ML13316C013

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Insp Repts 50-206/89-09,50-361/89-09 & 50-362/89-09 on 890306-10 & 0403-07.Violations Noted.Major Areas Inspected: New Installation of Nuclear Instrumentation Sys & Assessment of Adequacy of Main Feedwater Flow Elements at Facility
ML13316C013
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 05/02/1989
From: Gee F, Jim Melfi, Richards S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13316C011 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-1.D.2, TASK-2.E.1.2, TASK-2.F.2, TASK-TM 50-206-89-09, 50-206-89-9, 50-361-89-09, 50-361-89-9, 50-362-89-09, 50-362-89-9, NUDOCS 8905230107
Download: ML13316C013 (14)


See also: IR 05000206/1989009

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION V

Reports Nos:

50-206/89-09, 50-361/89-09, 50-362/89-09

Docket Nos.

50-206, 50-361, 50-362

License Nos.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

P. 0. Box 800

2244 Walnut Grove Avenue

Rosemead, California, 91770

Facility Name:

San Onofre Units 1, 2 and 3

Inspection at:

San Onofre Nuclear Generating Station Units 1, 2 and 3.

Inspection Conducted:

March 6 -

10 and April 3 - 7, 1989

Inspectors:

,

7.

______

d< F. Melfi, Reactor Aspector

DAte*Signed

F. S. Gee, Reactor Inspector Trainee

Date Signed

Approved By.:231

S. A. Richards, Chief, Engineering Section

Date Signed

Summary:

Inspections on March 7 -

10, 1989 and April 3 - 7, 1989

(Report 50-206/89-09, 50-361/89-09, 50-362/89-09)

Areas Inspected:

A routine, unannounced inspection by regional based

inspectors of the new installation of the nuclear instrumentation system and

an assessment of the adequacy of the Main Feedwater (MFW) flow elements at San

Onofre Nuclear Generating Station (SONGS), Unit 1. Items from the TMI action

plan (NUREG-0737) were also inspected and updated for Unit 1, and followup of

previously identified items was conducted for Units 2 and 3. Inspection

procedures 30703, 37701, 37702, 2515/065 and 92701 were used.

Safety Issue Management System (SIMS) items

TMI item II.E.1.2 was closed, and the following TMI issues were updated on the

SIMS system:

I.D.2 -

Safety Parameter Display System Implementation

II.F.2 -

Inadequate Core Cooling Level Instrumentation

8905230107 890505

PDR

ADOCK 05000206

PDC

-2

Results:

General Conclusions and Specific Findings:

The installation of the new Nuclear Instrumentation System (NIS) was reviewed.

The inspectors performed a documentation review and walked down most of the

new installation. The training of the operators, QA/QC involvement in this

installation, and the noise reduction efforts were also assessed. The

installation of the new Nuclear Instrumentation System (NIS) seemed to be

performed adequately.

Significant Safety Matters:

The 10 CFR 50.59 violation issued in this report

and the licensee's considerations on why their 10 CFR 50.59 review.was

appropriate may indicate a problem with their approach to 10 CFR 50.59

reviews.

Summary of Violations:

Two violations were identified during this

inspection. One violation concerning an inadequate 10 CFR 50.59 review for

Unit 1 regarding a NIS block of a Start-Up Rate Trip (paragraph 5.C).

The

other violation was addressed at housekeeping in Unit 2/3 electrical cabinets

(paragraph 10) and electrical maintenance in Unit 3 (paragraph 10).

Open Item Summary:

No new open items.

0II

O

'DETAILS

1. Persons Contacted

a. San Onofre Nuclear Generating Station

  • H. Morgan, Station Manager
  • S. McMahan, Asst. Maintenance Manager
  • C. Couser, Compliance Engineer
  • G. Gibson, Licensing Engineer
  • C. Balog, Site Nuclear Engineering Manager
  • K. O'Connor, Construction Manager
  • R. Plappert, Compliance Engineer
  • R. Baker, Compliance Engineer
  • G. Stavinicey, Project Engineer
  • T. Elkins, Engineer
  • R. Reiss, QA Engineer

T. Elkins, Engineer

A. Eckhart, Nuclear Engineer

A. Hernadez, Engineer

T. Straw, Training Instructor

P. Kuhner, Training Instructor

J. Ibarra, EQ Engineer

b. USNRC

  • R. Huey, Senior -Resident Inspector
  • J. Tatum, Resident Inspector
  • Attended Exit Meeting, March 10, 1989 and April 7, 1989

The inspectors also held discussions with other licensee and

contract personnel during the inspection. This included plant staff

engineers, technicians, administrative and clerical assistants.

