ML083120510

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Prairie Island Nuclear Generating Plant, NRC Special Inspection Report 05000282/2008008; 05000306/2008008, Preliminary White Finding
ML083120510
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 11/07/2008
From: Pederson C
Division Reactor Projects III
To: Wadley M
Northern States Power Co
References
EA-08-272 IR-08-008
Download: ML083120510 (34)


See also: IR 05000282/2008008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

November 7, 2008

EA-08-272

Mr. Michael D. Wadley

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company-Minnesota

1717 Wakonade Drive East

Welch, MN 55089

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT -

NRC SPECIAL INSPECTION REPORT 05000282/2008008; 05000306/2008008,

PRELIMINARY WHITE FINDING

Dear Mr. Wadley:

On October 6, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed a Special

Inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The Special

Inspection Team evaluated the facts and circumstances surrounding the Unit 1 reactor trip and

the failure of 11 turbine-driven auxiliary feedwater pump (TDAFWP) to run, which occurred on

July 31, 2008. Additionally, the team evaluated the facts and circumstances associated with the

declaration of a Notice of Unusual Event (NOUE) on August 3, 2008, due to indications of

excessive levels of hydrazine in the condenser pit area of Unit 1. The enclosed Inspection

Report documents the results of the inspection, which were discussed on October 6, 2008, with

you and other members of your staff.

Based on the deterministic criteria provided in Management Directive (MD) 8.3, ANRC Incident

Investigation Program,@ the incident met MD 8.3 Criterion h, AInvolved questions or concerns

pertaining to licensee operational performance.@ The special inspection evaluated the causes of

the reactor trip; the failure of the TDAFWP to run when demanded; and the NOUE; as well as

the actions taken by your staff in response to the reactor trip and recovery.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The enclosed inspection report discusses a finding for Unit 1 that appears to have low to

moderate safety significance (White). As documented in Section 4OA3.3 of this report, due to a

configuration control issue, which isolated the discharge pressure switch associated with

11 TDAFWP, the pump was rendered inoperable for a time period that significantly exceeded

the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> time limit allowed by Technical Specifications.

M. Wadley -2-

This finding was assessed based on the best available information, including influential

assumptions, using the applicable Significance Determination Process (SDP). The preliminary

safety significance of the finding was determined assuming 11 TDAFWP was inoperable for

138 days, during an operational Mode that required two operable trains of auxiliary feedwater.

This finding was not an immediate safety concern because the 11 TDAFWP was not required to

mitigate the trip and, upon identification of the issue, your staff took prompt corrective actions to

restore the mispositioned valve to its normal (open) position; performed valve lineups to verify

correct equipment configurations for the remaining auxiliary feedwater pumps; and performed

appropriate surveillance testing on the 11 TDAFWP to verify the components operable status.

The finding is also an apparent violation of NRC requirements and is being considered for

escalated enforcement action in accordance with the NRC Enforcement Policy. The current

Enforcement Policy is included on the NRCs web site at http://www.nrc.gov/reading-

rm/adams.html.

In accordance with Inspection Manual Chapter (IMC) 0609, we intend to complete our

evaluation using the best available information and issue our final determination of safety

significance within 90 days of this letter. The SDP encourages an open dialog between the

staff and the licensee; however, the dialogue should not impact the timeliness of the staffs

final determination.

Before the NRC makes its enforcement decision, we are providing you an opportunity to either:

1) present to the NRC your perspectives on the facts and assumptions used by the NRC to

arrive at the finding and its significance at a Regulatory Conference, or (2) submit your position

on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held

within 30 days of the receipt of this letter and we encourage you to submit supporting

documentation at least one week prior to the conference in an effort to make the conference

more efficient and effective. If a conference is held, it will be open for public observation. The

NRC will also issue a press release to announce the conference. If you decide to submit only a

written response, such submittal should be sent to the NRC within 30 days of the receipt of this

letter. If you decline to request a Regulatory Conference or to submit a written response, you

relinquish your right to appeal the final SDP determination; in that, by not doing either you fail to

meet the appeal requirements stated in the Prerequisite and Limitation Sections of Attachment 2

of IMC 0609.

Please contact Richard Skokowski at 630-829-9620 within 10 days of the date of this letter to

notify the NRC of your intended response. If we have not heard from you within ten days, we

will continue with our significance determination and enforcement decision. You will be advised

by a separate correspondence of the results of our deliberations on this matter.

M. Wadley -3-

Since the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for this inspection finding at this time. Please be advised that the number and

characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA by Gary L. Shear, Acting for/

Cynthia D. Pederson, Director

Division of Reactor Projects

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

Enclosure: Inspection Report 05000282/2008008; 05000306/2008008

w/Attachments:

1. Supplemental Information

2. Timeline of Events Unit 1

3. Special Inspection Charter

DISTRIBUTION

See next page

Letter to M. Wadley from C. Pederson dated November 7, 2008

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT -

NRC SPECIAL INSPECTION REPORT 05000282/2008008; 05000306/2008008,

PRELIMINARY WHITE FINDING

cc w/encl: D. Koehl, Chief Nuclear Officer

Regulatory Affairs Manager

P. Glass, Assistant General Counsel

Nuclear Asset Manager

J. Stine, State Liaison Officer, Minnesota Department of Health

Tribal Council, Prairie Island Indian Community

Administrator, Goodhue County Courthouse

Commissioner, Minnesota Department of Commerce

Manager, Environmental Protection Division

Office of the Attorney General of Minnesota

Emergency Preparedness Coordinator, Dakota

County Law Enforcement Center

M. Wadley -3-

Since the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for this inspection finding at this time. Please be advised that the number and

characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA by Gary L. Shear, Acting for/

Cynthia D. Pederson, Director

Division of Reactor Projects

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

Enclosure: Inspection Report 05000282/2008008; 05000306/2008008

w/Attachments:

1. Supplemental Information

2. Timeline of Events Unit 1

3. Special Inspection Charter

DISTRIBUTION:

See next page

DOCUMENT NAME: G:\PRAI\Prairie Island 2008 008.doc

G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" =

Copy with attach/encl "N" = No copy

OFFICE RIII RIII RIII

NAME RSkokowski:cms GShear for PLougheed for

CPederson KOBrien

DATE 11/06/08 11/07/08 11/06/08

OFFICIAL RECORD COPY

Letter to M. Wadley from C. Pederson dated November 7, 2008

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT -

NRC SPECIAL INSPECTION REPORT 05000282/2008008; 05000306/2008008,

PRELIMINARY WHITE FINDING

DISTRIBUTION:

Tamara Bloomer

RidsNrrPMPrairieIsland

RidsNrrDorlLpl3-1

RidsNrrDirsIrib Resource

Cynthia Carpenter

Nick Hilton

Greg Bowman

Mary Ann Ashley

Mark Satorius

Kenneth Obrien

Jared Heck

Carole Ariano

Linda Linn

Cynthia Pederson

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports@nrc.gov

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

Report No: 05000282/2008008 and 05000306/2008008

Licensee: Northern States Power - Minnesota

Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2

Location: Welch, Minnesota

Dates: August 4 through October 6, 2008

Inspectors: S Thomas, SRI, Monticello (Lead)

