ML14178A158

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Insp Rept 50-261/91-20 on 910907-1011.Apparent Violation Noted.Major Areas Inspected:Operational Safety Verification, Maint Observation,Onsite Review Committee Activities, Esfs Walkdown & Followup
ML14178A158
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 10/25/1991
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A157 List:
References
50-261-91-20, NUDOCS 9111220017
Download: ML14178A158 (15)


See also: IR 05000261/1991020

Text

RE~O

UNITED STATES

/0

NUCLEAR REGULATORY COMMISSION

REGION lI

0

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/91-20

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: September 7 -

October 11, 1991

Lead Inspector:

L. W. Garner, Senior Resident rspector

Ddte Signed

Other Inspector(s): K. R. Jury, Resident Inspector

Approved by:~ 6 (?L

oe

r.).

Christensen, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, maintenance observation, onsite review committee

activities, engineered safety feature system walkdown, and followup.

Results:

An apparent violation was identified involving inadequate Engineering design

.control and interfaces (paragraph 5).

Three non-cited violations were identified involving: a security watchperson's

failure to perform an adequate personnel search; non-licensed operators

performing licensed operator duties; and a failure to provide adequate

procedures for performing Technical Specification surveillance testing

(paragraph 2).

An unresolved item was identified relating to Loss of Coolant Accident analyses

conformance with 10 CFR 50.46 requirements (paragraph 5).

Operator performance (i.e.,

command and control) was professional during two

reactor power reductions (paragraph 2)).

9111220017 911025

PDR

. ADOCK (,5000261

G

2

Immediate corrective actions taken in response to the OT Delta T issue were

timely and extensive (paragraph 5).

REPORT DETAILS

1. Persons Contacted

  • R. Barnett, Manager, Outages and Modifications
  • C. Baucom, Senior Specialist, Regulatory Compliance
  • F. Bishop, Principal Engineer, Nuclear Assessment Department
    • R. Chambers, Plant General Manager
  • C. Dietz, Vice President, Robinson Nuclear Project
  • D. Dixon, Manager, Control and Administration
  • W. Gainey, Manager, Plant Support
  • W. Jackson, Engineer, Technical Support
    • J. Kloosterman, Manager, Regulatory Compliance
  • A. Padgett, Manager, Environmental and Radiation Control
  • M. Page, Manager, Technical Support
  • R. Parsons, Manager, Robinson Engineering Support
  • D. Stadler, Onsite Licensing Engineer, Nuclear Licensing
  • R. Steele, Shift Supervisor, Operations
  • A. Wallace, Acting Manager, Operations

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and office personnel.

  • H. Christensen, Section Chief, Division of Reactor Projects was on site

October 9, 10,

and 11,

1991,

to meet with the resident inspectors and

plant management.

  • Attended exit interview on October 11, 1991.
    • Attended exit interview on October 21, 1991.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements.

These activities were confirmed by direct observation, facility tours,

interviews

and discussions with licensee personnel

and management,

verification of safety system status, and review of facility records.

To verify equipment operability and compliance with TS,

the inspectors

reviewed shift logs, Operation's records, data sheets, instrument traces,

and records of equipment malfunctions.

Through work observations and

discussions with Operations staff members,

the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to alarms,

adhered to procedures and applicable administrative controls, cognizant of

2

in-progress surveillance and maintenance activities, and aware of

inoperable equipment status.

The inspectors- performed channel

verifications and reviewed component status and safety-related parameters

to verify conformance with TS.

Shift changes were observed, verifying

that system status continuity was maintained and that proper control room

staffing existed.

Access to the control

room was controlled and

operations personnel carried out their assigned duties in an effective

manner. Control room demeanor and communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment,

and to

verify that radiological controls, fire protection controls, physical

protection controls,

and equipment tagging procedures were properly

implemented.

Non-Licensed Operators Standing Watch

On September 5, 1991, the licensee identified that two individuals who had

recently completed SRO training performed the duties of RO license

positions (stood watch) prior to receiving their NRC SRO licenses.

The

docket numbers for these individuals was telephonically transmitted on

August 19, 1991.

At that time, the licensee erroneously believed that a

docket number was sufficient basis to allow these individuals to stand

watch (i.e., docket number issuance was equivalent to license issuance).

One individual had an inactive RO license and was in the process of

license reactivation when he received his docket number. This individual

stood watch as RO and BOP operator on seven occasions prior to license

issuance.

