ML14178A231

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Insp Rept 50-261/92-11 on Stated Date.Violations Noted. Major Areas Inspected:Operations Safety Verification, Response to Events,Surveillance Observation,Maint Observation & Mods
ML14178A231
Person / Time
Site: Robinson 
Issue date: 06/01/1992
From: Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A229 List:
References
50-261-92-11, NUDOCS 9206230109
Download: ML14178A231 (13)


See also: IR 05000261/1992011

Text

6V REGO

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/92-11

Licensee: Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: April 11, 1992 - May 10, 1992

Lead Inspector:

-

0./

-z

L. W. Garner, Sr. Residt

spector

Date Signed

Accompanying Personnel:

C. R. Ogle, Resident Inspector

Approved by: /

C7

A. 0. Christensen, Section Chief

Da e Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of

operational safety verification, response to events, surveillance

observation, maintenance observation, and modifications.

Results:

A violation was identified for failure to inhibit the north cable

vault fire suppression system prior to performing hot work in the

area. The actuation of the fire suppression system resulted in a

declaration of an Alert due to a toxic gas release within the

protected area. The event resulted from an established work

practice involving signing a section of the hot work permit which

indicated that the fire system had been inhibited before actually

doing so (paragraph 3).

A violation was identified for failure to follow instructions, in

that, service water system valves were removed before they were

scheduled. This resulted in the operating portion of the service

water system being in a configuration which had not been

seismically evaluated (paragraph 5).

9206230109 920601

PDR ADOCK 05000261

Q

PDR

2

A violation was identified for failure to correctly translate a

Residual Heat Removal system design basis into modification

instructions (paragraph 6).

An unresolved item was identified involving strainers being

installed in the component cooling water (CCW) pumps' suction

piping (paragraph 5).

An inspector followup item was identified involving proposed

control circuit modifications to allow both channels of the

emergency bus undervoltage load shed logic to trip the C CCW pump

(paragraph 4).

The emergency response to the unusual event and alert

declarations of April 13 and 15, respectively, were good

(paragraph 3).

The licensee demonstrated sensitivity to shutdown risk by

securing all work in and around areas associated with the safety

buses' normal offsite power source when both emergency diesel

generators became inoperable (paragraph 3).

Actions to preclude inadvertent removal of core components during

the upper internals package removal were well planned and

implemented (paragraph 3).

REPORT DETAILS

Persons Contacted

  • R. Barnett, Manager, Outages and Modifications

C. Baucom, Senior Specialist, Regulatory Compliance

J. Benjamin, Shift Outage Manager, Outages and Modifications

  • R. Beverage, Manager, Quality Assurance

W. Biggs, Manager, Nuclear Engineering Department Site Unit

  • S. Billings, Technical Aide, Regulatory Compliance
  • R. Chambers, Plant General Manager, Robinson Nuclear Project

T. Cleary, Manager -

Balance of Plant Systems and Reactor

Engineering, Technical Support

  • D. Crook, Senior Specialist, Regulatory Compliance
  • J. Curley, Manager -

Robinson Engineering Support, Nuclear

Engineering Department

  • C. Dietz, Vice President, Robinson Nuclear Project
  • D. Dixon, Manager, Control and Administration
  • J. Dobbs, Manager, Nuclear Assessment Department Site Unit
  • W. Flanagan, Manager, Operations
  • W. Gainey, Manager, Plant Support

B. Harward, Manager - Mechanical Systems, Technical Support

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

  • R. Labelle, Project Engineer, Nuclear Assessment Department

Site Unit

A. McCauley, Manager -

Electrical Systems, Technical Support

R. Moore, Shift Supervisor, Operations

  • P. Musser, Manager -

Engineering Assessment, Nuclear

Assessment Department Site Unit

D. Nelson, Shift Outage Manager, Outages and Modifications

A. Padgett, Manager, Environmental and Radiation Control

  • M. Page, Manager, Technical Support

D. Seagle, Shift Supervisor, Operations

  • E. Shoemaker, Project Engineer, Operations
  • R. Smith, Manager, Maintenance
  • D. Stadler, Onsite Licensing Engineer, Nuclear Licensing

G. Walters, Operating Event Followup Coordinator, Regulatory

Compliance

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians,

operators, engineers, mechanics, security force members, and

office personnel.

