ML053080243

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IR 05000219-05-011; 08/25/2005 - 09/23/2005; Oyster Creek Generating Station; Event Followup Inspection; Emergency Classification
ML053080243
Person / Time
Site: Oyster Creek
Issue date: 11/04/2005
From: Blough A
Division of Reactor Safety I
To: Crane C
AmerGen Energy Co
Lorson R, RI/DRS/PEB, (610) 337-5282
References
EA-05-199 IR-05-011
Download: ML053080243 (24)


See also: IR 05000219/2005011

Text

November 4, 2005

EA-05-199

Mr. Christopher M. Crane

President and CEO

AmerGen Energy Company, LLC

200 Exelon Way, KSA 3-E

Kennett Square, PA 19348

SUBJECT:

OYSTER CREEK NRC EVENT FOLLOWUP INSPECTION REPORT

05000219/2005011; PRELIMINARY WHITE FINDING

Dear Mr. Crane:

On September 23, 2005, the U. S. Nuclear Regulatory Commission (NRC) completed an

inspection of an event that occurred at your Oyster Creek Generating Station on August 6,

2005, involving sea grass intrusion into your intake structure. The enclosed inspection report

documents the inspection findings, which were discussed with Mr. B. Swenson, Site Vice

President, and other members of your staff during an exit meeting held on September 23, 2005.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed procedures, records, investigation and analysis reports and

interviewed personnel.

This report documents one finding that appears to have low to moderate safety significance.

This finding involved the failure to properly utilize the Oyster Creek Emergency Plan (E-Plan)

emergency action level (EAL) matrix during an actual event. This resulted in operators not

recognizing that plant parameters met the EAL thresholds for declaring an unusual event (UE)

and a subsequent Alert. Specifically, a large amount of sea grass had clogged the north side

intake structure screens resulting in a decrease in the intake structure water level.

Subsequently, the intake water level decreased over a period of approximately 60 minutes

meeting the values expected for a UE and then an Alert.

The finding was assessed using the emergency preparedness significance determination

process dated March 6, 2003, as a potentially safety significant finding that was preliminarily

determined to be White (i.e., a finding with some increased importance to safety which may

require additional NRC inspection). The finding appears to have low to moderate safety

significance because a Risk Significant Planning Standard implementation problem occurred

during an actual event. The fact that the shift crew did not recognize Alert conditions prevented

the activation of both onsite and offsite emergency response organizations (ERO). Had the

event degraded further, the onsite ERO could not have been readily available to assist in the

mitigation of the event and the offsite agencies could have been prevented from taking initial

Mr. Christopher M. Crane

2

offsite response measures. Although the shift crew took actions to mitigate the event and the

actual consequences of this event were minimal, the performance problems that caused the

failure to classify, if uncorrected, could result in inadequate protection of the public health and

safety under different circumstances.

Your staff implemented immediate corrective actions, including providing additional guidance to

the operators and operator training on implementation of the E-Plan. Therefore, the finding

does not present an immediate safety concern. We understand that long-term corrective and

preventive measures are being developed.

The finding is an apparent violation of NRC requirements (10 CFR 50.54(q) and 50.47(b)(4))

and is being considered for escalated enforcement action in accordance with the NRC

Enforcement Policy. The current policy is included on the NRCs website at

http://www.nrc.gov; select What We Do, Enforcement, then Enforcement Policy.

We believe we have sufficient information to make a final risk significance determination on this

issue. However, before we make a final decision on this matter, we are providing you an

opportunity to: (1) present to the NRC your perspectives on the facts and assumptions used by

the NRC to arrive at the finding and its significance, at a Regulatory Conference, or (2) submit

your position on the finding to the NRC in writing. If you request a Regulatory Conference, it

should be held within 30 days of the receipt of this letter and we encourage you to submit

supporting documentation at least one week prior to the conference in an effort to make the

conference more efficient and effective. If a Regulatory Conference is held, it will be open for

public observation and a press release will be issued announcing it. If you decide to submit

only a written response, such submittal should be sent to the NRC within 30 days of the receipt

of this letter.

Please contact Mr. Raymond K. Lorson at (610) 337-5282 within 7 days of the date of this letter

to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on this matter.

