ML14176A876

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Insp Rept 50-261/90-11 on 900411-0510.No Violations Noted. Major Areas Inspected:Operational Safety Verification, Monthly Surveillance Observation,Monthly Maint Observation, Action on Previous Insp Findings & Mods
ML14176A876
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 06/06/1990
From: Dance H, Garner L, Jury K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14176A874 List:
References
50-261-90-11, NUDOCS 9006210522
Download: ML14176A876 (13)


See also: IR 05000261/1990011

Text

6R REG(

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/90-11

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: April 11 -

May 10, 1990

Inspectors:

.(.,

L. .Grrfer'Senior

Resi'dentfhspector

DAe Signed

K. R.

  • ry,

R

dent Inspector

Da

Approved by:

L

H. C. Dance, Section Chief

Dat Si ned

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification; monthly surveillance observation; monthly maintenance

observation; onsite followup of written reports of nonroutine events; action

on previous inspection findings; and design, design changes, and modifications.

Results:

A similar violation was identified involving inadequate procedures for performing

Technical Specification required surveillance tests.

The procedure review

which identified this item was considered a strength (paragraph 5).

The Corporate Nuclear Safety/plant support of the pre-outage "focus on safety"

meeting was a reflection of the licensee's commitment to safety first

(paragraph 2).

A weakness was identified in operation's utilization of temporary procedure

changes (paragraph 3).

2

A weakness was identified in the Onsite Nuclear Safety evaluation process

for information notices and Part 21 reports.

Steps were not always taken to

ensure that all the previous vendor names associated with a component were

researched when determining if a specific vendor's component was installed in

a safety-related application (paragraph 5).

Discrepancies associated with the electrical distribution system design basis

document were processed in accordance with approved procedures and with the

proper emphasis on safety. A weakness was identified in that open items, those

with less significance than discrepancies, were not being prioritized or

tracked for resolution (paragraph 7).

REPORT DETAILS

1. Persons Contacted

R. Barnett, Manager, Outage Management

C. Baucom, Senior Specialist, Regulatory Compliance

C. Bethea, Manager, Training

R. Chambers, Engineering Supervisor, Plant Performance

D. Crook, Senior Specialist, Regulatory Compliance

J. Curley, Manager, Environmental and Radiation Control

C. Dietz, Manager, Robinson Nuclear Project

J. Eaddy, Supervisor, E & RC Support

R. Femal, Shift Foreman, Operations

S. Griggs, Technical Aide, Regulatory Compliance

  • E. Harris, Manager, Onsite Nuclear Safety
  • J. Kloosterman, Director, Regulatory Compliance

D. Knight, Shift Foreman, Operations

R. Moore, Shift Foreman, Operations

  • R. Morgan, Plant General Manager

D. Nelson, Shift Outage Manager, Outage Management

  • M. Page, Manager, Technical Support

D. Quick, Manager, Plant Support

0. Seagle, Shift Foreman, Operations

J. Sheppard, Manager, Operations

  • R. Smith, Manager, Maintenance

R. Steele, Shift Foreman, Operations

  • H. Young, Director, Quality Assurance/Quality Control

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on May 16, 1990.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements.

These activities were confirmed by direct observation, facility tours,

interviews and discussions with licensee personnel and management,

verification of safety system status, and review of facility records.

To verify equipment operability and compliance with TS,

the inspectors

reviewed shift logs, operation's records, data sheets, instrument traces,

and records of equipment malfunctions.

Through work observations and

discussions with operations staff members,

the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to alarms,

adhered to procedures and applicable administrative controls, was cognizant

2

of in-process surveillance and maintenance activities, and was aware of

inoperable equipment status.. The inspectors performed channel verifica

tions and reviewed component status and safety-related parameters to

verify conformance with TS.

Shift changes were routinely observed,

verifying that system status continuity was maintained and that proper

control room staffing existed. Access to the control room was controlled

and operations personnel carried out their assigned duties in an effective

manner. Control room demeanor and communications continued to be informal

yet effective.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment,

and to

verify -that radiological controls, fire protection controls, physical

protection controls,

and equipment tagging procedures were properly

implemented.