H. Christensen, Section Chief, Division of Reactor Projects,

was onsite April 14, 15, and 16, 1992, to meet with the

resident inspectors and plant management. Mr. Christensen

along with the inspectors observed the emergency prepared

ness response to the April 15 Alert (see paragraph 3).

  • Attended exit interview on May 13, 1992.

2

Acronyms and initialisms used throughout this report are

listed in the last paragraph.

2. Plant Status

RO 14 continued during the report period with fuel reload

scheduled for the third week of May. The core was fully off

loaded on April 22, 1992, to allow work on the CCW and RHR

systems, as well as to minimize shutdown risk. An NOUE

occurred when both EDGs became inoperable on April 13 and an

Alert was declared on April 15, when carbon dioxide gas was

released in a vital area (see paragraph 3).

At the end of

the report period, preparations were in progress to support

fuel reload.

3.

Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that

the facility was being operated safely and in conformance

with regulatory requirements. These activities were

confirmed by direct observation, facility tours, interviews

and discussions with licensee personnel and management,

verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the

inspectors reviewed shift logs, Operations' records, data

sheets, instrument traces, and records of equipment

malfunctions. Through work observations and discussions

with Operations staff members, the inspectors verified the

staff was knowledgeable of plant conditions, adhered to

procedures and applicable administrative controls, and were

aware of inoperable equipment status.

Shift changes were

observed, verifying that system status continuity was

maintained and that proper control room staffing existed.

Plant tours and perimeter walkdowns were conducted to verify

equipment operability, assess the general condition of plant

equipment, and to verify that radiological controls, fire

protection controls, physical protection controls, and

equipment tagging procedures were properly implemented.

Upper Internals Package Removal

On April 20, 1992, the inspectors witnessed the upper

internals package removal. Lighting and visibility in the

refuel cavity was good. In addition to personnel visually

observing the removal, a camera was utilized to look under

the upper internals package as soon as it was lifted above

the vessel flange. The inspectors concluded that the

actions to preclude inadvertent removal of core components

had been well planned and implemented.

3

NOUE Declaration Due To EDG Inoperability

On April 13, at approximately 10:00 a. m., the B EDG was

secured during routine surveillance testing because the

fitting downstream of the engine driven fuel oil pump showed

increased fuel oil leakage. At the time the B EDG was

considered to be available for service (TS do not require

any EDGs to be operable during cold shutdown).

The A EDG

was not available for service since it was partially

disassembled for PM work activities. Plant management,

after considering shutdown risk, decided to remove the B EDG

from service to repair the fitting. The inspectors verified

that appropriate considerations and actions were taken to

ensure that the remaining power sources, normal offsite

power and the dedicated shutdown DG were and would continue

to be available. These actions included securing all work

activities in the switchyard and around critical electrical

distribution components. At 1:43 p.m. when the B EDG was

placed under clearance, the plant entered a NOUE declaration

in accordance with its emergency plan (i.e., loss of both

EDGs).

The inspectors witnessed replacement of the fitting

and the subsequent successful fuel oil line leak test.

After verifying that the B EDG would start and run without

additional difficulties, the B EDG was considered to be

available for service. The routine testing was completed

later the same day. The inspectors verified by direct

observations, record reviews, and personnel interviews that

the emergency preparedness plan (including notifications)

had been implemented as required.

Alert Declaration Due To Carbon Dioxide Release Inside Vital

Area

On April 15, 1992, at 12:23 p.m., fire detection system zone

9 actuated releasing carbon dioxide fire suppressant into

the north cable vault area. Personnel evacuated the area

and fire brigade members were on the scene within one to two

minutes. The alarm and actuation were determined to be

spurious (i.e., there was no evidence of a fire).