In addition, this report documents four findings of very low safety significance (Green), one of

which was licensee-identified. Three of the four green findings involved violations of NRC

requirements. However, because of the very low safety significance and because they are

entered into your corrective action program, the NRC is treating those three findings as non-

cited violations consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest

any non-cited violations in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission,

ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region I, the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Oyster

Creek facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response if any will be made available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

Mr. Christopher M. Crane

3

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Should you

have any questions, please contact Mr. Raymond K. Lorson at (610) 337-5282.

Sincerely,

/RA/

A. Randolph Blough, Director

Division of Reactor Safety

Docket No.

50-219

License No.

DPR-16

Enclosure:

Inspection Report 05000219/2005011

w/Attachments A and B

cc w/encl:

Chief Operating Officer, AmerGen

Site Vice President, Oyster Creek Nuclear Generating Station, AmerGen

Plant Manager, Oyster Creek Generating Station, AmerGen

Regulatory Assurance Manager, Oyster Creek, AmerGen

Senior Vice President - Nuclear Services, AmerGen

Vice President - Mid-Atlantic Operations, AmerGen

Vice President - Operations Support, AmerGen

Vice President - Licensing and Regulatory Affairs, AmerGen

Director Licensing, AmerGen

Manager Licensing - Oyster Creek, AmerGen

Vice President, General Counsel and Secretary, AmerGen

T. ONeill, Associate General Counsel, Exelon Generation Company

J. Fewell, Assistant General Counsel, Exelon Nuclear

Correspondence Control Desk, AmerGen

J. Matthews, Esquire, Morgan, Lewis & Bockius LLP

Mayor of Lacey Township

K. Tosch, Acting Assistant Director of Radiation Programs, State of New Jersey

Chief, Bureau of Nuclear Engineering, NJ Dept. of Environmental Protection

R. Shadis, New England Coalition Staff

N. Cohen, Coordinator - Unplug Salem Campaign

W. Costanzo, Technical Advisor - Jersey Shore Nuclear Watch

E. Gbur, Chairwoman - Jersey Shore Nuclear Watch

E. Zobian, Coordinator - Jersey Shore Anti Nuclear Alliance

J. Picciano, Acting Regional Director, FEMA Region II

Mr. Christopher M. Crane

4

Distribution w/encl: (VIA E-MAIL)

S. Collins, RA

M. Dapas, DRA

R. Bellamy, DRP

R. Fuhrmeister, DRP

M. Ferdas, DRP, Senior Resident Inspector

J. DeVries, DRP, Resident OA

S. Lee, RI OEDO

R. Laufer, NRR

P. Tam, PM, NRR

T. Colburn, NRR

J. Boska, NRR

ROPreports@nrc.gov

Region I Docket Room (with concurrences)

M. Johnson, OE

S. Figueroa, OE

M. Elwood, OGC

K. Farrar, ORA , RI

D. Holody, EO, RI

R. Urban, ORA, RI

C. ODaniell, ORA, RI

R. Kahler, NSIR/EPD

S. LaVie, NSIR/EPD

A. Blough, DRS

R. Lorson, DRS

N. McNamara, DRS

DOCUMENT NAME: E:\\Filenet\\ML053080243.wpd

SISP Review Complete: NSP (Reviewers Initials)

After declaring this document An Official Agency Record it will be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RI/DRS

RI/DRS

RI/DRP

RI/DRS/SRA

RI/OE

NAME

NMcNamara (NTM)

RLorson(NSPfor)

RBellamy (RLF for) WCook (WLS for)

RUrban (RJU)

DATE

11/01/05

11/01/05

11/01/05

11/02/05

11/01/05

OFFICE

NSIR/EPD

RI/DRS

NAME

LaVie (via email)

ABlough (ARB)

DATE

11/02/05

11/04/05

OFFICIAL RECORD COPY

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.

50-219

License No.

DPR-16

Report No.

05000219/2005011

Licensee:

AmerGen Energy Company, LLC (AmerGen)

Facility:

Oyster Creek Generating Station

Location:

Forked River, New Jersey

Dates:

August 25, 2005 - September 23, 2005

Inspectors:

Nancy T. McNamara, Emergency Preparedness Inspector

Jeffrey Herrera, Resident Inspector, Oyster Creek

Steven Dennis, Operator Licensing Examiner

Andrew Rosebrook, Project Engineer

Approved by:

