ML13323A925

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IE Insp Rept 50-206/80-34 on 801201-24.Noncompliance Noted: Failure to Implement Physical Security Plan Requirement & Insufficent Review of safety-related Procedure
ML13323A925
Person / Time
Site: San Onofre 
Issue date: 01/22/1981
From: Faulkenberry B, Miller L, Pate R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13323A921 List:
References
50-206-80-34, NUDOCS 8103180361
Download: ML13323A925 (9)


See also: IR 05000206/1980034

Text

Report No. 50-206/80-34

Dbcket No. 50-206

nse u0.DPR-13

Safeguards Group

Licensee: Southern California Edison Company

P. 0. Box 800

2244 Walnut Grove Avenue

Rosemead, California 91770

Facility Name:San onnfr linit 1

Inspection a,:San Onofre, California

Inspection conacred: December 1-24,

1980

Inspectors:

f

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L. Miller, Resident Inspector

D

Sighec

R. Pate, Senior Residet

n eto

Dae Signeu

B. H.

ate Signed

SU =9ry:

Inspection on December 1-24, 1980 (Report No. 50-206/80-34)

Areas Inspected:

Routine, resident inspection of plant operations during

-long term outage; monthly maintenance observations; review of plant operations;

followup on licensee event reports; independent inspection (followup on inspector

identified items); TI 2415/46; and followup on Systematic Appraisal of Licensee

Performance (SALP). The inspection involved 70 inspector hours by two NRC

inspectors.

Results:

Two items of noncompliance were identified (Failure to implement

a physical security plan requirement - Severity Level IV; Insufficient review

of a safety-related procedure - Severity Level V).

RV Form

219 (2)

DETAILS

1. Persons Contacted

  • H. E. Morgan, Superintendent, Units 2 and 3
  • R. Brunet, Superintendent, Unit 1
  • 8. Katz, Station Supervising Engineer
  • W. Frick, Compliance Engineer
  • J. Tate, Supervisor of Plant Operations
  • R. V. Warnock, Supervisor of Chemistry and Radiation Protection
  • E. A. Rinard, Unit 1 Warehouse Supervisor
  • J. D. Dunn, Project Quality Assurance Supervisor
  • K. N. Hadley, Station Security Supervisor
  • R. W. Rutland, Quality Assurance Engineer

The inspector also interviewed other licensee employees on the maintenance,

security, and operations staffs during this inspection.

  • Denotes those attending the Exit Interview on December 29, 1980.

2. Monthly Surveillance Observations

The inspector observed licensee personnel load test the #1 125 vdc battery,

perform area radiation monitoring system checks, and perform radiation

surveys. Surveillance activity was relatively-low. The activities observed

were performed in

accordance with the appropriate procedures. Limiting

conditions for operation were met where applicable.

Logs and records

were kept, and were reviewed independently where required. The licensee's

records indicate that all surveillances required to be completed during

this period were completed.

No items of noncompliance or deviations were identified.

3.

Monthly Maintenance Observations

a. Routine Activities

The inspector observed portions of the following maintenance:

  1. 1 Diesel Generator Turbocharger Inspection and Repair

The inspector determined that this activity did not violate limiting

conditions for operation, that required administrative approvals

and tagouts were obtained prior to initiating the work, that approved

procedures were being used by qualified personnel, and that fire

prevention controls were adequate.

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Licensee personnel stated that the four turbocharger thrust bearings

on the #1 Diesel Generator had failed. The apparent cause for

this failure was believed to be insufficient lubrication while

the diesel was being started. A similar degradation of these bearings

on the #2 Diesel Generator is suspected. A licensee representative

stated his understanding that complete turbocharger failure would

not disable these diesels, that all turbochargers would be inspected

and repaired, that a Licensee Event Report would be submitted,

and that any further reductions in power redundancy would be discussed

in advance with the Resident Inspector (01 80-34-01).

b. Steam Generator Repair Program

In this inspection period, the licensee continued surface hcning

and boroscopic inspection of tubes in each steam generator. The

scope of boroscopic inspection was expanded to include all tubes

to be sleeved. Approximately 75% of these had been boroscopically

verified to be acceptable.

The start of production brazing was delayed due to unexpected difficulty

encountered in brazing below the sludge line. The licensee and

contractor were actively evaluating possible techniques to resolve

this problem while honing and boroscoping continued.

