ML061030559

From kanterella
Jump to navigation Jump to search
Withdrawal of Finding and Response to Two Disputed Noncited Violations (Inspection Report 05000313-05-004 and 05000368-05-004); Arkansas Nuclear One
ML061030559
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 04/13/2006
From: Howell A
NRC/RGN-IV/DRP
To: Mitchell T
Entergy Operations
References
EA-06-005, EA-06-006, EA-06-007, IR-05-004
Download: ML061030559 (10)


See also: IR 05000313/2005004

Text

April 13, 2006

EA-06-005; EA-06-006; EA-06-007

Timothy Mitchell

Acting Vice President Operations

Arkansas Nuclear One

Entergy Operations, Inc.

1448 S.R. 333

Russellville, AR 72801-0967

SUBJECT:

WITHDRAWAL OF FINDING AND RESPONSE TO TWO DISPUTED

NONCITED VIOLATIONS (INSPECTION REPORT 05000313/2005004 AND

05000368/2005004); ARKANSAS NUCLEAR ONE

Dear Mr. Mitchell,

Thank you for your letter dated December 19, 2005, in response to the subject inspection report

issued on November 7, 2005. In your response, you disputed a finding, and two noncited

violations (NCVs). These issues were associated with: (1) the inadvertent energizing of

pressurizer heaters during the implementation of maintenance work instructions, (2) the failure

to adequately conduct a risk assessment when taking equipment out of service for

maintenance, and (3) an inadequate procedure that led to damaging a reactor coolant pump

seal which required entry into a reduced reactor coolant inventory condition to repair. By letter

dated January 9, 2006, we informed you that we were evaluating your reply and would inform

you of the results of our evaluations.

The NRC conducted a review of your response, including the applicable licensing and

regulatory documents. The review was conducted by an NRC staff member who was not

involved in the initial inspection effort, and the results have been reviewed by the NRC's Office

of Enforcement.

Regarding issue (1), upon further review, the NRC staff agrees that the performance deficiency

did not constitute a finding of more than minor safety significance and will be withdrawn. The

principal basis for this determination was that the plants response to all pressurizer heaters

energizing was within the normal control limits of the pressurizer pressure control system which

should preclude any kind of transient that would challenge the plants protection systems.

Therefore, this constitutes an example of a minor procedural inadequacy; in this case

inadequate maintenance work instructions (EA-06-005).

With regard to issue (2), you contend that an adequate risk evaluation was conducted in

accordance with 10 CFR 50.65(a)(4), and that a violation of requirements did not occur. Our

understanding of the event and subsequent review concluded that a violation did occur as

originally documented (EA-06-006). The enclosed evaluation provides the basis for our

conclusion.

Entergy Operations, Inc.

-2-

With regard to issue (3), you contend that no performance deficiency occurred and, therefore,

no violation occurred. On the basis of a further review of this issue, the NRC identified that, in

addition to an inadequate procedure, there were a number of other causes and contributors of

the damaged reactor coolant pump seal which resulted in the plant incurring additional risk to

repair. These included: insufficient pre-evolution assessment of the reactor coolant system fill

evolution given the plant was in an atypical configuration (i.e., reactor coolant pump uncoupled);

inadequate coordination and communication between the outage control organization,

maintenance personnel, and control room personnel during conduct of the reactor coolant

system fill evolution; not promptly and thoroughly investigating indications of abnormally low

seal injection flow; and inadequate communications between engineering personnel and vendor

personnel that resulted in an inadequate operability evaluation of the seal condition.

Notwithstanding these additional causes and contributors, fundamentally, the existing

procedural guidance was insufficient to prevent such an occurrence. Therefore, we have

concluded that a performance deficiency did occur and that the original basis for the NCV

involving an inadequate procedure documented in Inspection Report 05000313/2005004 and

05000368/2005004 remains valid. Additionally, we have determined that this issue more

appropriately pertains to the Barrier Integrity Cornerstone; therefore, the cornerstone

assignment will be revised from the Mitigating Systems Cornerstone to the Barrier Integrity

Cornerstone. Further, the crosscutting aspect will be revised from human performance to

problem identification and resolution (EA-06-007). The details of our evaluation are provided in

the enclosure to this letter.