2.

Introduction

This inspection focused on the activities surrounding the installation of

the new Nuclear Instrumentation System (NIS) at San Onofre Unit 1. The

purpose of this new installation was to replace the older nuclear

instruments with newer instruments. Since the NIS has reactor trips and

rod blocks, which are important to reactor safety, this installation is

an important safety-related change to the plant. The inspection focused

on a review of the design packages implementing the installation, an

assessment of the licensee's efforts to solve electronic noise problems

an assessment of Quality Assurance (QA) and Quality Control (QC)

involvement, a review of the instrument calibrations, and an assessment

of the training of the licensee's staff on the new instrumentation.

0II

2

The inspectors also loQked at issues surrounding the Main Feedwater (MFW)

flow orifices, the TMI Action Plan items for Unit 1, and the enforcement

and followup items for Units 2 and 3:

3. Nuclear Instrumentation Noise Reduction Effort

The nuclear instrumentation (NI) for Unit 1 was replaced during the Cycle

X refueling outage by the licensee with upgraded equipment which offers

improved system performance and readily available parts for maintenance

and repair. Because of the improved sensitivity of the new NI,

electronic noise induction and interference by energized plant equipment

became significant in magnitude to produce, at plant shutdown conditions,

erroneous startup rate trips and power level. readings on the NI source

and intermediate ranges. One purpose of the inspection by the regional

inspectors was to observe and to identify any potential safety issue in

the licensee's NI noise reduction effort.

A meeting was held on March 7, 1989, with the Instrumentation and Control

group to discuss the ongoing noise reduction effort in the newly

installed nuclear instrumentation. The following Retrofit Problem

Reports (RPR's) were identified as the licensee's effort in the noise

reduction. The RPR numbers were 1997, 1998, 1999, 2228, 2297, and 2523.

The corrective actions taken by the licensee for the RPR's were as

follows:

A.

Sent the new source and intermediate range rate amplifier boards

back to the supplier (Westinghouse) for modification to decrease the

sensitivity (i.e. to increase the time constant) to that of the old

NI.

B.

Installed Sola isolation transformers on the instrument and control

power supplies to the NI and on the control power supply to the

coincidentors.

C.

Installed separate insulated ground cable from each of the four NI

cabinets, tied the insulated ground cables at one point, and

grounded the single insulated cable at a dedicated ground point

outside the building.

0.

Installed a RC circuit for AC relays and a diode for.DC relays to

suppress internally generated noise from the coincidentors to the

NI.

E. Changed the source of power from regulated buses to vital buses,

enhanced the shielding and grounding of field conduits, and added

inner to outer shield grounding on all power range detector "A"

signal cables at the drawers to reduce externally generated noise on

the NI to an acceptable level.

F. Modified at the supplier factory the inDermediate range rate boards

to provide a rate output only above 10 % poser to minimize the

noise effect on the NI from stroking HV-852A and CV-737A. The

licensee had initiated the modification.

3

Awalkdown was performed on the new NI system installation. The items

included in the walkdown were as follows:

A. The lead-lined enclosure for the preamplifiers and the high voltage

lead-in cables outside Unit 1 containment.

B. Containment NI cable penetrations from inside the containment.

C.

NI cable routing inside the containment.

D. The three newly installed independent and dedicated ground bars (2

used, one spare) for the NI in the open area exterior to the control

room building and near the diesel generator building.

E. Grounding of conduits and NI cabinets in the control room building.

F. The installation of noise suppressors RC circuit on AC relays and

diodes on DC relays in the two coincidentor cabinets in the control

room building.

G. The installation of Sola isolation transformers on the control and

instrument power supplies for the NI and on the control power supply

for the coincidentors.

H. The ongoing NI modification on the control board in the control

room.

I. The cable installation in the J-console in the control room.

J. The battery room.

A significant amount of good work was done on the NIS noise reduction as

shown by the reactive actions that were taken to resolve those Retrofit

Problem Reports. Yet the lack of proactive effort was evident in

establishing formal procedures to systematically identify the noise

effect from all plant equipment and their synergistic contributions to

noise on the NI during full operation. It was understood by the

inspectors that the existing shutdown plant conditions prevented the

availability of some plant equipment to be energized, and thus the

related noise effect, if any, on the NI will not be observable until full

plant operation. Examples of such equipment were the control rod drive

mechanisms.

