective manner. Control room demeanor and

communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were properly

implemented.

Shift Technical Advisor (STA) Departs Before End Of Shift

On the morning of September 16, 1993, the inspectors were present in the

control room during turnover of the oncoming day shift, when it was

noted that the off-going STA was absent. From a subsequent review of

security access records, the inspector determined that the offgoing STA

had left the protected area approximately 5 minutes prior to the arrival

of the oncoming STA.

Although the inspectors noted from a review of TIS 6.2.3.c, that the STA

was not required during cold shutdown conditions, an individual was

specified to fill the STA position by the watchstanders listing posted

3

in the control room. Operations Management Manual, OMM-008, Minimum

Equipment List and Shift Relief, discusses turnover responsibilities for

the STA position. Though some of the responsibilities of OMM-008 are

not applicable while in cold shutdown, some are meaningful during a

turnover in any plant condition. Additionally, OMM-008 specifically

requires that shift operating personnel remain on duty with full

responsibilities of their position until properly relieved. OMM-008

requires that this turnover be conducted at the normal watchstation.

The inspectors requested that the licensee provide details concerning

the premature departure of the STA. Licensee management advised the

inspectors that the individual left without having been granted

permission by the onwatch shift supervisor and that he had done so of

his own volition because he felt that he was not needed due to plant

conditions.

The licensee counselled the individual concerning management's

expectation that watchstanders remain until properly relieved. The

licensee also stated their intention to review this expectation with all

watchstanders.

The failure of the STA to conduct a watch turnover is a violation of the

requirements of OMM-008. However, this identified violation is not

being cited because criteria specified in Section VII.B of the NRC

Enforcement Policy were satisfied. This is identified as a non-cited

violation, NCV 93-21-01: Failure Of STA To Conduct Turnover Required By

OMM-008.

Sewage Overflow In Protected Area

At approximately 8:00 a.m. on September 17, 1993, the licensee

discovered sewage overflowing a manhole in the protected area. The

licensee stopped the overflow and a septic tank service was utilized to

lower the system level.

In response to this overflow, the licensee notified the South Carolina

Department of Health and Environmental Control on September 17, 1993.

As a result of the notification to the state, the licensee made a 4-hour

non-emergency notification to the NRC in accordance with the

requirements of 10 CFR 50.72 (b) (2) VI.

The licensee notified the

resident inspectors prior to the 10 CFR 50.72 notification.

On October 7, 1993, two subsequent sewage spills occurred at the site.

These spills were stopped and recovery actions were taken by the

licensee. As a result of notification of state authorities, the

licensee made initial and followup notifications to the NRC in

accordance with 10 CFR 50.72 (b) (2) VI at 2:25 p.m. and at 5:30 p.m. on

October 7, 1993.

4

Based on their review of these events, the inspectors concluded that the

licensee met the requirements for NRC notification specified in 10 CFR

50.72. The inspectors have no further questions on these events.

Reactor Coolant System Draindown

On September 17, 1993, the inspectors witnessed the performance of

General Procedure, GP-008, Draining The Reactor Coolant System. This

draindown was accomplished to reduce RCS level to approximately 10

inches below the reactor vessel flange to support vessel head removal.

The inspection effort included a partial walkdown of the reactor coolant

level standpipe system prior to the draindown, attending the pre-shift

briefing for the evolution, and observation of control room activities

during the level change.

Overall, the inspectors concluded that the evolution was well controlled

with a proper emphasis on safety. There was a strong effort by

operations personnel to ensure that RCS level was closely monitored and

that appropriate overlap existed in available level instruments. The

Management Designated Monitor conducted the pre-shift briefing which

included information from previous draindown events. He also remained

present in the control room during the level change. The inspectors

have no further questions on this evolution.

Operator Inadvertently Deenergized Motor Control Center MCC-5

At approximately 10:00 p.m. on September 19, 1993, power to MCC-5 was

interrupted when an operator inadvertently opened the normal power

supply breaker for the MCC. The operator had been dispatched to

transfer service water pump D to the emergency power supply, but in

fact, commenced the transfer sequence at the wrong switchboard. After

power to MCC-5 was interrupted, the operator recognized the mistake,

reclosed the normal power supply breaker, and informed the control room

of his actions. The MCC-5 loads which were stopped as a result of the

power interruption were then restarted. Service water pump D was

subsequently transferred to its alternate power supply.

The inspectors interviewed the operator involved; reviewed log entries

in the shift supervisor's and control operator's logs; and reviewed an

Off Normal Condition Analysis (ONCA) form generated for the event.