This letter will be made available electronically for public inspection in the NRC Public

Document Room or from the NRCs document system (ADAMS), accessible from the NRC

public web site at http://www.nrc.gov/reading-rm/adams.html (The public reading room).

Should you have any further questions, please contact Mr. David N. Graves at (817) 860-8147.

Sincerely,

/RA/

Arthur T. Howell, III, Director

Division of Reactor Projects

Docket Nos. 50-313, 50-368

License Nos. DPR 51, NPF-6

Enclosure: Disputed Violation Evaluation and Conclusions

cc w/Enclosure:

Senior Vice President

& Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Entergy Operations, Inc.

-3-

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Manager, Washington Nuclear Operations

ABB Combustion Engineering Nuclear

Power

12300 Twinbrook Parkway, Suite 330

Rockville, MD 20852

County Judge of Pope County

Pope County Courthouse

100 West Main Street

Russellville, AR 72801

Winston & Strawn LLP

1700 K Street, N.W.

Washington, DC 20006-3817

Bernard Bevill

Radiation Control Team Leader

Division of Radiation Control and

Emergency Management

Arkansas Department of Health

4815 West Markham Street, Mail Slot 30

Little Rock, AR 72205-3867

James Mallay

Director, Regulatory Affairs

Framatome ANP

3815 Old Forest Road

Lynchburg, VA 24501

Entergy Operations, Inc.

-4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (RWD)

Branch Chief, DRP/E (DNG)

Senior Project Engineer, DRP/E (GLG)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

K. S. Fuller, RC/ACES (KSF)

M. R. Johnson, D:OE (MRJ1)

OE:EA File (RidsOeMailCenter)

DRS STA (DAP)

S. O'Connor, OEDO RIV Coordinator (SCO)

ROPreports

ANO Site Secretary (VLH)

SUNSI Review Completed: _GLG__

ADAMS: / Yes

G No Initials: _GLG_____

/ Publicly Available G Non-Publicly Available G Sensitive

/ Non-Sensitive

R:\\_REACTORS\\ANO\\2005\\ANO 2005-04denial.wpd

RIV:C:DRP/E

D:DRP

ACES

D:ACES

OE

DNGraves;mjs

ATHowell III

GMVasquez

KDFuller

JGLuehman

/RA/

/RA/

MSHaire for

/RA/

E-DNGraves

3/27/06

4/2/06

3/28/06

3/29/06

4/7/06

D:DRP sign

RA

ATHowell III

BSMallett

/RA/

/RA/

4/13/06

4/11/06

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

E-1

ARKANSAS NUCLEAR ONE

INSPECTION REPORT 05000313/2005004; 05000368/2005004

DISPUTED VIOLATION EVALUATION AND CONCLUSIONS

EA-06-006 Noncited Violation 05000313/2005004-04 - Issue (2)

Summary of Licensee Response and NRCs Evaluation

Entergy Response: Entergy denies NCV 05000313/2005004-04, Failure to adequately assess

risk for an isolated pressurizer Electromatic Relief Valve (ERV). Entergy disagrees that a

violation of regulatory requirements occurred. Entergys objections to the violation are as

follows:

Objection 1:

The risk associated with isolating the ERV was appropriately considered.

NRC Position: NRC acknowledges and agrees that the operators were aware of and

qualitatively considered the risk associated with isolation of the ERV as a single component.

Discussions between the operators and the inspector at the time of occurrence determined that

they were aware of the risk associated with isolating the ERV in conjunction with other

equipment that had previously been removed from service (Inverter Y-25 and High Pressure

Injection Pump P-36A), and that the ERV was available if needed by manually opening the

block valve from the control room.

Objection 2:

The risk associated with the ERV removed from service was appropriately considered when

Low Pressure Injection (LPI) Train B was removed from service the following shift.