Raymond K. Lorson, Chief

Plant Support Branch 1

Division of Reactor Safety

ii

Enclosure

TABLE OF CONTENTS

Page

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iii

1.0

EVENT DESCRIPTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.1

Event Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

2.0

PLANT RESPONSE: PERSONNEL . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

2.1

Operator Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

3.0

EMERGENCY PREPAREDNESS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

3.1

Emergency Response Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

4.0

EVENT ROOT CAUSES AND CAUSAL FACTORS . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

4.1

Root Causes Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

5.0

Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

6.0

Meetings, including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

ATTACHMENT A: SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

ATTACHMENT B: SEQUENCE OF EVENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . B-1

iii

Enclosure

SUMMARY OF FINDINGS

IR 05000219/2005-011; 08/25/2005 - 09/23/2005; Oyster Creek Generating Station; Event

Followup Inspection; Emergency Classification.

The report covered an event followup inspection by three regional inspectors and one resident

inspector. Four Green findings, three of which were non-cited violations (NCVs), and one

apparent violation (AV) with preliminary White significance were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual

Chapter (IMC) 0609, Significance Determination Process (SDP). The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing non-cited violation (NCV) of Technical Specification 6.8.1 was

identified for failure to follow an abnormal operating procedure that resulted in the loss

of the No. 1 North Intake Service Water Pump, the No.1 Emergency Service Water

system and the associated containment spray heat exchangers. The licensee took

immediate corrective actions which included the issuance of standing orders to reinforce

managements expectations and provided interim guidance related to the shortcomings

of the shift crews performance.

This finding is greater than minor because the failure to follow the abnormal procedure

impacted the control rooms ability to adequately monitor intake levels and impacted

prompt operator response actions due to decreasing intake level. This finding is

associated with the cornerstone objectives of Initiating Events, Mitigating Systems and

Containment Barriers Cornerstones. The attributes affected are protection against

external factors such as loss of heat sink, equipment performance in availability and

reliability, human performance in human error (pre-event), containment structure system

and component and barrier performance. The cause of the finding is related to the

cross-cutting element of human performance (personnel). (Section 2.0)

Cornerstone: Emergency Preparedness (EP)

Preliminary White. An NRC-identified apparent violation (AV) of 10 CFR 50.47(b)(4)

was identified. This AV, which has low to moderate safety significance, occurred

because the Oyster Creek E-Plan EAL matrix was not properly utilized to determine if a

plant parameter met the EAL threshold for declaring an emergency classification. This

resulted in not recognizing during an actual event, that plant parameters met the EAL

thresholds for declaring a UE and a subsequent Alert. Immediate corrective actions

were taken in which shift crews were retrained on the implementation of E-Plan

requirements.

The finding is greater than minor because it is associated with the EP cornerstone

attribute of response organization (RO) performance (actual event response). It affects

the cornerstone objective of ensuring the capability to implement measures to protect

the health and safety of the public during an emergency. The licensee did not use the

Oyster Creek E-Plan EAL matrix when plant parameters met the EAL thresholds for

iv

Enclosure

declaring a UE and a subsequent Alert. As a consequence, both the onsite and offsite

EROs were not activated during actual Alert conditions. Had the event degraded

further, the onsite ERO would not have been readily available to assist in the mitigation

of the event and the offsite agencies could have been prevented from taking initial

offsite response measures. This finding is of low to moderate safety significance

because it constituted a failure to implement a Risk Significant Planning Standard during

an actual event in which plant conditions met an Alert. The cause of the finding is

related to the cross-cutting element of human performance (personnel). (Section 3.1)

Green. A self-revealing NCV of 10 CFR 50.47(b)(2) was identified in which state and

local agencies were not notified within 15 minutes after declaring a UE. The licensee

immediately re-trained shift managers in the offsite notification process and proper

completion of the notification form.

This finding is greater than minor because it affects the RO performance (actual event

response) attribute of the EP cornerstone. Failure to notify offsite agencies in a timely

manner impacts the EP cornerstone objective of ensuring that the licensee is capable of

implementing adequate measures to protect the public health and safety during an

emergency. Timely offsite notifications enable state and local agencies to make

decisions for taking initial offsite response measures that could affect the general public.

This finding is of very low safety significance because it was a failure to implement a

Risk Significant Planning Standard during an actual event associated with the

notification of a UE. The cause of this finding is related to the cross-cutting element of

human performance (personnel). (Section 3.1)

Cornerstone: Miscellaneous

Green. The inspectors identified a green finding for ineffective corrective actions in that

the root cause analysis team did not correctly identify the amount of time Alert

conditions existed during the August 6, 2005, event. AmerGen initiated some of their

immediate corrective actions and their analysis of the significance of this event based on

the Alert lasting for five minutes when it actually lasted for approximately 45 minutes.