Based on this effort, the inspectors determined that the operator became

distracted while enroute to accomplish the transfer of service water

pump D to the alternate power supply. This distraction occurred while

the operator explained the operation of the plant's interlocked power

supply breakers to a watchstander trainee. As a result, the operator

positioned himself at the MCC-5 normal and emergency supply breakers as

opposed to the normal and emergency supply breakers for service water

pump D. These switchboards are similar in appearance and function, and

though not adjacent, are in close proximity to one another.

5

Technical Specification 6.5.1.1, Procedures, Tests, and Experiments

requires, in part, that written procedures be established, implemented,

and maintained covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev. 2. 1978. Appendix A, Paragraph 4 requires

instructions for operation of onsite electrical systems. Operating

Procedure, OP-603, Electrical Distribution is provided these

instructions.

Contrary to the above, on September 19, 1993, an operator deviated from

OP-603 while transferring service water pump D from normal to emergency

power. As a result of this deviation, power was lost to motor control

center, MCC-5. This is the first of two examples which in the aggregate

comprise a violation, VIO 93-21-02: Failure To Follow Procedures, Two

Examples.

Sludge Lance Rig Vent Valve Misaligned

During the ongoing refueling outage the licensee accomplished sludge

lancing on the steam generators secondary sides. The equipment used to

accomplish this work was mounted on a tractor trailer external to the

containment. Two containment vent valves, V12-12 and V12-13, were

removed and necessary hoses and electrical cables to support the

evolution were routed through the idle penetration. To permit lancing

while containment integrity or containment closure were required, the

system incorporated a foam-filled CV penetration collar which bolted

onto the V12-12 flange, a "closed" sludge lance system outside of

containment and a vent hose from the sludge lancing equipment back into

containment. Each of the hoses which penetrated containment were also

equipped with a pair of isolation valves on either side of the

containment penetration. Special Procedure, SP-1231, S/G Sludge Lance

and Inspection was developed to provide the guidance necessary to

accomplish the lancing.

On September 21, 1993, during a routine tour, the inspectors observed

that a vent valve for the slurry tank on the trailer mounted rig was

open. At the inspector's request, the valve was confirmed to be open by

a contractor assigned to operate the sludge lancing rig. The valve was

then closed by the contractor.

This open valve on the slurry tank provided a direct vent path from the

rig to atmosphere and hence, since sludge lancing was in progress, a

direct path from the containment to atmosphere. The contractor

indicated that he was unsure why the valve was open. CV closure was in

effect at the time of this observation, however, CV integrity was not

required.

SP-1231 required that all vent paths on the sludge lance rig be

identified by the system engineer and caution tagged prior to opening

the isolation valves for the rig. The open vent valve identified by the

inspectors was not caution tagged. When questioned on the lack of a

caution tag, the cognizant supervisor stated that a walkdown had been

performed but failed to identity this valve as a potential vent path.

6

Technical Specification 6.5.1.1. Procedures, Tests, and Experiments,

requires, in part, that written procedures be established, implemented,

and maintained, for the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev 2. 1978. Paragraph 9 of Appendix A requires

that maintenance be performed in accordance with written procedures.

Special Procedure, SP-1231, Steam Generator Sludge Lance and Inspection,

was written to provide instructions for conducting sludge lancing of the

steam generators secondary sides.

Contrary to the above, on September 21, 1993, a vent path to atmosphere

was not identified and caution tagged as required by SP-1231. As a

result, a vent valve on the sludge lancing rig was open and a vent path

from the containment existed. This is the second of two examples which

in the aggregate comprise a violation, VIO 93-21-02: Failure To Follow

Procedures, Two Examples.

The inspectors also noted that there was no procedural requirement in

SP-1231 to conduct another verification that the potential vent paths in

the sludge rig were properly isolated prior to establishing integrity

for refueling. When questioned by the inspectors, the system engineer

stated his intentions were to perform an additional system walkdown of

the sludge lancing rig prior to establishing integrity.

Area Fire Watch Vacates Post

On September 22, 1993, the licensee determined that an area firewatch

had vacated his assigned post prematurely. The watch had been stationed

in the Emergency Switchgear/Safeguards Room as required by Fire

Protection Procedure (FP-012), Fire Protection Systems Minimum Equipment

and Compensatory Actions, when the halon suppression system for that

area (zone 20) was disabled. The system was disabled at 8:34 p.m. on

September 22, 1993, to support maintenance in the room. At 11:50 p.m.

Operations personnel noted that the area fire watch had left the room

while zone 20 was still disabled.