NRC Position: The inspectors review of the licensees risk assessment during this

maintenance period concluded that the licensee had initially used their risk management

program to qualitatively assess the risk of isolating the ERV with the ongoing maintenance on

high pressure injection Pump P-36A and Inverter Y-25. During the following shift, licensee staff

commenced maintenance on low pressure injection Valve CV-1429, which removed the Green

train of Low Pressure Injection (LPI) from service. Based on inspector discussions with the shift

manager who was on shift at the time of removing the LPI train from service, the inspector

determined that there was an increased quantifiable risk associated with the potential for a

pressurizer safety valve to lift while the ERV was isolated, and that this risk increase was not

considered prior to removing the LPI train from service. Although the licensee had previously

considered the risk of the ERV being isolated and the risk of removing the LPI train from

service, the licensee had not considered, prior to removing the LPI train from service, the

increased reliance on the pressurizer code safety valves for reactor coolant system over

pressure events with the ERV isolated and the potential that these valves might not close after

an open demand. Therefore, the risk evaluation was incomplete in that the increased potential

for a code safety valve to lift (due to the ERV isolated) and not reseat was not considered.

Enclosure

E-2

Objection 3:

No performance deficiency occurred. The definition of Performance Deficiency from NRC

Inspection Manual Chapter 0612 states:

Performance Deficiency: An issue that is the result of a licensee not meeting a

requirement or standard where the cause was reasonably within the licensees

ability to foresee and correct, and that should have been prevented. The

licensee does not have to be committed to a standard in order to determine

whether there is a performance deficiency (PD). For example, a PD is

determined to exist if the licensee fails to adhere to a widely accepted industry

standard.

NRC Position: NRC determined, based on interviews with the control room operators that were

on shift when the LPI train was removed from service, that the increased risk associated with a

pressurizer safety valve lifting while the ERV was isolated was not considered prior to removing

the LPI train from service. Although the licensee had considered the risk of the ERV being

isolated and the risk of removing the LPI train from service, the inspectors determined that the

licensee had not considered the increased reliance on the pressurizer code safety valves for

reactor coolant system over pressure events and the increased risk that these valves might not

close after an open demand while the LPI train was out of service. 10 CFR 50.65(a)(4),

requires in part that, "the licensee shall assess and manage the increase in risk that may result

from the proposed maintenance activities." In this instance, the increase in risk was not

properly assessed, and that failure to do so constitutes a performance deficiency and a violation

of the stated requirement.

Conclusion: NRC concluded that these circumstances reflect a performance deficiency and a

violation of 10 CFR 50.65(a)(4) in that licensee staff failed to adequately assess the risk

associated with the ERV being isolated prior to removing LPI Train B from service. NRC

determined that this finding was greater than minor because it related to a licensee's risk

assessment which had known errors (i.e., failure to consider the increased risk associated with

the pressurizer safety valve lifting) that had the potential to change the outcome of the

assessment. Using Appendix K, Maintenance Risk Assessment and Risk Management

Significance Determination Process, of MC 0609, Significance Determination Process, the

finding was determined to have very low safety significance (Green) because the incremental

increase in core damage probability was less than 2.24 X 10-8. The performance deficiency

also exhibited human performance crosscutting aspects related to a lack of attention to detail

while assessing risk.

EA-06-007 Noncited Violation 05000313/2005004-07 - Issue (3)

Summary of Licensee Response and NRCs Evaluation

Entergy Response: Entergy denies NCV 05000313/2005004-07, Inadequate procedure leads

to reactor coolant pump seal damage. Entergy disagrees that either a performance deficiency

or a violation of regulatory requirements occurred. Entergys objections to the violation are as

follows:

Enclosure

E-3

Objection 1: The root cause of this event was a lack of vendor information and operating

experience. Because of this, it was not understood that the reactor coolant pump (RCP) seal

could be damaged by pressurizing the seal with the pump uncoupled.

NRC Position: NRC determined that the vendor supplied information did not include

information that would inform the licensee that damage would occur if the pump seal was

pressurized with the pump uncoupled from the shaft and that a review of operating experience

did not identify that this damage could occur. However, the NRC concluded that

Procedure 2103.002, Filling and Venting the RCS, was inadequately scoped. The licensee

placed the RCP and its seal in a condition (uncoupled) that was not previously reviewed for seal

injection flow. Procedure 2103.002, Step 7.10, allowed initiation of seal injection to an

uncoupled pump. This configuration (uncoupled with seal injection initiated), which is not a

common configuration, was introduced without analyzing the potential effects of aligning seal

injection. The lack of analysis regarding the potential effects of initiating seal injection in this

