ML14176A603

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IE Insp Rept 50-261/81-08 on 810221-0310.Noncompliance Noted:Breaker Overload Trip Settings Improperly Set Due to Inadequate Procedures & Performance Testing & Safety Relief Valve Position Monitor Improperly Installed
ML14176A603
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 03/26/1981
From: Julian C, Skolds J, Weise S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14176A597 List:
References
50-261-81-08, 50-261-81-8, NUDOCS 8105080437
Download: ML14176A603 (8)


See also: IR 05000261/1981008

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REQION II

101 MARIETTA ST., N.W., SUITE 3100

ATLANTA, GEORGIA 30303

Report No.

50-261/81-08

Licensee: Carolina Power and Light Company

411 Fayetteville Street

Raleigh, NC

27602

Facility Name:

H. B. Robinson Steam Electric Plant

Docket No. 50-261

License No. DPR-23

Inspection at Robinson site near Hartsville, South Carolina

Inspectors:

C

/

.

S. Weise(Resident Ins ector, Robinson

Date Signed

J. Skold!.. Resident In

ector, V. C. Summer

Date Signed

Approved by:__

6

/

C. Julia6J Acting Section Chief, Division of

5ate Signed

Resident and Reactor Project Inspection

SUMMARY

Inspection on February 21 - March 10, 1981

Areas Inspected

This routine announced inspection involved 128 resident inspector-hours on site

in the areas of technical specification compliance,

reportable occurrences,

housekeeping, operations performance, quality assurance practices, maintenance

activities, site security procedures,

radiation control activities, licensee

action on previous inspection findings, event followup,

IE Bulletin followup,

review of

IE Circulars

and

Notices,

surveillance activities, review of

outstanding items, and TMI Action Plan Category A requirements.

Results

Of the fifteen areas inspected,

no items of noncompliance or deviations were

identified in thirteen areas; one violation was found in one area (failure to

control modification activities, paragraph 5.)

and one deviation was found in one

area (Failure to keep relief valve position monitor installed as committed,

paragraph 13.d).

81050.80q(3

DETAILS

1.

Persons Contacted

Licensee Employees

  • R. B. Starkey, Plant Manager
  • H. S. Zimmerman, Manager Technical and Administration
  • M. Page, Project Engineer

W. Flanagan, Project Engineer

J. Curley, Engineering Supervisor

F. Lowery, Operations Supervisor Unit 2

Other licensee employees contacted included technicians, operators,

mechanics, security force members,

and office personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on March 16,

1981 with

those persons indicated in Paragraph 1 above.

Licensee representatives.

acknowledged their understanding of the findings.

W

3.

Licensee Action on Previous Inspection Findings

(Closed) Unresolved item 79-24-01-Monitoring teams duties/responsibilities.

This item dealt with the qualifications of the personnel

performing

monitoring duties during an emergency drill.

The plan for the emergency

drill scheduled for March 11-12,

1981 states that evaluators will be

qualified personnel and not trainees as was allowed in previous drills.

This item is closed.

(Closed) Unresolved item 80-19-03-Technical Specification discrepancy. This

item documented that Technical Specifications covering Diesel Generator

Testing were not the same as standard technical specifications.

The com

parison was done at IE Headquarters request. Any changes will be originated

from IE Headquarters, therefore this item is closed.

(Closed) Unresolved item 80-19-02-Failure of PCV-1716 to close. This item

concerned the failure of PCV-1716 during the performance of PT-2.1.

Licensee Event Report 80-18 reported this occurrence. Adequate corrective

action was taken to close out LER 80-18. The licensee could not determine

when the override switch was placed on override, and therefore must assume

it was placed in override during plant operations. However, the plant was

in cold shutdown

when the condition was discovered and

no further

operational action was required.

This item is closed.

2

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve noncompliance or

deviations.

New unresolved items identified during this inspection are

discussed in paragraph 8.b.

5.

Event Followup

On January 29,

1981,

H. B. Robinson Unit 2 experienced a transient which

resulted in a containment isolation signal.