The inspectors reviewed the shift supervisor's log and the on-shift fire

technician's log. Additionally, the inspectors interviewed the

cognizant maintenance and fire protection supervisors. Based on the

information obtained from this effort, the inspectors concluded that the

area fire watch was unaware of his responsibility to remain at his

assigned station until the fire suppression system was restored to

service.

In response to this event, the licensee committed to providing training

to area fire watches reiterating the need for the watch to remain posted

until the fire suppression system is fully returned to service. The

licensee has also developed a sheet which outlines the responsibilities

of area fire watches. As described by the licensee, this information

sheet will be provided to area fire watches upon deactivation of fire

zones. The inspectors reviewed the sheet and noted that it specifically

addressed the responsibility of area fire watches to remain in assigned

zones until authorized to depart by the on-shift fire technician.

7

The failure of the area fire watch to remain in Zone 20 is a violation

of the requirements of FP-012. This violation will not be subject to

enforcement action because the licensee's efforts in identifying and

correcting the violation meet the criteria specified in Section VII.B of

the Enforcement Policy. This is identified as a non-cited violation,

NCV 93-21-03: Area Fire Watch Vacates Post.

Failure To Maintain Containment Integrity During Fuel Movement

On September 27, 1993, the unit was in cold shutdown condition, in a

scheduled refueling outage with core off-load underway. At approximately

10:30 a.m. that morning, licensee Technical Support personnel were

requested to check the adequacy of the containment building equipment

hatch seals after the Resident Inspectors noted that the hatch was

leaking air into the building. The licensee visually verified air

inleakage, and at approximately 11:30 a.m., Operations personnel were

notified of the existence of the leakage. Although core off-load had

been completed approximately 10 minutes earlier, the leak path existed

during fuel movement operations.

The NRC operations duty officer was notified of this event at 3:21 P.M.

that afternoon as a condition that alone could have prevented the

fulfillment of the safety function of the structures or systems needed

to control the release of radioactive material.

Upon discovery of this event, attempts were made to eliminate the

leakage by tightening the hatch bolts, but these attempts were un

successful.

Subsequently, the equipment hatch was removed and the seals

and flange surfaces were inspected. The results of the inspection

revealed that the seals and seating surfaces were in relatively good

condition with one of the seals intact, and only minor damage noted on

the other seal.

The cause of this event is attributed to the lack of controls for the

re-installation of the equipment hatch during an outage, to support

activities requiring containment integrity, such as fuel movement.

Operations management manual procedure OMM-033 provides only limited

guidance for the re-installation of the hatch for containment

closure/refueling integrity. Adverse Condition Report 93-173 was

initiated to document this condition and to facilitate a root cause

investigation.

Plant Procedure CM-603 is used to secure the equipment hatch to meet

containment integrity requirements for reactor operations. Procedure

OMM-033, was developed to provide guidance for equipment hatch

installation to support, in part, refueling operation. However, this

procedure appeared to be inadequate to ensure that containment closure

(integrity) was achieved. In addition, the procedure was not used on

September 23, 1993, when the hatch was installed to support refueling

operations.

8

Technical Specification 3.8.1., refueling operations, requires that the

equipment hatch be "properly closed".

Implicit in this requirement is

the requisite that the hatch be capable of performing its intended

safety function, which in this case is to prevent the release of

radioactive material to the environment given a fuel handling accident

or a prolonged loss of core cooling.

Furthermore, Technical Specification 6.5.1.1, Procedures, Tests, and

Experiments requires, in part, that written procedures be established,

implemented, and maintained covering the activities recommended in

Appendix A of Regulatory Guide 1.33, Rev. 2. 1978. Appendix A,

Section 3.f(1) requires instructions for maintaining containment

integrity. Implicit in this requirement are the requisites that the

procedures be adequate to facilitate the applicable evolution and that

personnel use the procedures during the performance of the evolution.

Contrary to those requirements, on September 23, 1993, the licensee did

not use a procedure to facilitate the re-installation of the containment

building equipment hatch when they were preparing for refueling

operations. This resulted in the inadequate installation of the

equipment hatch in that it was not "properly closed" and as such was not

capable of performing its intended safety function. This is a Violation,

93-21-04: Failure To Maintain Containment Integrity During Fuel

Movement.

A review of this event revealed that there was only minor safety

significance involved with the leak at the equipment hatch. The major

vulnerability involves fuel damage during refueling operations which

could lead to the release of fission products to the containment

atmosphere. However, there does not appear to be a viable scenario

which would result in containment pressurization which in turn would

result in release of radioactive material to the environment.