uncoupled configuration resulted in the inadequate procedure not being identified and

corrected, and consequently, seal injection was lined up to the uncoupled pump damaging the

seal. If the uncommon configuration had been questioned by the licensee, NRC believes it is

not unreasonable to expect that the cognizant plant staff, knowing the operational bounds of the

equipment they are responsible for, would have been able to determine in advance that

initiation of seal injection with the pump uncoupled could result in seal damage. As discussed

further below, the argument that an equipment problem cannot be foreseen simply because

there is a lack of operating experience or a lack of written notification by the vendor (who, in

fact, was aware of the potential for the problem to occur) should not override the fact that

indicators in plant conditions were not questioned prior to or during implementation of a

procedure that could impact plant equipment, in this case the RCP seals.

Objection 2: There is little or no safety significance associated with this event.

NRC Position: NRC had originally documented that this issue was associated with the

Mitigating Systems Cornerstone configuration control attribute. After further review of the

information you provided, NRC determined that this performance deficiency is greater than

minor, but that it is more accurately described as affecting the Barrier Integrity Cornerstone

RCS procedure quality attribute and affected the cornerstones objective of providing

reasonable assurance that physical design barriers (RCP seals) protect the public from

radionuclide releases caused by accidents or events. This determination is more appropriate in

that the inadequate procedure resulted in establishing seal injection flow to the uncoupled

pumps seal causing damage to the seal. The damage was recognized after the pump was

recoupled and the reactor coolant system was filled, resulting in leakage from the reactor

coolant system into containment.

Placing the reactor in an unplanned reduced inventory condition, which was necessary to repair

the RCP seal, constituted a higher risk configuration as analyzed utilizing NRC Manual Chapter 0609, Significance Determination Process, Appendix A. The estimated increase in core

damage frequency was 1E-7/year, which is a condition of very low safety significance (Green).

If the condition had been adequately analyzed prior to occurrence, or identified and repaired,

while the reactor was defueled, prior to declaring the seal operable, then the issue would have

been characterized as an in-process minor issue in accordance with NRC Manual

Enclosure

E-4

Chapter 0612, Power Reactor Inspection Reports, Appendix E, and would not have been

documented. In this situation, there would have been little or no safety significance because a

reduced inventory evolution with fuel in the reactor vessel would not have been performed.

Objection 3: No performance deficiency occurred because the condition was not within the

licensees ability to foresee and correct.

NRC Position: A performance deficiency (PD) is defined as, An issue that is the result of a

licensee not meeting a requirement or standard where the cause was reasonably within the

licensees ability to foresee and correct, and that should have been prevented. The licensee

does not have to be committed to a standard in order to determine whether there is a PD. For

example, a PD is determined to exist if the licensee fails to adhere to a widely accepted industry

standard.

NRC noted several instances in which this event could have either been prevented or the risk

significance could have been reduced. If the procedure had been adequately written and

reviewed to anticipate seal damage under these conditions, then there would have been a

check and perhaps no damage. Operators in the control room were not aware that the RCP

was uncoupled when they commenced the RCS fill and vent procedure. During interviews with

the inspector, the operators indicated that they would not have initiated seal injection to the

pump if they had known the pump was uncoupled; although, the reason was based on staffing

and ALARA concerns and not the potential for pump seal damage. If the control room staff had

known the pump was uncoupled, given the unusual configuration, there would have been an

opportunity for the licensee staff to have reviewed in more detail the impact of seal injection

initiation.

Additionally, during conduct of the fill and vent procedure, once seal injection flow was initiated

to the RCP using one charging pump, abnormal seal flows were observed by the operators

(because the normal flow path of seal injection water into the reactor coolant system was

blocked by the uncoupled pump resting on the recirculation impeller). Instead of stopping the

procedure to investigate the abnormal indications, the operators continued increasing flow until

3 charging pumps were running. If this abnormal indication had been promptly and thoroughly

reviewed, the pump seal damage might have been prevented or identified and corrected during

the period when the reactor was defueled.

When the flow conditions to the RCP seal were recognized as inappropriate, an operability

evaluation was conducted to determine the condition of the seal. This evaluation was

conducted with vendor input. However, during communications with the vendor, the licensee

did not inform the vendor that seal injection had been initiated with the pump uncoupled.

