ML053130249

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IR 0500482-05-004; 6/27/05 - 9/26/05; Wolf Creek Generating Station; Operator Performance During Nonroutine Evolutions and Events, Operability Evaluations, Access Control to Radiologically Significant Areas, & Identification and Resolution
ML053130249
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 11/09/2005
From: William Jones
NRC/RGN-IV/DRP/RPB-B
To: Muench R
Wolf Creek
References
IR-05-004
Download: ML053130249 (29)


See also: IR 05000482/2005004

Text

November 9, 2005

Rick A. Muench, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839 Wolf Creek Nuclear Operating Corporation

SUBJECT: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION

REPORT 05000482/2005004

Dear Mr. Muench:

On September 26, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Wolf Creek Generating Station. The enclosed integrated report documents

the inspection findings which were discussed on September 28, 2005, with Mr. Steve Hedges

and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one NRC identified and two self-revealing findings of very low safety

significance (Green). The findings were determined to involve violations of NRC requirements;

however, because of the very low safety significance and because the findings were entered

into your corrective action program, the NRC is treating these violations as noncited violations

consistent with Section VI.A of the NRC Enforcement Policy. In addition, an apparent violation

was identified involving fire protection suppression water system degradation. The NRC is

performing a significance determination process Phase 3 analysis to determine the safety

significance. If you contest these violations, you should provide a response within 30 days of

this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory

Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the

Regional Administrator Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Wolf Creek

Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Wolf Creek Nuclear Operating Corporation -2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

William B. Jones, Chief

Project Branch B

Division of Reactor Projects

Docket: 50-482

License: NPF-42

Enclosure:

NRC Inspection Report 05000482/2005004

w/attachment: Supplemental Information

cc w/enclosure:

Vice President Operations/Plant Manager

Wolf Creek Nuclear Operating Corp.

P.O. Box 411

Burlington, KS 66839

Jay Silberg, Esq.

Shaw Pittman, LLP

2300 N Street, NW

Washington, DC 20037

Supervisor Licensing

Wolf Creek Nuclear Operating Corp.

P.O. Box 411

Burlington, KS 66839

Chief Engineer

Utilities Division

Kansas Corporation Commission

1500 SW Arrowhead Road

Topeka, KS 66604-4027

Office of the Governor

State of Kansas

Topeka, KS 66612

Attorney General

120 S.W. 10th Avenue, 2nd Floor

Topeka, KS 66612-1597

Wolf Creek Nuclear Operating Corporation -3-

County Clerk

Coffey County Courthouse

110 South 6th Street

Burlington, KS 66839-1798

Vick L. Cooper, Chief, Air Operating

Permit and Compliance Section

Kansas Department of Health and

Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Chief Technological Services Branch

National Preparedness Division

Department of Homeland Security

Emergency Preparedness & Response Directorate

FEMA Region VII

2323 Grand Boulevard, Suite 900

Kansas City, MO 64108-2670

Wolf Creek Nuclear Operating Corporation -4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (KMK)

Senior Resident Inspector (ELC1)

Resident Inspector (TBR2)

SRI, Callaway (MSP)

Branch Chief, DRP/B (WBJ)

Senior Project Engineer, DRP/B (RAK1)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

ROPreports

WC Site Secretary (SLA2)

SISP Review Completed: __WBJ__ ADAMS: / Yes G No Initials: __WBJ____

/ Publicly Available G Non-Publicly Available G Sensitive / Non-Sensitive

R:REACTORS\_WC\2005\WC2005-04RP-ELC.wpd

RIV:SRI:DRP/B RI:DRP/B ASRI:DRP/B C:DRS/EB

FLBrush TBRhoades ELCrowe CJPaulk

E-WBJones E-WBJones T-WBJones /RA/

11/7/05 11/7/05 11/8/05 11/7/05

C:DRP/OB C:DRS/PS C:DRS/PEB C:DRP/PBB

ATGody MPShannon LJSmith WBJones

/RA/ /RA/ /RA/ /RA/

11/8/05 11/8/05 11/4/05 11/9/05

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-482

License: NPF-42

Report: 5000482/2005004

Licensee: Wolf Creek Nuclear Operating Corporation

Wolf Creek Generating Station

Location: 1550 Oxen Lane NE

Burlington, Kansas

Dates: June 27 through September 26, 2005

Inspectors: F. L. Brush, Senior Resident Inspector

E. L. Crowe, Acting Senior Resident Inspector

T. B. Rhoades, Resident Inspector

L. C. Carson II, Senior Health Physicist

J. L. Dixon, Resident Inspector, Arkansas Nuclear One

R. A. Kopriva, Senior Project Engineer

M. S. Peck, Senior Resident Inspector, Callaway

B. K. Tharakan, Health Physicist

Approved By: W. B. Jones, Chief, Project Branch B

Enclosure

SUMMARY OF FINDINGS

IR 500482/2005004; 6/27/05 - 9/26/05; Wolf Creek Generating Station; Operator Performance

During Nonroutine Evolutions and Events, Operability Evaluations, Access Control to

Radiologically Significant Areas, and Identification and Resolution of Problems

The report covers a 3-month period of inspection by resident inspectors and regional specialist

inspectors. The inspection identified three Green noncited violations and an apparent violation.

The significance of most findings is indicated by their color (Green, White, Yellow, or Red)

using Inspection Manual Chapter 0609, Significance Determination Process. Findings for

which the significance determination process does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

when station personnel failed to adequately evaluate a maintenance activity on safety-

related equipment for potential energy/fluid transfer paths as required by Station

Procedure AP 21D-002, "Evaluation For Potential Energy/Fluid Transfer Paths." On

June 28, 2005, planned motor-operated valve actuator work on an isolation valve in the

safety injection system lead to the unplanned transfer of water from the volume control

tank to the refueling water storage tank. This issue involved human performance

crosscutting aspects associated with station personnel not following a station procedure.