K. Stoedter, SRI, Prairie Island

D. Betancourt, Reactor Engineer

Approved by: R. Skokowski, Chief

DRP Branch 3

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS..................................................................................................................... 2

4. OTHER ACTIVITIES (OA) ............................................................................................ 3

4OA3 Special Inspection (93812)................................................................................. 3

4OA6 Management Meetings .................................................................................... 13

SUPPLEMENTAL INFORMATION ............................................................................................. 1

KEY POINTS OF CONTACT .................................................................................................. 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ....................................................... 1

LIST OF DOCUMENTS REVIEWED....................................................................................... 2

LIST OF ACRONYMS USED .................................................................................................. 6

Enclosure

SUMMARY OF FINDINGS

IR 05000282/2008008; 05000306/2008008; August 4, 2008, to October 6, 2008, Prairie Island

Nuclear Plant, Units 1 and 2; Other Activities; SIT regarding the failure of 11 TDAFWP to run

following the reactor trip on July 31, 2008, and declaration of a NOUE on August 3, 2008.

This report covers a 64-day period of special inspection by one NRC Region III inspector and

two resident inspectors. One apparent violation, with potential safety significance greater than

Green, was identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination

Process" (SDP). Findings for which the SDP does not apply may be "Green" or be assigned a

severity level after NRC management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG 1649, "Reactor

Oversight Process," Revision 4, dated December 2006.

A. Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

  • AV: A self-revealing apparent violation of Technical Specifications was associated with

the licensees failure to adequately control the position of a valve that could isolate the

11 TDAFWPs discharge pressure switch. Because of the valve being closed, the

11 TDAFWP failed to run as required, subsequent to a reactor trip. The manifold

isolation valve was determined to have been shut for 138 days, rendering the

11 TDAFWP inoperable for a time period that significantly exceeded the Technical

Specification allowed outage time (72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />) for the pump. This issue has been

preliminarily determined to be of low to moderate safety significance (White) for Unit 1.

This issue was entered into the licensees corrective action program (CAP 01146005).

The licensee took prompt corrective actions to restore the mispositioned valve to its

normal (open) position; perform valve lineups to verify correct equipment configurations

for the remaining auxiliary feedwater pumps; and perform appropriate surveillance

testing on the 11 TDAFWP to verify the components operable status.

This finding was determined to be more than minor in accordance with IMC 0612,

Power Reactor Inspection Reports, Appendix B, Issue Screening, because it

impacted the configuration control attribute of the Mitigating Systems Cornerstone

objective to ensure the availability, reliability, and capability of the systems that respond

to initiating events to prevent undesirable consequences. The cause of this finding was

related to the cross-cutting element of human performance for resources (H.2.(c)).

(Section 4OA3.3)

B. Licensee-Identified Violations

No findings of significance were identified.

1 Enclosure

REPORT DETAILS

Summary of Plant Event

On July 31, 2008, at 8:17 a.m., Prairie Island Unit 1 tripped due to a spurious overtemperature

delta temperature (OTT) signal on the reactor protection system red channel concurrent with

planned testing on the reactor protection system yellow channel. After the reactor tripped, the

11 turbine-driven auxiliary feedwater pump (TDAFWP) started as required, then stopped

approximately 40 seconds later due to a low discharge pressure trip. The licensee determined

that the cause of the TDAFWP trip was an incorrect valve lineup associated with the auxiliary

feedwater pumps discharge pressure instrumentation. Prior to restarting the Unit, the licensee

replaced the faulty reactor protection system card that caused the spurious OTT signal,

corrected the valve lineup issue associated with the 11 TDAFWP discharge pressure

instrumentation, and successfully tested both systems.

On August 2, 2008, at 3:42 p.m., the licensee began to startup Unit 1 in accordance with station

procedures. Early in the morning on August 3, 2008, while holding at approximately 30 percent

power to allow secondary chemistry to stabilize, a technician reported an abnormal odor

adjacent to the Unit 1 condenser pit. Air samples taken in the vicinity of the Unit 1 condenser pit

indicated positive for hydrazine. The licensee took positive actions to control personnel access

to the affected area and, at 3:52 a.m., declared a Notification of Unusual Event (NOUE) for the

release of toxic gases deemed detrimental to the normal operation of the plant, in accordance

with their Emergency Plan. The licensee utilized extra ventilation in the affected areas to

reduce the hydrazine concentration. The licensee continued to take air samples over the next

several hours and, based on acceptable sample results, exited the Unusual Event at 10:20 p.m.

on August 3, 2008.

Based on the probabilistic risk and deterministic criteria specified in Management Directive

(MD) 8.3, "NRC Incident Investigation Program," and Inspection Procedure (IP) 71153,

"Event Followup," and due to the equipment performance problems that occurred, a Special

Inspection was initiated in accordance with IP 93812, "Special Inspection."

The inspection focus areas included the following charter items:

  • Identify the time-line for the event. Include plant conditions, system line ups, and operator

actions.

  • Review the licensees post-trip review to determine the cause of the reactor trip.

Independently review plant data and records to confirm the adequacy of the licensees

assessment, and corrective actions.

  • Review the circumstances surrounding the failure of the TDAFWP, including the most

likely cause of the pump failure; the length of time the pump may have been in an

unrecognized failed condition; and any potential for operators to recover the failed pump.

  • Determine if the licensee is performing a root cause for the reactor trip. As available,

evaluate the scope, schedule, staffing and results of the licensees root cause

investigation.

2 Enclosure

  • Determine if the licensee is performing a root cause evaluation for the TDAFWP failure.

As available, evaluate the scope, schedule, staffing and results of the licensees root

cause investigation.

  • Review procedures for the TDAFWP, including operational line-up procedures and testing

procedures, to assess any procedural or testing inadequacies that may have contributed

to the failure of the pump.

  • Determine if the licensee performed an extent-of-condition evaluation to assess if the

contributing causes to the failure of the TDAFWP have the potential to affect other

safety-related equipment.

  • Review for adequacy the licensees immediate corrective actions and planned long-term

corrective actions to prevent recurrence of both the reactor trip and the failure of the

TDAFWP.

Additionally, the Special Inspection team (SIT) was tasked with reviewing the circumstances

surrounding the August 3, 2008, declaration of the NOUE associated with release of toxic gases

(hydrazine) deemed detrimental to normal operation of the plant.

4. OTHER ACTIVITIES (OA)

4OA3 Special Inspection (93812)

.1 Establish the Sequence of Events Related to the Event, Including Plant Conditions,

System Lineups and Operator Actions

a. Inspection Scope

The inspectors reviewed operator logs, plant parameter recordings and computer

trending information, and conducted interviews with licensee personnel in developing the

sequence of events. In addition, the inspectors sequence of events was reviewed

against the licensee-generated sequence of events to ensure completeness and

accuracy.

b. Findings and Observations

No findings of significance were identified. The inspectors generated sequence of

events is included with this report as Attachment 1 and an event narrative summary

was presented in this reports Summary of Plant Event, discussed above.

