ML14178A387

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Insp Rept 50-261/93-19 on 930815-0911.Violations Noted.Major Areas Inspected:Operational Safety Verification,Surveillance Observation,Maint Observation,Engineered Safety Feature Sys Walkdown & Followup of Previously Identified Items
ML14178A387
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 10/04/1993
From: Christensen H, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A385 List:
References
50-261-93-19, IEIN-87-043, IEIN-87-070, IEIN-87-43, IEIN-87-70, NUDOCS 9310130066
Download: ML14178A387 (18)


See also: IR 05000261/1993019

Text

pV REGU

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/93-19

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: August 15 - September 11, 1993

Lead Inspector:

(--

. T. Orders, Senior Re S nt

pector

Date igned

Other Inspectors: C. R. Ogle, Resident Inspector

J. E. Tedrow, Senior Resident Inspector - Shearon Harris

Approved by: 9

'n

WH.

1. Christensen, Chief

Date 'Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

engineered safety feature system walkdown, and followup of previously

identified items.

Results:

One violation was identified involving an operator failing to follow the

applicable procedure during the performance of a surveillance test

(paragraph 3).

Another violation, with two examples, was identified concerning an inadequate

calibration program procedure (paragraph 6).

A non-cited violation was identified involving an area firewatch leaving his

post (paragraph 3).

9310130066 931005

PDR ADOCK 05000261

0

PDR

2

A second non-cited violation was identified involving a degraded diesel

generator ventilation system (paragraph 8).

An unresolved item was identified concerning the testing adequacy of component

cooling water pump start circuitry (paragraph 5).

A second unresolved item was identified concerning the manipulation of control

room ventilation dampers during performance of testing (paragraph 6).

A third unresolved item was identified pertaining to the adequacy of control

room ventilation system testing (paragraph 6).

The licensee's response to an ethylene glycol spill was poor; however, the

licensee met the reporting requirements of 50.72 (paragraph 3).

REPORT DETAILS

1. Persons Contacted

  • R. Barnett, Manager, Project Management

C. Baucom, Senior Specialist, Regulatory Compliance

S. Billings, Technical Aide, Regulatory Compliance

  • B. Clark, Manager, Maintenance
  • T. Cleary, Manager, Technical Support
  • D. Crook, Senior Specialist, Regulatory Compliance

C. Dietz, Vice President, Robinson Nuclear Project

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

S. Farmer, Manager Engineering Programs, Technical Support

R. Femal, Shift Supervisor, Operations

  • W.J

Flanagan Jr., Acting Plant General Manager

W. Gainey, Manager, Plant Support

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

J. Kozyra, Project Specialist, Licensing/Regulatory Programs

A. McCauley, Manager, Electrical Systems, Technical Support

R. Moore, Shift Supervisor, Operations

D. Morrison, Shift Supervisor, Operations

D. Nelson, Manager, Outage Management

  • A. Padgett, Manager, Environmental and Radiation Control

D. Seagle, Shift Supervisor, Operations

  • M. Scott, Manager, NSSS Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

  • A. Wallace, Acting Operations Manager

D. Waters, Manager Regulatory Affairs

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

  • Attended exit interview on September 15, 1993.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

Except for power reductions to perform required testing, the unit

operated at full power until initiating a shutdown at approximately

10:30 p.m., on September 10, 1993, to begin refueling outage 15.

The

unit-completed 351 days of continuous operation prior to the shutdown.

This was a record run for both Robinson and CP&L.

2

3. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operations records, data sheets, instrument traces,

and records of equipment malfunctions. Through work observations and

discussions with Operations staff members, the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to

alarms, adhered to procedures and applicable administrative controls,

cognizant of in-progress surveillance and maintenance activities, and

aware of inoperable equipment status. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS. Shift changes were routinely

observed, verifying that system status continuity was maintained and

that proper control room staffing existed. Access to the control room

was controlled and operations personnel carried out their assigned

duties in an effective manner. Control room demeanor and communications

were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were properly

implemented.

Boraflex Neutron Absorber

The resident inspectors performed a review of the licensee's use of

Boraflex in the spent fuel pool.

The inspectors determined that the

plant uses Boraflex as a neutron absorber in the high density fuel

racks. The licensee is aware of documented industry problems with

Boraflex and has evaluated IEN 87-43. At the close of this report

period, the licensee had not received IEN 93-70: Degradation Of Boraflex

Neutron Absorber Coupons. The licensee's operating staff is cognizant

of potential problems pertaining to spent fuel pool dilution and there

are procedural controls in place intended to prevent spent fuel pool

dilution.