The failure to correctly perform a required step of a station procedure for evalauting

emergency core cooling system interfaces is a performance deficiency. This finding

was determined to be more than minor because it affected the mitigating systems

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Using the Phase 1 worksheets in Manual Chapter 0609, "Significance

Determination Process," the finding was determined to have very low safety significance

because the finding did not represent a loss of a safety function or a train of safety

function and is not potentially risk significant due to external events. Wolf Creek

Nuclear Operating Corporation entered this finding into their corrective action program

as Performance Improvement Request 2005-2004 (Section R14).

  • Green. The inspectors documented a self-revealing, noncited violation of 10 CFR

Part 50, Appendix B, Criterion XVI, because Wolf Creek Nuclear Operating Corporation

failed to assure corrective actions taken in response to a significant condition adverse to

quality preclude repetition of the condition. On May 5, 2005, auxiliary feedwater flow

Transmitter ALFT-0011 indicated flow without existing flow in the auxiliary feedwater

system due to the buildup of debris from a previous steam generator chemical cleaning.

Following the May 5, 2005, event, Wolf Creek Nuclear Operating Corporation flushed all

auxiliary feedwater flow transmitters and the level transmitters for the steam generators.

On July 11, 2005, another auxiliary feedwater flow Transmitter ALFT-0003 indicated flow

-2-

without existing flow in the auxiliary feedwater system. This transmitter was flushed and

the conditions found on May 5, 2005, existed in this transmitter. This issue involved

problem identification and resolution crosscutting aspects, in that, station personnel did

not properly evaluate a condition adverse to quality that resulted in an auxiliary

feedwater flow transmitter becoming inoperable.

The failure to take appropriate corrective measures to address a significant condition

adverse to quality is a performance deficiency. This finding was determined to be more

than minor because it affected the mitigating systems cornerstone objective of ensuring

the availability, reliability, and capability of the auxiliary feedwater system that responds

to initiating events to prevent undesirable consequences (i.e., core damage). Using the

Phase 1 worksheets in Manual Chapter 0609, Significance Determination Process, the

finding was determined to have very low safety significance because the finding did not

represent a loss of a safety function and is not potentially risk significant due to external

events. Wolf Creek Nuclear Operating Corporation entered this finding into their

corrective action program as PIR 2005-2149 (Section R15).

when station personnel failed to follow Procedure AP 21E-001, Clearance Orders, and

operated a temporary component that had been established within a fire protection

suppression water system clearance boundary without instructions and authorization.

Specifically, personnel started a temporary fire pump which had been connected to the

stations fire protection suppression water system causing water to spray from an open

vent valve. The water spray wetted the control panel for the diesel driven fire pump

which resulted in the pump becoming inoperable for approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. This issue

involved human performance crosscutting aspects associated with personnel not

following a station procedure.

The failure to follow station procedures is a performance deficiency. The finding was

determined to be more than minor because if affected the mitigating systems

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Using the

Phase 1 worksheets in Manual Chapter 0609, Significance Determination Process, the

finding was determined to degrade the fire protection system suppression and was

evaluated using Appendix F, Fire Protection Significance Determination Process. This

finding requires a Phase 3 analysis and is currently under evaluation. Wolf Creek

Nuclear Operating Corporation entered this finding into their corrective action program

as PIR 2005-2142 (Section 4OA2).

Cornerstone: Occupational Radiation Safety

which requires procedures for radiation protection and personnel monitoring.

Specifically, on September 22, 2003, Wolf Creek Nuclear Operating Corporation failed

to perform an exit whole body count for a radiation worker that had entered the

radiologically controlled area and terminated their employment with Wolf Creek Nuclear

Operating Corporation.

Enclosure

-3-

The failure to perform an exit whole body count was a performance deficiency. The

finding was determined to be more than minor because it was associated with the

Occupational Radiation Safety cornerstone attribute of Programs and Process and

affected the cornerstone objective to ensure the adequate protection of worker health

and safety from exposure to radiation and radioactive materials. Because the

occurrence involved conditions that were contrary to licensee procedures related to

measuring worker dose, this finding was processed through the Occupational Radiation

Safety Significance Determination Process. The finding was determined to be of very

low safety significance (Green) because it did not involve: (1) as low as is reasonably

achievable planning and work controls, (2) an overexposure, (3) a substantial potential

for an overexposure, or (4) an impaired ability to assess dose. The finding was entered

into Wolf Creek Nuclear Operating Corporation's corrective action program as

PIR 2005-1653 (Section 2OS1).

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by Wolf Creek Nuclear

Operating Corporation, has been reviewed by the inspectors. Corrective actions taken

or planned by Wolf Creek Nuclear Operating Corporation have been entered into Wolf

Creek Nuclear Operating Corporation's corrective action program. This violation and

corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

The plant started the inspection period at 100 percent rated thermal power and remained at or

near this power level for the entire report period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather (71111.01)

a. Inspection Scope

The inspectors completed a review of Wolf Creek Nuclear Operating

Corporation's (WCNOC) readiness of seasonal susceptibilities involving extreme high

temperatures. The inspectors: (1) reviewed plant procedures, the Updated Final Safety

Analysis Report, and Technical Specifications to ensure that operator actions defined in

adverse weather procedures maintained the readiness of essential systems, (2) walked

down portions of the systems listed below to ensure that adverse weather protection

features were sufficient to support operability including the ability to perform safe

shutdown functions, (3) evaluated operator staffing levels to ensure WCNOC would

maintain the readiness of essential systems required by plant procedures, and

(4) reviewed the corrective action program to determine if WCNOC identified and

corrected problems related to adverse weather conditions.

