05000458/LER-2009-001, Standby Liquid Control System Inoperable Greater than Allowable Outage Time

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Standby Liquid Control System Inoperable Greater than Allowable Outage Time
ML090760981
Person / Time
Site: River Bend Entergy icon.png
Issue date: 03/11/2009
From: Lorfing D
Entergy Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RBF1-09-0022, RBG-46894 LER 09-001-00
Download: ML090760981 (6)


LER-2009-001, Standby Liquid Control System Inoperable Greater than Allowable Outage Time
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
4582009001R00 - NRC Website

text

~Entergy Entergy Operations, Inc.

River Bend Station 5485 U.S. Highway 61 N St. Francisville, LA 70775 Tel 225381 4157 Fax 225 635 5068 dlorfin@entergy.com David N. Lorfing Manager-Licensing March 11,2009 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555

Subject:

File No.

Licensee Event Report 50-458 / 09-001-00 River Bend Station - Unit 1 Docket No. 50-458 License No. NPF-47 G9.5 RBG-46894 RBF1-09-0022

Dear Sir or Madam:

In accordance with 10CFR50.73, enclosed is the subject Licensee Event Report.

This document contains no commitments.

Sincerely, David N. Lo-rfing 6~

Manager - Licensing DNL/dhw Enclosure 73iii7~~

Licensee Event Report 50-458 /09-001-00 March 11,2009 RBG-46894 RBF1-09-0022 Page 2 of 2 cc:

U. S. Nuclear Regulatory Commission Region IV 612 East Lamar Blvd., Suite 400 Arlington, TX 76011-4125 NRC Sr. Resident Inspector P. 0. Box 1050 St. Francisville, LA 70775 INPO Records Center E-Mail (MS Word format)

Mr. Jim Calloway Public Utility Commission of Texas 1701 N. Congress Ave.

Austin, TX 78711-3326 Mr. Jeffrey P. Meyers Louisiana Department of Environmental Quality Attn:, OEC-ERSD P.O. Box 4312 Baton Rouge, LA 70821-4312

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 08/31/2010 (9-2007)

, the NRC may digits/characters for each block) not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE River Bend Station - Unit 1 05000-458 1 of 4
4. TITLE Standby Liquid Control System Inoperable Greater than Allowable Outage Time
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH DAY YEAR 0I000 NUMBER NO.05 0

FACILITY NAME DOCKET NUMBER 01 14 2009 2009 - 001 - 00 03 11 2009o

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply) o 20.2201(b)

EC 20.2203(a)(3)(i)

C1 50.73(a)(2)(i)(C)

EC 50.73(a)(2)(vii) 1 C 20.2201(d)

[I 20.2203(a)(3)(ii)

EC 50.73(a)(2)(ii)(A)

EC 50.73(a)(2)(viii)(A)

[I 20.2203(a)(1)

EC 20.2203(a)(4)

C1 50.73(a)(2)(ii)(B)

[I 50.73(a)(2)(viii)(B)

E_ 20.2203(a)(2)(i)

[I 50.36(c)(1)(i)(A)

[I 50.73(a)(2)(iii) 0 50.73(a)(2)(ix)(A)

10. POWER LEVEL [I 20.2203(a)(2)(ii) 0 50.36(c)(1)(ii)(A)

EC 50.73(a)(2)(iv)(A)

[I 50.73(a)(2)(x) 0 20.2203(a)(2)(iii)

EC 50.36(c)(2)

[I 50.73(a)(2)(v)(A)

[1 73.71(a)(4)

C 20.2203(a)(2)(iv)

E] 50.46(a)(3)(ii)

EC 50.73(a)(2)(v)(B)

EC 73.71(a)(5) 100 [1 20.2203(a)(2)(v)

EC 50.73(a)(2)(i)(A)

[I 50.73(a)(2)(v)(C)

C OTHER [I 20.2203(a)(2)(vi) 10 50.73(a)(2)(i)(B) 0 50.73(a)(2)(v)(D)

Specify in Abstract below or in NRC Form 366A

12. LICENSEE CONTACT FOR THIS LER FACILITY NAME TELEPHONE NUMBER (Include Area Code)

David N. Lorfing, Manager - Licensing 225-381-4157CUE SYSTEM COMPONENT MAN U-REPORTABLE I

CAUE STMCOPN T

MANu-REPORTABLE

CAUSE

COMPONEN FACTURER TO EPIX USE COMPONENT FACTURER TO EPIX na I

- I
14. SUPPLEMENTAL REPORT EXPECTED
15. EXPECTED MONTH DAY YEAR SUBMISSION EC YES (If yes, complete 15. EXPECTED SUBMISSION DATE) 0 NO DATE ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)

,On January 14, 2009, an investigation of operational practices related to the standby liquid control (SLC) system concluded that for the period of March 14, 2003, to October 28, 2008, a seismic event could have rendered the system incapable of performing one of its design safety functions as credited in the station's accident analysis. This condition resulted from an inadequately evaluated change made to a surveillance test procedure that allowed water to remain in the system's test tank. The test tank is not seismically analyzed when full of water.

Administrative controls have been put in place concerning draining of the tank following future tests. Test procedure revisions are being developed. The safety significance of this event is negligible. This event is reportable in accordance with 1 OCFR50.73 as operations prohibited by Technical Specifications and a loss of the safety function of the SLC system.