When verifying that all

required containment isolation valves had shut, the operators discovered

that Fire Suppression water containment isolation valve (FP-248) had failed

to close. Containment isolation was maintained by the redundant isolation

valve FP-249,

and FP-248 was closed manually.

Investigation into this

failure determined that the valve motor breaker had tripped on the isolation

signal due to improper setting of the magnetic overload trip. This improper

trip setting was common to all four of the Fire Suppression water system

containment isolation valve motor breakers, although only one valve failed

to operate. Further investigation revealed that, of three separate breaker

replacements done on each valve motor circuit to satisfy modification #445,

the final replacement was done using the previous breaker installation

procedure and no post-modification testing was conducted. Since the second

set of breakers used a thermal overload trip and the present breakers use

magnetic overloads, use of the previous procedure was improper. Failure to

perform post-modification testing on the final breaker installation is not

in accordance with plant procedures. This failure to control modification

activities constitutes a violation (50-261/81-08-01).

This event was

reported by Licensee Event Report (LER)

81-06 and bears marked similarity to

the improper overcurrent trip setting on the MCC-5 transfer switch reported

in LER 80-04. Since the corrective action to prevent further recurrence in

LER's 80-04 and 81-06 are essentially the same,

the inspector feels that

additional action by the licensee is needed to adequately prevent future

recurrence.

6.

Plant Operations Review

The inspector periodically during the inspection interval reviewed shift

logs and operations records, including data sheets, instrument traces, and

records of equipment malfunctions. This review included control room logs,

auxiliary logs, operating orders, standby orders, jumper logs and equipment

tagout records. The inspector routinely observed operator alertness and

demeanor during plant tours. During abnormal events, operator performance

and response actions were observed and evaluated. The inspector conducted

random off-hours inspections during the reporting interval to assure that

operations and security remained at an acceptable level.

Shift turnovers

were observed to verify that they were conducted in accordance with approved

licensee procedures. The inspector had no further comments.

3

7.

Plant Tour

The inspector conducted plant tours periodically during the inspection

interval to verify that monitoring equipment was recording as required,

.equipment was properly tagged, operations personnel were aware of plant

conditions, and plant housekeeping efforts were adequate.

The inspector

determined that appropriate radiation controls were properly established,

excess equipment or material was stored properly, and combustible material

was disposed of expeditiously. During tours the inspector looked for the

existence of unusual fluid leaks, piping vibrations, pipe hanger and seismic

restraint abnormal settings, various valve and breaker positions, equipment

clearance tags and component status, adequacy of firefighting equipment, and

instrument calibration dates.

Some tours were conducted on backshifts.

The

inspector noted no violations or deviations.

8.

Technical Specification Compliance

During this reporting interval,

the inspector verified compliance with

selected limiting conditions for operation (LCO's) and reviewed results of

selected surveillance tests.

These verifications were accomplished by

direct observation of monitoring instrumentation, valve positions, switch

positions,

and review of completed logs and records.

The licensee's

compliance with selected LCO action statements were reviewed

as they

happened.

Findings were acceptable except as noted below:

a. A discrepancy was noted in a comparison of Technical Specifications and

plant procedures. Technical Specification 3.3.2.1.a requires that at.

least 2505 gallons (about

35% tank level) of 30% sodium hydroxide

solution be maintained in the spray additive tanks.

Plant procedure

PLS-7 states that the spray additive tank low level alarm is 33% + 1%.

After researching this item, the licensee commmitted to revise the low

alarm setpoint by April 30,

1981.

This is an open item (50-261/

81-08-02).

b. While monitoring the daily surveillance to measure safety-related heat

tracing currents, the inspector identified the following conditions:

(1) All primary and secondary safety-related heat tracing thermostatic

control junction boxes did not have their covers fastened in

place. Some contained considerable debris and boric acid. These

covers were apparently designed to protect the heat tracing

circuitry from adverse environmental conditions, as the cover data

plate emphasizes that the cover screws be kept tightly fastened.

The inspector questioned the practice of leaving these covers

open. The inspector also noted the cover fasteners were time

consuming to operate and would result in increased radiation

exposure to technicians performing the surveillance because of

their locations. The licensee committed to evaluate the need for

cover plates and commented that some design changes were being

considered from an ALARA standpoint.