  • July 15, 2005, WCNOC preparations for summer weather which included:

Steam heating for outdoor tanks, ventilation lineups for power block buildings,

and discussion of aspects of hot weather operations with licensee personnel.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

The inspectors: (1) walked down portions of the three risk important systems listed

below and reviewed plant procedures and documents to verify that critical portions of the

selected systems were correctly aligned and (2) compared deficiencies identified during

the walk down to WCNOC's corrective action program to ensure problems were being

identified and corrected.

C July 15, 2005, Train B motor-driven auxiliary feedwater system

C August 4, 2005, Train B safety injection system

Enclosure

-2-

C September 15, 2005, component cooling water system

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Area Walkdowns

a. Inspection Scope

The inspectors walked down the six plant areas listed below to assess the material

condition of active and passive fire protection features, their operational lineup, and their

operational effectiveness. The inspectors: (1) verified that transient combustibles and

hot work activities were controlled in accordance with plant procedures; (2) observed the

condition of fire detection devices to verify they remained functional; (3) observed fire

suppression systems to verify they remained functional; (4) verified that fire

extinguishers and hose stations were provided at their designated locations and that

they were in a satisfactory condition; (5) verified that passive fire protection features

(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration

seals, and oil collection systems) were in a satisfactory material condition; (6) verified

that adequate compensatory measures were established for degraded or inoperable fire

protection features; and (7) reviewed the corrective action program to determine if

WCNOC identified and corrected fire protection problems.

C July 5, 2005, circulating water screen house

C July 19, 2005, main steam enclosure

C August 4, 2005, residual heat removal Pump B room

C August 4, 2005, room containing safety injection Pump B, centrifugal charging

Pump B, and containment spray Pump B

C August 26, 2005, motor-driven auxiliary feedwater Pumps A and B rooms

C August 26, 2005, turbine-driven auxiliary feedwater pump room

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

Enclosure

-3-

1R11 Licensed Operator Requalification (71111.11)

Resident Inspector Review

a. Inspection Scope

The inspectors observed testing and training of senior reactor operators and reactor

operators to identify deficiencies and discrepancies in the training, to assess operator

performance, and to assess the evaluator's critique of the scenario listed below:

C August 3, 2005, training scenario, LR5001005, Large Break LOCA,

Revision 10, which involved a large break loss of coolant accident including

recovery and shifting to cold leg recirculation.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the two maintenance activities listed below to: (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSC functional

performance; (3) evaluate the role of work practices and common cause problems; and

(4) evaluate the handling of SSC issues reviewed under the requirements of the

Maintenance Rule, 10 CFR Part 50, Appendix B, and Technical Specifications.

C August 12, 2005, residual heat removal system

C Septernber 16, 2005, essential service water system

The inspectors reviewed two samples.

b. Findings

No findings of significance were identified.

Enclosure

-4-

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

Risk Assessment and Management of Risk

a. Inspection Scope

The inspectors reviewed the assessment activities listed below to verify:

(1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and

licensee procedures prior to changes in plant configuration for maintenance activities

and plant operations; (2) the accuracy, adequacy, and completeness of the information

considered in the risk assessment; (3) that WCNOC recognizes, and/or enters as

applicable, the appropriate licensee established risk category according to the risk

assessment results and licensee procedures; and (4) that WCNOC identified and

corrected problems related to maintenance risk assessments.

The inspectors reviewed operational risk assessments for planned maintenance and

actual, planned, and emergent work schedules for the following weeks:

C July 11, 2005

C August 29, 2005

C September 12, 2005

C September 19, 2005

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Nonroutine Evolutions and Events (71111.14)

a. Inspection Scope

For the plant evolution and event listed below, the inspectors: (1) reviewed operator

logs, plant computer data, and/or strip charts for the below evolutions to evaluate

operator performance in coping with nonroutine events and transients, (2) verified that

the operators response was in accordance with the response required by plant

procedures and training, and (3) verified that WCNOC has identified and implemented

appropriate corrective actions associated with personnel performance problems that

occurred during the nonroutine evolutions sampled.

  • June 28, 2005, inadvertent transfer of water from volume control tank (VCT) to

refueling water storage tank (RWST).

declaration of both trains of residual heat removal system containment sump

suction isolation Valves EJHV8811A and -8811B inoperable.

Enclosure

-5-

The inspectors completed two samples.

b. Findings

Introduction. The inspectors documented a self-revealing noncited violation of

Technical Specification 5.4.1a, which occurred when station personnel failed to

adequately evaluate a maintenance activity on safety-related equipment for a potential

energy/fluid transfer path as required by Station Procedure AP 21D-002, "Evaluation For

Potential Energy/Fluid Transfer Paths." Subsequently, maintenance on a motor-

operated isolation valve in the safety injection system lead to the unplanned transfer of

water from the VCT to the RWST.

Description. On June 28, 2005, WCNOC performed maintenance on the motor-

operated valve actuator for residual heat removal heat exchanger/chemical volume

control system to safety injection Pump A downstream isolation Valve EMHV8807B.

This maintenance involved the removal of the actuator from the valve which resulted in

partial opening of Valve EMHV8807B. This created an open pathway for the transfer of

water from the VCT to the RWST. Wolf Creek Nuclear Operating Corporation evaluated

the potential for water in the RWST to transfer to the VCT if VCT pressure was less than

25 psig. However, WCNOC failed to assess flow in the opposite direction. The

pressure in the VCT was sufficiently high to cause lowering of the VCT level due to

transfer of water to the RWST. Wolf Creek Nuclear Operating Corporation entered

Procedure OFN BB-007, "RCS Leakage High," to determine the location of the leak and

Technical Specification 3.4.13, "RCS Leakage," due to the appearance of a greater than

1 gallon per minute unidentified leak. The leak was isolated when the valve actuator

was re-installed and the valve closed. The leak existed for approximately 24 minutes.