Transformer Outage

The unit was removed from service on May 4, 1990, to upgrade the cooling

capacity of the main transformer banks.

The unit was scheduled to remain

in hot shutdown during the outage and be returned to service on May 14.

Major work on the main transformers included: replacement of the cooling

coils; installation of new fans, pumps, and conservator tanks; addition of

another bank of fans and pumps; drying of the windings; and replacement of

the transformer oil.

The work will lower the operating temperature and

reduce water content in the windings; thereby, potentially extending the

lifetime of the transformers.

In addition, the following work was

performed on the unit auxiliary transformer: the windings were dried, the

oil was replaced, and a new conservator tank was installed.

With. no capability to backfeed through the main transformer banks and

being aware of the Vogtle loss of.power event, steps were taken to ensure

that power remained available to safety-related equipment.: The area

around the startup auxiliary transformer (normal power source during a

shutdown) was roped off and all vehicular traffic in the switchyard was

being controlled by spotters.

Outage work around the offsite and onsite

power distribution system was limited, closely monitored, and controlled.

In addition, both the emergency diesel generators, the dedicated shutdown

deisel generator, both safety-related battery systems, and both loops of

motor driven AFW, SI, and RHR systems remained in service. Of the major

safety-related equipment, only the D SW pump was removed from service

(pump

replacement).

Work on secondary system components such as the

overhaul of the A main feedwater pump and the B heater drain pump

replacement did not have potential impact on safety-related systems.

On May 2, 1990, the inspectors attended a pre-outage "focus on safety"

meeting sponsored by ONS.

The purpose of the meeting was to review the

defined work scope and ensure that measures would be implemented to

3

control evolutions such that undesirable interactions between simultaneous

work activities would not result in unexpected safety system unavailability

or transients.

This concept was an extension of the pre-startup safety

review meeting at CP&L's BSEP facility.

The CNS/plant support of the

pre-outage focus on safety meeting was a reflection of the licensee's

commitment to safety first.

No violations or deviations were identified.

3. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LCOs were adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, and that the tests conformed to

TS requirements.

Upon' test completion, the inspectors verified the

recorded test data was complete, accurate, and met TS requirements; test

discrepancies were properly documented and rectified; and that the systems

were properly returned to service.

Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

EST-10 (revision 3)

Containment Personnel Airlock Leakage Test

MST-021 (revision 6)

Reactor Protection Logic Train B at Power

OST-202 (revision 21)

Steam Driven Auxiliary Feedwater System Component

Test

OST-615 (revision 9)

Low Voltage Fire Detection and Actuation

Systems, Zones 20, 21, and 22

OST-905 (revision 9)

Radiation Monitoring System

OST-910 (revision 11)

Dedicated Shutdown Diesel Generator

During the performance of OST-202, steps 7.2.7 and 7.2.8, the inspectors

noted that neither condensate or vapor was observed from the SDAFW pump

steam line drain to atmosphere when valve MS-159 was opened.

The

operators verified that the system was properly aligned. They then closed

MS-156 and MS-158 in an unsuccessful attempt to observe vapor from the

line.

The system was re-aligned and the lack of condensate in the line

was verified by observing proper operation of the steam trap and

verification that the line was hot.

Because the intent of the steps

(demonstration of no water in the line) was met, steps 7.2.7 and 7.2.8

4

were signed-off as complete.

The inspectors discussed with the cognizant

operating personnel the desirability of using a temporary procedure change

when a given methodology provided in a procedure does not provide the

expected results.

Not issuing a temporary procedure change under this

circumstance was identified as a-weakness in the operation's utilization

of temporary procedure changes.

No violations or deviations were identified.

4. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS and approved procedures.