The pool is maintained at a boron concentration of greater than 1950.

ppm.

The licensee has a chemistry sampling program in place to

routinely evaluate the boron concentration of the spent fuel pool.

The

results of the last three samples indicate a concentration in excess of

2100 ppm.

The licensee evaluates the integrity of the Boraflex absorber by

periodically analyzing coupon samples for signs of degradation.

3

According to the licensee's engineering staff, there has been no

evidence of the current, industry reported degradation in samples from

the Robinson SFP.

Turbine Runback During OST-005

At 11:28 a.m., on August 14, 1993, the unit experienced a runback during

the performance of OST-005, Nuclear Instrumentation Power Range (Bi

Weekly). The runback occurred when the SRO performing the OST

inadvertently mispositioned the dropped rod mode switch on power range

nuclear instrument N-41.

Following the SRO's recognition that a turbine runback was in progress,

the switch was restored to the correct position and the shift responded

to the transient. Following recovery from the transient, the unit was

restored to 100 percent power.

The inspectors interviewed the operator conducting OST-005; reviewed the

ACR and shift supervisor logs associated with the transient; and

analyzed the ERFIS printout for the runback. Additionally, the

inspectors reviewed the transient with the system engineer. Based on

this inspection effort, the inspectors determined that the operator

mispositioned the dropped rod mode switch when the OST was recommenced

following a brief interruption in the procedure. This interruption

occurred when the operator stopped the OST to obtain assistance in

monitoring an adjacent panel for an expected alarm. When the OST was

restarted, the operator manipulated the dropped rod mode switch instead

of the required operation selector switch.

Technical Specification 6.5.1.1, Procedures, Tests, and Experiments

requires, in part, that written procedures be established, implemented

and maintained, covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev 2. 1978. Regulatory Guide 1.33 Paragraph

8.b. requires that procedures be written for technical specification

surveillances. Implicit in this is the requirement that these

procedures be followed while performing technical specification required

surveillances. Operations Surveillance Test Procedure, OST-005, Nuclear

Instrumentation Power Range (Bi-Weekly) is provided to satisfy a

Technical Specification required surveillance for the power range

nuclear instruments.

Contrary to the above, on August 14, 1993, an on-duty operator deviated

from OST-005 and repositioned the dropped rod mode switch to normal

position from the specified bypass position. This action resulted in a

turbine runback. This is identified as a potential violation, VIO

93-19-01:

Operator Deviation From OST-005 Results in Turbine Runback.

From the review of the ERFIS printout, the inspectors noted anomalies

associated with the runback. These observations included an unexpected

1.5 second interruption in the turbine load limit runback.

Additionally, the time delay relay actuation did not occur concurrently

with the turbine load limit runback as expected. These observations

4

were provided to the system engineer. Following his review of the

transient, and confirmation of these observations, the system engineer

indicated that the performance of the system would be examined during

the upcoming outage. This commitment was also reaffirmed by the

cognizant engineering supervisor.

As turbine power was decreased by the runback, an expected deviation in

the reactor coolant reference temperature (Tref) and the average reactor

coolant temperature (Tave) developed. In response to this deviation, an

automatic insertion .of control rods occurred. This insertion eventually

resulted in control rod bank D being inserted below the rod insertion

limit. This condition was cleared after a boric acid addition and

restoration of control rods to normal position in the subsequent

recovery. The control rod bank D rods were below the insertion limit

for approximately 5 minutes. During a subsequent review of the

transient the licensee recognized that the insertion limit had been

exceeded and generated an ACR and LER to address this situation.

TS 3.10.1.3 requires that the control rod insertion limits be satisfied.

However, no action statements or LCOs are provided for inability to

maintain the rod insertion limits.

During their review, the licensee concluded that the rod insertion

limits may be violated during transients. The licensee has indicated

their intention to revise TS 3.10.1.3 to incorporate this conclusion and

provide an action statement for restoring rod positions. The inspectors

have no further question on this item.