Analysis

The failure to properly follow station procedures is a performance deficiency. This

finding was determined to be more than minor because it affected the mitigating

systems cornerstone objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences (i.e.,

core damage). Using the Phase 1 worksheets in Manual Chapter 0609, "Significance

Determination Process," the finding was determined to have very low safety significance

because the finding did not represent a loss of a safety function and is not potentially

risk significant due to external events. This issue involved human performance

crosscutting aspects associated with station personnel failing to adequately implement

procedural requirements to evaluate potential fluid transfer paths.

Enforcement

Technical Specification 5.4.1a requires procedures be implemented in accordance with

Regulatory Guide 1.33, Revision 2, Appendix A. Section 9 to Regulatory Guide 1.33

requires maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

Enclosure

-6-

documented instructions, or drawings appropriate to the circumstances. Contrary to the

above, on June 28, 2005, WCNOC personnel performed an inadequate evaluation of

potential energy/fluid transfer paths for planned maintenance on Valve EMHV8807B

which resulted in an inadvertent transfer of water from the VCT to the RWST. A similar

event occurred in 1995. Because the failure to prevent transfer of water was of very low

safety significance and was entered into the corrective action program as PIR 2005-

2004, this violation is being treated as a noncited violation, consistent with Section VI.A

of the NRC Enforcement Policy: NCV 05000482/0500401, failure to adequately

implement station procedures results in transfer of water from VCT to RWST.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

For the three operability evaluations listed below, the inspectors: (1) reviewed plant

status documents such as operator shift logs, emergent work documentation, deferred

modifications, and standing orders to determine if an operability evaluation was

warranted for degraded components; (2) referred to the Updated Safety Analysis

Report and design basis documents to review the technical adequacy of licensee

operability evaluations; (3) evaluated compensatory measures associated with

operability evaluations; (4) determined degraded component impact on any Technical

Specifications; (5) used the significance determination process to evaluate the risk

significance of degraded or inoperable equipment; and (6) verified that WCNOC has

identified and implemented appropriate corrective actions associated with degraded

components.

containment recirculation valves

PIR 2005-2149 July 13, 2005, auxiliary feedwater flow

Transmitters ALFT0003, -0004, -0009, and -0011

  • PIR 2005-2478 August 29, 2005, grid disturbances resulting in low

voltage alarms

The inspectors completed three samples.

b. Findings

Introduction. The inspectors documented a Green self-revealing, noncited violation of

10 CFR Part 50, Appendix B, Criterion XVI, because WCNOC failed to prevent the

recurrence of a plant event which resulted in the additional failures of auxiliary

feedwater flow transmitters following steam generator chemical cleaning.

Description. On April 10, 2005, WCNOC injected advanced scale conditioning agent

(ASCA) into steam Generator B. Steam Generator C was injected with ASCA on

Enclosure

-7-

April 11, 2005. ASCA is a chemical formulation that aids to soften, dislodge, and

partially dissolved sludge and scale deposits. Immediately following the April 11, 2005,

injection, WCNOC found steam Generator C auxiliary feedwater flow

Transmitter ALFT0011 indicating 22,000 lbm/hr without any flow in the auxiliary

feedwater system. Approximately during the same period, a second auxiliary feedwater

flow transmitter on steam Generator C (ALFT0004) indicated approximately

40,000 lbm/hr without auxiliary feedwater flow. Wolf Creek Nuclear Operating

Corporation flushed both transmitters and a dark black liquid with suspended solids

issued from the flush lines. No other auxiliary feedwater flow transmitters were flushed

at this time. These transmitters are utilized in the Wolf Creek emergency operating

procedures to verify proper auxiliary feedwater flow during accident conditions. On

May 5, 2005, WCNOC discovered auxiliary feedwater flow Transmitter ALFT0011

indicating 22,000 lbm/hr without corresponding auxiliary feedwater flow. This

transmitter was flushed on May 6, 2005, and the dark black liquid with suspended

solids issued from the flush lines. On May 8, 2005, WCNOC flushed auxiliary

feedwater flow Transmitters ALFT0003 and -0009 which provide auxiliary feedwater

flow indication for steam Generator B and discovered the dark black liquid with

suspended solids in these transmitters. Wolf Creek Nuclear Operating Corporation

also flushed low point drains in the auxiliary feedwater system and took samples of the

dark black liquid which were sent to an offsite vendor for analysis.

On July 11, 2005, control room operators identified that an auxiliary feedwater flow

Transmitter ALFT0003 was indicating a flow rate of approximately 15,000 lbm/hr flow

with no auxiliary feedwater flow. Wolf Creek Nuclear Operating Corporation removed

and cleaned the flow transmitter on July 13, 2005, and discovered a black substance

plugging the sensing line and at several instrument line fittings. Wolf Creek Nuclear

Operating Corporation stated this substance was similar to that identified during the

previous erroneous auxiliary feedwater flow transmitter indications. Wolf Creek

Nuclear Operating Corporation again flushed the other auxiliary feedwater flow

transmitters for steam Generators B and C and did not observe any foreign substance.

Wolf Creek Nuclear Operating Corporation also implemented a monthly flushing of all

the auxiliary feedwater flow transmitters. Wolf Creek Nuclear Operating Corporation

received the results of the vendors chemical analysis the second week of September

2005 which indicated the presence of the chemical ASCA.

