ML102810670

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IR 05000361-10-006, 05000362-10-006 and Notice of Violation for Errata - San Onofre, Problem Identification and Resolution Inspection
ML102810670
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 10/07/2010
From: Hay M
Division of Reactor Safety IV
To: Sheppard J
Southern California Edison Co
References
FOIA/PA-2011-0221 IR-10-006
Download: ML102810670 (6)


See also: IR 05000361/2010006

Text

October 7, 2010

Mr. James J. Sheppard

Senior Vice President and

Chief Nuclear Officer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

SUBJECT:

ERRATA - SAN ONOFRE NUCLEAR GENERATING STATION -

NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000361/2010006; 05000362/2010006 AND NOTICE OF VIOLATION

Dear Mr. Sheppard:

Please replace page 10 of the Summary of Findings section as well as page 38 of the Report

Details in NRC Inspection Report 05000361/2010006; 05000362/2010006, dated July 30, 2010,

with the enclosed revised pages. These changes are needed to correct a typographical error

listing the crosscutting aspect of the finding involving inadequate procedures for radiation

monitoring of the component cooling water. Specifically, the error is that the crosscutting aspect

is listed as P.1(c), when it should be P.1(a). The description of the crosscutting aspect is

correct.

Sincerely,

/RA/ Dale A. Powers for

Michael C. Hay, Chief

Technical Support Branch

Division of Reactor Safety

Dockets: 50-361; 50-362

Licenses: NPF-10; NPF-15

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Southern California Edison Company

- 2 -

cc:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Assistant Director-Resources

City of Riverside

3900 Main Street

Riverside, CA 92522

Mark L. Parsons

Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Gary H. Yamamoto, P.E., Chief

Division of Drinking Water and

Environmental Management

1616 Capitol Avenue, MS 7400

P.O. Box 997377

Sacramento, CA 95899-7377

Michael L. DeMarco

San Onofre Liaison

San Diego Gas & Electric Company

8315 Century Park Ct. CP21C

San Diego, CA 92123-1548

Director, Radiological Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

The Mayor of the City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Southern California Edison Company

- 3 -

Douglas K. Porter, Esquire

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Doug Bauder

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Steve Hsu

Department of Health Services

Radiologic Health Branch

MS 7610, P.O. Box 997414

Sacramento, CA 95899-7414

R. St. Onge

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Chief, Technological Hazards Branch

FEMA Region IX

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Institute of Nuclear Power Operations (INPO)

Records Center

700 Galleria Parkway SE, Suite 100

Atlanta, GA 30339

Southern California Edison Compan

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins

Deputy Regional Administrator (Chu

DRP Director (Kriss.Kennedy@nrc.g

DRP Deputy Director (Anton.Vegel@

DRS Director (Roy.Caniano@nrc.go

DRS Deputy Director (Troy.Pruett@

Senior Resident Inspector (Greg.Wa

Resident Inspector (John.Reynoso@

Branch Chief, DRP/D (Ryan.Lantz@

Senior Project Engineer, DRP/D (Do

SONGS Administrative Assistant (H

Project Engineer, DRP/D (Peter.Jay

Project Engineer, DRP/D (Zachary.H

Public Affairs Officer (Victor.Dricks@

Public Affairs Officer (Lara.Uselding

Project Manager (Randy.Hall@nrc.g

Branch Chief, DRS/TSB (Michael.Ha

RITS Coordinator (Marisa.Herrera@

Regional Counsel (Karla.Fuller@nrc

Congressional Affairs Officer (Jenny

OEMail Resource

OEDO RIV Coordinator (Margie.Kot

Eric.Ruesch@nrc.gov

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ADAMS ML

SUNSI Review Complete

Reviewer Initials:

Publicly Available

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Non-publicly Available

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T=Telephone E=E-mail

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F=Fax

-10- Enclosure 2

Notification 200871387, and actions were implemented to require periodic

grab sampling of the train which was not being monitored.