.2 Reactor Trip Report

a. Inspection Scope

The inspectors reviewed the licensees post-trip report to determine if the licensee

adequately evaluated and corrected the cause of the reactor trip. Specific information

reviewed by the inspectors included: reactor trip report; operators logs; emergency

response computer system alarm post-trip data; troubleshooting log for the failed OTT

3 Enclosure

reactor protection channel; troubleshooting log for the 11 TDAFWP trip; the reactor trip

and trip recovery procedures; and recorder traces for various reactor plant parameters.

b. Findings and Observations

No findings of significance were identified.

.3 Trip of the 11 Turbine-Driven Auxiliary Feedwater Pump

a. Inspection Scope

The inspectors reviewed the circumstances surrounding the failure of the 11 TDAFWP to

run subsequent to the reactor trip, after receiving a valid start signal. The specific focus

of this inspection was to determine the most likely cause of the pump failure; the length

of time prior to the trip that the pump was inoperable; and the probability of success for

the recovery of the failed pump.

b. Findings and Observations

Introduction

A self-revealing apparent violation of Technical Specifications (TS) 3.7.5.B was identified

due to the licensees failure to control the position of the 11 TDAFWP discharge

pressure switch manifold block valve. The failure to control the position of this valve

resulted in the 11 TDAFWP being inoperable for 138 days.

Description

A timeline of the relevant information subsequent to the July 31, 2008, Unit 1 reactor trip

is as follows:

  • 8:17 a.m.; the Unit 1 reactor tripped from full power. Shortly thereafter, both of

the Units auxiliary feedwater pumps received valid start signals due to expected

low post-trip water levels in the steam generators;

  • 8:21 a.m.; the 11 TDAFWP Low Suction/Discharge Pressure Trip annunciator

was received in the control room;

steam generator levels were maintained using the main feedwater system;

  • 9:15 a.m.; the licensee determined that the 11 TDAFWP had started upon receipt

of the valid start signal, but tripped approximately 42 seconds later;

  • 1:23 p.m.; the licensee discovered an unlabeled manifold block valve associated

with the 11 TDAFWPs discharge pressure switch to be shut.

The inspectors reviewed licensee testing procedures and work orders that would have

manipulated the manifold block valve. In addition to the work documents that directly

manipulated the block valve, the inspectors also reviewed several other procedures,

which manipulated similar manifold valves that are located in close proximity to the

mispositioned block valve. The inspectors determined that the last documented activity

that repositioned the block valve was the performance of SP1234, 11 Aux Feedwater

4 Enclosure

Pump Suction and Discharge Pressure Switches Calibration, completed on

February 23, 2008.

Analysis

The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1,

Significance Determination of Reactor Inspection Findings for At-Power Situations.

Since the performance deficiency affected the ability of the 11 TDAFWP to start and run

upon the receipt of a valid actuation signal, the inspectors used the Phase 1 SDP

worksheet for the Mitigating System Cornerstone to determine the significance of the

finding. The finding was determined to require a Phase 2 SDP review because the

finding resulted in the loss of function of a single train for greater than its TS allowed

72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> outage time limit.

It is not known when the manifold isolation valve was closed, rendering the pump

unavailable for automatic actuation. Based on the inspection results, the valve was last

manipulated on February 23, 2008, as part of the Unit 1 refueling outage activities.

Therefore, it was assumed that the pump was unavailable since Unit 1 entered Mode 3

on March 15, 2008, until the problem was discovered on July 31, 2008.

Recovery of the 11 TDAFWP was determined to be feasible. The pump would start and

run if the control selector switch in the control room was taken to Manual. The

licensees alarm response Procedure C47010, 11 TDAFWP Lo Suct or Disch Press

Trip, instructed operators to restart the pump using Abnormal Operating Procedure

1C28.1AOP4, Restarting Unit 1 AFWP After Low Suction/Discharge Pressure Trip.

This procedure directed operators to put the selector switch in Manual. The inspectors

estimated that the time required to perform the actions in the procedure was

approximately 15 minutes. Since the time to core damage, assuming a loss of all

feedwater was much longer than 15 minutes; adequate time for recovery of the pump

was available.

The Phase 2 pre-solved worksheets modeled Unit 2 components only. The significance

of the Unit 2 TDAFWP pump being unavailable for greater than 30 days was Red. This

result was overly conservative because it did not include credit for recovering the pump.

The result was also conservative because the Phase 2 pre-solved worksheets assumed

the exposure period was one year and the actual exposure period was 138 days.

Therefore, a Phase 3 SDP analysis was completed.

The SPAR-H model for Prairie Island Unit 1, Revision 3.45 was used for the internal

events Phase 3 SDP analysis. For the internal events analysis the basic event

AFW-TDP-FS-TDP11, the 11 TDAFWP Fails to Start, was set to True and the basic

event AFW-XHE-XL-TDPFS, Operator Fails to Recover AFW Pump Fail to Start, was set

to a failure probability of 2.2E-2 based on a SPAR-H analysis for operators failing to

recover the pump. The SPAR-H analysis assumed that all performance-shaping factors

for both diagnosis and action were nominal with the exception of the Stress performance

shaping factors. The scenario of a transient with the loss of all feedwater was

considered to be high stress. Using these assumptions and the 138-day exposure

period, the change in core damage frequency (CDF) was calculated to be less than

1.0E-6/yr.

5 Enclosure

For the Phase 3 SDP analysis, the Senior Reactor Analyst (SRA) also considered

the risk contributions from internal flooding, external events, and large early release

frequency. Only internal fire scenarios were determined to contribute to the risk

significance of this finding. The 11 TDAFWP was the only credited means of decay heat

removal in the licensees Appendix R safe shutdown analysis for 10 different fire areas.

The licensees Individual Plant Examination for External Events (IPEEE) results and the

NRCs Risk Assessment of Operational Events (RASP) Handbook for External Events

were used as the best available information to estimate the fire risk contribution

associated with the unavailability of the 11 TDAFWP.

For fire scenarios that do not involve control room evacuation, the same recovery human

error probability (HEP) used in the internal events analysis was applied, since operators

have appropriate indications and annunciators to implement the abnormal operating

procedure in the control room. However, recovery of the pump would be different and

more complex for fire scenarios involving control room evacuation. Licensee

Procedure F5, Control Room Evacuation (Fire) directed operators to trip the reactor

and the main feedwater pumps prior to evacuating the control room and proceeding to

the hot shutdown panels. The procedure also directed operators to open breakers for

the motor-driven AFW pumps, leaving only the 11 TDAFWP available for decay heat

removal. Since the 11 TDAFWP would have tripped due to the mispositioned discharge

pressure switch manifold isolation valve, no auxiliary feedwater pumps would be

available without further operator action.