Analysis

The failure to take appropriate corrective measures to address a significant condition

adverse to quality is a performance deficiency. This finding was determined to be more

than minor because it affected the mitigating systems cornerstone objective of ensuring

the availability, reliability, and capability of the auxiliary feedwater system that is used to

respond to initiating events to prevent undesirable consequences (i.e., core damage).

Using the Phase 1 worksheets in Manual Chapter 0609, Significance Determination

Process, the finding was determined to have very low safety significance because the

finding did not represent a loss of a safety function and is not potentially risk significant

due to external events. This issue involved problem identification and resolution

crosscutting aspects in that station personnel did not properly evaluate and implement

Enclosure

-8-

adequate corrective actions to prevent the accumulation of sludge in the auxiliary

feedwater flow transmitters.

Enforcement

In part, 10 CFR 50, Appendix B, Criterion XVI, states that for significant conditions

adverse to quality, measures shall be established to assure that corrective actions

taken preclude repetition. Contrary to the above, WCNOC personnel failed to

adequately evaluate and implement corrective actions to prevent the accumulation of

sludge in the auxiliary feedwater flow transmitters following the initial identification of

the concern in May 2005. Because the failure to adequately prevent the buildup of

sludge in the flow transmitters was determined to be of very low safety significance and

was entered into the corrective action program (PIR 2005-2149), this violation is being

treated as a noncited violation consistent with Section VI.A of the NRC Enforcement

Policy: NCV 05000482/200500402, inadequate corrective actions fail to prevent

subsequent failure of auxiliary feedwater flow transmitters.

1R16 Operator Workarounds (71111.16)

a. Inspection Scope

Cumulative Review of the Effects of Operator Workarounds

On September 8, 2005, the inspectors reviewed the cumulative effects of operator

workarounds to determine: (1) the reliability, availability, and potential for misoperation

of a system; (2) if multiple mitigating systems could be affected; (3) the ability of

operators to respond in a correct and timely manner to plant transients and accidents;

and (4) if WCNOC has identified and implemented appropriate corrective actions

associated with operator workarounds.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected three post maintenance test activities of risk significant

systems or components. For each item, the inspectors: (1) reviewed the applicable

licensing basis and/or design-basis documents to determine the safety functions,

(2) evaluated the safety functions that may have been affected by the maintenance

activity, and (3) reviewed the test procedure to ensure it adequately tested the safety

function that may have been affected. The inspectors either witnessed or reviewed test

data to verify that acceptance criteria were met, plant impacts were evaluated, test

Enclosure

-9-

equipment was calibrated, procedures were followed, jumpers were properly controlled,

the test data results were complete and accurate, the test equipment was removed, the

system was properly realigned, and deficiencies during testing were documented. The

inspectors also reviewed the corrective action program to determine if WCNOC

identified and corrected problems related to post maintenance testing.

C June 28, 2005, safety injection system Valve EMHV-8807B

C August 5, 2005, auxiliary feedwater Pump A room cooler replacement

C September 19, 2005, turbine-driven auxiliary feedwater pump

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

For the four surveillances listed below, the inspectors reviewed the Updated Final

Safety Analysis Report, procedure requirements, and Technical Specifications to

ensure that the four surveillance activities demonstrated that the SSCs tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the following significant surveillance test attributes

were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;

(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead

controls; (7) test data; (8) testing frequency and method demonstrated Technical

Specification operability; (9) test equipment removal; (10) restoration of plant systems;

(11) fulfillment of ASME Code requirements; (12) updating of performance indicator

data; (13) engineering evaluations, root causes, and bases for returning tested SSCs

not meeting the test acceptance criteria were correct; (14) reference setting data; and

(15) annunciators and alarms setpoints. The inspectors also verified that WCNOC

identified and implemented any needed corrective actions associated with the

surveillance testing.

  • July 7, 2005, STS EJ-100A, RHR System Inservice Pump A Test,

Revision 29

  • July 20, 2005, STS KJ-013B, Hot Restart of Emergency D/G NE02, Revision 4
  • August 12, 2005, STS BB-005, RCS Water Inventory Balance Using Excel,

Revision 5

  • September 8, 2005, STS KJ-015A, Manual/Auto Fast Start, Sync and Loading

of EDG NE10, Revision 19

Enclosure

-10-

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

The drill listed below contributed to drill/exercise performance and emergency response

organization performance indicators. The inspectors: (1) observed the training

evolution to identify any weaknesses and deficiencies in classification, notification, and

protective action requirements development activities; (2) compared the identified

weaknesses and deficiencies against WCNOC identified findings to determine whether

WCNOC is properly identifying failures; and (3) determined whether licensee

performance is in accordance with the guidance of the Nuclear Energy Institute 99-02

documents acceptance criteria.

  • June 29, 2005, the inspectors observed and reviewed emergency drill activities

in the simulator control room and the emergency offsite facility. The drill

scenario involved a loss of control room annunciators with a concurrent loss of

the plant computer, a generator trip with a failure of the control rods to

automatically trip, an offsite release due to a gas decay tank relief valve failure,

and a loss of normal power to the vital alternating current busses. The

inspectors attended the control room critique, reviewed drill related documents,

and discussed the drill activities with various licensee personnel.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess WCNOCs performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspector used the

requirements in 10 CFR Part 20, Technical Specifications, and WCNOCs procedures

required by Technical Specifications as criteria for determining compliance. The

Enclosure

-11-

inspector interviewed the stations ombudsman, licensing and radiation protection

personnel, and reviewed the following items:

  • Corrective action documents related to the access control program
  • Special report related to the access control program

The inspector completed 2 of the required 21 samples.

b. Findings

1. Introduction: The inspector identified a Green noncited violation of Technical

Specification 5.4.1a procedure. Specifically, on September 22, 2003, WCNOC failed to

perform an exit whole body count on a radiation worker who had terminated their

employment with WCNOC.