Consequently, the vendor concluded that no seal damage had occurred because the vendor did

not know the pump was uncoupled at the time of the injection. The licensees operability

evaluation was completed and concluded that the seal was operable, and plant operation

continued. Later, after refueling and coupling the RCP, when a reactor coolant system fill and

vent was performed, the seal was determined to be damaged and leaking. Subsequent

communications with the vendor indicated that the vendor was aware that seal injection should

not be applied to an uncoupled pump, but given that the licensee staff did not communicate the

status of the pump to the vendor, the potential for seal damage was not identified until after the

seal had been declared operable and demonstrated leakage following pump recoupling.

Enclosure

E-5

Although this communication deficiency is not directly related to the inadequate procedure, if

clear and complete communications had occurred at the time of occurrence, then a reduced

inventory condition (with fuel in the reactor vessel) could have been avoided.

NRC determined, as the licensee presented in its objection, that the vendor supplied

information did not include specific information that would inform the licensee that seal damage

would occur if the pump seals were pressurized with the pump uncoupled from the shaft, and

that a review of operating experience did not identify any events or information that specifically

addressed this event. The licensee contends that without operating experience and vendor

input, there was no way for them to have reasonably predicted or prevented this occurrence.

While NRC acknowledges that operating experience and vendor input are necessary and useful

for enhancing safe operation of a nuclear facility, the NRC believes that in this particular

instance, even without these elements, this condition could have been prevented or its

significance could have been reduced. As noted in NRCs Position to Objection 1 regarding this

issue, the unusual combination of filling and venting the reactor coolant system with an

uncoupled reactor coolant pump should have prompted the licensee to make a more detailed

evaluation of the actions associated with initiating seal injection flow. Accordingly, this NCV

related to Technical Specification 6.4.1, Procedures, will be sustained as a finding of very low

risk significance (Green).

With regard to the crosscutting aspects of this finding, NRC initially determined that this finding

had crosscutting aspects related to human performance in that the pump seal damage was

caused by an inadequate procedure. Since the procedure had existed in this form for many

years, the human performance crosscutting aspect of the inadequate procedure would not be

indicative of recent licensee performance. However, there were missed opportunities, as

indicated above, to review the procedure to ensure its adequacy for the unusual plant

configuration prior to and during use that is indicative of recent performance. Utilizing

crosscutting aspect guidance from NRC Manual Chapter 0612, Power Reactor Inspection

Reports, this finding was determined to have problem identification and resolution crosscutting

aspects. The Plant Issues Matrix entry will be revised to reflect this determination.

Objection 4: Entergy does not agree that a maintenance condition that requires a reduced

inventory window to correct would affect the Mitigating Systems Cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

NRC Position: NRC agrees that this issue did not affect the Mitigating Systems Cornerstone.

However, upon further review and as previously discussed, NRC finds that the Barrier Integrity

Cornerstone attribute of procedure quality was affected due to the implementation of an

inadequate procedure that allowed the initiation of seal injection to an uncoupled RCP. The

Performance Issues Matrix will be updated to reflect Barrier Integrity as the affected

cornerstone.

Conclusion: Unit 2 Technical Specification 6.4.1, "Procedures," states that written procedures

shall be established covering the applicable procedures in Regulatory Guide 1.33, Revision 2,

Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 3.a states, in part,

that instructions for filling and venting should be prepared for the reactor coolant system.

Contrary to the above, the procedure for filling and venting the reactor cooler system,

Procedure 2103.002, was inadequate in that it allowed the initiation of seal injection to an

Enclosure

E-6

uncoupled reactor coolant pump which caused damage to the pump seals. The additional risk

incurred from the repair of the pump seal could have been avoided with an adequate RCS fill

procedure and if there had been effective identification and evaluation of unusual plant

conditions associated with the use of this procedure. The violation will be sustained as an issue

of very low safety significance for the performance deficiency related to an inadequate

procedure. Additionally, ineffective communications between organizations was a contributing

cause to this condition. The crosscutting aspect of human performance will be revised to

problem identification and resolution, and the cornerstone will be revised from Mitigating

Systems to Barrier Integrity.