The inspector reviewed the licensee's Nonconformance Report NCR

SO1-P477 dated October 13, 1980. This NCR contained as an enclosure

a Westinghouse internal memorandum which estimated the corrosion

rate of the aluminum nozzle seal cover plate that was dropped into

the reactor coolant system. At the end of this inspection the

seal had been submerged approximately ten weeks. A Westinghouse

representative stated that an evaluation of the effects and amounts

of the aluminum released to the coolant would be presented to the

Resident Inspector (01 80-34-02).

The inspector reviewed the procedures and procedure revisions written

during this inspection period for the steam generator repair program.

One of these revisions was Procedure Change Notice (PCN) #3 to

SPE-307, "Sleeve Insertion, Expansion and Mandrel Removal Hands On."

The change was a "Procedure for Operation of One Revolution Cutter

Tool," a procedure to intentionally perforate a selected tube of

the steam generator to test the leak tightness of the braze for

that tube.

The basic procedure, SPE-307, had as its purpose, "sleeving tubes

of a Series 27 vertical steam generator, hydraulically expanding

the regions of the sleeve, installation and removal of the expansion

mandrel after the expansion process has been satisfactorily completed."

The procedure revision was approved by two members of the On-Site

Review Committee on December 6, 1980 and implemented that day on

at least one tube of the "B" steam generator. A licensee representative

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stated that this change, PCN #3, to the procedure SPE-307 had not

altered the intent of the procedure, and therefore it was permissible

under the exception of Technical Specification 6.8.3 to Technical

Specification 6.8.2. The basic specification requires that each

procedure change shall be reviewed by the On Site Review Committee

prior to implementation, while the exception allows changes which

do not change the intent of the procedure to be made without prior

approval of the full On Site Review Committee. The inspector stated

that the change to the procedure dealt with an entirely.separate

and independent process (tube cutting of the primary pressure boundary)

from the original procedure (which dealt with adding sleeves to

existing tubes), and thus was a new procedure requiring complete

review by the On Site Review Committee prior to implementation.

Technical Specification 6.8.1 states that written procedures

shall be established that meet or exceed the requirements and

recommendations of Appendix "A" of USNRC Regulatory Guide 1.33, Rev. 1,

Quality Assurance Program Requirements (Operation). Among these

recommendations is one for "Repair of PWR Steam Generator Tubes"

(Paragraph 9C(1)).

Technical Specification 6.8.2 requires that each procedure of 6.8.1

above and changes thereto shall be reviewed by the On Site Review

Committee and approved by the Plant Manager prior to implementation.

Contrary to these requirements, Procedure Change Notice No. 3 to

SPE -307, "Procedure for Operation of One Revolution Cutter Tool ,"

a procedure to intentionally perforate selected steam generator

tubes, was implemented on December 6, 1980 without the prior approval

of the On-Site Review Committee. The procedure, which was new,

had been attached to an existing, approved procedure SPE-307, "Sleeve

Insertion, Expansion and Mandrel Removal Hands On," which described

the procedures and methods for installing sleeves into the steam

generators. This is an apparent item of noncompliance.

(01 80-34-03)

4. Review of Plant Operations

The inspector inspected the licensee's warehouse, interviewed warehouse

personnel, and reviewed procurement records to verify that items were

procured in accordance with the licensee's procurement procedures. The

inspector observed that the licensee had a quarantine area and tagging

system for non-conforming items, that the warehouse was clean, temperature

controlled, rodent control measures were in effect, and combustibles

were segregated from other stored material. The inspector also observed

that no system existed to systematically control limited shelf-life

items at Unit 1. A licensee representative stated that a system similar

to that in effect for Units 2 and 3 would be implemented at Unit 1 to

ensure that limited shelf life items were in fact suitable for safety

related service when issued from storage.

(01 80-34-04)

The inspector reviewed three requisitions: No. 6784G for auxiliary feedwater

pump shaft work and parts, 1719F for auxiliary feedwater pump turbine

parts, and 1685F for charging pump seal injection line material.

The

purchase order, receipt records and certification records (where appropriate)

were verified to be present and appeared complete. The inspector observed

that the licensee does not require issue records for material procured

for a specific job, nor is the location of every item in storage recorded.

No items of noncompliance or deviations were identified.

5. Followup on Licensee Event Reports (LERS).

a. LER 80-28 (Nonconforming Pine Guides).