During the exit meeting on March 10, a draft outline of a planned NI

noise monitoring program was submitted to the inspectors after the lack

of a proactive effort in systematically identifying noise sources on the

NI was discussed with representatives of the licensee. A printout of a

listing of the design change packages on implementing groundings and

shieldings as part of the effort in resolving the RPR's was also

submitted to the inspectors.

During a subsequent inspection on April 3, the inspectors concluded that

the proactive test plan on the NIS noise reduction effort which the

licensee implemented since the March inspection was adequate. The

4

co.verage of the test plan and the recorded noise baseline data reflected

a conscientious attitude in correcting the previous lack of a proactive

effort.

The cable separation in the J control board was observed to be maintained

to the extent practical for the existing modification of the indicators

and the mode selector switch.

As the cables entered the control room in

the J-console, they were wrapped with fire retardant tape. As stated in

NRC Safety Evaluation dated December 13, 1988, the acceptability of this

separation will be included as part of the staff's ongoing review of

SONGS-1 compliance to the guidelines of Regulatory Guide 1.97.

4. QA/QC Involvement

The licensee's Quality Assurance (QA) and Quality Control (QC)

organizations have the function to provide, in part, an independent

-assessment of the adequacy and quality of new safety-related

installations. This independent assessment of quality can include a

review of the areas of design control, receipt and procurement, testing,

training, procedures, craft workmanship and resolution of design

deficiencies of the installation. Since the installation of a new

Nuclear Instrumentation System (NIS) is a large safety-related change to

Unit 1, the inspector desired to review QA/QC assessments of the NI

system and determine the extent of their involvement.

The licensee's QA groups were initially involved i-n reviewing the work on

the NIS after it had been completed. The inspector was informed that the

licensee's Quality Assurance (QA), Independent Safety Engineering Group

(ISEG) and the Nuclear Safety Group (NSG) initiated an expanded,

coordinated effort in mid January, 1989, to look at the new NIS

installation at Unit 1. These three groups presented their Operational

Readiness Assessment Plan for the NIS to the inspector. The plan's

objectives were to assess the ongoing efforts, provide 24-hour QA

coverage, and be involved in the daily activities surrounding the

installation. The daily activities included looking at the design change

review, the test criteria and results of the testing, reviewing the

calibration and operating procedures, and a review of operator training

on the new system. These QA groups were also planning to monitor the

start-up activities on a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> basis.

The QA groups have issued Nonconformance Reports (NCRs) and Retrofit

Problem Reports (RPRs) on the NI system. The inspectors reviewed the

issued RPRs and NCRs on the system. The actions taken by the licensee

seem to be appropriate.

The licensee's Quality Control (QC) organization was involved in the

manufacture of the NIS, with several QC inspectors witnessing the

reassembly of the system. The inspectors discussed the QC involvement

with the QC inspectors, and determined that the review seemed to be

adequate.

The licensee's QA and QC organizations appeared to take an aggressive,

proactive approach regarding the installation of the NIS. The inspector

did not identify any concerns with the licensee's QA/QC organizations.

5

5. Nuclear Instrumentation System Modifications

A.

Calibration of Source Range High Voltage

The source range detecto measures the power of the reactor at very

low power levels ( < 10 % power).

This detector provides an input

into a rod block (prevent rod withdrawal) if there is a high

start-up rate. The high voltage setting of this detector is

important, since the setting value affects how many counts would be

seen by the detector per incident neutron. A typical practice for

setting the source range detector voltage is that the voltage is set

at the "knee" of a detector voltage versus 'a logarithm of the count

rate curve. The licensee did not set the detector voltage in this

manner, but in a manner approved by the vendor (Westinghouse). The

inspectors reviewed the new method with the licensee, which does

place the detector voltage in the proper region for linearity of

response.

B.

Indicated Neutron Count Difference

The inspectors observed that at shutdown conditions, approximately a

decade of difference existed on the two intermediate range count

level meters of the newly installed nuclear instruments. The

.licensee indicated that the difference might be due to the geometry

of the detector locations and installations, and expected to see a

narrowing of the difference during and after power ascension.

C.