The inspectors determined

that these activities did not violate LCOs and that required redundant

components were operable. The inspectors verified that required

administrative, material,

testing, and fire prevention controls were

adhered to. In particular, the inspectors observed/reviewed the following

maintenance activities:

CM-008 (revision 6)

Steam Driven Auxiliary Feedwater Pump Overhaul

CM-010 (revision .3)

Service Water Pump Overhaul

WR/JO 90-AASB1

Replacement of D SW Pump.

WR/JO 90-AFHR1

Repair of SDAFW Pump Oil Leak

On April 30, 1990, the SDAFW pump was removed from service to repair an

oil leak. Upon removal of the bearing cover on the pump end of the shaft,

it was observed that heat shrink tubing around the thermocouple wires to

the bearings was blocking the oil return port. A similar situation on the

turbine end of the pump had been corrected in January 1990 (see IR 90-02).

In January, it had been surmised that the piece of heat shrink on the pump

side was shorter and if it had not swollen and blocked the return oil port

at that time, then it would probably not do so.

The inspectors witnessed portions of the disassembly and re-assembly of

the SDAFW pump. A damaged area, approximately one and one-half inches by

three sixteenths of an inch, appeared to the inspectors to have changed

since last observed during the Fall 1989 pump overhaul.

The system

engineer indicated that the area appeared as before. The area is only 2

3 mils deep and therefore represents no structural concern. Neither the

licensee nor the pump vendor representative could definitely identify the

mechanism of degradation. Since the mechanism of degradation is unknown,

the inspectors discussed with plant management the feasibility of

periodically inspecting this area. During the exit, the licensee indicated

5

that they would reinspect this area for changes during the Fall 1990

refueling outage.

The licensee currently has on order a new impeller

which they plan to install during the next pump overhaul.

On May 9, 1990, in accordance with the PM program, the D SW pump was.

replaced with a factory rebuilt spare.

During testing, the rebuilt pump

experienced approximately 10 percent greater shutoff head than expected

and an acceptable yet higher than expected vibration.

The old pump and

motor was re-installed and successfully tested. The rebuilt pump will be

returned to the vendor for inspection and correction of the deficiency.

No violations or deviations were identified.

5. Onsite Followup of Written Reports of Nonroutine Events (92700)

(Closed)

P2189-01,

Brown Boveri K-line, K-225 through K-2000 Circuit

Breakers Delivered Prior to 1974 Need Rebound Spring Added to Slow Close

Pin.

The inspectors reviewed the Onsite Nuclear Safety OEF Evaluation

Sheet dated February 9, 1989.

The evaluation stated "HBR 2 does not use

Brown Boveri breakers in any safety or non-safety system by design and by

review of HBR 2's CMMS records and

EDBS listings."

The inspectors

observed that non-safety related 480 V switchgear bus no. 5 has Brown

Boveri breakers.

The ONS reviewer, indicated that this meant no Brown

Boveri K-line breakers.

The inspectors had also observed that the

breakers used for transfer of normal power to the dedicated shutdown

diesel power bus for MCC-5 and D SW pump are K-600 breakers. The reviewer

informed the inspectors that these breakers were no longer considered

breakers but manually operated transfer switches since the trip function

had been defeated.

Thus,

by walkdown of all safety-related switchgear,

and discussions with cognizant personnel, the inspectors confirmed that no

K-line breakers were installed in safety-related applications.

During the licensee's review of Brown Boveri supplied breakers, the K-line

transfer switches had not been identified by the record review.

This

occurred because the transfer switches were listed under the original

manufacturer's name, ITE Gould.

No search had been performed using that

name.

The reviewer indicated that, routinely, no precautions have been

taken to ensure all previous manufacturer's names were used when a

specific vender's component was being researched.

Since ONS performs

initial applicability screening for NRC Information. Notices, as well as

Part 21 reports , this is considered a programatic weakness.

This was

brought to the attention of the ONS manager.

Subsequently, the ONS

manager has indicated that this item has been discussed with all the ONS

reviewers.

The weakness is being reviewed by ONS for additional required

action.