The licensee confirmed the error, revised the root cause analysis report and entered this

issue into their corrective action program.

The finding was more than minor because if left uncorrected, it could have resulted in a

more significant safety concern. Specifically, failure to accurately identify information

pertaining to operating events can lead to deficiencies in corrective actions. Because

this finding does not involve a violation of regulatory requirements, this finding is not

suitable for SDP evaluation, but has been reviewed by NRC management and is

determined to be a finding of very low safety significance. The cause of the finding is

related to the cross-cutting element of problem identification and resolution. (Section

4.0)

B.

Licensee-Identified Findings

A violation of very low safety significance, which was identified by the licensee has been

reviewed by the inspector. Corrective actions taken or planned by the licensee has

been entered into the licensees corrective action program. The violation and corrective

action tracking number are listed in Section 5.0 of this report.

Enclosure

REPORT DETAILS

1.0

EVENT DESCRIPTION

1.1

Event Summary: During the evening of August 5, 2005, Oyster Creek had a higher than

normal level of sea grass build up on the north side of the intake structure. AmerGen

dispatched a team to clear the intake structure screens of the grass. By 1:57 a.m., on

August 6, 2005, conditions had deteriorated resulting in a control room alarm due to

high traveling water screen differential pressure. AmerGen determines the intake water

level from a differential pressure reading via a gas bubbler at the screen wash control

panel located at the north side of the intake structure. There is no indicator in the

control room for monitoring intake level; therefore, operators have to rely on the

information being communicated from personnel in the field. At 2:35 a.m., the level was

reported at <1.4 pounds per square inch gauge (psig) which required the shift crew to

enter Abnormal Operating Procedure (ABN), No. 32, Abnormal Intake Level. Based

on water level, Procedure ABN-32 required operators to monitor the intake water level

every 15-minutes and to refer to the Oyster Creek E-Plan to evaluate the plant

parameter against the EAL matrix. Operators did not monitor intake water level as

required and also did not refer to the E-Plan EAL matrix at the time the procedure

directed.

At approximately 3:05 a.m, the control room was notified that conditions had further

degraded. The sea grass caused a trash rack on each of the three bays of the north

side of the intake structure to collapse. This placed a heavy load on each of the north

side traveling water screens and caused the screens shear pin to break. The three

screens on the south side were not affected during the event. Water level downstream

of the screens on the north side lowered due to the operation of two circulating water

pumps with the clogged intake. In response to the continued lowering of the north

intake bay level, the operators conducted a rapid reactor power reduction to 75% power

and tripped one of the two operating circulation pumps taking a suction form the north

intake bay. This action decreased the possibility of a reactor scram due to low

condensers vacuum conditions and reduced the water flow across the north intake bay

traveling screen, allowing level downstream of the screens to increase.

The level reduction in the north intake bay rendered the No. 1 Emergency Service Water

Pump, the No. 1 Emergency Service Water (ESW) system and associated containment

spray heat exchangers inoperable. The shift crew entered technical specification

Limiting Condition for Operation (LCO) 3.4.C.3 and continued to reduce power. It was

reported to the control room at 3:10 a.m., that the differential pressure level was 0.5 psig

and rising slowly. Sometime between 2:35 a.m. and 3:05 a.m., plant parameters had

met the thresholds for declaring a UE and a subsequent Alert. However, since the

operators had not instituted level monitoring or entered the E-Plan, they were not

cognizant that plant parameters had met the EAL thresholds for making an emergency

declaration.

At 3:35 a.m., the shift technical advisor (STA), who had been supervising the activities

at the intake structure in the capacity of the field supervisor, returned back to the control

room. The STA reviewed the E-Plan EAL scheme and requested a confirmation of the

current intake water level which was reported at 0 psig. Apparently, the water level did

not recover on a consistent upward trend as initially believed at 3:10 a.m. This was due

to the second circulating water pump still operating, causing the water level to fluctuate

2

Enclosure

up and down. The STA informed the shift manager that the Alert threshold had been

met. At 3:45 a.m., with power reduced to 44%, the second circulating water pump was

secured and all north side intake loads were transferred to the south side intake

structure or removed from service. At that time, the intake water level recovered to 2.7

psig, which no longer met the Alert conditions.