Suppression of Intermediate Range Startup Rate Trip

The licensee elected to install a suppression of the intermediate

range Start Up Rate (SUR) trip, to reduce the effects of random

noise on the intermediate range instruments. This suppression

blocks any signal to the 4Reactor Protection System below a certain

power level (approx. 10 % power). This suppression of the SUR trip

was not in the old installation (as noted in the Updated Final

Safety Analysis Report (UFSAR)) or originally considered for the new

installation (as noted in the Safety Evaluation with Technical

Specification Amendment 117).

10 CFR 50.59 allows the licensee to make any change to the plant

without prior NRC approval as long as that change does not involve

an unreviewed safety question or a change to the technical

specifications. As part of the change to the intermediate range SUR

trip, the licensee included a 10 CFR 50.59 review with

Nonconformance Report (NCR) S01-P-7112.

The licensee concluded in NCR S01-P-7112 that this change did not

involve an unreviewed safety question in that the operability of the

intermediate range trip was not assumed for accident analysis and

that any power excursion generated below 10 4% power will not

present a challange to the integrity of the core. In further

discussions with the licensee, the licensee stated that the setpoint

was set at approximately the power level equivalent to the lower

limit of sensitivity of the old intermediate range NIS. The NCR

6

also concluded that there was no change in any margin of safety as

defined in any technical specification.

The inspectors evaluated this change and noted that Technical

Specification 3.5.1 states that the trip is required to be operable

in.mode 1 (below 10% power) and in mode 2. In discussions with

licensee personnel4 it was determined that the reactor would go

critical below 10 % power during plant startup, and therefore be in

mode 2.

In reviewing the UFSAR, it was noted that there was no block

described associated with the intermediate range SUR trip.

Technical specification amendment 117, which included a NRR safety

evaluation of the NIS system changes into the license, was also

reviewed. The NRR safety evaluation of the new NIS system also did

not mention any blocking of the intermediate range SUR trip during

startup.

Based on the information porvided by the licensee, the inspectors

did not identify a technical issue with the licensee's actions.

However, the blocking of the intermediate range SUR trip was not

described or addressed by the UFSAR, the technical specifications,

or the associated license amendment, although blocking functions of

this type are clearly typically addressed. Therefore, the

inspectors concluded that this modification did involve a change to

the technical specifications and is an apparent violation of 10 CFR

50.59. (50-206/89-09-01). The licensee has since submitted a

technical specification amendment request.

D. Disabling of Source Range Detectors

On April 4, 1989, the inspectors noted in Instrument and Test

Procedure SO1-II-1.6.5.1, Revision 0, TCN 0-3, page 53, Sections

6.18.4 5and 16.18.5 that the source range high voltage cutoff 6is set

at 10

% power and the required reset point is set at 8x10

%

power. -he source range high voltage cutoff is about a decade lower

than 10

% power, the intermediate range suppressed

startup-rate-trip setpoint. In this case, there is no rod stop

startup rate trip protection for about a decade. After the

discrepancy was identified to the licensee, the inspectors were told

that the procedure was scheduled to be changed, and the change was

made on April 5, 1989. The change4implemented the disabling of the

source range high voltage at 3x10

% power on power ascension and

the enabling at 1.5x10

% power on descending power level.

E. Incore/Excore Correlation

The location of the Nuclear Instrument Detectors remained the same,

except for the change of one detector to a spare assembly. This

change- was reviewed by the office of Nuclear Reactor Regulation

(NRR), and was approved.

The inspectors noted that there is no check source of neutrons

available to the new instruments. From the use of a check source,

7

it could be possible to ascertain beforehand the neutron flux the

detectors should see. The licensee is not using a check source, but

is instead relying on the decay of neutrons from fission products.

The detectors are registering neutron pulses from the core, and the

licensee is performing an analysis to verify if the amount of pulses

seen is approximately correct. The licensee is also going to do an

incore to excore check during their power ascension program, to

verify the excore detector accuracy.

The licensee's actions seem appropriate.

6. Nuclear Instrumentation System Qualification

Certain components of the NIS system equipment are required by Regulatory

Guide 1.97, (as noted in 10 CFR 50.49 (b)(3)) to have an environmental

qualification (EQ) appropriate for the environment that the equipment is

located in. The wide range nuclear instrument (intermediate range) is

required to be environmentally qualified, to give an indication of

nuclear power after design basis events.