Area Fire Watch Vacates Post

On August 31, 1993, the licensee determined that an area fire watch had

vacated his assigned post prematurely. The watch had been stationed in

the Unit 2 cable spread room as required by Fire Protection Procedure

FP-012, Fire Protection Systems Minimum Equipment and Compensatory

Actions, when the halon suppression system for that area (zone 19) was

disabled. The system was disabled at 9:29 a.m., on August 31, 1993, to

support work on penetrations associated with an ongoing plant

modification. At 5:36 p.m. that same day, while restoring the zone 19

system to service, the on-shift fire technician determined that the area

fire watch had left the cable spread room prior to the restoration of

the system.

The inspectors interviewed the area fire watch and on-shift fire

technician. Additionally, the inspectors reviewed the security log

printout for the area; reviewed the shift supervisor and on-shift fire

technician logs; and discussed the event with the cognizant supervisors.

Based on this effort, the inspectors determined that the area fire watch

was unaware of his responsibility to remain at his assigned station

until the fire suppression system was restored to service.

Instead, the

area fire watch had left when the modification work being performed that

day had been completed.

5

The licensee has documented the event on a Condition Evaluation Report

and covered the event with a portion of the Craft Resources Unit. The

licensee also committed to reviewing this event with all members of the

Project Management Section who perform area fire watch duties.

The failure of the area fire watch to remain in the cable Spread Room

with the fire suppression system disabled is a violation of FP-012.

However, this violation will not be subject to enforcement action

because the licensee's efforts in identifying and correcting the

violation meet the criteria specified in Section VII.B of the

Enforcement Policy. This item is identified as a non-cited violation,

NCV 93-19-02:

Area Fire Watch Vacates Post.

Ethylene Glycol Spill

On Monday, August 30, 1993, the licensee management was informed by a

chemistry technician of a spill of approximately one gallon of ethylene

glycol (antifreeze) which occurred on Saturday, August 28, 1993. Since

this spill exceeded the reportable quantity specified in the licensee's

Best Management Plan, a notification was made to the South Carolina

Department of Health and Environmental Control at 9:50 a.m., on August

30. Additionally, a notification to the National Response Center was

made at 9:55 a.m. that same day. As a result of these notifications,

the licensee made a 4-hour non-emergency notification to the NRC in

accordance with the requirement of 10 CFR 50.72(b)(2)(VI), Offsite

Notification, at 11:05 a.m., on August 30, 1993.

Based on interviews of individuals involved, the inspectors determined

that the spill occurred when a 55-gallon drum of antifreeze was

accidently dropped and punctured during a routine movement. The spill

occurred at a site storage area and was limited to the ground in the

immediate vicinity of the drum. Immediately following the spill, the

on-shift chemistry technician was notified. Based upon his review of

the spill, the small quantity involved, and information provided on the

Material Safety Data Sheet, he concluded that the hazard presented by

the spill was minimal.

As a result, no further action was taken until

he notified his supervisor of the spill on Monday, August 30. Following

this, the dirt in the vicinity of the spill was removed and the

notifications discussed above were made. Based on their review of this

event, the inspectors concluded that while the licensee's initial

response to the spill was poor, the licensee met the requirements for

NRC notification specified in 10 CFR 50.72. The inspectors have no

further questions on this event.

4. Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, testing was accomplished by qualified

personnel in accordance with an approved test procedure, test

6

instrumentation was properly calibrated, and that the tests conformed to

TS requirements. Upon test completion, the inspectors verified the

recorded test data was complete, accurate, and met TS requirements; test

discrepancies were properly documented and rectified; and that the

systems were properly returned to service. Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

OST-352

Containment Spray System Component Test

OST-401

Emergency Diesels (Slow Speed Start - EDG A Only)

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

5. Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in .

accordance with TS, approved procedures, and appropriate industry codes

and standards. The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following maintenance

activities:

WR/JO 93BTQ371

Calibrate CS Pump Discharge Pressure Gauges In

Accordance With Procedure PIC-302, Process

Instrument Calibration Procedure Pressure and

Vacuum Gauges.

WR/JO 93BVY371

Calibrate The CCW Pumps Pressure Instrumentation

(PC-611 Only)

WR/JO 93AIGX1

Replace Misaligned Gasket On EDG A

WR/JO AILN2

Solenoid Valve EV 1727 Venting Continuously

Adequacy of Testing For CCW Pump Autostart Feature

During followup on the calibration of the CCW pump discharge pressure

switch PC-611, the inspectors noted that the calibration procedure did

not fully verify the logic associated with the switch. The switch

actuates on a low pressure condition in the CCW discharge header to

provide an automatic start of idle CCW pumps. The pressure switch (PC

611) operates to energize a relay, the contacts of which operate to

start the standby pumps. The calibration procedure only checked the

actuation of the contacts in PC-611.