Procedure F5 provided direction to the operator to locally operate the 11 TDAFWP. If it

was not running, the operator was directed to take action to bleed off the air supply to

the turbine steam supply valve. This action failed the valve open and allowed the turbine

to roll and start the pump if the pump had previously tripped from the low discharge

pressure trip signal.

The recovery actions were directed to be performed by the Unit 1 Shift Supervisor who

would be stationed at the Hot Shutdown Panels in the Auxilairy Feedwater Pump

Rooms. This individual was first tasked with making the decision to evacuate the control

room; assure appropriate notifications are made; and determine if self-contained

breathing apparatus use is required. The Unit 1 Shift Supervisor was responsible for

operating both the Unit 1 and Unit 2 TDAFWPs and directing operators in the plant

performing other manual actions. Due to the heavy workload of the operator, complexity

of the procedure, high stress of the postulated scenario, and limited experience with this

procedure, the SRA determined that the failure probability for manual plant shutdown

outside the control room would be increased because of this finding.

To obtain a quantitative estimate of the delta CDF, the SRA reviewed the top 100 cut

sets submitted with the licensees IPEEE analysis. The nominal failure probability for

manual shutdown outside the control room (SHTDWN-OUT) was 6.4E-2. The SRA used

SPAR-H to estimate a HEP for shutdown outside the control room given the

performance deficiency. Assuming that the actions involve high stress, high complexity,

low experience/training, and poor work processes (the Shift Supervisor was responsible

for recovering the pump), the SRA calculated an action HEP of 0.13. This estimate was

approximately double the nominal failure probability. Using this value as the failure

probability for manual shutdown outside the control room for evacuation scenarios and a

pump non-recovery probability of 2.2E-2 for other fire scenarios, the top 100 cut-sets

6 Enclosure

were recalculated for an exposure period of 138 days. The delta CDF was estimated to

be approximately 1.6E-6/yr.

The RASP external events handbook for internal fires was also used to evaluate the fire

risk as a sensitivity analysis because of the uncertainty in the frequency of fires leading

to control room evacuation scenarios. Since the dominant fire risk sequences from the

licensees IPEEE were fires involving control room evacuation; only those scenarios

were addressed. These scenarios involved fires in the control room and relay room.

Using the RASP handbook data on initiating event frequencies and non-suppression

probabilities, the SRA confirmed that the change in core damage frequency from internal

fires was above the 1.0E-6 threshold for a low to moderate safety significance (White)

finding.

The result of the Phase 3 SDP analysis was a delta CDF of 1.6E-6/yr, considering both

contributions from internal events and internal fire scenarios. The licensee performed a

risk evaluation of the internal events contribution and the result was similar to the NRCs.

The licensee had not yet completed an evaluation of the fire risk contribution.

The inspectors determined that the performance deficiency affected the crosscutting

area of Human Performance, having resources components, and involving aspects

associated with ensuring complete, accurate and up-to-date design documentation,

procedures, work packages, and correct labeling of components. [H.2.(c)]

Enforcement

Technical Specification 3.7.5 states, in part, that two auxiliary feedwater trains be

operable during plant operation in Modes 1, 2, and 3. Additionally, TS 3.7.5.B states, in

part, if one auxiliary feedwater train is inoperable in Modes 1, 2, and 3, the affected train

be restored to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or place the plant in Mode 3 within

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to this requirement, as a result of the

11 TDAFWP pumps discharge-low-pressure pressure switch being isolated for

approximately 138 days, the pump was inoperable for a time period which significantly

exceeded the time allowed by TSs. For Unit 1, this is an apparent violation of

TS 3.7.5 pending the completion of the final significance determination.

(AV 05000282/2008008-01)

.4 Evaluation of the Root Cause Report Associated with the Reactor Trip

a. Inspection Scope

The inspectors monitored the licensees root cause team activities and reviewed the final

Root Cause Evaluation Report, U1 OTT RX Trip, associated with CAP 1145953.

b. Findings and Observations

The inspectors noted that the licensees root cause team used industry accepted root

cause evaluation tools (i.e., Toubleshooting/Failure Analysis, Barrier Analysis, Event and

Causal Factor Charting, Why Staircase, Fault Tree Analysis). The inspectors also noted

that the licensees root cause team was comprised of multi-disciplined individuals from

systems engineering, electrical maintenance, and operations.

7 Enclosure

The licensee determined that the equipment root cause was that the 1TC-405L FQ

proportional controller failed high due to a failure of a solid-state device within the

controller. The licensee also concluded that the organizational root cause was due to

lack of previous Foxboro H-Line component failures that had adverse consequences.

Prairie Island did not adequately prioritize or apply the human resources necessary to

develop and implement a preventive maintenance strategy for the components within the

reactor protection and control system. The SIT determined that the licensees efforts to

identify the root causes associated with this event were adequate.

The SIT reviewed the licensees immediate corrective actions and found them to be

acceptable. Additionally, the Team reviewed the corrective actions to prevent

recurrence and additional long-term corrective actions and determined, if the licensee

fully implemented the corrective actions in a timely manner, the corrective actions would

appropriately address the root causes for this event.

This inspection also represented the completion of one maintenance effectiveness

(71111.12) inspection sample.

No findings of significance were identified.

.5 Evaluation of the Root Cause Report Associated with the Failure of the 11

Turbine-Driven Auxiliary Feedwater Pump Failure-to-Run Upon the Receipt of a

Valid Demand Signal

a. Inspection Scope

The inspectors monitored the licensees root cause team activities and reviewed the final

Root Cause Evaluation report, 11 Turbine-Driven Auxiliary Feedwater Pump Discharge

Pressure Switch Manifold Isolation Mispositioning, associated with CAP 1146005.

b. Findings and Observations

The inspectors noted that the licensees root cause team used industry accepted root

cause evaluation tools (i.e., Why Staircase, Barrier Failure Analysis, Failure Mode

Analysis, Event and Causal Factor Charting). The inspectors also noted that the

licensees root cause team was comprised of multi-disciplined individuals from

engineering, maintenance, and operations.

The licensee determined that the root cause for this event was inadequate configuration

controls for components that have the potential to adversely impact the design function

of safety related structures, systems and components. The SIT determined that the

licensees efforts to identify the root cause associated with this event were adequate.

The SIT reviewed the licensees immediate corrective actions and found them to be

acceptable. Additionally, the Team reviewed the corrective actions to prevent

recurrence and additional long-term corrective actions and determined, if the licensee

fully implemented the corrective actions in a timely manner, the corrective actions would

appropriately address the root causes for this event.

No findings of significance were identified.