Although the shift manager recognized that the Alert no longer existed, he erroneously

believed that conditions still met the criteria for a UE. Therefore, at 4:03 a.m., the shift

manager declared a UE based on low intake level.

The designated on-shift communicator, who was performing other assigned duties at

the rad waste building and the intake structure, returned to the control room at 4:11 a.m.

The communicator attempted to contact the State of New Jersey via the automatic ring-

down phone which was found to be out of service. The communicator contacted the

state manually and completed the notification by 4:26 a.m., followed by the notification

to the NRC. At 7:55 a.m., AmerGen terminated the UE.

There were no injuries or radiation release associated with this event.

The licensee performed a root cause analysis and identified several operator

performance problems which were related to: inadequate communications; not

recognizing the significance of the degrading conditions; lack of teamwork; and,

inadequate command and control. Short and long-term corrective actions to prevent

recurrence were being developed as a result of the root cause analysis.

2.0

PLANT RESPONSE: PERSONNEL

Cornerstone: Initiating Events

2.1

Operator Performance

a.

Inspection Scope

The inspectors reviewed and assessed licensed operator performance during an actual

event which occurred on August 6, 2005, due to low intake water level. The inspectors

reviewed and evaluated the operators use and adherence to abnormal and emergency

procedures during transient mitigation and subsequent plant operations. The inspectors

interviewed licensed operators involved in the event to assess operator performance

during the transient. Documents reviewed included the following:

1.

operator logs;

2.

normal and abnormal operating procedures;

3.

Exelons corporate event investigation team report; and

4.

AmerGens prompt investigation report.

b.

Findings

Introduction. A self-revealing Green NCV of Technical Specification 6.8.1 was identified

for failure to follow an abnormal operating procedure that resulted in the loss of the No.

3

Enclosure

1 North Intake Service Water Pump, the No.1 ESW system and the associated

containment spray heat exchangers.

Description. During the August 6, 2005, event, control room operators did not establish

a plan to monitor the intake water level as directed by Procedure ABN-32. They never

stationed an individual to specifically monitor the intake level every 15 minutes as

directed by the procedure. This led them to miss a significant drop in level between

2:35 a.m. and 3:05 a.m., which met the UE and Alert classification thresholds. The

failure to follow procedure ABN-32, directly impacted the operators ability to track, trend

and recognize the degrading conditions. This resulted in the loss of the No. 1

Emergency Service Water Pump, the No. 1 ESW system, the associated containment

spray heat exchangers and missed entry into the E-Plan EALs. Refer to Sections 1.0

and Appendix B for additional details of the actions taken by the shift crew while

mitigating the event.

Immediate corrective actions were taken in that the licensee issued standing orders

reinforcing managements expectations and provided interim guidance related to the

shortcomings of the shift crews performance. Long-term corrective actions to prevent

recurrence were being developed as a result of the root cause analysis.

Additionally, the root cause analysis identified previous corrective action items (CAP

Nos. 02003-2361, 02004-0165, and 02004-0123), regarding communication challenges

with respect to the monitoring of intake level from the control room. AmerGen proposed

that a modification to add a control room indicator for recording the intake level be made

to resolve reliance on verbal communications between the control room and operators in

the field. The enhancement was never made a priority or scheduled for implementation

and had remained open since 2003.

Analysis. In accordance with IMC 0612, Appendix B, Issue Disposition Screening, the

inspectors determined that this finding was more than minor because the failure to

follow the abnormal procedure impacted the control rooms ability to adequately monitor

intake levels and impacted prompt operator response actions due to decreasing intake

level. Specifically, operators did not adequately monitor intake levels for degrading

intake conditions which rendered the No. 1 Emergency Service Water Pump, the No. 1

ESW system and associated containment spray heat exchangers inoperable.

The finding is associated with the Initiating Events cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during power operations. The attributes affected include protection against external

factors such as loss of heat sink, equipment performance availability and reliability, and

human performance. The finding is also associated with the Mitigating Systems

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

The attributes affected include protection against external factors such as loss of heat

sink, equipment performance in availability and reliability, and human performance error

(pre-event). In addition, the finding is associated with the Barrier Integrity cornerstone

objective to provide reasonable assurance that physical design barriers protect the

public from radionuclide release caused by accidents or events. The attributes affected

included containment structure system, and component and barrier performance. The

4

Enclosure

cause of the finding is related to the cross-cutting element of human performance

(personnel).