No check was made of the

associated relay or its contacts.

7

The inspectors noted from a review of the "Preliminary Revision" of the

CCW Design Basis Document that the low pressure autostart capability was

a design feature of the system. Based on this, the inspectors requested

that the license address the adequacy of the existing calibration

procedure to verify this potential design feature. The licensee had not

completed this evaluation prior to the end of the inspection period.

Pending the resolution of this issue, this item will be tracked as an

unresolved item, URI 93-19-03: Adequacy Of Testing For CCW Pump

Autostart Feature.

No violations or deviations were identified. Except as noted above, the

area/program was adequately implemented.

6. ESF System Walkdown (71710)

Control Room Ventilation System Walkdown

The inspectors reviewed the control room habitability system with

primary emphasis on the ventilation portion of the system. This effort

included a walkdown of the ventilation equipment; a review of the

calibration of installed instrumentation; a review of testing

accomplished to satisfy TS requirements; and a verification of selected

portions of the control room envelope. The inspectors also witnessed the

operation of the system in the emergency pressurization mode. Based on

this review, the inspectors concluded that the system was properly

aligned and capable of performing its intended safety function.

However, deficiencies were identified in material storage, completeness

of testing, instrument calibration, and design control.

During a physical inspection of the interior of the Main Control Room

HVAC System Instrument Panel Safety Train A on August 25, 1993, the

inspectors noted foreign material stored in the panel. This panel

houses differential pressure instrumentation associated with the

operation of the control room ventilation system. The material

identified included 2 bottles of gas leak detector, 1 bottle of soap

solution for leak checks, and 1 bottle of refrigerant oil.

This

information was conveyed to the shift supervisor for resolution. The

storage of these items in a panel for Technical Specification required

equipment is considered a weakness. During a subsequent inspection of

the panel, the inspectors noted that the material had been removed.

During a review of instrument calibration, the inspectors noted that

temperature controllers TC-6559 A and TC-6559 B, used to verify control

room temperature within the limits of TS 4.15.a, were not included in

the plant instrument calibration program. These instruments not only

provide a display of the control room temperature, but are also used for

WCCU operation. Following the identification of this item, the licensee

began monitoring control room temperature using alternate calibrated

temperature instruments. The licensee also performed calibrations of

TC-6559 A and B. The inspectors reviewed the results of these

calibrations and noted that both instruments were found in calibration.

The licensee also indicated that the instruments would be added to the

8

calibration program. The inspectors reviewed documentation provided by

the licensee which demonstrated that TC-6559 A and TC-6559 B were

calibrated in December 1990 when installed as part of a modification to

upgrade the control room ventilation system.

Technical Specification 6.5.1.1, Procedures, Tests, and Experiments

requires, in part, that written procedures be established, implemented,

and maintained, covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev. 2 1978, including procedures for ensuring

calibration of instruments. Maintenance Management Manual Procedure,

MMM-006, Calibration Program, is provided to ensure calibration of

installed plant instrumentation.

Contrary to the above, on August 31, 1993, MMM-006 was found to be

inadequate, in that, TC-6559 A and TC-6559 B (the instruments used to

verify compliance with Technical Specification limits on control room

temperature) were not included. This is one of two examples which in

the aggregate comprise a violation, VIO 93-19-04:

Failure To Properly

Maintain Instrument Calibration Program, Two Examples.

Based on the as-found data for the instrument being within tolerance and

observations of control room temperatures over the last operating cycle,

the inspectors concluded that this finding had minimal safety

significance.

The second item observed by the inspectors involved calibration of DPI

6520, Control Room Differential Pressure. The inspectors noted that

this instrument, which is used in surveillance testing to verify control

room pressurization capability, had not been calibrated within the

frequency specified in MMM-006. When queried by the inspectors on this

observation, the licensee stated that the instrument currently installed

as DPI-6520 is a manometer, which does not require calibration. The

calibration program had not been revised to reflect this change.