8 Enclosure

.6 Review Procedures Associated with the Turbine-Driven Auxiliary Feedwater Pump to

Assess Procedural or Testing Inadequacies Which May have Contributed to the Failure

of the Pump

a. Inspection Scope

The inspectors reviewed surveillance procedures, planned maintenance activities,

operational line-up procedures, administrative procedures, and corrective action

documents to identify issues that may have contributed to the configuration control

issue, which resulted in the 11 TDAFWP failure to run upon receipt of a valid start signal.

b. Findings and Observations

The inspectors determined that the last activity that required the manipulation of the

manifold isolation valve for the 11 TDAFWP discharge pressure switch was SP 1234A,

11 Auxiliary Feedwater Pump Suction and Pressure Switches Calibration, which was

completed on February 23, 2008. Although several other surveillances required the

operation of components in the general vicinity of the manifold isolation valve, the

inspectors did not identify any additional activities that required manipulation of the valve

during February 23, 2008, to July 31, 2008.

The inspectors noted the following licensee weaknesses that may have contributed to

the configuration control issue associated with the mis-positioned manifold isolation

valve:

were not labeled with a means of permanent identification.

  • Instrument and control technicians identify manifolds by tracing sensing lines

back from the applicable instrument to its associated manifold. This identification

method and instructions describing how to operate each type of manifold,

including how to identify the function of valves on each manifold, was covered as

part of instrument and control technician training.

  • A double standard existed at Prairie Island regarding how a component must be

identified prior to its operation. Operators were required to positively identify a

component, by means of an approved label, prior to operating a component.

Instrument and control technicians were not held to the same standard, and

routinely operate unlabeled instrument manifolds and associated valves.

  • The licensee did not positively control minor components that could impact the

performance of safety related equipment. A specific example of this was that,

even though the root valve for the 11 TDAFWP low discharge pressure switch

was locked and positively controlled via licensee processes, the manifold

isolation valve, which can perform the same isolation function and is positioned

between the root valve and the pressure switch, had no positive means to ensure

that it remained open.

The inspectors reviewed the licensees immediate and long term corrective actions

(CAP 1146005) associated with addressing the issues described above and determined

9 Enclosure

that the scope and extent of condition of the corrective actions were appropriate to

address these issues.

No findings of significance were identified.

.7 Licensees Actions to Immediately Assess the Extent-of -Condition Associated with the

11 Turbine-Driven Auxiliary Feedwater Pump Configuration Control Issue

a. Inspection Scope

The inspectors reviewed the licensees extent of condition evaluation associated with the

configuration control issue that resulted in the isolation of the 11TDAFWP discharge

pressure switch. The inspectors evaluated the licensees immediate and interim

corrective actions, associated with the licensees extent-of-condition evaluation, as they

specifically pertained to this event.

b. Findings and Observations

The inspectors reviewed documentation associated with the licensees immediate and

interim corrective actions, as they relate specifically to auxiliary feedwater and on how

they relate to similar components associated with other safety-related systems at Prairie

Island. These corrective actions included:

and Instrument & Controls Departments;

  • Surveillance testing was performed on the 11 TDAFWP to verify pump

operability;

  • Surveillance and post maintenance testing was performed on the 11 TDAFWP

discharge and suction pressure switches to verify switch functionality;

  • The suction and discharge pressure switch manifold isolation valves for all four

auxiliary feedwater pumps were lock-wired in the open position; and

  • The licensee performed a sampling of similar manifold valve positions located in

other safety related systems.

The inspectors determined that the scope of the initial assessment of the extent-of-

condition associated with this event and related corrective actions were adequate.

This inspection also represented the completion of one post maintenance test

(71111.19) inspection sample.

No findings of significance were identified.

10 Enclosure

.8 Licensees Immediate Corrective Actions and Planned Long Term Corrective Actions to

Prevent Recurrence for Both the Reactor Trip and the Failure of the Turbine-Driven

Auxiliary Feedwater Pump

a. Inspection Scope

The inspectors reviewed the adequacy of the licensees immediate, interim corrective

actions, corrective actions to prevent recurrence, and long term corrective actions

associated with the reactor trip and the failure of the 11 TDAFWP to run.

b. Findings and Observations

The inspectors determined that the licensees immediate and interim corrective actions

were adequate to address the short-term challenges presented by the reactor trip and

configuration control issue associated the 11 TDAFWP.

The SIT evaluated both events, reviewed their associated root cause evaluation, and

evaluated the licensees proposed corrective actions to prevent recurrence. For the

reactor trip event, the corrective actions to prevent recurrence included:

  • Replace or refurbish all flux tilt penalty (FQ)proportional controllers;
  • Develop and implement a preventive maintenance strategy for the Foxboro

H-Line components in the reactor protection and control system; and

  • Ensure a life cycle management plan for the reactor protection and control

systems was implemented to ensure timely preventive replacement of the

Foxboro H-Line components.

For the failure of the TDAFWP to run, the most significant corrective action to prevent

recurrence was to utilize a multi-phase process to conduct a comprehensive review of

the licensees configuration control standards. As part of this effort, the licensee will:

  • Develop a process to review safety related systems to determine if there are any

small components that may adversely affect the function of a safety-related

system structure or component (SSC);

  • Perform a trial of the methodology on a significant safety related system; and
  • Complete this process to systematically identify all components that may

adversely affect safety related SSCs for each safety related system.

  • Implement necessary changes per the process that was developed.

The inspectors noted that the corrective actions to prevent recurrence for each of these

events presented a significant challenge to the licensee to implement. The SIT

determined that if the licensee fully implemented these corrective actions in a timely

manner, the corrective actions would appropriately address the causes of each event.

No findings of significance were identified.

11 Enclosure

.9 Circumstances Surrounding the Notice of Unusual Event Declared for the Release of

Toxic Gases (Hydrazine) Deemed Detrimental to Normal Operation of the Plant and

Evaluation of the Root Cause Event Report Associated with this Event

a. Inspection Scope

The inspectors used direct observation of the event and subsequent licensee activities in

conjunction with reviews of logs and the sequence of events, and personnel interviews

to assess the circumstances associated with the event. Additionally, the inspectors

monitored the licensees root cause team activities and reviewed the final Root Cause

Evaluation report, Hydrazine NUE, associated with CAP 1146374.

b. Findings and Observations

Members of the resident staff observed the licensees response to the event from inside

the control room. Overall, the NOUE classification was declared in a timely manner and

was appropriately classified in accordance with the stations emergency plan.

The inspectors noted that the licensees root cause team used industry accepted root

cause evaluation tools (i.e., Change Analysis; Event and Causal Factor Charting; Why

Staircase). The inspectors also noted that the licensees root cause team was

comprised of multi-disciplined individuals with backgrounds in health physics, chemistry,

radiation protection, and performance assessment.

The inspectors confirmed that the addition of hydrazine to the feedwater system

following the reactor trip was performed in accordance with Electirc Power Research

Institute guidance and approved station procedures. However, the inspectors

discovered that these procedures were vague regarding what to expect when adding

hydrazine during times when the feedwater system was in a non-typical configuration.

The inspectors noted that even though existing chemistry procedures specifically

identified that the existing main condenser status and feedwater lineup was not typical,

no additional guidance was provided to the chemist on how the secondary plant would

behave differently based on that non-typical configuration. The objective of the

hydrazine addition to the feedwater system was to lower oxygen concentration by

maintaining an 8 to 1 ration of hydrazine to oxygen, but consideration was not made as

to how the non-typical configuration would affect the reaction mechanism; in this case,

the generation of airborne hydrazine/ammonia.