The other individual was an "instant" SRO who was previously

licensed at another licensee facility (Shearon Harris).

He stood watch on

three occasions as RO and once as BOP operator prior to receiving his

license.

After recognizing this problem, the licensee immediately relieved the one

individual who was on shift. An ACR,91-317, was generated to document

and perform a root cause analysis on this problem.

Apparently, the

licensee believed the docket number to be sufficient documentation to

allow potential ROs or SROs who had taken and passed the NRC license

examination to stand watch.

Discussions were held between the licensee

and the Region II Operations Branch Chief to resolve this issue and to

discuss the historical basis for the licensee's position.

The licensee

was informed that ROs and SROs are not permitted.to perform licensed

duties before license issuance.

10 CFR 55.3 requires that a person must

be authorized by a license to perform the function of an operator or

senior operator.

10 CFR 55.53 (e) delineates the requirements to

reactivate a license.

Failure of these individuals to.meet the

requirements of 10 CFR 55 is a violation. However, this violation meets

the criteria specified in Section V.G.1. of the NRC Enforcement Policy (10

CFR 2, Appendix C) for not issuing a Notice of Violation and is not cited.

This violation is identified as an NCV: Non-Licensed Operators Performing

Licensed Operator Duties, 91-20-01.

7@

3

Inadequate Personnel Search

On September 12,

1991,

the inspector observed an inadequate personnel

search at PAP West.

The search was inadequate, in that, a watchperson

assigned to the metal detector did not perform a visual inspection of an

item which was not processed through the X-ray detector.

The inspector

questioned the watchperson and determined the watchperson was unaware of

what the unsearched item was.

The watchperson then stopped the employee

prior to him accessing the PA and searched the item.

The watchperson

determined that the item was permitted inside the PA.

After discussion of this event with security management, the licensee

performed a comprehensive investigation, took appropriate disciplinary

action, and provided emphasis (through a "Lessons Learned" memorandum) to

all security personnel on the necessity to follow procedures.

Security procedures require that all items or equipment be searched by

visual inspection or by processing through special purpose detectors.

The

watchperson's failure to perform the search as described above is a

violation.

However,

this violation meets the criteria specified in

Section V.A. of the NRC Enforcement Policy (10 CFR 2, Appendix C) for not

issuing a Notice of .Violation and is not cited.

This violation is

identified as an NCV: Failure To Perform An Adequate Personnel Search,

91-20-02.

Emergency TS Amendment Due To Inadequate Surveillance Testing

During internal electrical distribution system reviews on September 13,

1991, the licensee questioned whether or not each channel associated with

the loss of power load shed feature had been tested as required by TS

Table 3.5-3, item 3.a.

The licensee additionally questioned if

load

shedding upon a simulated loss of all-normal AC coincident with a safety

injection signal,

had been demonstrated as required by TS 4.6.1.2.

An

operability determination (91-20) was initiated to determine the status of

testing and compliance with TS requirements.

On September 14, based upon engineering reviews, the licensee determined

that the applicable TS surveillance requirements had not been fully

satisfied.

These reviews identified instances in which the ability of

both channels to initiate load shedding had not been tested. In addition,

breakers were identified which had not been demonstrated to open when a

load shed signal was initiated.

Upon the determination that these

surveillance requirements had not been properly implemented, the loss of

voltage instrument channels were declared inoperable (TS Table 3.5-3, item

3.a).

An 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to hot shutdown LCO was appropriately entered at 4:50

p.m. Based upon the circuit components known to have been tested and the

reliability of the components which were either not tested or still under

evaluation, the licensee determined that a high confidence level existed

that the loss of voltage instrumentation safety function would be

accomplished

if

called upon(i.e.,

the condition had minor safety

significance).

However, due to the complexity of developing a test

4

procedure, testing could not be performed prior to LCO expiration. Thus,

the licensee requested a Wavier of Compliance from Region II to determine

the feasibility of developing a test procedure which could be performed

with the plant on line and/or the need for emergency TS relief.

Regional

management, after consultation with NRR, agreed to a Waiver of Compliance

which authorized continued power operation until midnight on September 18.

A condition of the waiver was to train Operations personnel

on

compensatory actions which could be taken if

load shedding would fail to

occur.

The inspectors verified, through attending training sessions and

interviews with personnel, that the committed training was provided.