Description: On May 3, 2005, the NRC requested that WCNOC respond to a concern

about whether an exit whole body count was performed as required by procedure.

Wolf Creek Nuclear Operating Corporation conducted an investigation and concluded

that on September 22, 2003, WCNOC failed to perform an exit whole body count on a

radiation worker during their last day at work, and that no subsequent whole body count

had been performed. An entry was made into the radiologically controlled area since

the last whole body count for the individual. The investigation also concluded that

WCNOC did not generate a required form when an exit whole body count was not

performed.

Analysis: The failure to perform an exit whole body count is a performance deficiency.

This finding is determined to be more than minor because it is associated with the

Occupational Radiation Safety Cornerstone Attribute of Programs and Process, and it

affected the cornerstone objective to ensure the adequate protection of worker health

and safety from exposure to radiation and radioactive materials. This finding was

processed through the occupational radiation safety significant determination process

because the occurrence involved conditions that were contrary to licensee procedures

related to measuring worker dose. The finding was determined to be of very low safety

significance (Green) because it did not involve: (1) as low as is reasonably

achievable (ALARA) planning and work controls, (2) an overexposure, (3) a substantial

potential for an overexposure, or (4) an impaired ability to assess dose.

Enforcement: Technical Specification 5.4.1a requires procedures be implemented in

accordance with Regulatory Guide 1.33, Revision 2, Appendix A. Section 7e, to

Regulatory Guide 1.33 requires radiation protection procedures for personnel

monitoring. Station Procedure RPP 03-405, step 9.5.2, requires that a whole body

count be performed. In addition, step 9.5.4 of the procedure states, in part, that if a

whole body count is not performed, and an entry was made into the radiologically

controlled area since the last whole body count, generate a request for exit whole body

count. It was determined that this request for exit whole body count could not be

located and that an exit whole body count was not performed. Because this violation

was of very low safety significance and was entered into WCNOCs corrective action

Enclosure

-12-

program as PIR 2005-1653, it is being treated as a noncited violation, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 005000482/200500403, failure to

perform an exit whole body count.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual

and collective radiation exposures ALARA. The inspectors used the requirements in

10 CFR Part 20 and WCNOCs procedures required by Technical Specifications as

criteria for determining compliance. The inspectors interviewed licensee personnel and

reviewed:

  • Five outage and online maintenance work activities scheduled during the

inspection period and associated work activity exposure estimates which were

likely to result in the highest personnel collective exposures

  • Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

  • Exposure tracking system
  • Workers use of the low dose waiting areas
  • Exposures of individuals from selected work groups
  • Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

  • Source-term control strategy or justifications for not pursuing such exposure

reduction initiatives

  • Specific sources identified by WCNOC for exposure reduction actions and

priorities established for these actions and results achieved against since the

last refueling cycle

  • Declared pregnant workers during the current assessment period, monitoring

controls, and exposure results

  • Resolution through the corrective action process of problems identified through

postjob reviews and postoutage ALARA report critiques

  • Corrective action documents related to the ALARA program and followup

activities such as initial problem identification, characterization, and tracking

Enclosure

-13-

  • Self-assessments, audits, and special reports related to the ALARA program

since the last inspection

  • Effectiveness of self-assessment activities with respect to identifying and

addressing repetitive deficiencies or significant individual deficiencies

The inspector completed 6 of the required 15 samples and 7 of the optional samples.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

Resident Inspector Annual Sample Review

a. Inspection Scope

The inspectors evaluated the effectiveness of WCNOCs corrective action program as

applied to corrective action document PIR 2005-2142. This document was initiated to

address the conditions and events that led to the inoperability of both site fire protection

pumps. Attributes considered during this review included the following:

  • Completeness, accuracy, and timeliness of problem identification
  • Operability and reportability evaluation
  • Extent of condition evaluation
  • Apparent cause evaluation
  • Prioritization
  • Corrective action effectiveness

The inspectors completed one sample.

b. Findings

Failure to Follow the Clearance Order Procedure

Introduction: An apparent violation (AV) of Technical Specification 5.4.1a occurred

when station personnel failed to follow Procedure AP 21E-001, Clearance Orders,

and manipulated a component inside a fire protection piping clearance boundary

without instructions and authorization. The starting of a temporary fire pump resulted in

water spraying on the controller of the operable diesel-driven fire pump through an

open vent valve, which rendered the pump inoperable.

Enclosure

-14-

Description: On June 30, 2005, the motor of the electric fire pump experienced a short

in its winding which led to a fire at the motor. The plant took the appropriate

compensatory measures and started parallel paths to restore the fire suppression water

system within the allotted 14 days. One path involved a temporary modification to the

fire protection system that installed a temporary motor-driven fire pump, which was

accomplished on July 11, 2005. The temporary fire pump was tested on July 12, 2005,

to verify it would provide the required flow of water suppression; however, the pump

failed this test.

Station fire protection personnel requested a clearance order to isolate the temporary

fire pump from the fire protection piping but failed to make station operations personnel

aware of the desire to run the temporary fire pump following repairs. Once repairs to

the pump were completed, the vendor under the direction of station fire protection

personnel started the pump believing they had authorization to operate the temporary

fire pump. This resulted in water issuing from an open vent valve which sprayed the

controller of the diesel-driven fire pump. Station fire protection personnel discovered

the wet controller and notified the control room. Control room personnel declared the

diesel-driven fire pump inoperable. The diesel-driven fire pump was returned to service

in approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The inspectors reviewed Procedure AP-10-103, Fire Protection Impairment Control,

Revision 19, which identified the compensatory measures for the loss of fire

suppression water systems. With the motor driven and the diesel driven fire pump

inoperable (approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />) the impairment control procedure required that a

backup fire pump be provided within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. In this case, both the motor driven and

the diesel driven fire pumps were restored within approximately 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />. This issue

involved human performance crosscutting aspects associated with station personnel

not following a station procedure.