The inspectors noted that the timely identification of actual levels of hydrazine/ammonia

present in the lower levels of the Unit 1 turbine building was hampered by the chemists

lack of understanding associated with the air sampling equipment limitations. The

equipment used to sample for hydrazine was adversely impacted by the presence of

ammonia. The licensee concluded that if test equipment without a cross-sensitivity to

ammonia interference had been used; the airborne chemical levels would have been

appropriately characterized, eliminating the need for an evacuation of the turbine

building and declaration of a NOUE.

The SIT reviewed the licensees immediate corrective actions and found them to be

acceptable. Additionally, the Team reviewed the corrective actions to prevent

recurrence and additional long-term corrective actions and determined, if the licensee

12 Enclosure

fully implemented the corrective actions in a timely manner, the corrective actions would

appropriately address the root causes for this event.

No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On October 6, 2008, the inspectors presented the inspection results to Mr. M. Wadley

and members of his staff, who acknowledged the findings. The licensee acknowledged

the information presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary

information was identified.

.2 Interim Exit Meetings

No interim exits were conducted.

ATTACHMENTS: 1. SUPPLEMENTAL INFORMATION

2. TIMELINE OF EVENTS UNIT 1

3. SPECIAL INSPECTION TEAM CHARTER

13 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Wadley, Site Vice President

S. Northard, Plant Manager

C. Mundt, General Supervisor I&C Maintenance

S. Nelson, Fleet RP/Chemistry Manager

R. Hite, RP/Chemistry Manager

M. Kent, General Supervisor, RP

L. Clewett, Operations Manager

M. Schmidt, Maintenance Manager

S. Myers, Design Engineering Manager

S. Lappegaard, On-Line Work Manager

J. Callahan, Emergency Preparedness Manager

J. Muth, Nuclear Oversight Manager

E. Weinkam, Director, Nuclear Licensing

J. Anderson, Regulatory Affairs Manager

M. Davis, Regulatory Compliance Analyst

Nuclear Regulatory Commission

R. Skokowski, Chief, Branch 3

S. Thomas, Senior Resident Inspector [Monticello]

K. Stoedter, Senior Resident Inspector [Prairie Island]

P. Zurawski, Resident Inspector [Prairie Island]

D. Betantcourt, Reactor Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000282/2008008-01 AV 11 TDAFWP Inoperable for a Time Period Which

Significantly Exceeded Time Allowed by TS

Closed

None

Discussed

None.

1 Attachment 1

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

WORK ORDERS

Number Description or Title Date or Revision

00365604 Red Channel OTDT Failure Investigation January 31, 2008

55698-02 EC Power Ascension Test 8

00365655 Investigation of 11 TDAFW Pump Trip

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

Number Description or Title Date or Revision

01145953 Red Channel Setpoint Failed Low Causing Reactor

Trip

00866960 Top Ten Equipment List Addition - Foxboro H-Line

01146430 Potential Adverse Trend in Manifold Valve Operation

01145943 11 AFW Pump Started and then Tripped

01145964 11 AFWP Trip after Plant Trip

01145996 Temporary Oil Lift Pump had Inadequate Pressure

01146005 Mispositioned Block Valve on 11 TDAFWP

01147573 RPIP 3005 Procedure Compliance Issue

01010095 Benchmark Industry Regarding Labeling of

Instrument Valves

01146889 USAR AFW Time Critical Actions for MFW/MSL

Break Question

01146027 CC Piping Adjacent to HELB Location in Unit 2

Turbine Building

2 Attachment 1

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

Number Description or Title Date or Revision

01146120 U1 Secondary Exceeds EPRI Guidelines for

Oxygen/Hydrazine Condensate Oxygen is 6500ppb

01146304 NUE HU3.1- Potential Plant Equipment Impact from

Hydrazine

01146374 U1 NOUE: High Airborne Hydrazine Levels on 695

EL Turbine Building

01146357 Minor Errors in NRC Notification Forms for Hydrazine

Event

AR 01146974 Prompt Investigation for NUE: Airborne Hydrazine

Excursion

PROCEDURES

Number Description or Title Date or Revision

SP 1003 Analog Protection Functional Test 63

SP 1002A Analog Protection System Calibration 37

C1.6A.1-1 Unit 1 - Integrated Operations Checklist Prior to 10

Heatup, First Floor Turbine Building

C28-7 Auxiliary Feedwater System Unit 2 49

C1.6A.1-2 Unit 2 - Integrated Operations Checklist Prior to 9

Heatup, First Floor Turbine Building

C1.6A.3-1 Unit 1 - Integrated Operations Checklist Prior to 8

Heatup, First Floor Auxiliary Building

1ES-0.1 Reactor Trip Recovery 23

C47010-0205 11 TD AFWP Lo Suct or Disch Press Trip 38

1C28.1 AOP4 Restarting Unit 1 AFWP after Low Suction/Discharge 3

Pressure Trip

SWI O-35 Emergency Operating Procedure Verification, 6

Validation and Maintenance

SP 1102 11 Turbine-Driven AFW Pump Monthly Test 89

SP 1054 Turbine Stop, Governor, Reheat Stop and Reheat 35

Intercept Valve Exercise.