Technical Specification 6.5.1.1., Procedures, Tests, and Experiments

requires, in part, that written procedures be established, implemented,

and maintained, covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev. 2, 1978, including procedures for ensuring

calibration of instruments. Maintenance Management Manual Procedure

MMM-006, Calibration Program, is provided to ensure calibration of

installed plant instrumentation.

Contrary to the above, on August 30, 1993, MMM-006 was found to be

inadequate, in that, DPI-6520, Control Room Differential Pressure

Instrument, was inappropriately included. This is the second of two

examples which in the aggregate comprise a violation, VIO 93-19-04:

Failure To Properly Maintain Instrument Calibration Program, Two

Examples.

The inspectors reviewed surveillance testing conducted on the control

room ventilation system and the surveillance requirements for the system

in Technical Specifications. Specifically, the following surveillances

9

were reviewed: EST-023, Control Room Ventilation System; OST-163, Safety

Injection Test and Emergency Diesel Generator Auto Start On Loss of

Power and Safety Injection and Emergency Diesels Trips Defeat; OST-924,

Radiation Monitoring System; and OST-750, Control Room Emergency

Ventilation System.

The inspectors noted that EST-023 performed on May 1, 1992, made

reference to backflow through the air cleaning unit while it was idle.

The EST noted that this was corrected by operating the dampers

associated with the unit several times. When questioned by the

inspectors on this issue, the system engineer indicated he was aware of

intermittent problems associated with the dampers on the ACU fans in-the

past. However, he stated that counterweights had been added to the

dampers to alleviate the problem. He was unsure if these additional

weights were added before or after the conduct of the EST. The

inspectors requested additional information on the sequence of these

events.

Pending resolution of this item it will be tracked as an

unresolved item, URI 93-19-05: Manipulation Of Air Cleaning Unit

Dampers During Performance Of Testing.

The inspectors also noted that the testing accomplished by OST-163 and

OST-924 does not fully comply with the requirements of TS 4.15.3. TS 4.15.3 requires verification that on an SI test signal or high radiation

test signal the system switches into the emergency pressurization mode

with flow through the air cleaning unit (ACU). Neither OST verifies

flow through the ACU. Instead, both merely check for proper alignment

of dampers and starting of fars. The inspectors requested clarification

from the licensee on the methodology used to satisfy the TS

surveillance. Pending the resolution of this issue, it will be tracked

as an unresolved item, URI 93-19-06: Adequacy Of Control Room

Ventilation System Surveillance Testing.

TMI Action Plan Requirement Item III.D.3.4, Control Room Habitability

Requirements, is considered closed. Closing this item is based on .

reviews and evaluations provided in NRC letters to CP&L dated May 17,

1991, and October 26, 1990, as well as the walkdown described above.

7.

Employee Concerns Program

The inspector reviewed the licensee's employee concern Quality Check

program which was created to provide employees an alternate path from

their supervisor and normal line management to express safety concerns

or allegations. As part of this inspection, the inspector reviewed the

program implementing procedure and discussed the program/process with

the site Quality Check Representative. Survey reports of Quality Check

activities were also reviewed. See attachment for questions addressed

during this inspection.

The licensee had established several methods for submission of employee

concerns which included employee interviews, telephone, or by submission

of Quality Check Report (QCR) forms in one of several Quality Check

Station lockboxes. The inspector was informed that confidentiality of

10

the submitter was maintained. The Manager - Quality Check was

responsible for reviewing the QCRs and identifying nuclear safety issues

or other matters requiring management attention. Employee concerns were

classified in one of three categories. Nuclear safety issues or

technical/quality issues received the classification of a "Case" which

required an investigation and some form of action. Other concerns, such

as personnel issues, resulted in classification of Management

Information Items (MIls) or Notices of Information. Only Cases and MIIs

required a formal response from line management. After review by the

Manager - Quality Check, the concern was then transferred to Quality

Check forms and routed to assigned evaluators/investigators. The

inspector found that consideration was provided for reportability

determination by reference in the Quality Check forms to the licensee's

Corrective Action Program. The surveys of Quality Check activities for

1991, 1992, and through July 1993, indicated that 111 employee concerns

had been expressed. Of these, only 1 remained open.

8. Followup (92700, 92701, 92702)

(Closed) Unresolved Item 93-11-04, Degraded Diesel Generator Ventilation

System.