Analysis: The failure to follow station procedures is a performance deficiency. The

finding was determined to be more than minor because it affected the mitigating

systems cornerstone objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

the Phase 1 worksheets in Manual Chapter 0609, Significance Determination

Process, the finding was determined to degrade the fire protection system suppression

and was evaluated using Appendix F, Fire Protection Significance Determination

Process. This finding requires a Phase 3 analysis and is currently under evaluation.

Wolf Creek Nuclear Operating Corporation entered this finding into their corrective

action program as PIR 2005-2142

Enforcement: Technical Specification 5.4.1a requires procedures be implemented in

accordance with Regulatory Guide 1.33, Revision 2, Appendix A. Regulatory

Guide 1.33, Appendix A, Section 9, requires procedures for the performance of station

maintenance. Contrary to the above, on July 13, 2005, station personnel operated

components inside an established fire protection piping clearance boundary without

work instructions or control room authorization as required by Station

Procedure AP 21E-001, Clearance Orders, Section 6.6.8. This resulted in an

Enclosure

-15-

adjacent diesel-driven fire pump becoming inoperable. Pending determination of the

final safety significance of this issue, this violation is being treated as an AV consistent

with Section VI.A of the NRC Enforcement Policy: AV 05000482/0500404,

manipulation of plant component without proper authorization results in inoperable fire

protection pumps.

Corrective Action Effectiveness

There were no findings identified that were associated with the corrective actions for

this event. However, the inspectors made the following observations from their review

of the apparent cause evaluation and the associated corrective actions: The apparent

cause evaluation states that some fire protection personnel are unfamiliar with the

clearance order program because, for them, clearance orders are infrequently

performed evolutions. Additionally, the evaluation states that some groups mistakenly

believed it was acceptable to work on vendor equipment inside clearance order

boundaries without proper authorization or an approved procedure. These evaluation

results suggest a clearance order program knowledge deficiency within the fire

protection group. Yet, the corrective action for these contributing causes was

counseling only the one individual involved with this event.

.2 Cross-References to Problem Identification & Resolution Findings Documented

Elsewhere

Section 1R15 documents a condition where station personnel did not properly evaluate

a condition adverse to quality regarding debris in the auxiliary feedwater flow

transmitters.

.3 Access Control to Radiologically Significant Areas and ALARA Inspections

Section 2OS1 evaluated the effectiveness of WCNOC's problem identification and

resolution processes regarding access controls to radiologically significant areas and

radiation worker practices. The inspectors reviewed corrective action documents for

root cause/apparent cause analysis against WCNOCs PI&R process. No findings of

significance were identified.

Section 2OS2 evaluated the effectiveness of WCNOC's PI&R processes regarding

exposure tracking, higher than planned exposure levels, and radiation worker practices.

The inspector reviewed the corrective action documents listed in the attachment

against WCNOCs PI&R program requirements. No findings of significance were

identified.

Enclosure

-16-

4OA4 Crosscutting Aspects of Findings

Cross-Reference to Human Performance Findings Documented Elsewhere

Section 1R14 describes a condition associated with station personnel failing to follow

procedure requirements to adequately complete an evaluation of energy/fluid transfer

paths.

Section 2OS1 describes a condition associated with station personnel not following a

procedure for the performance of an exit whole body count.

Section 4OA2 describes a condition associated with station personnel not following a

clearance order procedure that rendered the remaining fire pump inoperable.

4OA5 Other

1. Temporary Instruction (TI) 2515/161 - Transportation of Reactor Control Rod Drives in

Type A Packages

a. Inspection Scope

This area was inspected to verify that WCNOCs radioactive material transportation

program complies with specific requirements of 10 CFR Parts 20 and 71, and

Department of Transportation regulations contained in 49 CFR Part 173. The inspector

interviewed licensee personnel and determined that WCNOC had undergone

refueling/defueling activities between January 1, 2002, and present, but it had not

shipped irradiated control rod drives in Department of Transportation Specification 7A,

Type A packages.

b. Findings and Observations

No findings of significance were identified.

4OA6 Meetings, including Exit

On May 12, 2005, the inspector discussed the TI 2515/161 inspection findings with

Ms. P. Bedgood, Superintendent, Chemistry/Radiation Protection. The inspectors

asked WCNOC whether any materials examined during the inspections should be

considered proprietary. No proprietary information was identified.

On July 1, 2005, the inspector discussed the access control to radiologically significant

areas inspection findings with Ms. P. Bedgood, Superintendent, Chemistry/Radiation

Protection, and other members of your staff who acknowledged the findings. The

inspector verified that no proprietary information was provided during the inspection.

On July 1, 2005, the inspector presented the ALARA planning and controls inspection

results to Mr. M. Sunseri, Vice President Oversight, and other members of his staff who

Enclosure

-17-

acknowledged the findings. The inspector confirmed that proprietary information was

not reviewed during the inspection.

On July 14, 2005, the inspector discussed the inspection findings with Ms. P. Bedgood,

Superintendent, Chemistry/Radiation Protection, and Mr. B. Muilenburg, Licensing

Engineer, Licensing, who acknowledged the findings. The inspector verified that no

proprietary information was provided during the inspection.

On August 17, 2005, the inspector presented the results of TI 2515/163, Operational

Readiness of Offsite Power, Follow-up, with Mr. K. J. Moles, Manager, Regulatory

Affairs, and other members of the staff, who acknowledged the findings. The inspector

verified that no proprietary information was provided during the inspection.