Loose Part In Fuel Assembly

During the ongoing refueling outage, the licensee examined a number of

fuel assemblies for damage. To facilitate this inspection, the fuel

assembly tie plates were replaced with a special vendor supplied guide

plate. This guide plate was fastened to the control rod guide tubes

with three anchors. The anchors consist of a shaft and nut which

interface to expand a split tube. This expanded split tube provides a

grip with the guide tube inner diameter to hold the guide plate in

place. When the guide plate was removed from assembly U24, the shaft of

one of the three anchors was broken. The retaining nut, the split tube,

and the end of the shaft were missing from the tool.

At that time, the

vendor technicians performing this service, assumed that the pieces had

fallen into the spent fuel pit, but failed to notify the licensee.

Following the inspection of assembly U24, an attempt was made to load an

RCCA in the assembly. The vertical travel of the RCCA was blocked

approximately 2 feet above its fully loaded position. When the RCCA

would not insert into the assembly, it was inspected with a camera. The

9

split tube from the aforementioned fuel inspection tool was found to be

on the end of one of the RCCA fingers and consequently removed. Thus,

the remaining pieces in the guide tube were the retaining nut and the

shaft end. During a later inspection, it was verified that the

retaining nut is lodged at the transition area. Because of the design

of the tool, the shaft end is free of the retaining nut and is located

in the bottom of the guide tube, below the retaining nut.

The licensee elected to leave the tool fragments in the guide tube and

move the assembly to a non-controlled (no control rod) position in the

core. This decision was justified by the licensee's fuel vendor,

Siemens.

A copy of that evaluation was forwarded to the RII office for followup.

Pending completion of that analysis, this issue will be tracked as IFI

93-21-05: Fuel Assembly Loose Part.

ECCS Piping Flush

On September 27, 1993, the inspectors witnessed accomplishment of

Special Procedure, SP-1163: SI-891 C, SI-891 D, and SI-863 B Flush.

This special procedure was accomplished to flush selected ECCS piping to

the RWST to ensure that no white plastic remained in any uninspected or

unflushed portion of the system. Additional information concerning the

discovery and removal of the white plastic material is contained in NRC

Inspection Report 50-261/92-24. This procedure was accomplished

coincident with cavity draindown and directed flow to the RWST through

the flushed piping.

Overall, the accomplishment of SP-1163 was satisfactory. However, the

inspectors noted that total flowrate through the operating RHR pump

exceeded the maximum flow rate specified in Operating Procedure, OP-201,

Residual Heat Removal System. This was identified to the system

engineer and cognizant engineering supervisor. The inspectors requested

that the licensee review this issue to determine if the maximum runout

flow for the RHR pump had been exceeded. After their review, the

licensee provided documentation that despite exceeding the precautional

limit of OP-201, the pump flow had not exceeded runout conditions. The

inspectors independently reviewed the documentation and concurred with

the licensee's conclusions. The inspectors had no further questions on

SP-1163.

Summary

Two separate noncited violations for watchstanders (an STA and a fire

watch) leaving their assigned duty prematurely indicates that

improvements in this area are warranted. The RCS partial draindown

activity was well controlled and received adequate monument attention.

A violation with two examples of failure to follow procedural

requirements is a concern because they represent a continuing pattern of

plant personnel not complying with procedures. A second violation was

10

identified for accomplishing a maintenance task without using the

applicable procedure. An inspector followup item was identified for

loose parts in a fuel assembly guide tube.

4. Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS, and approved procedures. The inspectors determined

that these activities did not violate LCOs and that required redundant

components were operable. The inspectors verified that required

administrative, material, testing, and radiological controls were

adhered to. In particular, the inspectors observed/reviewed the

following maintenance activities:

WR/JO

92ARSN4

Discharge Testing of Battery

Charger Al

WR/JO

93AHYLl

Replace Flow Switch For HVE-16

GP-010

Refueling (Fuel Offload)

Retest Program For Environmental Qualification Of The Patel Conduit

Seals

On August 2, 1993, the NRC conducted a special inspection at Wyle Labs

in Huntsville Alabama to review the retest program for the EGS (formerly

Patel) conduit seals. This program was implemented by the licensee to

resolve 10 CFR 50.49 Environmental Qualification (EQ) issues identified

by the NRC in Inspection Report 50-261/91-03. The inspector met with

representatives from CP&L, EGS, and Wyle Labs to discuss the preliminary

results of the retest program. The licensee stated during this meeting

that the four test specimens exposed to the H.B. Robinson LOCA/

Submergence accident profiles did not experience any leakage past the

seals during the entire test. One anomaly was identified during the

test and it was resolved by extending the duration of the test. The

test specimens were examined prior to being removed from the LOCA

chamber. The test specimens/setup was observed to be similar to that

described in, Re-Test Procedure for Submergence Qualification of Conduit

Seals, (Report No. EGS-TR-841215-07, Revision B), however, unlike the

procedure end caps were added to the specimens to protect the wires

against direct spray.