As detailed in Inspection Report 93-11, during the June 10, 1993

performance of bi-weekly surveillance test OST-401 on the A EDG,

licensee personnel observed that the room ventilation air return damper

was partially open when it was to have been closed. The damper is

designed to automatically close when the ambient air temperature is

above 55 degrees F. With the damper partially open, the efficiency of

the ventilation system was degraded. The licensee found that the damper

had been manually blocked open by a wooden wedge which had apparently

been manufactured for that purpose. At the close of that report period,

the licensee was evaluating the impact of this unauthorized modification

on the system's ability to perform its intended safety function and in

turn, the operability of the EDG. Pending the completion of that

evaluation, the issue remained unresolved.

The resident inspectors reviewed the licensee's safety analysis of the

event which indicated that the event had minimal impact on plant safety,

in that, the operability of the diesel was not jeopardized.

Specifically, the analysis indicated that under accident conditions,

operators would investigate the source of an abnormal temperature in the

room, and would have been able to take corrective actions (i.e., remove

the block of wood) prior to conditions causing a threat to the diesel.

Although the unauthorized modification of the ventilation system did-not

result in a significant diesel generator operability challenge, it

represents a failure to maintain system design integrity.

10 CFR 50 Appendix B, Criterion III Design Control, requires in part,

that measures be established to ensure that the design basis for

structures systems and components be maintained. Contrary to these

requirements, the design integrity of the A Emergency Diesel Generator

11

Ventilation System was not maintained in that the system underwent an

unauthorized modification which decreased its ability to performs its

intended function. However, this violation will not be subject to

enforcement action because the licensee's efforts in identifying and

correcting the violation meet the criteria specified in Section VII.B of

the Enforcement Policy. This item is identified as a non-cited

violation, NCV 93-19-07: Degraded Diesel Generator Ventilation System.

9. Exit Interview (71701)

The inspection scope and findings were summarized on September 15, 1993,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. The licensee did not identify as

proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

During the exit meeting, the licensee stated that the runback on

August 14, 1993, was the result of operator error. The licensee

questioned the appropriateness of a potential violation for a failure to

follow the applicable procedure in that the SRO did not willfully fail

to follow the procedural guidance. The inspectors acknowledged that the

violation did not appear to be willful, but informed the licensee that

the net result of the operator's error was a departure from the sequence

specified in the procedure, which in this case resulted in a turbine

runback. It was this deviation from the procedure which served as the

basis of the violation.

The licensee also questioned the characterization of the violation for

failing to calibrate TC-6559 A and B and maintaining DPI -6520 in the

calibration program as a failure to properly maintain MMM-006. The

licensee stated that these instruments had not been included in the

calibration program as a result of a failure in the modification process

(that being the failure of the modification which installed the

instrumentation) to provide appropriate documentation to revise MMM-006.

The licensee also stated that the inspectors had been informed of this

during the inspection period.

The inspectors acknowledged that they had been advised of this potential

inadequacy in the modification process during the inspection period.

However, the inspectors detected this problem during an ESF walkdown

while comparing the instruments installed in the control room

ventilation system against instruments listed in MMM-006. Since the

identification of the violation occurred while reviewing the

completeness of MMM-006, the inspectors concluded that it would be

appropriate to cite the violation against the inadequate procedure.

The following items were identified and reviewed during this inspection

period:

12

Item Number

Description/Reference Paragraph

93-19-01

VIO: Operator Deviation From OST-005 Results In

Turbine Runback (paragraph 3).

93-19-02

NCV: Area Firewatch Vacates Post (paragraph 3).

93-19-03

URI: Adequacy Of Testing For CW Pump Autostart

Feature (paragraph 5).

93-19-04

VIO: Failure To Properly Maintain Instrument

Calibration Program, Two Examples (paragraph 6).

93-19-05

URI: Manipulation Of Air Cleaning Unit Dampers

During Performance Of Testing (paragraph 6).

93-19-06

URI: Adequacy Of Control Room Ventilation

System Surveillance Testing (paragraph 6).

93-19-07

NCV: Degraded Diesel Generator Ventilation

System (paragraph 8).

10.