C28-1 Auxiliary Feedwater System - Unit 1 44

3 Attachment 1

PROCEDURES

Number Description or Title Date or Revision

ICPM 1-416 11 Turbine Driven Aux Feed Pump Instruments 3

Calibration

D14.4 AOP1 Chemical Leak or Spill Implementing Procedure 8

SP 1103 11 Turbine-Driven Auxiliary Feedwater Pump Once 45

Every Refueling Outage Shutdown Flow Test

SP 1193 Cycling AFWP and CLG Water MVs 33

SP 1376 AFW Flow Path Verification Test after each Cold 11

Shutdown

SP 1355A Train A AFW Check Valve Testing 11

SP 1234A 11 Aux Feedwater Pump Suction and Discharge 6

Pressure Switches Calibration

SP 1100 12 Motor Driven AFW Pump Monthly Test 75

5AWI 3.10.5 Plant Equipment Labeling 13

RPIP 3002 EPRI Secondary Water Chemistry Guidelines 17

RPIP 3000 Plant Startup Guidelines 12

RPIP 3005 Secondary Chemical Feed System 14

RPIP 3001 Plant Shutdown Guidelines 10

RPIP 3303 Airborne Chemical Determination 4

REFERENCES

Number Description or Title Date or Revision

N/A Top 10 Equipment List; Foxboro H-Line July 15, 2008

N/A Reactor Trip Report for July 31, 2008, Reactor Trip

NF-39222 Flow Diagram - Unit 1 Feedwater System 76

NF-40312-1 Interlock Logic Diagram - Unit 1 Auxiliary Feedwater 76

System

N/A LCO Entry Report for 12 MDFP for the Time Period of

February 1, 2008 to July 31, 2008

N/A Strategic Water Chemistry Plan for PINGP Secondary 8

Water Chemistry

N/A RPCHEM On-the-Job Training and Task Performance 8

Evaluation Review Guide

4 Attachment 1

REFERENCES

Number Description or Title Date or Revision

N/A RPCHEM On-the-Job Training and Task Performance 0

Evaluation Guide

5 Attachment 1

LIST OF ACRONYMS USED

CAP Corrective Action Program

CDF Core Damage Frequency

HEP Human Error Probability

IMC Inspection Manual Chapter

IP Inspection Procedure

IPEEE Individual Plant Examination for External Events

MD Management Directive

NCV Non-Cited Violation

NOUE Notice of Unusual Event

NRC Nuclear Regulatory Commission

OTT Overtemperature Delta Temperature

RASP Risk Assessment of Operational Events

SSC System Structure or Component

SDP Significance Determination Process

SIT Special Inspection Team

SRA Senior Reactor Analyst

TDAFWP Turbine-Driven Auxiliary Feedwater Pump

TS Technical Specification

6 Attachment 1

Historical Timeline of Events for THE Reactor trip, 11 Turbine-Driven Auxiliary feedwater

pump fail to run, and the turbine building hydrazine unusual event

DATE, 2008 TIME DESCRIPTION

February 23 1833 SP 1234A Suction/Discharge Pressure Switch Calibration

March 8 PM 3132-1-11 11 TDAF Pump Minor Periodic Maintenance

C1.6A.1-1 Integrated Operation Checklist Prior to Heat Up Includes

March 11 1500

the Verification of 17700 Bottom Isolation in the Open Position

SP 1301- 11 TDAFW Pump Auto Start and Functional Refueling

March 12 Outage Test. Closed and then Open 17704 Bottom Isolation Valve

(in the vicinity of 17700)

March 26 2226 SP 1102 - 11 TDAFW Pump Monthly Test

May 1 0049 SP 1102 - 11 TDAFW Pump Monthly Test

May 29 0441 SP 1102 - 11 TDAFW Pump Monthly Test

June 26 0423 SP 1102 - 11 TDAFW Pump Monthly Test

SP 1003 Analog Protection Functional Test

July 31

[yellow channel bistables in per SP]

Unit 1 Reactor Trip and 11 TDAFW Pump Auto Start Operators

0817 Enter 1E-0

11 TDAFW Pump Low Discharge Pressure trip (42 sec run) Unit 1

0818

Enters Mode 3

0819 Operators Transition to 1ES-0.1, Reactor Trip Recovery

11 TDAFWP Low Suction/Discharge Pressure Trip Annunciator.

0821

Operator Dispatched

After Trip of AFWP, with Severe Weather, PRA is Yellow for both

0822

Unit 1 and Unit 2

Attachment J of 1E-0, Isolate Unit 1 MSR's, is Complete 0905

0826

Operators Transition to 1C1.3, Unit 1 Shutdown

12 MDAFW Pump Stopped and SG Level Control via Main FW via

0855

Bypass Valves

RP Tour of Aux Building Indicated no Alarms, Leaking Water or

0914

Steam

11 TDAFW Pump Reported to have Auto Started and Run for

0915

Approximately 50 Seconds

1012 Operators Notify NRC of Reactor Trip per 10 CFR 50.72

1055 11 TDAFW Pump Area Quarantined

Completed C28-2 (U1 AFW System Checklist) Found Manifold

1323

Block Valve for 17700 Closed

1 Attachment 2

1400 Commenced Breaking U1 Condenser Vacuum

1500 SP 1102 - 11 TDAFW Pump Monthly Test

SP 1234A Suction/Discharge Pressure Switch Calibration Close

August 1 0619

then Open 17700 Bottom Isolation

FW Chemistry: 9575 ppb Oxygen; 31132 ppb N2H4 ; Condenser

August 2 1200

Chemistry: 7424ppb Oxygen

1543 U1 Reactor Entered Mode 2

1738 U1 Reactor Critical

1815 Reactor Power at Point of Adding Heat

FW Chemistry: 9032 ppb Oxygen; 37410 ppb N2H4 ; Condenser

2000

Chemistry: 7247 ppb Oxygen

2007 Initiated Condenser Vacuum

2133 U1 Entered Mode 1

FW Chemistry: 165 ppb Oxygen; Condenser Chemistry: 163 ppb

2315

Oxygen

August 3 0028 Started Rolling U1 Main Turbine to 600 rpm

0040 Started Rolling U1 Main Turbine from 600 rpm to 1800 rpm

0125 Reactor Power 8%

0208 Reactor Power 15%

Duty Chemistry Reports Positive Hydrazine Air Sample Results

from Unit 1 Condenser Pit and the 695' Level Top of a Stairway

0341

into Condenser Pit (value less than IDLH). Chemist Placed

Barriers to Stop Access.

0352 Declared NOUE (HU3.1)

Announcement Made to Evacuate Unit 1 695 Turbine Building and

0356

Condenser Pit

Air Sample Results from Hydrazine: 695' by Old Admin Building

0403 Door 0.25 ppm; 715' Outside Access Control 1 ppm; 735' Next to

HP Turbine 3 ppm; Control Room < 0.1 ppm

NRC Resident Inspector and Duty Station Manager Notified of

0416 NOUE Declaration HU3.1 due to High Levels of Hydrazine in Unit 1

Turbine Building Sump Area

Chemist Reports no Detectible Hydrazine in Air Sample outside D1

0440

and D2

Chemist Air Samples Show that 715 and 735 Levels of Unit 1

0506

Turbine Building had Stayed Habitable

2 Attachment 2

All Hydrazine Samples on the 735' Unit 1 Turbine Building are

Below the 1.00 ppm Permissible Exposure Limit (PEL); Highest

0647

was 0.75 ppm at the HP Turbine. Normal Access Restored to 735'

Unit 1 Turbine Building.

Access to the 695' Unit 1 Turbine Building Restored with the

0818

Exception of the Southwest Corner Marked with Danger Tape.

Entered Loss of Hydrazine Feed Condition (PINGP 1597 & PINGP

0910

1537; RPIP-3002) for Securing Hydrazine Addition

Hydrazine air samples are as follow: 735' HP Turbine area and

715' by 15 A FWH < 0.1 ppm; 715' by Hoggers 0.5 ppm; 695' on

top of stairs at SW corner of condenser pit 2ppm; 675' north side at

1040 bottom of the stairs 0.75 ppm; 675' by Amertap control panel 3

ppm; sump area under catwalk 0.75 ppm; South side of Condenser

pit by the Heater Drain Pumps < 0.1 ppm; and Next to Turbine

Building Sump Bay # 2 3 ppm

Entered Action Level 1 for Loss of Hydrazine. Hold at < 30%

1115

Power for Low Oxygen Levels and Hydrazine

Chemistry Pulled Liquid Dample from Both Unit 1 Turbine Building

1200 Sump Bays for Hydrazine Analysis. Airborne Level at #2 Bay was

< 0.1 ppm

Liquid Samples Reported as 18 ppb (bay 1), 21 ppb (bay 2) and 53

1337

ppb (bay 3). No Action Required for These Concentrations.