The test specimens were removed from the LOCA

chamber and were inspected for visual signs of leakage past the seals

(e.g. grommet and wire integrity).

In addition the break away torque

was measured for one of the samples. The above inspections had

satisfactory results. The inspector examined the data sheets for the

last six days of the test which covered the period July 27 - August 1,

1993, with no anomalies observed. The inspection concluded with the

specimens being packaged for transporting to EGS for further examination

and study. The licensee indicated that the final test report should be

issued by the end of the year. This issue will remain open pending

review of the final test report and the revised EQ files.

Discharge Testing Of Battery Charger A-i

On September 21, 1993, the inspectors witnessed the setup and initial

steps accomplished to perform discharge testing of battery charger A-1.

The discharge test was aborted when the system engineer recognized that

the load bank had been incorrectly attached to charger A-1.

During installation of the cables to the load bank, the output power

leads to the output terminal block in the charger were removed. The

load bank cables were then attached to this terminal block. The intent

of the procedure was to remove the cables between the terminal block and

the DC bus and attach the load bank cables in their place.

Following the recognition of this deficiency, the load bank cables were

removed, the charger restored to normal configuration, and the test

rescheduled for a later date.

RWST Inspection

On September 30, 1993, the inspectors witnessed preparations for and the

subsequent entry of a diver into the RWST. This entry was accomplished

to permit an inspection of the RWST following a flush of selected ECCS

piping to the RWST in accordance with Special Procedure, SP-1163, SI

891C, SI-891D, and SI-863B flush. The diver's efforts were tracked by

personnel outside the tank on a monitor fed from a camera operated by

the diver.

As described by the diver, visibility in the tank was good with only a

few pieces of debris observed on the bottom. A few flakes of white

material were reported on the tank floor, however, they could not be

recovered due to their small size.

No discrete pieces of plastic were

reported by the diver (see paragraph 3 for additional information on the

plastic material).

Items recovered included small pieces of string, a

short piece of wire, and a bolt.

The overall performance of the evolution was satisfactory. However, the

inspectors noted that the benefit provided by monitoring the screen

outside the tank was marginal.

Both poor lighting used with the camera

and the small monitor size made vidio evaluation of objects by support

personnel difficult. This was a marked reduction in capability over

that observed by the inspectors during previous dives into the RWST.

The inspectors were informed that this particular camera/monitor setup

was used for this inspection due to the desired camera/monitor rig being

unavailable. The inspectors were also advised that the camera output

was being videotaped for potential future review. The inspectors had no

further questions on this evolution.

Use of Temporary Leak Sealants

The inspectors conducted a review of the controls associated with the

use of temporary leak sealants. This review included procedures,

management oversight, engineering and safety evaluations, and

12

application of temporary leak sealants on plant equipment. The

inspectors found that temporary leak sealants are used on both safety

and non-safety related equipment. Application of temporary leak

sealants was controlled by the temporary modification process. The

vendors procedures for installing the temporary leak sealant were

included in the temporary modification package and reviewed with the

temporary modification. The temporary modification also delineated the

type and amount of temporary leak sealant that could be used. If

additional sealant was necessary, an engineering evaluations was

typically required. TMM-031, Evaluation of On-Line Flowable Packing,

provided additional guidance for evaluating the temporary leak sealant.

As required by the temporary modification process, all temporary

modifications were subject to a 10 CFR 50.59 safety evaluation.

Furthermore, temporary modifications to safety related equipment were

reviewed as design changes. Typically QC was involved in the review

process when a "Q" component was affected. Temporary modifications to

non-safety related equipment received a technical review. Each

temporary modification was reviewed and approved by senior plant

management before being implemented. As required by the temporary

modification process, temporary leak sealants were required to be

replaced at the next refueling outage.

Battery Post Fractures

While performing routine maintenance of the "B" battery during RF015,

the licensee detected that the battery posts on many of the cells were

deformed, and some of the terminal posts had experienced fractures.

One of the cells of the "B" battery (cell 31) was sent to the Harris E&E

Center, where the posts were examined. Some subsurface fracturing was

observed, with evidence of oxidation along the fracture lines.

