ML053250417

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Preliminary Issue List, with Handwritten Notes
ML053250417
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 11/15/2005
From:
NRC Region 4
To:
References
FOIA/PA-2004-0307
Download: ML053250417 (2)


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Preliminary Issue List Palo Verde Nuclear Generating Station Augmented Inspection Team NOTE: This is NOT an all-inclusive list.

230 kV Liberty Transmission Line, Tower#73, Phase "C"Insulator Failure C - single phase to ground fault resulted in loss of offsite power and three unit trip E Auxiliary Relay, Liberty Transmission Line Fault Detection/Protection System Failure q , A inadequate design resulted in single failure vulnerability d>

  • additional single failure design issues identified and corrected to extent practical
  • licensee also did not appear to make resolution of this issue a startup issue until the concern was raised by the AIT
  • 4Jnit I Atmospheric Dump Valve 185 Fail e n:rooe ristra ction with minimal impact on event response
  • apparent cause being determined
  • Unit 1 Letdown Heat Exchanger Isolation Failure
  • licensee performance deficiency associated with understanding implications of temporary modification installed in plant
  • little impact on control room response to event
  • some potential impact on fire response being reviewed by AIT
  • UiUtlancdL3General-Electric-Magne Blast Circuit Breaker Failures (J complicated event recovery efforts taii t ereturn of offsite power to ESF

{ZieQ determined apparent cause as "breaker not cycled frequently enoug!P VA AlThl lctse een-apparent caseara ncern regaaigttrret

5gtrj %functionality of breakers resident staff following as potential operability issue

'e .fapparent cause wa ode ure n e er circuit -7 ,-,xA _

  • Unit 2, Train "E" Positive Displacement Charging Pump Trip a
  • operator error resulted in suction line isolation and protective trip of pump
  • AIT identified that auxiliary operator was delayed approximately 10 minutes at the RCA access point even after the operator explained he was on a time critical mission
  • *when RCA access delay was discussed with licensee, AIT determined that the licensee was unaware of delay information in this record was deleted in accordance with the reedOM1 of InfoFMation

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  • Unit 3 Bypass Valve/Control Cabinet Malfunctions

-S good operator actions minimized impact on plant, was operator distraction O-C potential design modification issue being reviewed by AIT as apparent cause

  • no impact on trip but some minor impacts on recovery
  • potential design issue associated with set point of thermal overloads
  • Unit 3 Low Pressure Safety Injection System In-leakage (Check Valve V217)
  • little impact on event, operator distraction to take manual actions to prevent over

_pressurization

  • apparent cause was Borg-Warner check valve leakage, potential maintenance issue a* -nit 3Variable Over PowerTrD-ReactorCoolant Pump Speed Increase to 67 Hz license- in stigating potential impacts o I A; . AIT-raisudiqest-ios aboutydrrauic affects, if any

'-:> Technical Support Center Emergency Diesel Generator Failure

  • apparent cause was test switch out of position
  • maintenance personnel failed to use restoration procedure six days prior to event following testing
  • some Impact on emergency response organization which needed to use alternate TSC
  • complicated recovery efforts by delaying RCP restoration
  • appears minimum amperage basis'involved NPSH limits
  • high voltage in switchyard resulted in low amperage J1X i~ Emergency Response Organization Notification Issues
  • some delay in notification occurred but little impact
  • apparent cause associated with procedure adequacy and communication failures
  • Initial Notification of State and Local Official Issues
  • Unit I and Unit 3 did meet their guidelines on timeliness of initial notification
  • little overall impact because Unit 2 Alert Notification was timely
  • apparent cause being reviewed