ML13323A883

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IE Insp Rept 50-206/80-28 on 800904-26.Noncompliance Noted: Failure to Observe Reactor Coolant Chemistry Limit & to Follow Radwaste Discharge Procedure
ML13323A883
Person / Time
Site: San Onofre 
Issue date: 10/23/1980
From: Faulkenberry B, Miller L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13323A879 List:
References
50-206-80-28, NUDOCS 8012040319
Download: ML13323A883 (6)


See also: IR 05000206/1980028

Text

U. S.

NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMNT

REGION V

Report No.

50-206-80-28

Docket No.

50-206

License No.

DPR-13

Safeguards Group

Licensee:

Southern California Edison Company

P. 0. Box 800 - 2244 Walnut Grove Avenue

Rosemead, California 91770

Facility Name:

San Onofre Unit 1

Inspection at:

San Onofre, California

Inspection conducted:

September 4-26, 1980

Insoectors:

L. Miller, Resident Inspector,

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Date Signed

Summary:

Inspection on September 4-26, 1980 (Report No. 50-206/80-28)

Areas Inspected:

Routine, resident inspection of plant operations during long

term outage, monthly maintenance and surveillance observations, and independent

inspection. The inspection involved 62 inspector-hours by one NRC inspector.

Results: Two items of noncompliance were identified (failure to observe reactor

coolant chemistry limit - deficiency; failure to follow radioactive waste

discharge procedure deficiency).

RV Form 219 (2)

80o 1L2 04 0 '/

DETAILS

1. Persons Contacted

  • H. Ottoson, Manager, Nuclear Engineering and Safety
  • J. M. Curran, Manager, San Onofre Nuclear Generating Station
  • D. Nunn, Manager, Quality Assurance
  • R. Brunet, Superintendent, Unit 1
  • J. R. Tate, Supervisor, Plant Operations
  • R. Warnock, Supervisor, Chemistry and Radiation Protection
  • G. McDonald, Supervisor, Quality Assurance/Quality Control
  • E. S. Medling, Assistant Chemistry and Radiation Protection Engineer
  • E. J. Bennett, Division Chemical Foreman
  • G. E. Davis, Division Chemical Foreman

M. Wharton, Supervising Engineer, Unit 1

The inspector also interviewed other licensee employees on the maintenance,

security and operations staffs during this inspection.

  • Denotes those attending the Exit Interview on September 26, 1980.

2. Monthly Maintenance Observations

a. Routine Activities

The inspector observed portions of the following maintenance:

Spent letdown demineralizer resin transfer to spent resin tank.

Steam driven auxiliary feedwater pump repair.

The inspector determined that these activities did not violate limiting

conditions for operation, that required administrative approvals and

layouts were obtained prior to initiating the work, that approved

procedures were being used by qualified personnel, and that

radiological and fire prevention controls were appropriate for the

activities.

b.

Steam Generator Repair Program

In this inspection period, the licensee completed the test brazing of

three steam generator tube sleeves to their respective tubes. The

first two were not successful. The inspector observed a portion of

this activity and stated that the licensee's controls appeared adequate.

Later in the period, the licensee began to decontaminate the "B"

steam generator hot leg channel head with a water and magnetite grit

mixture under high pressure. Prior to commencement of decontamination,

the inspector reviewed the licensee's work package, entitled "Steam

Generator Decontamination Process for Sleeving Program San Onofre Unit 1

(Revision 1)". This document described .the organization, administrative

controls, drawings, technical description, safety review, health

physics controls, and decontamination procedures. The inspector stated

that, if implemented, these procedures appeared adequate to safely

control the contamination work. The inspector interviewed several

decontamination equipment operators and Westinghouse and Southern

California Edison shift supervisors. Those interviewed were

knowledgeable concerning these procedures. In addition, the

inspector attended a pre-decontamination briefing of all participants

conducted by licensee representatives at which the integrated operation

and safety precautions were adequately explained. The inspector

observed the initiation of steam generator "B" decontamination on

September 17, 1980.