On September 16, Engineering recommended, and plant management concurred,

that on-line testing was not desirable.

Thus, emphasis was shifted to

emergency TS change development to allow continued operation until RO 14

or an outage of sufficient length to allow time for test procedure

development and performance.

On September 18,

per letter NLS-91-245,

the licensee submitted an

emergency request for license amendment.

Enclosure 5 of this letter

identified the circuit components and functions which were not fully

tested.

The

PNSC meetings which approved the emergency request for license

amendment is discussed in paragraph 5. A Waiver of Compliance was granted

on September 18, 1991, to allow continued operation pending NRC review and

approval of the emergency request. On September 27, 1991, the NRC issued

Amendment No. 136 to grant authorization to operate until testing can be

performed on, or no later than, RO 14.

The failure to perform surveillance testing as required by TS is a

violation.

A previous violation (90-11-01) was issued in June 1990 for

failure to take adequate corrective action to preclude inadequately

established surveillance procedures.

In response to this violation, a

program was initiated to ensure that established procedures adequately

implement instrumentation surveillance test procedures.

At the time of

discovery, this process had not yet been performed on the TS surveillance

requirements

in question.

The identification of this violation by

engineering personnel was considered a strength.

No violation is being

cited as the criteria of Section V.G.1 of the NRC Enforcement Policy (10

CFR 2, Appendix C) was met.

The violation is identified an an NCV:

Failure To Provide Adequate Procedures For Performing TS Surveillance

Testing, 91-20-03.

B Condensate Pump Motor Ground

On September 19, 1991, at 11:41 p.m., a 4160V switchgear ground alarm was

received on the RTGB.

Although I & C verified that the alarm input was

valid, there were not any other indications that a ground existed.

Additional troubleshooting early the following morning, revealed that the

4160V buss 4 ground device had actuated as indicated by closed relay

contacts; however,

the normal visual indicator, a red flag, did not drop.

5

Shortly after 9:00 a.m.,

smoke was smelled in the vicinity of the power

cable conduit associated with the B condensate pump motor. At 9:18 a.m.,

a reduction to 50 percent power was initiated to allow removal of the B

condensate pump. from service.

When the B condensate pump motor breaker

was opened, the ground alarm reset. Inspection of the field power cables

to the motor stabs revealed damage indicative of a current path in this

area (i.e., electrical short).

The motor windings were found to be

undamaged.

The motor was shipped offsite for repairs.

Shop inspection

revealed that a breakdown had occurred in the B phase stab's insulation

which had initiated a current pathway through the fiberglass stab holder

block to one of the stab holder block's. mounting bolts.

The damaged

components were replaced or repaired as necessary.

The motor was

re-installed, successfully tested, and returned to service on September

24, 1991.

Power escalation to 100 percent was initiated, but was delayed

due to repairs to a leaking relief valve on the 5B FW heater and the 6A FW

heater's level indicating column and level control valve.

Full power

operation resumed on September 26, 1991.

Investigation into the failure of the ground relay flag to actuate

disclosed that a design problem exists.

The amount of current which

activates the flag's positioning relay is determined by the high

resistance of the annunciator circuit.

Due to this high resistance, the

current was not sufficient to activate the relay. The licensee was in the

process of evaluating possible design changes to correct the condition, as

well as reviewing other-circuits to determine if similar conditions exist.

This is an IFI: Review Corrective Actions Associated With Failure Of A

Ground Relay Flag To Drop, 91-20-04.

Turbine Drain Line Steam Leak

On September 27,

1991,

a leak developed in the number 4 governor valve

drain line.

After consideration of possible on-line repairs, the licensee

decided to remove the unit from service to replace the affected line and

inspect similar lines from the other governor valves. Since repairs were

expected to require less than a day, reactor power was maintained at

approximately 0.01 microamperes as indicated on the intermediate range

power monitors.

The affected line and two others which had unacceptable

wall thinning, as determined by ultrasonic inspections, were replaced.

The unit was returned to service the next day and resumed 100 percent

power operation on September 29.

The line failure was attributed to

errosion.

The licensee is re-evaluating the

scope of their

errosion/corrosion program.

Both power reductions described above were witnessed by the inspectors.

The Operations staff demonstated good command and control during these

evolutions, as both power reductions were professionally performed without

incident.

Three non-cited violations were identified.

6

3. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS,

approved procedures,

and appropriate industry codes

and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material,

testing,

radiological,

and fire prevention controls were adhered to.