At

approximately 12:30 p.m., fire brigade members in SCBA

initiated oxygen concentration measurements. At 12:42 p.m.,

the control room was informed that oxygen concentrations as

low as 12 percent had been found. After evaluation of the

EALs, an Alert declaration was issued at 12:53 p.m., based

upon a toxic gas release inside a vital area. The approved

emergency procedures classified gases which can create an

oxygen deficient atmosphere (such as carbon dioxide) as

toxic gases. Actions were taken to ventilate the affected

area to the plant stack. At 1:28 p.m., oxygen measurements

in the north cable spread area indicated normal air

concentrations. At 1:56 p.m., a final oxygen concentration

survey was completed in adjacent and lower elevations of

4

containment and the auxiliary building. This survey also

confirmed oxygen concentrations were normal and there were

no pockets of carbon dioxide trapped in low areas. Since

turnover to the TSC was in progress at the time, it was

decided to complete this process and allow the TSC to review

the plant conditions and actions taken. The TSC was fully

staffed and turnover from the control room was completed at

2:06 p.m. Based upon a review of the plant conditions, the

SEC in the TSC declared the Alert condition terminated and

the event over at 2:11 p.m. The inspectors verified by

direct observation, record reviews, and personnel interviews

that the emergency preparedness plan had been properly

implemented during this event.

ACR 92-103 was issued to review the spurious actuation cause

and develop corrective actions. The inspectors interviewed

personnel involved in the event and reviewed applicable

records and the draft ACR conclusions. The ACR indicated,

and the inspectors confirmed, that the event had occurred

due to a long standing work practice (over 11 years) of

authorizing hot work permits prior to defeating the fire

detection or suppression systems. In this specific

instance, the fire technician had signed and dated the hot

work permit no.92-247, FP-005 attachment 7.1 section III

item 3, before inhibiting the fire suppression system for

zone 9. Item 3 states "Hot Work Permit approved, system(s)

inhibited (if applicable), ready for shift foreman's

approval."

The fire technician had identified on the hot

work permit that the fire suppression system for zone 9

would need to be inhibited. The person receiving the permit

was unaware that he was to contact the fire technician prior

to beginning work so that the fire technician would inhibit

the zone 9 fire suppression system. Thus, when grinding

activities for M-1074, Electrical Penetration Replacement

Project -

Phase II, began at 12:41 p.m., the system had not

been inhibited. This work practice had apparently existed

as a method to expedite work activities by already having

the authorized hot work permit at the location when the fire

detection or suppression system was inhibited. The

circumstances surrounding this event was of concern because

of the long duration involved and that individuals in

Operations outside the fire protection group should have

been aware of the practice. The failure to inhibit the zone

9 fire suppression system was identified as a VIO: Failure

To Implement FP-005 Resulted In Alert Declaration,

92-11-01.

One violation was identified. Except as noted above, this

program area was adequately implemented.

5

4.

Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with license

requirements. For the surveillance test procedures listed

below, the inspectors determined that precautions and LCOs

were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, testing was

accomplished by qualified personnel in accordance with an

approved test procedure, test instrumentation was properly

calibrated, the tests were completed at the required

frequency, and that the tests conformed to TS requirements.

Upon test completion, the inspectors verified the recorded

test data was complete, accurate, and met TS requirements,

test discrepancies were properly documented and rectified,

and that the systems were properly returned to service.

Specifically, the inspectors witnessed/reviewed portions of

the following test activities:

OST-401

Emergency Diesels (Slow Speed Start)

SP-1080

Safety Injection System Flow Test

SP-1128

Bus Undervoltage And Load Shed Test For

Emergency Bus El

SP-1129

Bus Undervoltage And Load Shed Test For

Emergency Bus E2

SP-1080

SP-1080 was performed to obtain flow, pressure, and

temperature test data to be used for future system

evaluations such as determining the feasibility of balancing

the SI cold leg flows. Preliminary evaluation of the data

confirmed that either the A or B SI pump could deliver, via

any two cold leg injection pathways, a flow rate in excess

of that assumed in the accident analyses. However, the data

contained discrepancies which appeared to limit the data's

usefulness for rigorous analyses. Specifically, the

inspectors observed that when the minimum flow isolation

valves SI-856A and B were closed, the pressure in the three

injection paths increased; however, the flow rates in two

paths increased as expected while the flow rate in the third

path decreased by approximately 5 percent (13 gpm).