In accordance with IMC 0609, Appendix A, "Significance Determination of Reactor

Inspection Findings for At-Power Situations," the inspectors conducted a significance

determination process (SDP) Phase 1 screening and determined that this finding

required a Phase 2 approximation based upon the finding affecting the Initiating Events,

Mitigating Systems, and Containment Barriers Cornerstones. The inspectors conducted

a Phase 2 evaluation using the Risk-Informed Inspection Notebook for Oyster Creek

Nuclear Generating Station, Revision 1. The inspectors made the following

assumptions: the duration of the low intake water level event was less than one hour,

accordingly, the Table 1, < 3 days column was used to assign Initiating Event

Likelihood; the special initiator worksheet Table 3.10, "Loss of Intake Water Pump Pit

(TIW)" was used for the Phase 2 approximation; the initiating event likelihood value was

increased by one order of magnitude, in accordance with IMC 0609, Appendix A,

Attachment 2 Rule 1.3; and no operator recovery credit was provided. The approximate

change (increase) in core damage frequency as a result of this performance deficiency

was mid E-9, or of very low risk significance (Green). The most dominant core damage

sequence involved a loss of intake water to pump pit, followed by the failure of an

electromatic relief valve (stuck open) and subsequent failure of the low pressure

injection system. For the short duration of the actual event, the adjacent intake bay was

unaffected, and thus, ensured the availability of the redundant trains of mitigating

equipment.

Enforcement. Technical Specification 6.8.1 states that written procedures shall be

established, implemented, and maintained covering the items referenced in AmerGens

Appendix "A" of Regulatory Guide 1.33 as referenced in the licensees Quality

Assurance Topical Report. Abnormal procedures are included in Regulatory Guide 1.33. Contrary to the above, the licensees failure to monitor intake level, as required by

procedure ABN-32, led to an untimely response to a degrading condition caused by

heavy grassing at the intake. As a consequence, the No. 1 Intake Service Water Pump,

the No. 1 ESW system and the associated containment spray heat exchangers were

rendered inoperable. However, because the violation was of very low safety

significance and has been entered into the licensees corrective action program under

issue report (IR) 360630, this violation is being treated as a NCV, consistent with

Section VI.A of the NRC Enforcement Policy. (NCV 05000219/2005011-01, Failure to

Follow Procedures)

3.0

EMERGENCY PREPAREDNESS

3.1

Emergency Response Performance

a.

Inspection Scope

The inspectors reviewed and assessed the licensees performance related to

emergency response and the implementation of the E-Plan during the August 6, 2005,

event. The assessment included interviews with control room operators and plant

personnel who responded to the intake structure to remove the grass. Items reviewed

included the following:

5

Enclosure

operator logs;

abnormal procedures;

Oyster Creek Exelon/AmerGen Radiological Emergency Plan;

emergency plan implementing procedures;

state/local notification forms;

Exelons corporate event investigation team report; and

AmerGens prompt investigation report.

b.

Findings

One NRC-identified preliminary White finding and one self-revealing Green finding are

documented in the section below.

Emergency Classification

Introduction. An NRC-identified apparent violation (AV) was identified of low to

moderate safety significance (White) associated with the emergency classification

during an actual event. AmerGen did not properly utilize the Oyster Creek EAL matrix

which resulted in not recognizing that plant parameters had met the EAL thresholds for

declaring a UE and a subsequent Alert.

Description. Procedure, ABN-32, step four, requires the evaluation of the condition

using the E-Plan EAL matrix, which lists the initiating condition threshold values for

making an emergency declaration. The EAL threshold for intake canal water level

(differential pressure) is <0.94 psig for meeting a UE and <0.50 psig for meeting an

Alert classification. The control room received notification at 2:35 a.m., that the water

level at the north side of the intake structure was measured at <1.4 psig. Sometime

between 2:35 a.m. and 3:05 a.m. plant conditions had met the EAL criteria for declaring

a UE and a subsequent Alert due to the level dropping 1.4 psig to 0 psig. The inspector

determined that the shift manager did not properly utilize the E-Plan EAL matrix as

required by the abnormal procedure, to determine if an emergency classification was

warranted.