Started Adding Hydrazine to Unit 1 FW System. Walkdowns of

1349 Hydrazine Addition Piping Indicates no Visual Leakage. Access

Limited to 695' Unit 1 Turbine Building Until Surveys Completed

Surveys of 695' U1 Turbine Building Indicate no Levels Above 0.1

1420

ppm and All Postings of that Level Removed

Hydrazine Air Samples 30 Minutes after Initiating Injection to

Feedwater System were: 695' at top of Condenser Pit Stairway

SW Corner < 0.1ppm, Postings Taken Down from Entire 695' Level

1430 and Cleared for Normal Access; 675' by Unit 1 Turbine Building

Sump Bay 2 was 5 ppm; Amertap Control Panel 1 ppm; MCC 1EA

Bus 2 2.0 ppm; and Chemist Reported that the Ammonia Smell

was Limited to Small Pockets of Stagnant Air

Exited Action Level 1 and loss of Hydrazine Conditions. Exited

1448

Chemical Hold on Power

1530 Commenced Power Accession to 50%

3 Attachment 2

Ventilation Fans Started on the North and South Sides of Unit 1

1618

Condenser Pit for Mixing

1629 Commenced power accession to 70%

Hydrazine Air Samples are as Follows: Airborne near Turbine

Building Sump Bay 2 < 0.1 ppm; and near MCC 1EA Bus 2 0.3

ppm

1649

Liquid samples Reported as 8.2 ppb (bay 1), 7.7 ppb (bay 2) and

13.8 ppb (bay 3)

Maintenance Workers Entered Unit 1 Condenser Pit to Place Fans

1709

in Pit.

Exited the Notification of Unusual Event (NOUE) HU3.1, Release

2220 of Toxic or Flammable Gases after 3 Consecutive Samples

Returned Less than Detectable Hydrazine (< 0.1 ppm)

4 Attachment 2

August 1, 2008

MEMORANDUM TO: Christopher S. Thomas, Senior Resident Inspector

Monticello Station

FROM: Cynthia D. Pederson, Director

Division of Reactor Projects

SUBJECT: SPECIAL INSPECTION CHARTER FOR REACTOR TRIP AND

TURBINE-DRIVEN AUXILIARY FEED WATER FAILURE ON

JULY 31, 2008

On July 31, 2008, at 8:17a.m., the Unit 1 reactor tripped at the Prairie Island Site. At the time,

the yellow train of reactor trip system (RTS) instrumentation was out of service for RTS testing.

The red channel then received an overtemperature T signal. This met the 2 of 4 channel logic

which caused the reactor trip. At this time the cause of the overtemperature T signal on the

red channel is unknown, but the licensee believes it was a spurious signal.

Following the reactor trip, the turbine driven auxiliary feedwater pump started and ran for

approximately 50 seconds before tripping on low suction/pressure. The pressure switch for

discharge pressure was found to be closed. The closure of this switch caused the pump to trip

as part of the pump protection features. The last time a surveillance test was performed on the

turbine driven auxiliary feedwater pump was over 30 days before on June 21, 2008, however

the discharge pressure switch impact may not have been challenged during this surveillance

test.

The sequence of events and the cause of the problem are being investigated by the licensee.

Based on the deterministic criteria provided in Management Directive 8.3, ANRC Incident

Investigation Program, @ the incident met MD 8.3 criterion h, AInvolved questions or concerns

pertaining to licensee operational performance.@ A Region III Senior Reactor Analyst completed

a SPAR model event assessment using a transient initiating event and failure of the auxiliary

feed water system to run and the pre-existing maintenance unavailability of instrument air

compressor 121. The assessment resulted in a preliminary Incremental Conditional Core

Damage Probability (ICCDP) value of approximately 5.2E-6.

Accordingly, based on the deterministic and risk criteria in MD 8.3, and as provided in Regional

Procedure 8.31, ASpecial Inspections at Licensed Facility,@ a Special Inspection Team will

commence an inspection on July 31, 2008. The Special Inspection Team will be led by you and

will include Karla Stoedter, the Senior Resident Inspector, Prairie Island, and Diana Betancourt,

Reactor Engineer, Region III.

CONTACT: Richard Skokowski

630-829-9620

1 Attachment 3

C. Thomas -2-

The special inspection will determine the sequence of events, and will evaluate the facts,

circumstances, and the licensee=s actions surrounding the July 31, 2008 incident. The specific

charter for the Team is enclosed.

Enclosure: As Stated

cc w/encl: J. Caldwell, Regional Administrator, Region III

M. Satorius, Deputy Regional Administrator, Region III

H. Peterson, DRS, Chief, Operator Licensing Branch

K. Stoedter, SRI, Prairie Island

P. Zurawski, RI, Prairie Island

D. Betancourt-Roldan, Reactor Engineer, RIII

2 Attachment 3

PRAIRIE ISLAND SPECIAL INSPECTION CHARTER

This Special Inspection Team is chartered to assess the circumstances surrounding the

deviation from the required safety system lineup of the auxiliary feed water system during a

reactor shutdown on July 31, 2008. The Special Inspection will be conducted in accordance

with Inspection Procedure 93812, Special Inspection, and will include, but not be limited to, the

items listed below.

1. Identify the time-line for the event. Include plant conditions, system line ups, and

operator actions.

2. Review the licensees post-trip review to determine the cause of the reactor trip.

Independently review plant data and records to confirm the adequacy of the licensees

assessment, and corrective actions.

3. Review the circumstances surrounding the failure of the turbine-driven auxiliary

feedwater pump, including the most likely cause of the pump failure; the length of time

the pump may have been in an unrecognized failed condition, and any potential for

operators to recover the failed pump.

4. Determine if the licensee is performing a root cause for the reactor trip. As available,

evaluate the scope, schedule, staffing and results of the licensees root cause

investigation.

5. Determine if the licensee is performing a root cause for the turbine-driven auxiliary

feedwater pump failure. As available, evaluate the scope, schedule, staffing and results

of the licensees root cause investigation.

6 Review procedures for the turbine-driven auxiliary feedwater pump, including operational

line-up procedures and testing procedures, to assess any procedural or testing

inadequacies which may have contributed to the failure of the pump.

7. Determine if the licensee performed an extent-of-condition evaluation to assess if the

contributing causes to the failure of the turbine-driven auxiliary feedwater pump have the

potential to affect other safety-related equipment.

8. Review for adequacy the licensees immediate corrective actions and planned long term

corrective actions to prevent recurrence for both the reactor trip and the failure of the

turbine-driven auxiliary feedwater pump.

Charter Approval

/RA/ R. Skokowski, Chief, Branch 3, DRP

/RA by G. Shear for/ C. Pederson, Director, Division of Reactor Projects

3 Attachment 3