This condition raised concerns over the acceptability of the battery

with respect to meeting the electrical requirements of providing the

required output for safety-related functions, and the seismic integrity

of the battery. The "B" battery is a safety-related battery, which

supplies power to the "B" train of safety-related equipment, as well as

some non-safety related loads. The "B" safety train is one of the two

redundant trains of equipment designed to safely shut the plant down in

case of an accident. Cell 31 is one of the original cells installed in

the battery in 1978 and was chosen as representing the most significant

fracturing visually observed on the battery. The positive post of Cell

31 was determined to have had random fractures extending over

approximately 90 percent of a cross-sectional area for a section taken

through the bolt hole parallel to the top surface of the battery cell.

The cause of the fracturing is apparently due to over-torquing.

The major concern is that the fractures and deformation of the posts

could cause an increase in the resistance of the intercell connections.

This would result in a reduction in the load carrying capability of the

battery and a reduction in voltage from individual cells, which would

result in an overall reduction in the battery voltage.

13

The capability of the battery to support the electrical load

requirements is documented during refueling outages by the performance

of either MST-920 or MST-921. MST-921 is a service test which tests the

load profile for the battery for a one hour duration. This test is done

every refueling outage. MST-920 is a performance test, which tests the

performance of the battery with a continuous load for an eight hour

duration. MST-920 is performed every five years.

MST-920 was performed on the "B" battery on September 26, 1993, and

showed that the "B" battery had a capacity of 103.1 percent. This test

was performed before the fracturing was observed. The licensee stated

that this test demonstrated that the battery capacity had not been

adversely impacted by the fracturing. MST-920 was also performed during

RF013 in 1988 and showed a capacity of 102.1 percent.

Preventative Maintenance Procedure, PM-411 measures the resistance of

the intercell connections with an acceptance level of less than 50

micro-ohms across the strap connections. These tests are consistently

below the acceptance criteria and have not shown an increasing trend

toward higher resistance levels. PM-411 also covers torquing values for

the intercell connections. Torque values for these connections did not

exist prior to 1987.

The licensee stated that the effect of battery cell-to-cell seismic load

transfer is not addressed by design basis documents for the Robinson

site. However, considerable information is available to demonstrate

that there is little likelihood of battery cell failure due to battery

cell terminal post or connecting strap malfunction. The licensee stated

that this conclusion is valid even considering the as-found condition of

the "B" battery cells at Robinson.

The licensee concluded that the battery will perform its safety

functions with the observed fractures in the posts.

This issue is being referred to the Region II Division of Reactor Safety

for followup and will be tracked as IFI 93-21-06: Vital Battery Terminal

Fractures.

For the maintenance observations no violations or deviations were

identified. One inspector followup item concerning battery post

fractures was identified.

5. Followup (92700, 92701, 92702)

(Closed) URI 93-19-05, Ventilation System Damper Manipulation During

Performance Of Surveillance Testing. Inspection Report 93-19 discusses

manipulation of air cleaning unit dampers on May 1, 1992, during

Engineering Surveillance Test Procedure, EST-023, Control Room Emergency

Ventilation System. As documented in the completed EST, this

manipulation was required to eliminate backflow through the idle ACU

fans due to the backdraft dampers not fully shutting. When questioned

on the appropriateness of this action, the system engineer stated that

14

counterweights had been added to the dampers to eliminate this problem.

However, the system engineer was unsure if these additional weights were

added before or after the May 1, 1992, performance of EST-023.

On September 27, 1993, the system engineer informed the inspectors that

the damper counterweights had been added approximately 5 months prior to

the May 1 performance of the EST. Hence, the counterweights failed to

ensure that the backdraft dampers shut during performance of the EST.

The system engineer stated that no further corrective actions, beyond

manipulating the dampers during the test had been performed.

The licensee also stated that this manipulation would not be necessary

with an ACU fan operating since the fans aid in damper closing. An ACU

fan starts when the ventilation system shifts to its safeguards

configuration.

Additionally, the system engineer pointed out that the operation of

these dampers is also checked every two weeks during the performance of

Operations Surveillance Testing, OST-750, Control Room Emergency

Ventilation System Test and that failure of these dampers to operate has

not been observed. Based on this information and observations by the

inspectors of control room ventilation system operation, the inspectors

concluded that there was no safety significance to the initial damper

manipulation.

(Closed) IFI 91-16-01, Review Methods to Achieve Criticality in the

Source Range. The SRNIs and IRNIs were retracted about two feet as part

of corrective actions for ACR 91-285. A decrease in SRNI indication by

about a factor of two was observed. The inspector reviewed EST-050,

Refueling Startup Procedure, completed for Cycle 14 and Cycle 15

startups.