The shift manager did not review the E-Plan EAL matrix until approximately 3:40 a.m.,

after being prompted by the STA that plant conditions had met an Alert. Between 3:40

a.m. and 4:00 a.m., the shift manager reviewed the EAL technical basis document and

determined, based on the intent of the EAL, an Alert had been warranted. The shift

manager recognized the Alert no longer existed because the level had recovered to 2.4

psig. However, he erroneously believed the conditions still met the criteria for a UE and

at 4:03 a.m., the shift manager declared a UE based on low intake level.

Analysis. The performance deficiency associated with the response to this actual event

is the Oyster Creek E-Plan EAL matrix was not properly utilized to determine if a plant

parameter met the EAL classification thresholds. Although the intake level exceeded an

EAL threshold sometime between 2:35 a.m. and 3:05 a.m., it was not recognized until

approximately 3:40 a.m., that plant parameters met the EAL threshold for declaring an

Alert. However, an emergency declaration was not made until 4:03 a.m. The inspectors

determined that the licensee should have known of the exceeded EAL threshold by 3:05

a.m., and the delay in recognition and classification could not be reasonably attributed to

6

Enclosure

competing safety-related activities. The inspectors also determined that this finding was

indicative of a cross-cutting weakness in the area of human performance (personnel).

The finding was greater than minor because it is associated with the EP cornerstone

attribute of RO performance (actual event response). It affects the cornerstone

objective of ensuring the capability to implement measures to protect the health and

safety of the public during an emergency. The inspectors reviewed this finding using

IMC 0609, Appendix B, "Emergency Preparedness Significance Determination Process,

Sheet 2, Actual Event Implementation Problem. The finding has low to moderate safety

significance (White) because a Risk Significant Planning Standard implementation

problem occurred during an actual event in that the Oyster Creek E-Plan EAL matrix

was not properly utilized when plant conditions met an Alert. This prevented the

activation of both onsite and offsite EROs during an actual event. Had the event

degraded further, the onsite ERO would not have been readily available to assist in the

mitigation of the event. Additionally, state and local agencies, which rely on information

provided by the facility licensee, could have been prevented from taking initial offsite

response measures.

Immediate corrective actions were taken in that shift crews were re-trained on the

implementation of E-Plan requirements during transient events. Therefore, the finding

does not present an immediate safety concern. Long-term corrective actions to prevent

recurrence were being developed as a result of the root cause analysis.

Enforcement. In accordance with 10 CFR 50.54(q), a licensee authorized to possess

and operate a nuclear power reactor shall follow and maintain in effect emergency plans

which meet the standards in 10 CFR 50.47(b). In accordance with 10 CFR 50.47(b)(4)

a standard emergency classification and action level scheme shall be in use by facility

licensees. State and local response plans call for reliance on information provided by

facility licensees for the determination of minimum initial offsite response measures.

Contrary to the above, between 2:35 a.m. and 3:40 a.m., on August 6, 2005, AmerGen

did not use the Oyster Creek E-Plan EAL matrix during an actual event to determine if

plant parameters met the EAL thresholds for declaring a UE and a subsequent Alert. As

a consequence, AmerGen failed to make an Alert declaration and, as a result, failed to

activate their ERO to assist operators in mitigating the event. Additionally, state and

local agencies, which rely on information provided by the facility licensee, could have

been prevented from taking initial offsite response measures. This finding is identified

as an apparent violation of low to moderate safety significance (White), in accordance

with the NRC Enforcement Policy and was entered into AmerGens corrective action

program as IR 360630. (AV 05000219/2005011-02, E-Plan EAL Matrix Not Reviewed

During Alert Conditions)

Notification of State and Local Agencies

Introduction. A Green self-revealing NCV was identified in that state and local

governmental agencies were not notified within 15 minutes of the declaration of a UE.

Description. As stated previously, at 4:03 a.m., the shift manager declared a UE. The

licensee is required to notify state and local governmental agencies within 15 minutes

after making a declaration. However, for reasons unrelated to the delay in making the

7

Enclosure

declaration, the notification to the State and local governmental agencies was not

completed until 4:26 a.m. The completion time exceeded the notification time criterion

by seven minutes.

The following performance and equipment problems were identified as contributing

factors to the untimely notification: the notification form was not completed in a timely

manner; there was a delay in requesting the on-shift communicator to report to the

control room; on-shift communicator was not able to immediately report to the control

room as required by procedure due to other responsibilities; the state/local automatic

ringdown telephone was inoperable; and, the on-shift communicator was not familiar

with the backup notification process. The inspectors determined that the notification

delays could not be reasonably attributed to competing safety-related activities.