The inspectors determined that this finding was more than minor because

this issue impacted the Public Radiation Protection Cornerstone and its

objective to ensure adequate protection of public health and safety from

exposure to radioactive materials released into the public domain as a

result of routine civilian nuclear reactor operation. Specifically, the

radiation monitors for component cooling water were not sufficient to

ensure adequate release measurements. The inspectors evaluated the

significance of this finding using Phase 1 of Inspection Manual Chapter 0609.04 and determined that the finding screened to Inspection

Manual Chapter 0609, Appendix D, Public Radiation Safety Significance

Determination Process. The inspectors evaluated the significance of this

finding using Inspection Manual Chapter 0609, Appendix D, and

determined that the finding was of very low safety significance (Green)

because dose did not exceed Appendix I criteria. This finding was

determined to have a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program

in that the plant operators did not have a low threshold for identifying

deficiencies in procedures. P.1(a)(Section 4OA2.5g)

Cornerstone: Miscellaneous

Severity Level IV. The inspectors identified a Severity Level IV noncited

violation of 10 CFR 50.73, Licensee Event Report System, in which the

licensee failed to submit a licensee event report within 60 days following

discovery of an event meeting the reportability criteria. On

January 26, 2010, the valve which isolates nonseismic piping from

condensate storage tank T-120 failed its in-service test when the hand

wheel stem snapped after a leveraging device was used in an attempt to

close the valve. This isolation valve, 2HV5715, must be closed within 90

minutes of an operating basis earthquake in order to prevent the loss of

condensate storage tank T-120 water inventory from a line break in the

nonseismic portion of the condensate system. The failure of this valve

resulted in a condition prohibited by Technical Specification 3.7.6 and

therefore was reportable. This finding was entered into the licensees

corrective action program as Nuclear Notification 200888616, and the

licensee was taking actions to send a licensee event report to the NRC

for this event.

The inspectors determined that traditional enforcement was applicable to

this issue because the NRC's regulatory ability was affected. Specifically,

the NRC relies on the licensee to identify and report conditions or events

meeting the criteria specified in regulations in order to perform its

regulatory function. The inspectors determined that this finding was not

suitable for evaluation using the significance determination process, and

-38- Enclosure 2

sufficient to ensure adequate release measurements. The inspectors evaluated

the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609.04 and determined that the finding screened to Inspection Manual

Chapter 0609, Appendix D, Public Radiation Safety Significance Determination

Process. The inspectors evaluated the significance of this finding using

Inspection Manual Chapter 0609, Appendix D, and determined that the finding

was of very low safety significance because dose did not exceed Appendix I

criteria. This finding was determined to have a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action

program in that plant operators did not have a low threshold for identifying

deficiencies in procedures. P.1(a)

Enforcement. Technical Specification 5.5.1.1.a. requires, in part, that written

procedures be established, implemented, and maintained covering the activities

specified in Appendix A, Typical Procedures for Pressurized Water Reactors

and Boiling Water Reactors, of Regulatory Guide 1.33, Quality Assurance

Program Requirements (Operations), dated February 1978; Section 7.g requires

procedures for radiation monitoring operation. Contrary to the above, prior to

April 22, 2010, the licensee failed to establish procedures for component cooling

water system alignments that would prevent unmonitored leakage to the

environment through leakage into the Salt Water Cooling system. Because the

violation was of very low safety significance and was entered into the corrective

action program as Nuclear Notification 200871387, this violation is being treated

as noncited violation, consistent with the NRC Enforcement Policy VI.A:

NCV 05000361/2010006-07, Failure to Establish Component Cooling Water

Radiation Monitoring Procedures.

h.

Failure to Revise Procedures with Known Technical Errors

Introduction. The inspectors identified a cited violation of Technical

Specification 5.5.1.1a for the failure to maintain written procedures covered in

Regulatory Guide 1.33. Specifically, as of April 2010, the licensee failed to

properly control procedure changes associated with plant modifications resulting

in procedures with known technical deficiencies being used at the facility.

Description. On April 8, 2010, the inspectors reviewed corrective actions from

two previous noncited violations for the licensees failure to maintain procedures.

The first noncited violation was 05000361:05000362/2009003-02 and was

associated with the licensees failure to implement controls over its backlog of

procedure change requests such that procedures with known technical

deficiencies were in use in the field (before being revised). The second noncited

violation was 05000361:05000362/2009009-02 and also involved the licensees

failure to implement controls over its backlog of procedure change requests such

that procedures with known technical deficiencies were in use in the field.

During this inspection, the inspectors identified that the backlog of procedure

change requests had increased to 3,389. The inspectors identified that most of

these procedure changes were appropriately classified according to the TEAM