In

particular, the inspectors observed/reviewed the following maintenance

activities:

CM-507

Emergency Diesel Lube Oil Strainer

PM-007

Emergency Diesel Generator Inspection

Number 1

WR/JO 91-ALNAl

Exhaust Turbocharger Oil Leak

WR/JO 91-ALEMI

Air Receiver Relief Valve Replacement

WR/JO 91-FMA392

EDG B Compresser Oil Change

No violations or deviations were identified.

4. Onsite Review Committee (40500)

The inspectors evaluated certain activities of the PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements. In particular, the inspectors attended

the September 16 and 17,

1991 PNSC meetings in which the request for a

Waiver of Compliance from the requirements of TS Table 3.5.3 and

surveillance requirement 4.6.1.2 was reviewed.

(See paragraph 2 for

details concerning this issue.)

During the September 16 meeting, the

inspectors observed that the PNSC members mixed their safety review

function with their management function.

The focus of this meeting

shifted from evaluating the safety implications (risk and potential

consequences) of the issue to improving the wording of the Waiver of

Compliance to maximize the probability it would be approved.

This was

manifested by the PNSC expending almost all of the two and one half hour

PNSC meeting in rewording and rewriting the proposed request for

regulatory relief.

The

PNSC recognized that another review would be

necessary and scheduled one for the next day. After the first meeting,

the inspectors expressed concerns about the conduct of the meeting with

plant management. The inspectors subsequently determined that even though

the potential scope of the problem was recognized on September 16,

the

degree to which various components had been tested, if at all, was not

known by the PNSC members.

Prior PNSC meetings,

both routine and

special, have typically been well conducted with the appropriate emphasis

on safety. The September 17, 1991 meeting which approved the request for

Waiver of Compliance was more typical of the manner in which PNSC meetings

have been conducted. On September 27, 1991, the inspectors met with the

Plant General Manager and the Regulatory Compliance Manager to discuss

concerns with the PNSC's performance.

The inspectors expressed concern

about the focus of the September 16 PNSC meeting, the potential conflict

7

due to possible ownership by the PNSC for a document which the PNSC had

essentially generated, and the lack of a total understanding of what had

not been tested (i.e., could not make an adequate evaluation of the

issue's safety significance).

The Plant General Manager acknowledged the inspectors concerns.

Though

not totally agreeing with the inspectors comments,

he did indicate that

the September

16

PNSC

meeting was atypical and had not met his

expectations.

Both the inspectors and plant management agreed that

between the two meetings,

the PNSC had adequately discharged its duties

during the review of the Waiver of Compliance request. It was determined

that provisions of the TS dealing with membership, review process,

frequency, and qualifications were satisfied.

No violations or deviations were identified.

5.

Followup (92700, 92701, and 92702)

(Closed)

URI 91-14-01,

Review Impact Of Entrainment Losses On

LOCA

Analysis, and URI 91-19-01, Determine Safety Significance and Root Causes

Of Excessive OT Delta T and OP Delta T RPS Time Delays.

These issues (discussed in IRs 91-14 and 91-19, respectively) involved

numerous design/engineering breakdowns.

However,

at the time the

associated IRs were issued, questions involving ECCS performance during a

SBLOCA had not been fully resolved. Also, the licensee's review into the

significance and root causes of the excessive OT Delta T and OP Delta T

RPS time delays had not been completed.

The following paragraphs

summarize the LOCA issues and related analyses (SI issue),

as well as,

provide an update to the excessive OT Delta T and OP Delta T RPS time

delays

The SI issue involved the effects of entrainment inventory losses and

securing ECCS flow during the transfer from the injection phase to the

recirculation phase of a LOCA. The amount of inventory prior to and the

rate of inventory loss during the time ECCS is interrupted, determines the

PCT during the transfer.

The transfer is performed via Emergency

Procedure EPP-9, Transfer to Cold Leg Recirculation.

EPP-9

is required to be initiated when the RWST level reaches 27 percent and the

actual transfer is to be completed prior to RWST level reaching 9 percent.

The procedure restricts the time that ECCS flow is interrupted to ten

minutes for SI system component re-alignments when RCS system pressure is

above the shutoff head of the RHR pumps and to three minutes when the RCS

system pressure is below this value. The former case corresponds to small

SBLOCAs while the latter case corresponds to the larger SBLOCAs and

LBLOCAs.