This is an Unresolved item

(50-261/81.-08-03.)

4

(2) The protective armor cable for safety-related heat tracing wiring

to the thermostatic control junction boxes was broken on at least

six boxes.

(3) In the Boron Injection Tank room, the motor wiring conduit for

safety injection valve SIS-870 B for cold leg injection was not

fastened to its supports and the flexible protective cable to the

motor was broken.

The licensee committed to correct the discrepancies noted in items 2 and 3

above and also the debris and boric acid in and around the thermostatic

control junction boxes

by May 31,

1981..

This item is open (50-261/

81-08-04).

9. Physical Protection

The inspector verified by observation and interview during the reporting

interval that measures taken to assure the physical protection of the

facility met current requirements.

Areas inspected included the organi

zation of the security force, the establishment and maintenance of gates,

doors and isolation zones in the proper condition, that access control and

badging was proper, that search practices were appropriate,

and that

escorting and communications procedures were followed.

10.

Licensee Event Report (LER) Followup

The inspector reviewed the following LER's to verify that the report details

met license requirements,

identified- the cause of the event, described

appropriate corrective actions, adequately assessed the event, and addressed

any generic implications. Corrective action and appropriate licensee review

of the below events was verified. The inspector had no further comments.

LER

EVENT

80-04

MCC-5 Transfer Switch Trip

80-05

CCW-626 Staking Problem

80-09

B Steam Generator Tube Leakage

80-11

Source Range Channels De-energized

80-18

Failure of PCV-1716 to Close

80-22

A and B Steam Generator Tube Leaks

80-23

Improper Charcoal Refill for Control Room Ventilation

80-26

Spray Additive Tank Isolated

78-03

Primary Pressure Exceeding Technical Specification

Limit

78-16

BIT Boron Concentration out of Specification

11.

Followup of IE Bulletins

For the following Bulletins, the inspector verified that the response was

timely, included the required information, contained adequate commitments

5

and that corrective action as described in the written responses was

completed.

a.

IEB 81-01 Surveillance of Mechanical Snubbers

The inspector reviewed the licensee's response to this Bulletin dated

February .18,

1981.

No mechanical

snubbers

are in use at H. B.

Robinson.

This item is closed.

b.

IEB 80-23 Valcor Solenoid Failures

The inspector reviewed the licensee's response to this Bulletin dated

December 8, 1980.

No such parts or solenoids are in use at H. B.

Robinson.

This item is closed.

12.

Review of IE Circulars and Notices (IEC's and IEN's)

The inspector verified that IE Circulars and Notices had been received

onsite and reviewed by cognizant licensee personnel.

Selected applicable IE

Circulars and Notices were discussed with licensee personnel to ascertain

the licensee's actions on these items. The inspector also verified that IE

Circulars and Notices were reviewed by the Plant Nuclear Safety Committee in

accordance with facility administrative policy.

Licensee action on the

following IE Circulars and Notices were reviewed by the inspector and are

closed.

IE Circulars

IE Notices

80-03.

79-17

79-34

79-31

79-35

79-32

80-06

79-33

13.

TMI Action Plan Category A Items

a.

TAP No.

I.C.3,

NUREG 0578, Section 2.2.1.a Shift Supervisor Respons

ibilities. The inspector reviewed plant Administrative Instructions

and corporate directives to verify that the four elements of this task

have been implemented.

No violations or deviations were observed in

this area.

b. TAP No. 11.6.1., NUREG 0578, Section 2.1.1. Natural Circulation Power

Supplies. The inspector verified that the components were powered and

qualified as required by this item.

c. TAP No. II.E.4.2, NUREG 0578, Section 2.1.4. Containment Isolation

Dependability.

The inspector reviewed the manually operated

non

essential containment isolation valves and found that the licensee has

administratively locked all such valves shut. Modifications have been

completed which ensure that isolation valves associated with the below

systems remain closed on resetting the containment isolation signal:

6

1) Steam generator blowdown and sample lines

2)

Instrument air

3)

Containment atmosphere monitor lines

No violations or deviations were observed in this area.

d.