(Closed)

LER 89-05, Reactor Trip Due To Inadvertent Closure Of Main Steam

Isolation Valve.

The inspectors reviewed the scram report.

All safety

systems performed as expected. Corrective actions identified in the LER

were the same as that provided in response to VIO 89-08-01, which is

discussed in paragraph 6 of this report.

6

(Open) LER 90-005, Failure To Test RPS Logic Channels In Accordance With

TS.

The subject report identified that the power range high flux -

low

setpoint reactor trip and two-out-of-three loop low flow reactor trip

logic channels were not completely tested monthly during power operations

as required by TS Table 4.1-1 item 27.

Test procedures were revised and

these features were successfully tested on March 14 and 15,

1990.

These

items were identified by the licensee during procedure reviews.

The

licensee also identified that the source range high flux - low setpoint

reactor trip and the intermediate range high flux reactor trips were not

tested monthly.

Neither the source range trip nor the intermediate range

trip is assumed to mitigate any UFSAR Chapter 15 accident. The licensee

developed a position that these were not required by TS, but determined it

was prudent to implement procedures to test the source range trip prior to

startup if not tested in the previous 7 days, and to test the intermediate

range high flux trip monthly. Subsequent to the report period the licensee

successfully performed testing on the trip functions prior to a restart on

May 14, 1990.

During a May 16, 1990 conference call with NRC Management,

the licensee was informed that, as written, TS item 27 required monthly

logic testing of the source and immediate range reactor trips.

Though

disagreeing that this testing is required by TS, the licensee committed to

submit a waiver of compliance or exigent TS change request concerning the

monthly source range high flux test prior to the end of the next monthly

surveillance test interval.

The TS surveillance problem addressed above is repetitive, in that, on

June 23,

1988,

an NOV was issued regarding an inadequate procedure. for

testing TROTS as required by TS Table 4.1-1 item 28 (see IR 88-10 and

LER 88-11).

Accordingly, this is identified as a VIO: Failure To Take

Adequate Corrective Action

To Preclude Repetition Of Inadequate

Procedures Involving TS Required Tests, 90-11-01.

A review for previous occurrences revealed the following:

0

On March 7, 1986, the licensee identified that test procedures did

not perform channel functional testing of the AFW automatic initiation

during a station blackout as required by TS Table 4.8-1 (see

LER 86-008).

On November 18, 1985, the licensee identified that the steam/feedwater

flow mismatch with a low steam generator level reactor trip was not

being tested as required by TS Table 4-1-1, Item 39.

An NOV was issued June 19, 1984, concerning an inadequate procedure

to test SI initiation due to high steam line flow coincident with low

steam line pressure or low RCS average temperature as required by TS

Table 4.1-1 Item 27 (see IR 84-19).

Corrective actions to the 1984 violation discussed above determined

that procedures were not adequate for steam line isolation testing,

and SI initiation on CV pressure (see LER 84-05).

in response to NRC generic letter 83-20, the licensee discovered

that the manual reactor trip function was not routinely tested.

7

In 1982,

the licensee had conducted an independent review of TS

surveillances as a result of the surveillance problems identified at

CP&L's BSEP facility.

As indicated above, there has been a weakness in

being able to properly- implement surveillance testing of TS required

instrumentation.

One violation was identified.

6. Action on Previous Inspection Findings (92701, 92702)

(Closed) VIO 88-07-01, Failure To Declare An Unusual Event After Exceeding

An RCS Leak Rate Of 10 GPM. The inspectors reviewed the August 12, 1988

supplemental repsonse to the NOV.

The following corrective actions

contained in the supplemental response were verified to have been completed

as committed:

Directed transitions from AOPs to PEPs were incorporated in AOPs.

Procedures reviewed included:

APP (revision 6) Radiation Monitoring System

AOP-006 (revision 2) Turbine Vibration

AOP-009 (revision 0) Accidental Release of Waste Gas

AOP-016 (revision 5) Excessive Primary Plant Leakage

AOP-019 (revision 1) Malfunction of RCS Pressure Control

AOP-020 (revision 6) Loss of Residual Heat Removal

AOP-021 (revision 3) Seismic Disturbances

AOP-023 (revision 3) Loss of Containment Integrity

Operator Aid No.