On June 20,

1988, TS Amendment 119 was issued to support single SI pump

operation.

The analysis to support the amendment ,failed to address the

consequences of having only one SI pump available during implementation of

EPP-9.

In January 1989,

NFS Design Activity 89-001 was generated to

8

provide justification for a revision to EPP-9 to recognize that only one

SI pump may be available during a LOCA .

Utilizing a simple decay heat

model from a text book, written by El-Wakil,

Design Activity 89-001

demonstrated that the flow rate from one SI pump would be slightly greater

than the steaming rate due to decay heat.

Consequently, the licensee

concluded that core cooling is maintained during performance of EPP-9;

thus operation with one SI pump was deemed acceptable.

However, on May

14,

1991,

as a result of IPE activities, the licensee determined that

Design Activity 89-001 did not consider the inventory loss due to

entrained water in determining the flow out of the break.

The previous

analyses associated with a minimum operation of two SI pumps during EPP-9,

the plant configuration prior to February 1988,

had appropriately

incorporated entrainment losses.

Upon this discovery, reactor power was

reduced to 60 percent as previous analysis supported.

Following an

interim Westinghouse analysis justifying operation at 95 percent power

(assuming a 700 degree F maximum PCT after the injection phase and a core

heat load based on ANS 1979 decay heat plus 2 sigma),

power was increased

to 90 percent on May 15,

1991.

Later that day, the NRC informed the

licensee that use of the ANS 1979 decay heat model was not in compliance

with 10 CFR 50 Appendix K requirements.

Accordingly,

on May 16, the

licensee informed the staff that the interim analysis was reperformed

using the ANS 1971 decay heat plus 20 percent model and that acceptable

results were obtained for power operation up to 92.5 percent.

On May 29,

1991,

based on a more rigorous re-analysis which used the

ANS-1971 plus 20 percent model,

Westinghouse determined that the maximum

PCT while ECCS flow is interrupted per EPP-9 during a LBLOCA

was

approximately 1250 degrees F.

The results of this re-analysis were

discussed with the NRC,

and the unit was subsequently returned to full

power later that day.

(Based

on questions by the NRC regarding mass

quantity and distribution in the core, the maximum PCT while ECCS flow.is

interrupted per EPP-9 during a LBLOCA was subsequently revised to

approximately 1400 degrees F.)

Since. the licensee and Westinghouse assumed the LBLOCA to be the most

limiting case, none of the analyses discussed above addressed the affects

of a SBLOCA during the EPP-9 time frame. This bounding of the SBLOCA was

based upon the engineering judgement that prior to securing ECCS flow per

EPP-9 during a SBLOCA, the inventory in the vessel would be as great or

greater than that which would exist for a LBLOCA.

Prompted by the NRC.,

subsequent

SBLOCA analysis revealed that during the transfer to

recirculation with only one SI pump available, the SBLOCA is not bounded

by the LBLOCA. Specifically, this new analysis indicated that the SBLOCA

inventory level is significantly less than previously assumed (i.e., core

uncovery is greater and exists for a longer period of time than that

previously anticipated).

Thus, as calculated for the worst case SBLOCA (a

one and one-half inch break), the maximum PCT of 1936 degrees F during the

time ECCS flow is interrupted exceeds the worst case LBLOCA

PCT of

approximately 1400 degrees.

The SBLOCA PCT during EPP-9 is less than the

2200 degrees F 10 CFR 50.46 ECCS acceptance criteria and less than the

values calculated for both the SBLOCA and LBLOCA PCT during the initial

9

injection phase (i. e.,

2096 and 2178 degrees F, respectively).

When the

plant license was amended in June 1988 to allow the configuration of only

one .SI pump being available to mitigate the consequences of a design basis

accident, the licensee failed to analyze the consequences of only one SI

pump operation during ECCS switchover. This issue was identified by the

NRC during their review of re-analyses associated with the entrainment

issue. As determined, the SBLOCA is independent of the entrainment issue

due to the higher RCS pressures experienced.

Accordingly, URI 91-14-01

regarding entrainment losses is considered closed.

However,

the

acceptability of a second peak (i.e., approximately 1400 and 1936 degrees

F for the LBLOCA and SBLOCA, respecitvely) is still under review by the

NRC.

This is an URI:

Determine If The Existance Of Second Peak Is In

Accordance with 10 CFR 50.46, 91-20-05.