At 9:42 P.M. on September 21, 1980 during the decontamination of the

"B" steam generator hot leg channel head, the licensee determined that

the inflatable rubber seal installed in the "B" hot leg had ruptured

in service and consequently, a dilution of approximately 50 ppm of the

reactor coolant system had occurred. Licensee representatives stated

that the seal had ruptured due to the use of inadequate seal material,

and that its rupture had not been immediately detected because the

seal pressure monitoring gage was inadvertently out of service. They

further stated that the rupture had been suspected after decontamination

operators noted an excessive amount of makeup water being required for

the decontamination system, and decontamination was halted. The inspector

reviewed the records of this event. These records indicated that

from 9:09 P.M. until 9:42 P.M. when decontamination was halted, 61.6

gallons of water were lost from the system, a loss rate that was

nearly four times normal.

The inspector determined that due to an

unforeseen procedural inadequacy, this greatly increased loss rate did

not immediately result in the stopping of decontamination.

The procedure, IRS 2.2.2 Gen-13, "Steam Generator Channelhead Decontamination

Using Magnetite Grit and Water", required the surge tank to be refilled

to 22 plus or minus 2" at least once each 30 minutes. The procedure

required control room notification if the change between readings was

greater than 12 inches, and stopping decontamination if the change

between readings was greater than 23 inches. The records for

September 21 indicate that the surge tank was refilled much more frequently

than every thirty minutes; i.e. at 9:09, 9:16, 9:34 and 9:42 P.M.

Consequently, the difference between any two levels was not sufficient

to require any action according to the procedure. A critique of

this event was performed by the licensee for the Resident Inspector,

Senior Resident Inspector and representatives of the NRC Office of

Nuclear Regulation and Office of Inspection and Enforcement on September 26,

1980. As a result of this discussion, a licensee representative stated

that a revised 10 CFR 50.59 safety analysis and a revised decontamination

procedure would be developed prior to the resumption of steam generator

decontamination.

The representative stated that this analysis would address what

amounts of magnetite grit would be added to the reactor coolant system

assuming further dilutions due to seal rupture, how that amount of

grit would be recovered from the reactor coolant system prior to

startup, how pieces of ruptured loop seals would be recovered from the

reactor coolant system, what measures had been taken to prevent future

loop seal failures, and how future loop seal failures would be promptly

-3

detected. During this interview they stated that no abrasive,

corrosive, or mechanical plugging would result from the magnetite

grit which had already entered the reactor coolant system as a

result of the seal failure, nor was any such effect due to future

seal failures expected.

The licensee representative further stated that the decontamination

procedure would be revised to incorporate adequate controls to

promptly detect unexpected loss of system inventory, and that the

decontamination system would be modified to prevent isolation of the

remotely monitored loop seal pressure gage and to incorporate a more

reliable sealing material.

The inspector acknowledged these commitments and stated that the

results of them would be reviewed prior to any additional decontamination

by the licensee.

(0/I 50-206/80-28-01).

No items of noncompliance

or deviation were identified.

3. Monthly Surveillance Observations

The inspector witnessed portions of the following surveillance testing:

a. Hydrazine Tank Level Alarm Calibration Check (Instrument and Test

Procedure S-II-1.2).

b. Diesel Generator Monthly Testing (Operating Instruction S-2-11).

The inspector reviewed the surveillance activities to verify that

the testing was in accordance with the Technical Specification

requirements, the procedures were followed by qualified personnel,

and the system was properly restored to service. In addition, the

inspector observed that the test instrumentation for the level alarm

check was calibrated and the test date accurately recorded.

No items of noncompliance or deviation were identified.

4. Inspections during Lonq Term Shutdown.

The inspector observed control room operations for proper shift manning,

for adherence to procedures and limiting conditions for operation, and for

appropriate recorder and instrument indications.

The inspector reviewed

logs and operating records regularly, and verified that the radiation

controlled area access points were safe and clean.

The inspector noted that records of surveillance tests required during

the shutdown had been completed, that the equipment clearance -system was

in effect, and that the physical security-plan appeared to be properly

implemented. Frequent discussions with control room operators were held

by the inspector to discuss their understanding of the reasons for existing

indications and plant conditions. The inspector frequently toured throughout

the facility. The licensee's fire protection plan appeared to be properly

implemented and the cleanliness of the facility was adequate.