At the time of the inspection, the licensee had not yet fully reviewed

and qualified the intermediate range instrumentation. The licensee had

qualified different parts of the system (i.e. coaxial cables, detectors,

penetrations, etc), and provided the documentation packages for the

inspector's review. The inspector did not identify any problem with the

documentation packages.

During the walkdown of the system, the inspector

did not have any EQ concerns.

7. Operator Training

For safe operation of the new NIS, the control room Reactor Operators

(ROs), Senior Reactor Operators (SROs), Shift Supervisors, Plant

Equipment Operators, (PEOs) and Shift Technical Advisors (STAs) need to

be familiar with the operational characteristics of the new system. The

inspectors discussed the training of the operators with the licensee.

The licensee wrote a lesson plan, IXC 205, "Excore Nuclear

Instrumentation System," from vendor information, the design change

packages, and procedures. The inspectors discussed the lesson plan with

the licensee, and did not identify any concerns.

The inspectors also verified the training records for the plant staff on

the new system by looking at the course list.

The inspectors also discussed craft training on the new system with-the

licensee. The Instrumentation and Control (I&C) personnel were trained

by the vendor (Westinghouse) on 6/28/88 on the new system. The training

provided by Westinghouse included classwork and hands on training. The

hands on training also included training to find purposely placed faults

with the system. The training on the new system appeared appropriate.

Based on the inspectors' review, the training given seemed appropriate.

8.

Feedwater Flow Orifice Replacement

8

During Cycle X refueling outage, the orifice plates FE-456, FE-457 and

FE-458 for the three main feed lines were removed and inspected by the

licensee. The orifice plates were examined for their orifice diameter,

flatness, and inlet square edge. FE-456 was found in a marginal

condition with impact mark on the inlet face of the orifice plate,

possibly from loose debris.

FE-457 was found acceptable. FE-458 did not

meet the flatness and the orifice diameter tolerances. The three main

feedwater orifice plates were replaced by the licensee.

The duplicated orifice plates manufactured to the original specifications

were put into service by the licensee without actual flow calibration by

claiming the original flow test accuracy of 0.25% plus 0.6% for

duplication error. The licensee claimed a credit of 1% accuracy for the

duplicated plates with 0.15% of margin.

A flow test accuracy of 0.25% was obtained by Alden Hydraulic Laboratory

for the original calibrations of the flow element sections performed in

1965. The pressure taps of the flow sections were non-standard ASME

configurations.

A duplication error of 0.6% at 95% confidence level was claimed by the

licensee for manufacturing the three replacement orifice plates in

accordance with the original specification for the bore diameter, the

flatness, the thickness at the bore, and the upstream edge sharpness.

This assumption was supported by the calibrations performed at Alden

Research-Laboratory for the orifice plates of the main feed lines for the

Connecticut Yankee Nuclear Station. A comparison was made between the

flow discharge coefficients of the 1966 calibration of the original

plates and the 1986 calibration of the duplicated plates for the main

feed lines from the Connecticut Yankee Nuclear Station. The licensee

made eleven ultrasonic measurements to confirm that the pipe thickness

had not changed significantly to affect the inside diameter of the pipe.

The Connecticut Yankee data did show an in-service degradation of

accuracy. The licensee agreed to dimensionally verify the in-service

degradation of the orifices and to accumulate baseline data on the

degradation during subsequent outages. The baseline data are to be

collected to a point when the 0.15% margin is exceeded. Then replacement

of the respective orifice plate is to be scheduled before the 0.15%

margin is exceeded.

Based on the inspectors' review of the licensee's calculations and

applicable industry standards, and based on discussions with the

technical staff of NRR, the NRC staff had no regulatory concern regarding

the licensee's approach of replacing the orifice plates without

performing a direct calibration. The licensee's future monitoring of the

condition of the orifice plates will be followed as part of the ongoing

inspection program.

9. Feedwater Flow Transmitter Range Erroneously Transcribed and Calibrated

On March 8, 1989, the inspectors found that incorrect differential

pressure ranges were used for the calibration of the main feed flow

transmitters FT-456, FT-457, and FT-458 in Unit 1. The transcription

9

error occurred approximately in 1983. The incorrect ranges were shown in

Master Instrument List M37351. After being notified, licensee issued

Nonconformance Report Number SO1-P-7118. The incorrect ranges were

corrected by FIDCN J-2077 which was issued for the purpose of orifice

replacement.