89-01, Off Normal Event Notification, was issued as a

single reference for determining required reports. This was subsequently

cancelled March 9, 1990.

NRC reporting requirements are now contained in

AP-030, NRC Reporting Requirements.

Flowpath procedures EAL-1 and EAL-2 were issued to assist in emergency

classification determinations.

Per Collins to Eury letter dated

December 1, 1989, the NRC has reviewed revision 22 to the emergency plan

which contains these flowpaths.

Emergency Action Level Procedure User's Guide,

OMM-031,

was issued to

prescribe rules of usage for the EAL flowpaths and PEPs.

Training procedure, TI-909, Simulator Conduct Of Operations And Instructor

Qualifications, was rev-ised to ensure that the instructors verify that

PEP's are reviewed by operators to determine if they are applicable during

any off-normal event.

The above actions provided additional measures and aids to assist personnel

in the proper classification of an abnormal event. These actions should

prevent future occurrences of the violation.

(Closed)

VIO 88-28-02, Failure To Have A Program To Use Calibrated Stop

Watches For Required TS And ASME Section XI Testing.

The inspectors

reviewed the December 9, 1988 response to the NOV.

Procedure OMM-017,

Calibration Control/Repair Program For Portable Test Equipment,

was

revised to require that calibration of stop watches shall not exceed

twelve months.

The inspectors reviewed a sample of OSTs to verify that

calibrated stopwatches are

required to be used when timing

equipment associated with TS surveillances and ASME Section XI tests. The

inspectors have routinely observed the use of calibrated stopwatches

during OST performances.

(Closed) VIO 89-07-01, Initialing Procedure Step.Prior To Performing Work.

An improperly numbered sign-off step on the data sheet associated with

CM-111, Limitorque Limit Switch and Torque Switch Maintenance, contributed

to the event.

The inspectors verified that CM-111 has been revised to

correct the deficiency. The inspector discussed the lack of attention to

detail with the Maintenance Manager.

The Maintenance Manager indicated

that maintenance personnel have been cautioned on attention to detail

while-using procedures.

(Closed)

VIO 89-08-01,

Failure To Follow.OST-202 Results In A Reactor

Scram.

The inspectors reviewed the June 16,

1988 response to the NOV.

The inspectors verified that EST-013,

Auxiliary Feedwater Bearing

Temperature Test, revision 8, and OST-202, Steam Driven System Component

Test, revision 21,

contain instructions on how to properly perform these

tests simultaneously.

  • As committed in the response, the A MSIV was

inspected for damage. The evaluation of the inspection, attached to WR/JO

89-AEEF1,

dated October 9, 1989,

concluded that there was no physical

damage to the valve internals which would preclude the valve from seating.

The human factors review of the control board is being conducted as part

of the control room upgrade project.

The NRC is reviewing this latter

item as a separate issue.

9

(Closed)

VIO 89-09-01,

Procedure Inadequately Addresses Potential Pump

Runout With Only One SI Pump Injecting Into Two Hot Legs.

The subject

procedure was revised to incorporate the appropriate precaution.

The

inspectors verified that OMM-013,

Emergency Operating Procedure Writer's

Guide,

revision 2, was issued to require that a system engineer

participate in the verification of EOP changes.

This corrective action,

along with the EOP reviews being conducted as corrective action for

deficiencies identified in IR 89-16, should ensure required precautions and

limitations are contained in the EOPs.

(Closed) IFI 88-28-04,

Review Visual And Eddy Current Testing Of HVH 1-4

During November

1988 Refueling Outage.

The inspectors reviewed the

results of the HVH-4 eddy current examination presented in the Echoram

Technology,

Inc. final report dated November 1988.

Of the 108 tubes

inspected,

none were found with defects greater than 20 percent

through-wall.