The inspector witnessed a portion of the planned radioactivity release of

the west holdup tank from the control room. He observed that the radiation

monitoring alarm setpoint was set at 110,000 counts per minute (CPM) during

this activity, a value more than 95,000 cpm above the normal background

count rate. The Control Operator stated that this was standard practice

at the facility. The inspector discussed this condition with the Watch

Engineer, who ordered the release stopped. The Watch Enineer stated that

the high discharge count rate was a direct consequence of the

relatively high activity in the holdup tank for this release, and that the

high count rate was not necessarily indicative of an uncontrolled release

of radioactivity. The inspector reviewed the Radioactive Discharge

Permit and stated his agreement with this conclusion. However, the

inspector noted that Technical Specification 6.8.1 requires that written

procedures and administrative policies shall be established, implemented

and maintained that -meet or exceed the requirements and recommendation

of Appendix "A" of USNRC Regulatory Guide 1.33, Revision 1. Paragraph 7a(3)

of this Appendix, "Liquid Radioactive Waste System; Discharge to Effluents,"

i-s one of the recommended procedures. The licensee's Operating Instruction

S-3-2/27. "Receiving, Storage, Processing, and Discharge of Liquid Waste"

implements the Appendix "A" recommendation. Precaution III A of this

instruction states that "during holdup tank releases, the set point for

ORMS 1218 shall be set at a maximum of 20,000 cpm above background."

Contrary to this requirement, on September 24, 1980 the inspector observed

that while the west holdup tank was being discharged to the circulating

water system, the setpoint for ORMIS (Operational Radiation Monitoring System)

1218 was set at 110,000 cpm, approximately 95,000 cpm above the backgound

count rate.

This is a deficiency. (50-206/80-28-02)

5. Independent Inspection

The inspector reviewed the reactor coolant chemistry results for

September 1-18, 1980. These results indicated that on each daily sample

recorded from September 2-la, 1980, the chloride concentration of reactor

coolant had been in excess of the chloride limit of 0.15 ppm specified

by the Station Order S-E-2, "Operation, Maintenance and Chemical

Control of Heat Exchange Equipment."

This area was reviewed as part

of a continuing concern by the inspector which originated after a

Southern California Edison Corrective Action Request, S01-P-263, identified

a similar chloride concentration out of limits for the period from

April 12-17, 1980. As of the date of this inspection the licensee had

not completed corrective action for the April event to prevent recurrence.

of excessive chloride concentrations. Therefore, the inspector advised

the licensee that Technical Specification 6.8.1 requires that written

procedures and administrative policies shall be established, implemented

and maintained that meet or exceed the requirements and recommendations

of Appendix "A" of USNRC Regulatory Guide 1.33, Revision 1. Paragraph 10

of this Appendix states that procedures should be written to prescribe the

instructions maintaining water quality within prescribed limits, and the

limits on concentrations of agents that may cause corrosive attack on fouling

of heat transfer surfaces. Station Order S-E-2, "Operation, Maintenance

and Chemical Control of Heat Exchange Equipment," provides that

"Corrosion of the primary system components will be controlled by maintaining

the chloride levels within the defined limits."

Paragraph B.l.b of this

Station Order defines the chloride limit as "less than .15 ppm."

Contrary to the above, on each daily sample recorded from September 2 to

September 13, 1980, the chloride concentration was in excess of the

specified limit by an amount which varied from 0.03 to 0.35 ppm, or

20-233% in excess of the limit.

This is a deficiency. (50-206/80-28-03).

6. Exit Interview

An exit interview was held on September 26, 1980 to summarize the scope

and findings of this inspection. In addition, the inspector reconfirmed the

licensee's commitment to prepare emergency procedures for the loss of

d.c. buses prior to resuming operation; stated that the licensee's shift

turnover procedures and logs prepared in response to TMI Category "A"

item 2.2.1.C appeared adequate; and requested a copy of the revised

10 CFR 50.59 safety analysis for steam generator decontamination which

was to be prepared to incorporate the lessons learned from the inflatable

seal failure of September 21, 1980. Finally, the inspector requested a

copy of the Maintenance Order and any associated welding records which

the licensee had retained for the repair of the South Charging Pump

completed on June 6, 1980. A licensee representative stated that the

documents requested would be provided to the inspector.