List of Acronyms and Initialisms

ACU

Air Cleaning Unit

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CS

Containment Spray

DPI

Differential Pressure Instrument

EDG

Emergency Diesel Generator

ERFIS

Emergency Response Facility Information System

HVAC

Heating Ventilation Air Conditioning

IEN

Inspection Enforcement Notice

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

MII

Management Information Items

MMM

Maintenance Management Manual

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test

PIC

Process Instrument Calibration

PPM

Parts Per Million

QCR

Quality Check Report

SI

Safety Injection

SFP

Spent Fuel Pool

SRO

Senior Reactor Operator

TAVE

Average Temperature of the Reactor Coolant

TI

Temporary Instruction

TMI

Three Mile Island

TREF

Reference Temperature of the Reactor Coolant

13

TS

Technical Specification

URI

Unresolved Item

VIO

Violation

WCCU

Water Cooled Condensing Unit

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ATTACHMENT

EMPLOYEE CONCERNS PROGRAMS

PLANT NAME: Robinson

LICENSEE: CP&L

DOCKET #: 50-261

NOTE: Please indicate yes or no as applicable and add comments in the space

provided.

A.

PROGRAM:

1.

Does the licensee have an employee concerns program? Yes

2.

Has NRC inspected the program? No. Quality Check site representative

discusses current issues with the Senior Resident Inspector on a routine

basis.

B.

SCOPE: (Indicate all that apply.)

1.

Is it for:

a. Technical? Yes

b. Administrative? Yes

c. Personnel issues? Yes

2.

Does it cover safety as well as non-safety issues? Yes

3.

Is it designed for:

a. Nuclear safety? Yes

b. Personal safety? Yes

c. Personnel issues - including union grievances? Yes

4.

Does the program apply to all licensee employees? Yes

5.

Contractors? Yes

6.

Does the licensee require its contractors and their subs to have a

similar program? No

7.

Does the licensee conduct an exit interview upon terminating employees

asking if they have any safety concerns? Yes.

C.

INDEPENDENCE:

1.

What is the title of the person in charge? Manager, Quality Check

2.

To whom do they report? Manager, Nuclear Assessment Department

3.

Are they independent of line management? Yes

4.

Does the ECP use third party consultants? The licensee does not

normally use outside consultants as part of the program.

5.

How is a concern about a manager or vice president followed up? A

review of the concern is conducted by the next level of management.

Concerns directed against the Manager, Nuclear Assessment Department are

immediately forwarded to the [Executive] Vice President, Nuclear

Generation Group

D.

RESOURCES:

1.

What is the size of the staff devoted to this program? Four. One

manager and three site representatives.

2.

What are ECP staff qualifications (technical training, interviewing

training, investigator training, other)? Minimal.

"Interviewing"

training including OJT. Experienced QA/QC personnel in this position.

E. REFERRALS:

1.

Who has followup on concerns (ECP staff, line management, other)?

Concern is identified, reviewed and classified by ECP staff members and

then forwarded to line management personnel for investigation and

resolution.

F. CONFIDENTIALITY:

1.

Are the reports confidential? Yes

2.

To whom is the identity of the alleger made known (senior management,

ECP staff, line management, other)? Senior management and ECP staff

3.

Can employees:

a. be anonymous? Yes

b. report by phone? Yes

G. FEEDBACK:

1.

Is feedback given to the alleger upon completion of the followup? Yes.

Verbal communication of results/resolution.

2.

Does program reward good ideas? Yes. Good ideas are rewarded with a

letter of appreciation from the President or Chief Operating Officer.

3.

Who, or at what level, makes the final decision of resolution? Manager,

Quality Check

4.

Are the resolutions of anonymous concerns disseminated? No, only to

submitter.

H. EFFECTIVENESS:

1.

How does the licensee measure the effectiveness of the program? The

licensee has no formal measure of program effectiveness.

2.

Are concerns:

a. Trended? Yes. Monthly status of number received and total YTD;

semi-annual report to senior management.

b. Used? Yes

3.

In the last three years how many concerns were raised?

111

Of the concerns raised, how many were closed? 110

What percentage were substantiated? The licensee does not substantiate

concerns.

4.

How are followup techniques used to measure effectiveness (random

survey, interviews, other)? A random survey conducted by senior

management.

5 )A-2

5.

How frequently are internal audits of the ECP conducted and by whom?

Infrequent. Only one internal audit of the program has been performed

since 1990, that one being conducted in August 1993.

I. ADMINISTRATION/TRAINING:

1.

Is ECP prescribed by a procedure? Yes

2.

How are employees, as well as contractors, made aware of this program

(training, newsletter, bulletin board, other)?

Initial GET training,

bulletin boards, ECP boxes located throughout the plant, posters, and

brochures.

A-3