This

may have resulted from inaccuracies in the flow measuring

instrumentation. Also, the pressure gauges used to measure

pressure in the three injection headers were in 10 psig

divisions. Thus, the pressure instruments could not provide

the necessary precision to measure the small pressure

6

changes with sufficient accuracy to allow the data to be

used in analyses. Additional testing during the next RO was

being considered.

Emergency Bus UV Trip Channel Functional Testing

On September 27, 1991, the NRC issued TS Amendment no. 136

to authorize operation until RO 14 without the El and E2 UV

trip channels being fully tested as required by TS (see IR

91-20).

The inspectors observed performance of SP-1128 and

1129 which tested the previously untested portions of the UV

trip logic. SP-1128 was satisfactorily completed; however,

three problems were identified during performance of SP

1129.

The first problem involved a wiring discrepancy

between the as built configuration and the actual field

installation. The labels on two wires were switched inside

the electrical panel. This resulted in the test procedure

not working as written; however, the load shed function was

unaffected. Testing was continued after the wires were

labeled in accordance with the CWD. The second problem

involved the 480V Bus 3 Main Breaker (52/15B) not reclosing

after having been cycled once. The test was continued after

the breaker latching mechanism and alarm switch were

repaired. The third problem involved the discovery that the

C CCW pump received a trip signal from only one UV trip

channel. The B CCW pump received a trip signal from both UV

trip channels. The UV CWDs B-190628 sheets 276 and 277

showed contacts from both UV trip channels being in the

C CCW pump circuit, whereas the C CCW pump CWD B-190628

sheet 209 showed that only the channel 1 UV trip channel was

part of the pump control circuit. The C CCW pump breaker

was confirmed to be wired in accordance with the C CCW pump

drawing. SP-1129 was then completed without any further

major difficulties. At the end of the report period, a

temporary modification was being developed to wire the other

trip channel into the C CCW pump trip circuit. The

temporary modification will install wiring in the breaker

side of the cubical prior to restart. When the emergency

bus is de-energized during the next refueling outage for

PMs, a permanent modification will rewire the circuit in a

more conventional manner (i.e., in the back of the breaker

cubical).

Installation of the permanent modification is

identified as an IFI: Review C CCW Pump Trip Circuit

Modification Installation, 92-11-02.

No violations or deviations were identified. Except as

noted above, this program area was adequately implemented.

7

5.

Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance

activities on systems and components to ascertain that these

activities were conducted in accordance with TS, approved

procedures, and appropriate industry codes and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were

operable. The inspectors verified that required

administrative, material, testing, radiological, and fire

prevention controls were adhered to. In particular, the

inspectors observed/reviewed the following maintenance

activities:

CM-031

Service Water Booster Pump

Maintenance

PM-302

Crane Swing Check Valve Inspection

WR/JO 90-ANRZ1

A EDG Exhaust Expansion Joint

Replacement

WR/JO 91-AIGAl

A MDAFW Pump Inspection/PM

WR/JO 91-ANGR1

Unit Auxiliary Transformer Bus Bar

Inspection

WR/JO 92FLJ525

MCC 6 Compartment Inspection/PM

A MDAFW Pump Impeller Inspection

On April 16, 1992, while observing work activities

associated with WR/JO 91-AIGA1, the inspectors examined the

visible part of the A MDAFW pump rotating assembly. There

was no evidence of recirculation damage as observed in 1989

(see IR 89-17).