The inspector stated that this report would be reviewed together

with the licensee's final report on IE Bulletin 79-14, which is

to be submitted prior to the Unit's return to power. This report

remains open.

b. LERs 80-29, 34 and 36 (Inadvertent Dilutions of the Reactor Coolant

System).

The inspector reviewed these three similar events at the times

of their occurence. The inspector stated that the licensee's corrective

action of reinforcing and more carefully inspecting the inflatable

nozzle seals, together with the completion of the high pressure

grit spray decontamination process appeared adequate to prevent

recurrence.

In addition, the inspector stated his agreement with

the licensee's appraisal that the safety impact of the dilutions

had been negligible. These reports are closed.

(TERA Docket Nos.

50-206-800901, 50-206-800902 for LERs 80-34 and 80-36 respectively).

c.

LER 80-31 (50-206-800728) (Uncontrolled Modification of POV-6 Solenoid

Valve).

The inspector reviewed this report and discussed the corrective

action with licensee personnel.

The inspector requested further

clarification of what "recounseling" of station personnel consisted

of in this corrective action.

This report remains open.

d. LER 80-32 (Dessicant in Instrument Air System).

The licensee reported the failure of isolation valve CV-537, service

water to containment, to operate.

The valve was stuck in a mid

open position.

An investigation revealed that degraded desiccant

from the air dryers had entered the solenoid valve and prevented

it from operating.

An identical failure of this valve was reported

In LER/80-03.

Corrective actions resulting from the prior failure

may have contributed to this failure of valve CV-537. The instrument

air header was being blown down when the valve became stuck.

The blowdown of the instrument air header may have caused degraded

desiccant in the header to migrate to the valve solenoid. The

corrective action taken by the licensee as a result of the first

failure of valve CV-537 was discussed in inspection report 50-206/80-16.

Further investigation by the licensee found that the air supply

header pressure was higher than the maximum design operating pressure

of the solenoid for valve CV-537. This was corrected by installing

a pressure regulator. SCE reviewed the design of other similar valves

and did not find any additional valves that were being operated at

pressures higher than the design pressure.

SCE committed to remove the dearaded desiccant from the instrument

air header by completing the system blowdown and by subsequently

blowing down the supply line to each valve or safety related component.

Also SCE committed to take the following additional corrective actions.

1) Verify that each air operated safety related valve or component

functions properly. This will be done by inspecting each

pneumatic instrument or pilot valve for desiccant and by stroking

the valves and calibrating the instruments.

Instruments or

valves that display slow or erratic response will be repaired

or replaced. This inspection, calibration, stroking, repair,

or replacement will be accomplished in accordance with procedures

approved by the On-Site Review Committee.

2) Review the programmed drying cycle for the desiccant dryers

to ensure the manufacturer's recommendations are being met

and make corrections as necessary.

3)

Iodify the filters down stream of the desiccant dryers to

provide a more positive seal to preclude any possible bypass

of degraded desiccant. This modification will be reviewed

by the On-Site Review Committee and the Off-Site Nuclear Audit

PReview Committee (NARC).

4)

Determine the potential for free particles of iron or iron

oxide in the instrument air system and their possible deleterious

effect on safety related valves or instruments. Take corrective

action as necessary.

5) The On-Site Review Committee will review the status of the

instrument air system to assure the system will support safe

operation of the plant prior to returning to power.

6) A summary report of all actions and results will be prepared.

This report will be reviewed by the On-Site Review Committee

and will be available for review by the NRC.

This report remains open.

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e. LER 80-35 (50-206-800918) (Containment Isolation Valve Switch Defect).

Licensee personnel stated that switches of a different design would

be installed. The inspector stated that this corrective action

was acceotable provided that the switches were installed prior

to the Unit's return to power, but that it would probably not be

acceptable to rely only on system flow, pressure and temperature

process instrumentation to indicate valve position of containment

isolation valves of essential systems at power without a 10 CFR

50.59 analysis. This report remains open.

No items of noncompliance or deviations were identified.

6. Review of Plant Operations Durina Lonq Term Outace

The inspector observed that the control room was properly manned, procedures

and limiting conditions for operation were followed, and recorder and

instrument indications were appropriate for the plant status. The inspector

reviewed logs and operating records frequently and verified that radiation

controlled area access points were properly manned, equipped and operated.