Main Feed Flow Transmitters

Incorrect Ranges

Correct Ranges

FT-456

0-774"wc

0-769"wc

FT-457

0-772"wc

0-771"wc

FT-458

0-774"wc

0-764"wc

The use of incorrect differential pressure ranges for the main feed flow

transmitters affected neither the core thermal power evaluation nor the

nuclear overpower trip. The secondary calorimetric power used to

calibrate the excore power range nuclear instrumentation was calculated

from separate instruments, the Barton differential pressure indicators.

All three incorrect differential pressure ranges used were higher than

the respective correct ranges. These transmitters input into the main

feedwater flow/steam flow mismatch trip. With a higher differential

pressure range, the calculated feedwater flow for the feedwater

flow/steam flow mismatch trip was lower than the actual flow. With the

actual feedwater flow being higher than the calculated flow, the mismatch

trip point was in the conservative direction.

Based on the inspectors' review, the use of the incorrect feedwater flow

transmitter ranges did not result in a reduction of safety protection.

10. Housekeeping and Electrical Maintenance

On April 6, 1989, during a walkdown to inspect the work performed on

electrical separation in Units 2 and 3 as a followup of an earlier

violation, the inspectors found debris in three of four control room

cabinets inspected, 3CR50/3CR51, 3CR52, 3CR56,.and 3CR60, and the remote

shutdown panels of Units 2 and 3. The debris.included several tie wraps,

a spray can cap, a painted metallic safety light cover with partially

chipped bare metal surface exposed, a half of an inch thick 8.5" by 11"

paper pad with several pages of hand written note, a spare resistor,

non-metallic washers, a chipped terminal block cover plate, unmounted

embossed labels, and light bulbs.

The Units 2 and 3 remote shutdown panels are safety related panels and

the accesses are restricted by locks.

The inspectors noted that a previous notice of violation was issued on

the same noncompliance for an inspection conducted during 1987.

Furthermore, the licensee stated that cleanliness would be concurrently

evaluated with electrical separation inside electrical cabinets, in

responding to a 1988 NRC inspection of Regulatory Guide 1.97.

Especially, individual workers should recognize the safety functions that

the remote shutdown panel is called to perform and the gravity of the

10

plant conditions when the panel is called into service. The remote

shutdown panel should have not become a place for debris and material to

accumulate and a storage location for spare parts. The guidelines have

succinctly been set forth in SCE procedures that individuals shall

cleanup after themselves in a timely manner, any unused equipment shall

not be allowed to accumulate at any work place, and leftover material

shall be removed at the completion of the job.

This is an apparent violation (50-361/89-09-01).

On April 6, 1989, the inspectors observed in the Unit 3 remote shutdown

panel a pull rope extending beyond the end of a conduit entering at the

top of the cabinet. This pull rope was wrapped around several times an

unterminated coiled cable coming out of the same conduit and tied to the

side of the cabinet. The diameter of the coil of-the unterminated cable

was approximately two feet, and the coil was able to swing from side to

side within the cabinet. The conduit end was neither capped nor closed

by putty. A pull tape was also observed extending beyond the end of

another conduit in the same cabinet. This is a second example of

apparent violation 50-361/89-09-01.

Another example of incomplete maintenance work was observed on April 6,

1989. Four removed terminal block cover plates were found in the Unit 2

remote shutdown panel not being returned to their original installation

after maintenance. Three blue-coded terminal block cover plates for

Separation Group 0 (TB-384) and one green-coded terminal block cover

plate for Separation Group C (TB-383) were found on the floor inside the

cabinet, and the respective terminal blocks were exposed.

11.

TMI Action Plan Requirements (Unit 1) (2515/065)

This section includes the status of TMI Action Items as determined by the

inspector through a review of documentation and discussions with licensee

personnel.

Several of these items were also statused in inspection

report 50-209/88-29, 50-361/88-30, and 50-362/88-32.

A. (Open), I.D.2, "Safety Parameter Display System"

The previous inspection reports on this item were 50-206/85-35,

50-206/86-26, and 50-206/88-29.

The current status of this item remains open. The SPDS is not

currently installed in the control room. The licensee was not

planning on installing the SPDS this outage and is discussing with

NRR the implementation of this item. This item will remain open

pending installation of the SPOS, which is currently scheduled for

cycle 12.

B. (Closed), II.E.1.1.2, "Auxiliary Feedwater System Evaluation

Long-Term System Modifications"

This item on Auxiliary Feedwater (AFW) had been previously inspected

in inspection reports 50-206/85-35, 50-206/86-26, and 50-206/88-29.