SW Valve Removal Prior To Scheduled Removal

On April 21, SW valves SW-374 and 376 (the A and B SW pump

discharge check valves, respectively) were removed from the

piping system. These valves had been scheduled to be

removed after the fuel was off loaded from the reactor

vessel due to SW system seismic considerations. Since all

four SW pumps discharge into a common header, the removal of

the valves placed the operating portion of the SW in a

configuration which had not been seismically evaluated. An

engineering evaluation later determined that the piping in

the operating portion of the SW system had remained

seismically qualified. The early removal was in part caused

8

by the A and B SW pumps being under clearance, which allowed

personnel to believe that it would be alright to work these

valves early if they had the opportunity. Prior to their

removal, personnel failed to adequately coordinate the work

activity with the planning and scheduling organization. At

the end of the report period, long term corrective actions

had not been developed. The failure to implement

instructions appropriate to the circumstances (i.e., the

work schedule) was a violation of 10 CFR 50 Appendix B

Criterion V. This item is identified as a VIO: Failure To

Implement Appropriate Instructions During SW-374 and 376

Valve Maintenance, 92-11-03.

MCC 6 Inspection

On April 27, 1992, the inspectors witnessed performance of

PM route E-023 on safety related MCC 6. The route required

inspection of the motor starter contacts, circuit bridging

and meggering, and general inspection and cleaning. The

route also specified that the thermal overload be checked

for wear. Discussion with the I & C technicians performing

the work revealed that this instruction appeared not to be

very meaningful. The only check being performed for wear

was a visual external examination for signs of overheating.

The inspectors discussed this item with the WR/JO planner.

The planner indicated that he was unfamiliar with the intent

of this step. The planner initiated a note to the

maintenance procedure writers to clarify this item when the

route is revised under the rewrite program. The inspectors

observed that the MCC compartment components were in good

condition. Work requests were being issued to replace

pitted contacts when necessary.

B SWBP Discharge Check Valve Inspection

On May 6, 1992, the inspectors witnessed the B SWBP

discharge check valve (SW-560) disassembly in accordance

with PM-302.

During B SWBP operation, this valve had been

identified via the deficiency tag program as emitting an

unusual noise. Valve inspection revealed that the hinge

pin's staking pin had come out. This allowed the hinge pin

to wobble inside the disc arm causing significant wear to

the arm. However, the valve disc seated properly. The worn

components were replaced and the valve returned to service.

The staking pin was missing and could not be located. The A

SWBP discharge check valve is also to be inspected during

this RO.

CCW Pump Suction Strainers

During replacement of the three CCW pump suction isolation

valves, a strainer was found in the each of the pumps'

9

suction piping. P&ID no. 5379-376, sheet 1, revision 25,

contained a note which indicated that the temporary pump

suction strainers had been removed. Based upon this note,

the strainers were removed. A large rubber piece, possibly

part of a butterfly valve disc seal, was found in one of the

strainers. Actions were initiated via ACR 92-127 to locate

the source of the rubber piece and repair the component as

deemed necessary. The cognizant engineer indicated that the

rubber piece could have potentially restricted flow at the

pump impeller inlet. Engineering was evaluating the

desirability of installing new strainers in the CCW system.

The inspectors noted that the removed strainers were more

typical of permanently installed strainers than of the kind

usually used as temporary strainers. Whether or not the

strainers found in the piping were intended to be installed

is considered as an URI: Determine If CCW System Design

Included Pump Suction Strainers, 92-11-04.

One violation was identified. Except as noted above, this

program area was adequately implemented.

6.

Modifications (37828)

During revision of operating procedures, it was discovered

that the RHR recirculation piping configuration being

installed per M-1087, RHR Pumps Minimum Flow Recirculation,

would not allow the RHR Hx outlet temperature to be heated

to within 25 degrees F of the RCS prior to placing the RHR

system in shutdown cooling. The existing recirculation

line, located downstream of the RHR Hx bypass line, allowed

flow to bypass the RHR Hxs as necessary to allow warm-up of

the RHR system. The new RHR recirculation piping

configuration, involving larger and separate recirculation

flow paths for each RHR pump, was connected upstream of the

RHR Hx bypass line. The new configuration would recirculate

only cooled water back to the RHR pump suction line. Thus,

the new configuration did not provide the ability to warm

the RHR system to the above stated temperature criteria.