TAP No. II.D.3, NUREG 0578,

Section 2.1.3 Valve Position Indication,

Relief and SafetyValves

The control

room instruments for the safety relief valve vibration

monitors for position indication were inspected.

These monitors are

installed on the valve flanges. The-inspection revealed the following

concerns:

1) One safety relief valve (V-551A) does not have a vibration monitor

accelerometer. The accelerometer was lost during the fall of 1980

refueling outage and a replacement has not been received.

2) All three vibration monitor channels (one for each valve) have

continuous low level alarms. The low level alarm is designed to

help verify system operability, as a circuit failure should

normally result in a low level alarm due to a lower than normal

ambient noise level. The continuous alarm condition is a design

problem,

in that, the background noise at the monitors is lower

than

the

system

bandpass filters were

designed for.

An

engineering change is being developed by the system vendor.

No

compensatory measures are being taken to verify system operability

while the low level alarms are not functional.'

3) There is no audible annunicator associated with the low level

alarms, and no procedure exists for response to the low level

alarm condition.

4) The proposed Technical Specifications for surveillance of the

vibration monitors requires system testing every refueling outage.

The inspector is concerned that this infrequent testing may be

inadequate.

This is open item (50-261/81-08-05.)

5) Safety grade seismic and environmental qualification of this

system has not been completed by the vendor. Qualification of the

system is expected by the third quarter of 1981.

This was

documented in CP&L's letter to the Office of Nuclear Reactor

Regulation of December 10, 1980.

The system deficiencies noted in items. 1 and 2 above are an item of

deviation (50-261/81-08-06).

The inspector also requested that the

licensee commit to informing the office of Nuclear Reactor Regulation

by letter of the existence of the deficiencies noted in items 1 and 2

above, their proposed corrective action, and an anticipated schedule.

The licensee postponed this commitment pending Commission clarification

of reporting requirements for occurring deficiencies in TMI Action Plan

7

required equipment for which Technical Specifications have not -been

issued.

14.

Review of Outstanding Items

a.

(Open)

79-03-02

Wrong-valve

numbers

on Containment

Spray Q-list

drawing. This item documented that four valves had incorrect numbers

on the Q-list drawing.

The controlled drawings have been corrected,

however, in the two years since this minor item was brought to the

licensee's attention, no further generic corrective action has been

taken.

b.

(Closed) 79-07-02-Qualifications for personnel performing verification

mapping following fuel loading. This item dealt with an inspector's

concerns about who would be allowed to perform core verification and

about the desirability of making a videotape.

FT-

9.11 has been

revised to indicate that personnel from Engineering and QA will perform

and review the verification.

The procedure also indicates that a

videotape is highly desirable,

though not required.

This item is

closed.

c.

(Closed)

80-19-01-Revision to PT 2.1.

Previously,

PT 2.1 did not

specifically document that the SI pumps started during the test.

PT

2.1 has been revised to document SI pump starting times. This item is

closed.

d.

(Closed) 79-27-03-X-Y Potter. Previously, the X-Y plotter connection

to the Tavg signal from the process computer loaded down the circuit

causing an.error in the plotted Tavg value. Appendix E to CPL-R-6.0,

Refueling Startup Procedures, has been changed to eliminate this error.

This item is closed.

e.

(Open) 79-30-02-Current Procedure at Waste Evaporator Panel.

This item

dealt with the fact that there is no method in use to ensure that the

correct revision to procedures are used at local stations outside the

control room - specifically, the Waste Evaporator Panel.

Conversations

with plant personnel indicate that different methods have been tried,

but, none has

been totally successful.

The licensee intends to

establish a controlled set of procedures for the Waste Evaporator

Panel.

The licensee committed to implement this plan by April 30,

1981. This item will remain open pending future inspection after the

implementation date.

f.

(Closed) 81-03-01-Anticipated Transient Without Scram. The inspector

reviewed the licensee's changes to Abnormal Procedure-2 and Emergency

Instruction-14. The licensee's procedural actions resolve the original

concerns.

This item is closed.