The inspector compared the data taken during initial

criticality by boron dilution and found that criticality for Cycle 15

was achieved about a decade below the P-6 IRNI Low Flux Reactor Trip

block and SRNI de-energization setpoint. However, because new IRNI

detectors were installed during RFO 14, no meaningful comparison between

Cycle 14 and Cycle 15 data could be made. The inspector noted that the

POAH value for Cycle 15 was about a full decade below the value for

Cycle 14.

The inspector concluded that retracting the SRNIs and IRNIs

would allow criticality to be achieved before de-energizing the SRNIs.

(Closed) IFI 91-16-02, Review Enhancements to Procedure EST-050 to

Increase Guidance. This IFI dealt with additional guidance in EST-050

for activities associated with determining the POAH and establishing a

margin for the ZPTR, MTC calculation, and reactivity computer

calibration accuracy. The inspector reviewed EST-050, Revision 12, for

changes in response to this IFI.

A note was added before step 7.1.20 which listed plant parameter changes

that would indicate the POAH. These parameters included an increase in

pressurizer level, RCS T.,,

or RCS TH., or a decrease in reactivity

computer flux or reactivity. The inspector discussed these indications

15

with the licensee to verify which indication would be the most

responsive. The licensee stated the reactivity computer would respond

first due to the increased sensitivity to small flux changes. The

inspector then questioned if the other indications were sufficiently

responsive. The licensee stated that pressurizer level was the least

responsive indicator, but RCS T.,9 and RCS THt responded quickly because

the bypass manifold had been removed. Based on this review, the

inspector concluded these parameter changes were acceptable as

indications of the POAH.

EST-050 had been revised to establish the ZPTR Upper Limit up to one

decade below the POAH. The inspector reviewed the ZPTR limits

determined for the Cycle 15 startup and discussed these limits with the

licensee. The licensee stated that a 3/4 ZPTR decade Upper Limit was

used due to insufficient S/N for a full decade. The reduced S/N was

evidently due to lower neutron leakage for this particular core loading.

The inspector concluded that the one decade established sufficient

margin between the POAH and the ZPTR Upper Limit.

To provide additional resolution for the reactivity-temperature trace

used for MTC determination, an X-Y plotter was used to record the

reactivity-temperature data. Also, EST-050 directed the plotter scaled

to the maximum spans available for the paper size being used. The

inspector concluded the use of an X-Y plotter and maximizing the span

would enhance the ability to analyze the reactivity-temperature data.

The amount of data to be taken was specified as up to a 5*F change or

three or more inches of trace length. Because a heatup or cooldown rate

of 10*F/hr was required, the inspector questioned if trace length was

sufficient to obtain an acceptable reactivity-temperature relationship.

The licensee stated that the three inches of trace length historically

represented about a 4F temperature change. The inspector concluded the

specified trace length was an acceptable indication that sufficient data

was obtained.

Also EST-050 Attachment 8.4 was changed to require the two reactivity

computer calibration data set averages agree within +/-4%. The inspector

concluded this requirement was sufficiently accurate.

(Closed) IFI 93-12-05, NRC Review and Follow-up of Any SWS Heat

Exchanger Inspections and Tests During the 1993 Refueling Outage. The

inspector reviewed photographs of the EDG 'A' heat exchangers, the CCW

'A' heat exchanger, and the AFW 'A' lube oil cooler. These photographs

were taken immediately after these components were opened to record the

as-found condition.

The end bells for the EDG 'A' heat exchangers had soft sludge deposited

in defined rows. Also, nodules of the same soft sludge had deposited in

the water box of the heat exchangers. This sludge was easily removed and

there was insufficient accumulation to interfere with water flow through

the heat exchangers. There was a noticeable decrease in the amount of

sludge deposited when compared to the photographs for the previous

16

inspection. Small pebbles of manganese dioxide were found inside

several tubes. These pebbles did not obstruct flow. Some scale had

developed inside the tubes and some tubes were plugged with soft sludge.

The scale and soft sludge were removed during mechanical cleaning.

Prior to the heat exchanger final flush and closure, the inspector

checked the condition of the tubes.

Based on the visual examination,

the tubes were clear of any plugging, but some pebbles of manganese

dioxide were present. The licensee said these would be removed by the

final flush.

The AFW lube oil coolers were a four-pass heat exchanger in a four foot

long by six inch diameter jacket. The lube oil coolers were found to

have substantial fouling. The end bell was 90 percent fouled as were 30

percent of the tubes. The AFW 'A' lube oil cooler failed hydrostatic

testing and was replaced. The AFW 'B' lube oil cooler was mechanically

cleaned and reinstalled. The inspector reviewed the data for the last

six performances of OST-201, Motor Driven Auxiliary Feedwater System

Component Test, for indications of lube oil cooler degradation. The

lube oil differential temperature, which remained between 5'F and 7*F

over the last six performances, did not indicate any degradation. The

inspector discussed the substantial fouling of the lube oil coolers with

the licensee. The licensee stated the lube oil coolers historically

have had substantial fouling with no degradation indicated by OST-201.