11

The remaining NUREG-0737 requirements to be .completed for SONGS 1

were as follows:

(1) Upgrade the two control grade AFW trains to Safety Grade by the

end of the cycle 9 outage.

(2) The installation and upgrade to safety grade of a third train

of AFW by the end of the cycle 10 outage.

The licensee has installed the upgrade to the AFW system. This

modification put both the Turbine Driven Auxiliary Feedwater (TDAFW)

Pump and the Motor Driven Feedwater (MDAFW) Pump on the same train

(Train A).

The licensee has another pump to inject auxiliary

feedwater, the Dedicated Shutdown (DSD) Pump, which relies on a

separate diesel for its safety related power. The DSD pump is now

the train B pump. In discussions with the licensee, the inspectors

were informed that the train B pump is designed so that it would

start first, and the other train is interlocked from starting. On

failure of this pump to start, the train A pumps would start. The

licensee has performed a single failure analysis to show that this

configuration is safe.

The modification was performed under Design Change Package (DCP)

3364.OOTJZ. The inspectors reviewed the package, performed a

walkdown of the modification, and discussed the package with the

licensee. From this review, the licensee has finished the

installation, conducted preoperational testing, and revised the

procedures and drawings for the system.

Based on the inspectors' review, this TMI item is closed.

C.

(Open) II.F.2.3.B, "Instrumentation for Detection of Inadequate

Core Cooling - Installation of Level Instruments"

The previous inspection reports on this item were 50-206/85-35,

50-206/86-26, and 50-206/88-29.

The licensee is planning to implement this item in the cycle XI

outage. This item will remain open pending completion by the

licensee.

12.

Enforcement Items

(Closed) 50-361/88-18-02, "Lack of Separation in Post-Accident Monitoring

Cabinet"

This enforcement item was issued during the Regulatory Guide 1.97 team

inspection at San Onofre units 2 and 3. During that team inspection

walkdown, a condition was found in the unit 2 control room panel 59 which

was not in accordance with the licensee's specification for separation.

The licensee evaluated the situation and initiated corrective action to

separate the wires in that control room panel.

The licensee admitted the

violation in their letter dated August 29, 1989, and instituted

corrective actions to address possible generic concerns about separation.

12

The licensee trained personnel about separation according to their

separation specification and inspected cabinets for unit 3, which

happened to be in refueling at the time. As a result of this inspection

of other cabinets by the licensee, other Nonconforming Reports (NCRs)

were issued and dispositioned.

During this inspection, the inspectors reviewed the actions taken by the

licensee for the cabinets. Some of the NCRs that were written to improve

separation resulted in barriers being installed, rerouting of cables,

installing siltemp (an approved barrier) around wires, and grooming of

cables, which had drooped over time, to ensure wire separation.

The inspectors inspected the corrective actions of the licensee to

improve separation for six of the licensee's unit 3 cabinets.

The

corrective actions are summarized in a memo, Wambolt to Morgan dated

12/2/88. The inspectors noted the licensee's actions, and did not

identify any concerns with separation. The licensee is going to

implement the same program for unit 2 when that unit comes down for

refueling. The licensee's actions for Unit 2 will be followed up under

followup item number 50-361/88-18-03.

While the inspectors did not have any concerns about separation, the

inspectors were concerned about housekeeping in the cabinets. This is

further discussed in paragraph 10.

Based on the licensee's actions, and future Actions to address possible

separation concerns, this item is closed.

13.

Followup Items (92701)

(Closed) 50-362/88-19-01, "Followup on NCRs and Program to addressing

Separation"

This item was -issued during the Regulatory Guide 1.97 team inspection at

San Onofre Units 2 and 3. This item was to specifically follow up on the

licensee's corrective actions on separation for Unit 3. As noted in the

closeout of Enforcement item 50-361/88-18-02, the Unit 3 cabinets were

inspected and found to be satisfactory.

Based on the walkdown and discussions with the licensee, the licensee's

corrective actions seem appropriate.

This item is closed.

14. Exit Meeting

The inspectors met with the licensee representatives identified in

paragraph 1 on March 10 and April 7, 1989. The scope of the inspection

and the findings up to that date were discussed. The inspectors

identified -that some additional information for Unit 1 was needed. The

licensee sent the information to Region V, where it was reviewed, and the

findings were identified in this report.