Summarizing the SI issue, there were -significant breakdowns in the

technical reviews/analyses performed throughout the chronology.

These

included: (1) Failure to perform an analysis to support single SI pump

operation in June 1988; (2) Inadequate analysis performed in January 1989

(Design Activity 89-001)

to support single SI

pump operation; (3)

Inadequate analysis performed by Westinghouse to permit power operation up

to 95 percent power,

and this was not identified by the licensee prior to

power accession from 60 percent to 90 percent power; and (4) Incomplete

SBLOCA analysis performed due to the belief that the LBLOCA analysis was

more limiting.

Engineering/design control concerns similar to the SI issue discussed

above were also seen in the OT Delta T and OP Delta T excessive time delay

problem addressed in URI 91-19-01. The OT Delta T septpoint provides for

the on-line protection against DNB.

This setpoint is part of the RPS

circuitry, and provides a reactor trip when the core Delta T, a measure of

reactor power, exceeds the setpoint value.

The setpoint is calculated

based on inputs of core temperature,

pressure, and power distribution.

The plant safety analyses assume the OT Delta T trip function is used to

mitigate three UFSAR Chapter 15 events.

As discussed in IR 91-19, the problem resulted from capacitors (filters)

being installed in the OT Delta T and OP Delta T (which is not used in

accident analyses) RPS circuitry. These capacitors imparted an additional

approximate two second time delay on RTD system response time.

As a

result, the OT Delta T protection circuitry response time exceeded that

used in the accident analyses approximately 6.75 seconds versus the 4.75

seconds analyzed.

Based on a review by the fuel vendor (Siemens)

for

cycles 13 and 14,

the licensee has concluded that sufficient margin was

available to compensate for the additional channel response time, such

that the OT Delta T trip function would have performed as required to

maintain the MDNBR greater than the TS value of 1.17. However, actual RCS

flow rates had to be utilized for one of the three Chaper 15 events

(Uncontrolled Control Rod Assembly Withdrawal at Full Power) to obtain an

MDNBR greater than 1.17.

10

As identified by the licensee, the root cause of this event was that

Westinghouse,

the modification designer, failed to include capacitor

removal in the modification work instructions (FCN) or to perform a post

modification transient test of the associated circuitry. It appears that

an excessive reliance was placed on Westinghouse for FCN completeness and

neither the reviews performed on the FCN nor subsequent modification

reviews identified the fact these capacitors needed to be removed.

Additionally,

even

though

the

PLS

document

change

recommendation

identified the change in the capacitors' time delay (identified in PLS

document to be zero), the hardware changes required were not communicated

nor independently identified.

These problems indicate design control

breakdowns between Westinghouse and the

licensee's engineering

organizations.

The licensee's immediate corrective action after identifying this issue

was both timely and appropriate.

An independent investigation team,

including NSD and NAD, performed a thorough review/root cause analysis of

this issue and previous related OT Delta T issues.

While this issue's

safety significance (discussed above)

was not great,

the licensee

recognized the necessity of accurate RPS setpoints.

Long term corrective

actions will be tracked via LER 91-009 and the violation below (91-20-06).

Accordingly, URI 91-19-01 is considered closed.

The chronology of engineering review/communication breakdowns for the OT

Delta T and the SI issue indicates that there has been, and continues to

be, significant deficiencies in engineering design control and interfaces.

This is contrary to 10 CFR 50 Appendix B, Criterion III, and is identified

as an apparent Violation:

Inadequate Engineering Design Controls and

Interfaces, 91-20-06.

The following historical examples demonstrate that the adequacy of design

controls and interfaces has been a continuing problem for the licensee:

-

Inadequate engineering communications and reviews were issues in 1988

and 1989 related to OT Delta T concerns previously addressed in IRs

88-03 and 89-12.

These issues resulted in a violation of 10 CFR 50

Appendix B Criterion III in 1989 (Vio 89-12-02).

Inadequate

calculational, design, and modification testing review problems were

identified with the AFW NPSH issue in late 1989 ( EA 89-188 and IRs

89-11,

89-18,

and 89-20).

In addition, inadequate engineering

reviews were also identified in 1989 involving the Agastat relay

tolerance issue (IR 89-12).

-

During

1990

(IR

90-22),

concerns were identified with the

interdepartmental

communications during development of two

RMS

modifications.