The photographs of the CCW 'A' heat exchanger indicated minimal fouling.

Small quantities of the soft sludge had accumulated only in pockets and

crevices in the coating of the water box. The tubes appeared to be

clear of any fouling. Subsequent inside dimensional testing was

inconclusive and will be the subject of future inspection effort.

(Closed) LER 93-10, Diesel Generator Fire. At approximately 3:00 p.m.

on August 16, 1993, a small oil fire occurred on the exhaust manifold of

"A" Emergency Diesel Generator (EDG) during the performance of OST-401,

Emergency Diesels Slow Speed Start. The Unit was operating at 100

percent power at the time of the event. The fire was immediately

extinguished by the operator using a portable fire extinguisher. The

"A" EDG continued to operate for the period of time required by the OST

and the plant continued to operate at 100 percent power.

At approximately 3:20 p.m. the licensee declared an Alert, based on a

fire with the potential to affect safety-related equipment. The

Emergency Response Organization (ERO) was notified and the Technical

Support Center (TSC) was activated. Appropriate notifications were made

to State and Counties, the NRC, and other organizations as required.

Based on the fire being extinguished and the "A" EDG continuing to

operate in a loaded condition, the Alert was downgraded and the

emergency terminated at 4:37 p.m..

The licensee formed an incident evaluation team to determine the cause

of the fire and to recommend corrective actions. The incident

17

evaluation team identified that the gasket installed on the exhaust

manifold had been misaligned and crimped allowing oil from the pre-lube

process to leak into the heat shield where it later ignited and caused a

small fire.

The exhaust manifold gasket was replaced and the "A" EDG tested

satisfactorily. The licensee has committed to revising procedure CM

640, EDG Exhaust System Maintenance, to include more specific guidance

on the installation of the exhaust manifold gaskets. The procedure

change is to be completed by November 12, 1993.

6. Exit Interview (71701)

The inspection scope and findings were summarized on October 15, with

those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from

the licensee. The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

93-21-01

NCV: Failure Of STA To Conduct Turnover Required

By OMM-008 (Paragraph 3)

93-21-02

VIO: Failure To Follow Procedures, Two Examples

Concerning Opening The Incorrect Electrical

Breaker, and Sludge Lance Rig Vent Valve

(Paragraph 3)

93-21-03

NCV: Area Fire Watch Vacates Post (Paragraph 3)

93-21-04

VIO: Failure To Maintain Containment Integrity

During Refueling Operations (paragraph 3)

93-21-05

IFI: Fuel Assembly Loose Part (Paragraph 3)

93-21-06

IFI: Vital Battery Terminal Fractures (Paragraph

4)

7.

List of Acronyms and Initialisms

ACR

Adverse Condition Report

ACU

Air Cooling Unit

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CM

Corrective Maintenance

CV

Containment Vessel

EE

Engineering Evaluation

ECCS

Emergency Core Cooling System

18

EDG

Emergency Diesel Generator

EQ

Environmental Qualification

ERO

Emergency Response Organization

EST

Engineering Surveillance Test

FP

Fire Protection

GP

General Procedure

IFI

Inspector Followup Item

IR

Inspection Report

IRNIs

Intermediate Range Nuclear Instruments

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

MCC

Motor Control Center

MST

Maintenance Surveillance Test

MTC

Moderator Temperature Coefficient

CV

Non-cited Violation

OMM

Operations Management Manual

ONCA

Off Normal Condition Analysis Form

OP

Operations Procedure

OST

Operations Surveillance Test

PM

Preventive Maintenance

POAH

Point Of Adding Heat

RCCA

Rod Control Cluster Assembly

RCS

Reactor Coolant System

REV

Revision

RHR

Residual Heat Removal

RO

Refueling Outage

RWST

Refueling Water Storage Tank

S/G

Steam Generator

SI

Safety Injection

S/N

Signal-to-Noise Ratio

SP

Special Procedure

SRNIs

Source Range Nuclear Instruments

STA

Shift Technical Advisor

SWS

Service Water System

TAVG

Temperature Average

TMM

Technical Support Management Manual

TS

Technical Specification

TSC

Technical Support Center

WR/JO

Work Request/Job Order

ZPTR

Zero Power Testing Range