On September 28, 2005, the inspectors presented the resident inspection results to Mr.

S. E. Hedges and other members of licensee management after the conclusion of the

inspection. The inspector verified that no proprietary information was provided during

the inspection.

4OA7 Licensee-Identified Violations

The following finding is of very low significance, was identified by WCNOC and is a

violation of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as a noncited violation.

In part, 10 CFR 50.9(a) requires that information provided to the Commission by a

licensee shall be complete and accurate in all material respects. A Severity Level IV

violation of 10 CFR 50.9(a) was identified because from January 1, 1994, through

December 31, 2003, more than 850 radiation dose reports were submitted to the

Commission with inaccurate radiation dose information. The finding is greater than

minor because of the number of records involved and the duration of the

noncompliance. The finding is not suitable for significant determination process

evaluation, but has been reviewed by NRC management and is determined to be a

Green finding of very low safety significance. This finding is documented in WCNOCs

corrective action program as PIR 2004-2700.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

-1-

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

R. A. Muench, President and Chief Executive Officer

M. Sunseri, Vice President Oversight

K. A. Harris, Director, Performance Improvement and Learning

S. E. Hedges, Vice President Operations and Plant Manager

K. Scherich, Director Engineering

T. East, Manager, Emergency Planning

P. Bedgood, Superintendent, Chemistry/Radiation Protection

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

050000482/200500404 AV Manipulation of plant component without proper

authorization results in inoperable fire protection pumps

(Section 4OA2)

Opened and Closed

050000482/200500401 NCV Failure to follow station procedures results in transfer of

water from VCT to RWST (Section 1R14)

050000482/200500402 NCV Inadequate corrective actions fail to prevent subsequent

failure of auxiliary feedwater flow transmitters

(Section 1R15)

050000482/200500403 NCV Failure to perform an exit whole body count

(Section 2OS1)

LIST OF DOCUMENTS REVIEWED

In addition to the documents referred to in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the

inspection and to support any findings:

A-1 Attachment

-2-

Section 1R01: Adverse Weather

STN GP-001, Plant Winterization, Revision 34

Section 1R04: Equipment Alignment

CKL AL-120, Auxiliary Feedwater Normal Lineup, Revision 33A

CKL EG-120, Component Cooling Water System Valve, Switch and Breaker Lineup,

Revision 36

CKL EM-120, Safety Injection System Lineup Checklists, Revision 22A

Station Drawings:

M-12AL01, Revision 6

M-12EG01, Revision 9

M-12EG02, Revision 4

M-12EG03, Revision 3

M-12EM01, Revision 16

M-12EP01, Revision 5

Section 1R12: Maintenance Effectiveness

Residual heat removal system health report

Maintenance rule performance evaluations

Functional failure evaluations - residual heat removal and essential service water systems

Final scope evaluations for the residual heat removal system

Maintenance rule expert panel meeting minutes for residual heat removal system

PIRs 2005-1175, -1336, and -1477

Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Procedure AP 22C-003, Operational Risk Assessment Program, Revision 9.

Section 1R14: Operator Performance During Nonroutine Evolutions and Events

AP 21D-002, Evaluation for Potential Energy/Fluid Transfer Paths, Revision 8

OFN BB-007, RCS Leakage High, Revision 12

PIR 19952808

Section 1R15: Operability Evaluations

OE AL-05-001

PIRs 2005-1514 and -2247

Section 1R19: Postmaintenance Testing

A-2 Attachment

-3-

Proto HX model verification for room Cooler SGF02A

STN PE-036, Safety-Related Room Cooler Heat Transfer Verification and Performance

Trending, Revision 10

STN PE-037A, ESW Train A Heat Exchanger Flow and DP Trending, Revision 8

STS AL -103, TDAFW Pump Inservice Pump Test, Revision 38

STS PE-007, Periodic Verification of Motor-Operated Valves, Revision 2

Work Orders: 04-259616-009, 04-260057-000, -001, 05-273227-000, 05-273363-001, and

05-273773-002

Section 1R22: Surveillance Testing

STS-IC-615A, Slave Relay Test K615 Train a Safety Injection, Revision 18

Section 1EP6: Drill Evaluation

Emergency notification forms

Emergency response log

Sequence of events logs

Section 2OS1: Access to Radiologically Significant Areas

PIRs 2005-1652, -1653, and -1662

Special Report

Licensee response to Allegation No. RIV-2005-A-0046, dated June 2, 2005

Section 2OS2: ALARA Planning and Controls

Procedures

AP 25A-001, Radiation Protection Manual, Revision 11

AP 25B-100, Radiation Worker Guidelines, Revision 23

RPP 02-215, Posting of Radiological Controlled Areas, Revision 21

RPP 02-210, Radiation Survey Methods, Revision 25

RPP 02-105, Radiation Work Permit, Revision 22

RPP-03-405, Exposure History Files, Revision 13

ALARA Work Packages and Radiation Work Permits

050070, 051000, 051102, 053220, 053230, 054006, 054007, 054420, 055000, and 055031

A-3 Attachment

-4-

PIRs 2004-0734, -1044, -1120, -1254, -1341, -1420, -1597, -2700, 2005-0013, -0129, -0863, -

0943, -1171, -1324, and -1992

Self-Assessments/Audits

K-615, radiation protection

K-621, radiation protection program

OB-05-1062, RWP and ALARA review for steam generator bowl repair

Miscellaneous Documents

Wolf Creek ALARA long-range exposure/source-term reduction Plan 2002-2006

Strategic Primary Water Chemistry Plan, Revision 2

Personnel contamination event records

Dosimetry records

A-4 Attachment