Frequent discussions were held with licensee personnel at all levels

of responsibility to determine their awareness of existing plant conditions

and the significance of those conditions. The inspector frequently toured

the facility. The Unit's fire protection plan appeared to be properly

implemented, and the cleanliness of the facility appeared good. The

inspector reviewed the Temporary Modifications Log (lifted leads and

jumpers) and the active "Clearances".

Diesel generator starting air

"Clearance" tags were verified to be in place. The inspector noted

that all surveillance tests required and able to be completed in the

plant condition had been recorded as completed. The inspector walked

down portions of the breathing air, diesel generator starting air, and

feedwater systems to verify that they were correctly lined up for the

existing plant status.

(See Addendum 1 - 2.790 Material).

7. Systematic Appraisal of Licensee Performance (SALP)

The inspector reviewed the licensee's list of sixty-eight work packages

Planned for completion at Unit I as of December 4, 1980. From these

four were selected: pressurizer safety valve position indication, subcooling

monitor, sequencer modification for small break LOCA and LOP, and auxiliary

feedwater system automation. The inspector stated that these modifications

will be reviewed at several stages of their progress to ensure that

the concerns of the regional office letter of July 16, 1980 to Southern

California Edison had been addressed by the licensee.

(01 80-34-06)

III

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8. Review of Emergency Procedures for Coping with ATWS events at Operating

Power Reactors (TI 2515/46).

The inspector reviewed the licensee's procedure, S-3-5.33, "Failure

of the Reactor to Trip Following a Turbine Trip".

The procedure required

the licensed operator to manually scram, emergency borate, drive rods

in, and trip scram breakers locally, whenever automatic scram was required,

but did not function. A licensee representative stated that the title

of this procedure would be changed to "Failure of the Reactor to Trip",

and operators would be briefed on this chiange.

(01 80-34-07)

9. Followup on Inspector Identified Items.

a. 01 79-14-01 (Final Reoort on IE Bulletin 79-17).

The inspector reviewed the contractor's reports and recommendations.

A licensee representative stated that these recommendations for

greater environmental resistance would be considered. This item

is closed.

b.

01 79-14-02 (Switchyard Cutover Design Review).

The inspector noted that this cutover had been completed earlier

in the outage, and that the licensee had provided both the Office

of Inspection and Enforcement and the Office of Nuclear Reactor

Regulation an opportunity to review it. This item is closed.

C. 01 79-17-02 (Revision of Reactor Power Calculation Procedure).

The inspector observed that this procedure had been revised and

that it was more explicit, as requested. This item is closed.

d. 01 80-02-03 (Chronically Leaking Feedwater Snubbers).

The inspector observed that the snubbers in question now exhibit

normal leak tightness. This item is closed.

e. 01 80-02-04 (Plant Status Awareness Program).

The inspector observed that Task Action Plan Requirements for a

Nuclear Data Link had made this item obsolete. This item is closed.

f. 01 80-09-05 (Requirements for 12KV Tie Line Operability).

The inspector informed the licensee that this tie line was part

of the approved fire protection plan, and its operability would

be required whenever the unit was not in cold shutdown, except

for brief time periods no longer than that allowed for other fire

protection system components to be inoperable. The inspector noted

that this position might change in the future to the extent that

Appendix R to 10 CFR 50 mandated additional safe shutdown systems

at Unit 1. This item is closed.

g. 01 80-16-02 (Revision of Shutdown Margin Calculation Procedure).

The inspector verified that this revision had been performed to

make the procedure more explicit, as requested. This item is closed.

h. 01 30-16-05 (Formalization of the Use of Miniature Watch Engineer's

The inspector verified that this action had been completed. This

item is closed.

i. 01 80-32-05 (Raw Data for TAP III.D.1.1 Unavailable)

A licensee representative stated that the component-by-component

leak rate data for all miscellaneous potentially radioactive systems

outside of containment had not been retained. This item is closed.

j.

01 80-31-07 (Large Quantities of Visqueen Present in Containment).

The inspector observed that the amount of Visqueen present had

been substantially reduced, and that it no longer appeared to be

a smoke hazard in a fire. This item is closed.

10.

Exit Interview

An exit interview (Paragraph 1) was held on December 29, 1980 to summarize

the scope and findings of this inspection. In addition the inspector

noted that responsibility for the review of allegations by a station

electrical worker of unsafe electrical work practices at Unit 2 had been

transferred to the State of California Occupational Safety and Health

Administration (CAL-OSHA). No further inspection of these allegations

by the Resident Inspector is planned.

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