Engineering also failed to identify that one of the

modification's proposed radiation monitors was inadequately ranged.

-

Also in 1990, errors involving LBLOCA analysis computer codes and

interpretation of TS figure 3.10-5 (IR 90-23) indicated inadequate

oversight/communications between the licensee and the fuel vendor.

Additionally, a 1991 issue (VIO 91-01-03) was identified involving

inadequate engineering review of modification M-1016,

Electrical

Penetration Replacement.

(Closed)

VIO 89-09-05,

Design Control

Measures Were Not Adequately

Established to Assure That The 50 GPM Leak Isolation Capability Design

Basis

Was Correctly Translated Into Specifications,

Drawings,

and

Procedures for the RHR System.

The inspectors reviewed the licensee's

response dated July 26, 1989, to the NOV. The inspectors agreed that the

root cause was a lack of adequate design basis and that the DBD process

should correct this deficiency.

The inspectors reviewed modification

M-1017,

Eliminate RHR Pump Common Mode Failure, which provided enhanced

leak detection

and isolation capabilities.

This consisted of:

installation of RHR pit sump level indicators on the RTGB; control room

annunciation of high water level in the pit; installation of motors on the

RHR-752 A, B, valves; and movement of the isolation valves for the CCW

supply lines to the RHR pump Hxs' and SW supply lines to the RHR room

coolers into areas which would be accessible during the recirculation

phase of an accident. This modification provides adequate indication of a

leak in the RHR pit, as well as providing remote leak isolation

capability. This item is-closed.

(Open) LER 89-11, Auxiliary Feedwater System Flow Rate Could Exceed Limits

of Accident Analysis.

The SDAFW

pump discharge flow control valve,

FCV-6416, has been mechanically limited such that under steam line break

accident conditions, the maximum flow rate does not result in a mass input

into the CV in excess of that used in the safety analysis.

This

limitation results in the SDAFW pump being limited to approximately half

its flow capacity during normal plant transients.

Modification 1025,

Upgrade AFW FCV 6416, is being developed for installation in RO 14 to

correct the design deficiency.

This

item remains

open pending

installation and successfully testing of the modification.

One violation was identified.

6. Organizational Changes

On September 10, 1991, Mr. R.H. Chambers, Operations Manager, was named as

General Manager -

Robinson Plant. Mr. W. J. Flanagan, previosly Manager,

Modification Projects, and recently licensed as an SRO, was appointed to

the position of Operations Manager.

On September 18, 1991, Mr. C.R.

Dietz, Manager - Robinson Nuclear Project, was elected to the position of

Vice President.

7. ESF System Walkdown (71710)

This inspection was performed during the EDSFI conducted the weeks of

September 23-27,

October 7-11,

and 21-25,

1991.

The details of this

inspection will be documented in IR 91-21.

13

e.g.

For Example

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EPP

End Path Procedures

F

Fahrenheit

FCN

Field Change Notice

FCV

Flow Control Valve

FW

Feedwater

Hx

Heat Exchanger

I&C

Instrumentation & Control

IPE

Individual Plant Evaluation

IR

Inspection Report

KV

Kilovolt

LBLOCA

Large Break Loss of Coolant Accident

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

M

Modification

MDAFW

Motor Driven Auxiliary Feed Water

MDNBR

Minimum Departure from Nucleate Boiling Ratio

NCV

Non-cited Violation

NED

Nuclear Engineering Department

NFS

Nuclear Fuels Section

NLS

Nuclear Licensing Section

NOV

Notice of Violation

NPSH

Net Positive Suction Head

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

OT Delta T

Overtemperature Delta Temperature

p.m.

Post Meridiem

PA

Protected Area

PAP

Personnel Access Portal

PC

Protective Clothing.

PCN

Project Change Notice

PCT

Peak Cladding Temperature

PLS

Precautions, Limitations, and Setpoints

PNSC

Plant Nuclear Safety Committee

REV

Revision

RHR

Residual Heat Removal

RMS

Radiation Monitoring System

RNP

Robinson Nuclear Project

RO

Reactor Operator

RO

Refueling Outage

RPS

Reactor Protection System

RTD

Resistance Temperature Detector

RTGB

Reactor Turbine Generator Board

RWST

Reactor Water Storage Tank

SBLOCA

Small Break Loss of Coolant Accident

SI

Safety Injection

SRO

Senior Reactor Operator

SW

Service Water

14

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

VIO

Violation