NRC FORM 366 (9-2007)

PRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKET
6. LER NUMBER
3. PAGE SEQUENTIAL I REVISION YEAR NUMBER NUMBER River Bend Station - Unit 1 05000-458 2009 001 00 2

OF 4

REPORTED CONDITION On January 14, 2009, an investigation of operational practices related to the standby liquid control (SLC) (**BR**) system concluded that for the period of March 14, 2003, to October 28, 2008, a seismic event could have rendered the system incapable of performing one of its design safety functions as credited in the station's accident analysis. This condition resulted from an inadequately evaluated change made to a surveillance test procedure that allowed water to remain in the system's test tank (**TK**). The test tank is not seismically analyzed when full of water. This event is reportable in accordance with 10CFR50.73 as operations prohibited by Technical Specifications and a loss of the safety function of the SLC system.

BACKGROUND The SLC system is a safety related design feature installed to provide a means of shutting the reactor down in the event of a failure of the reactor control rod drive system. The system contains redundant pumps powered from the emergency diesel generators that would be used to inject a sodium pentaborate solution into the reactor when directed by operating procedures. The solution is contained in a tank that can supply either or both of the pumps.

A separate 250-gallon tank is built into the system to serve as a suction source of clean water for performing periodic surveillance testing of the pumps and the associated motor-operated valves. The test tank has steel supports that elevate it approximately 16 inches off the floor. The test tank is designed to remain intact in the event of the design basis seismic event, assuming that the tank is empty.

When RBS implemented License Amendment No. 132 (Alternative Source Term) in 2003, the SLC system gained a new design function related to operations following a postulated loss of coolant accident (LOCA). In order to mitigate the release of radionuclides into the primary containment atmosphere in the post-LOCA environment, the SLC system is assumed to be used for pH control of the suppression pool. The analysis assumes that the SLC system is initiated at a certain time in the event, and that the borated solution will leave the reactor vessel through the postulated break in the coolant system piping. The solution would drain to the suppression pool where it would provide a buffering effect in maintaining the pH above a value of 7.

Prior to the implementation of the Alternative Source Term amendment, suppression pool pH control was not a design function of the system.

CAUSAL ANALYSIS and IMMEDIATE CORRECTIVE ACTIONS The investigation of this event found that, in 1992, surveillance test procedures were revised to remove the requirement to drain the test tank upon completion of surveillance tests prior to returning the system to service. The review of the proposed procedure change did not surface the fact that the test tank is not designed to withstand seismic loading when it is full of water.U.S. NUCLEAR REGULATORY COMMISSION (9-2007)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKET
6. LER NUMBER
3. PAGE SEQUENTIAL I REVISION YEAR NUMBER NUMBER River Bend Station - Unit 1 05000-458 2009 001 00 3

OF 4

To determine whether the filled condition of the test tank had any adverse effects on the operability of the SLC system, an analysis was performed to identify the likely failure effects. It was found that the tank could possibly fall in two different directions due to failure of the supports. In the worst case scenario, cables attached to a junction box mounted in the immediate vicinity of the test tank outlet valve could be damaged due to impact. The limit switches on the test tank outlet valve are necessary to satisfy an "open" interlock with Division 1 and 2 outlet valves on the main storage tank (i.e.:, the storage tank outlet valves will not open unless the test tank outlet valve is fully closed). Breakage of the cable from the "CLOSED" limit switch would block any opening signal to the storage tank outlet valves. Since it could be postulated that both outlet valves would be affected, this scenario would render the SLC system incapable of performing its function.

When the status of the SLC test tank was originally questioned in October 2008, the tank was drained as a conservative measure since it was not clear what potentially adverse effects were posed by keeping the tank full. It was the investigation of that question that determined the specific details contained in this report.

CORRECTIVE ACTIONS TO PREVENT RECURRENCE An administrative tracking mechanism has been put into place for the affected surveillance test regarding the draining of the test tank. Guidance for draining the SLC test tank was incorporated into the system operating procedure.

Further procedure revisions are being developed. This action is being tracked in the station's corrective action program.

PREVIOUS OCCURRENCE EVALUATION A review of events reported by River Bend Station since January 2004 found no similar conditions.

SAFETY SIGNIFICANCE

The past condition of storing water in the SLC Test Tank had no actual impact on nuclear safety as there were no seismic events or other events requiring SLC system response. However, during the time period March 14, 2003, through October 28, 2008, the postulated test tank failure could have rendered the SLC system unable to respond following a postulated LOCAin conjunction with a seismic event. The resultant lack of suppression pool pH control could have resulted in aerosol particulate iodine (cesium iodide) deposited in the suppression pool to re-evolve and become airborne as elemental iodine. Prior to the implementation of the Alternative Source Term amendment, suppression pool pH control was not a design function of the system.

RBS has not performed a dose consequences evaluation with re-evolution of iodine. However, an iodine re-evolution study performed at a plant of similar design has concluded that the impact onU.S. NUCLEAR REGULATORY COMMISSION (9-2007)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKET
6. LER NUMBER
3. PAGE YEAR SEQUENTIAL I REVISION YA NUMBER NUMBER River Bend Station - Unit 1 05000-458 2009 001 00 4

OF 4

doses due to re-evolution is negligible. Thus, while RBS has not performed a plant specific dose consequences evaluation with 'respect to iodine re-evolution, it is reasonable to conclude that the impact on calculated dose from iodine re-evolution would be minor. Correspondingly, it is reasonable to conclude that given the margin between the RBS Alternate Source Term calculated doses and 1 OCFR50.67 limits, the minor change in dose from iodine re-evolution would not result in exceeding 10CFR50.67 limits.

(NOTE: Energy Industry Component Identification codes and system identification codes are annotated as (**XX**).)