The temperature criteria is contained in GP-007, Plant

Cooldown From Hot Shutdown To Cold Shutdown, revision 24,

step 5.2.32.10. M-1087 has been revised to retain the

existing recirculation line as well as installing the new

recirculation flow paths.

The normal development and review processes for M-1087

failed to detect the above described design deficiency. The

problem was detected by Operations personnel during

development of procedure changes required by M-1087.

The

inspectors noted that the procedures could have easily been

revised without detecting this problem; therefore, the

discovery reflected outstanding attention to detail by the

procedure preparer. During M-1087 development, the

10

responsible engineer apparently knew that the RHR system was

to be warmed prior to placing it in shutdown cooling.

However, he failed to understand that in this process the

bypass flow around the RHR Hxs was more significant that the

heat added by the RHR pumps. A contributor to the design

activity breakdown was the lack of documentation for the

functional or operating basis of the RHR recirculation line.

An ACR has been issued to review the design activities

associated with M-1087. However, corrective action to

preclude future similar events has not been developed. The

failure to assure that the design basis for the RHR system

was correctly translated into specifications, drawings,

procedures, and instructions as required by 10 CFR 50

Appendix B Criterion III is identified as a VIO: Failure To

Translate RHR System Design Basis Into M-1087, 92-11-05.

One violation was identified.

Except as noted above, this

program area was adequately implemented.

7.

Exit Interview (71707)

The inspection scope and findings were summarized on May 13,

1992, with those persons indicated in paragraph 1. The

inspectors described the areas inspected and discussed in

detail the inspection findings listed below and in the

summary. Dissenting comments were not received from the

licensee. The licensee did not identify as proprietary any

of the materials provided to or reviewed by the inspectors

during this inspection.

Item Number

Description/Reference Paragraph

92-11-01

VIO -

Failure To Implement FP-005

Resulted In Alert Declaration

(Paragraph 3)

92-11-02

IFI -

Review C CCW Pump Trip

Circuit Modification Installation

(Paragraph 3)

92-11-03

VIO -

Failure To Implement

Appropriate Instructions During

SW-374 and 376 Valve Maintenance

(Paragraph 5)

92-11-04

URI -

Determine If CCW System

Design Included Pump Suction

Strainers (Paragraph 5)

92-11-05

VIO -

Failure To Translate RHR

System Design Basis Into M-1087

(Paragraph 6)

8.

List of Acronyms and Initialisms

a.m.

Ante Meridiem

ACR

Adverse Condition Report

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CM

Corrective Maintenance

CWD

Control Wire Diagram

DG

Diesel Generator

EAL

Emergency Action Level

EDG

Emergency Diesel Generator

F

Fahrenheit

FP

Fire Protection

GP

General Procedure

gpm

gallons per minute

Hx

Heat Exchanger

I & C

Instrument And Control

i.e.

That is

IFI

Inspector Followup Item

IR

Inspection Report

LCO

Limiting Condition for Operation

M

Modification

MCC

Motor Control Center

MDAFW

Motor Driven Auxiliary Feedwater

NOUE

Notice of Unusual Event

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test

p.m.

Post Meridiem

P&ID

Piping and Instrumentation Diagram

PM

Preventive Maintenance

psig

pounds per square inch -

gage

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RO

Refueling Outage

SCBA

Self-contained Breathing Apparatus

SEC

Site Emergency Coordinator

SI

Safety Injection

SP

Special Procedure

SW

Service Water

SWBP

Service Water Booster Pump

TS

Technical Specification

TSC

Technical Support Center

URI

Unresolved Item

UV

Undervoltage

V

Volts

VIO

Violation

WR/JO

Work Request/Job Order