(Closed)

IFI 88-03-02,

Review Finalized Transition Document And Step

Deviation Report.

The subject documents were reviewed by the NRC during

the EOP team inspection conducted September 18 -

September 29,

1989.

Results are documented in IR 89-16 and the associated licensee's response

of December 8, 1989.

No violations or deviations were identified.

7. Design, Design Changes, and Modifications (37700)

On April 11 and 12,

1990, an inspection was performed in the corporate

engineering office of the status and resolution of discrepancies

identified through the preparation and validation of the Electrical Power

Distribution System DBD (DBD/R 87038/SD16) revision 0, issued May 23, 1989.

The inspectors determined that discrepancies were being processed in

accordance with approved procedures and with the proper emphasis on safety. A

significant weakness in the electric system documentation is the

non-availability of supporting calculations. . A table, denoted as

CACL-MATRIX,

has been developed which shows what calculations are

available and unavailable for different plant operating conditions and

electrical system configurations.

At the time of the inspection, the

licensee was in the process of determining which unavailable calculations

would be generated.

Most major calculations such as offsite AC power

system response and

EDG transient loading during a LOCA have been

completed or should be completed this fall to support modifications

scheduled for the 1990 refueling outage.

During the preparation and validation phases of the DBD process, a number

of open items (less safety significant than a discrepancy) have been and

are continuing to be found.

The items may include errors or enhancement

recommendations associated with drawings or procedures. .Though open items

10

are captured and assigned a number, the task of determining how and if the

items are to be resolved was not assigned to any individual.

For those

open items deemed beneficial or necessary to be implemented, there was no

tracking system to ensure that they are properly resolved.

The lack of a

review and tracking systems for open items is considered a weakness. This

was discussed with engineering supervision. The Technical Support Manager

expects to have someone assigned the responsibility of overseeing the

resolution of the DBD open items by June 30, 1990.

8. Exit Interview (30703)

The inspection scope and findings were summarized on May 16,

1990 with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. During the exit, and discussed in paragraph 4,

the licensee committed to reinspect the SDAFW pump's impeller during the

Fall 1990 refueling outage.

Dissenting comments were not received from

the licensee. Proprietary information is not contained in this report.

Item Number

Description/Reference Paragraph

90-11-01

VIO - Failure To Take Adequate Corrective Action

To Preclude Repetition of Inadequate Procedures

Involving TS Required Tests (paragraph 5).

10. List of Acronyms and Initialisms

AC

Alternating Current

AP

Administrative Procedure

AOP

Abnormal Operating Procedure

ASME

American Society of Mechanical Engineers

BSEP

Brunswick Steam Electric Plant

CM

Corrective Maintenance

CMMS

Corporate Material Management System

CNS

Corporate Nuclear Safety

CP&L

Carolina Power & Light

DBD

Design Basis Document

E&RC

Environmental and Radiation Control

EAL

Emergency Action Level

EDBS

Equipment Data Base System

EDG

Emergency Diesel Generator

EOP

Emergency Operation Procedures

EST

Engineering Surveillance Test

GPM

Gallons Per Minute

HBR

H. B. Robinson

HVH

Heating Ventilation Handling

I&C

Instrumentation & Control

IFI

Inspector Followup Item

IR.

Inspection Report

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

MS

Main Stream

MSIV

Main Steam Isolation Valve

MST

Maintenance Surveillance Test

NOV

Notice of Violation

NRC

Nuclear Regulatory Commission

OEF

Operating Experience Feedback

OMM

Operations Management Manual

ONS

Onsite Nuclear Safety

OST

Operations Surveillance Test

PEP

Plant Emergency Procedure

PM

Preventative Maintenance

RCS

Reactor Coolant System

RPS

Reactor Protection System

SDAFW

System Driven Auxiliary Feedwater

SI

Safety Injection

SW

Service Water

TI

Training Instruction

TROTS

Turbine Redundant Overspeed Trip System

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

V

Volt

VIO

Violation

WR/JO

Work Request/Job Order