Additionally, the completed notification form contained numerous errors and omissions

including an incorrect emergency classification. The form indicated the declaration of an

Alert when, the shift manager had declared a UE.

AmerGen took immediate corrective actions in which they retrained Oyster Creek shift

managers in the offsite notification process and proper completion of the notification

form. Long-term corrective actions to prevent recurrence were being developed as a

result of the root cause analysis.

Analysis. The inspectors concluded that a performance deficiency was identified

associated with timely notification to state and local governmental agencies during an

actual event. AmerGen did not notify state and local governmental agencies within the

required 15 minutes after declaring a UE. The inspectors also determined that this

finding was indicative of a cross-cutting weakness in the area of human performance

(personnel).

This self-revealing finding was greater than minor because it is associated with the EP

cornerstone attribute of RO performance (actual event response). It affects the

cornerstone objective of ensuring the capability to implement measures to protect the

health and safety of the public during an emergency. The inspectors reviewed this

finding using IMC 0609, Appendix B, "Emergency Preparedness Significance

Determination Process, Sheet 2, Actual Event Implementation Problem. Although a

timely notification was not made for either the UE or Alert condition, the inspectors

based the significance evaluation on a UE classification since the shift manager

ultimately declared a UE. The finding has low safety significance (Green) because it

was a failure to implement a risk significant planning standard during an actual event

associated with the declaration of a UE.

Enforcement. In accordance with 10 CFR 50.54(q), a licensee authorized to possess

and operate a nuclear power reactor shall follow and maintain in effect emergency plans

which meet the standards in 10 CFR 50.47(b). In accordance with 10 CFR 50.47(b)(5)

procedures shall have been established for notification of state and local response

organizations. Also,10 CFR Part 50, Appendix E.D.3, states that a licensee shall notify

the state and local governmental agencies within 15 minutes after declaring an event.

Contrary to the above, during the August 6, 2005, event, the licensee declared a UE at

4:03 a.m. and completed the notification to the State and local governmental agencies

8

Enclosure

at 4:26 a.m. Therefore, AmerGen did not notify state and local governmental agencies

within the required 15 minutes after making a declaration. Timely offsite notifications

enable state and local agencies to make decisions for taking initial offsite response

measures that could affect the general public. Since the violation was of very low safety

significance (Green) and since AmerGen entered the deficiency in to their correction

action program under IR 360630, this finding is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy. (NCV 05000219/2005011-03, Late State

Notification of UE)

4.0

EVENT ROOT CAUSES AND CAUSAL FACTORS

Cornerstone: Miscellaneous

4.1

Root Causes Analysis

a.

Inspection Scope

The inspectors reviewed AmerGens Root Cause Analysis Report, Revision 0 (IR

360630) and interviewed the root cause team leader to assess AmerGens capability to

determine the events causal factors for implementing the appropriate corrective actions

to prevent recurrence. Also the inspector reviewed Oyster Creek Procedure LS-AA-125-

1001, Root Cause Analysis Manual, to determine if the root cause analysis was

conducted in accordance with the procedure.

b.

Findings

Introduction: The NRC identified a green finding for ineffective corrective actions in that

the root cause analysis team did not correctly identify the amount of time Alert

conditions existed during the August 6, 2005, event. AmerGen initiated some of their

immediate corrective actions and their analysis of the significance of this event based on

the Alert lasting for five minutes when it actually lasted for approximately 45 minutes.

Description: NRC inspectors conducted interviews and reviewed operator logs to verify

and validate the licensees event time line and conclusions of the root cause analysis

report. The inspectors identified a significant discrepancy in the licensees event time

line concerning the amount of time the plant was in the Alert condition. The root cause

team had determined that the plant had only been in an Alert condition for a period of

approximately five minutes (3:05 a.m. - 3:10 a.m.) because the level was reported as

slowly rising. However, the NRC inspector discovered during an interview with the STA,

that at 3:35 a.m., the STA requested a pressure level measurement which was reported

at 0 psig. Apparently, the water continued to fluctuate until the second circulating water

pump was secured at 3:45 a.m. The STA stated it was due to this, he recommended to

the shift manager to declare an Alert. Thus, it appears the plant was actually in Alert

conditions for approximately 45 minutes versus the five minutes concluded by the root

cause team.

As a result of the erroneous assumption regarding the duration of the Alert, standing

orders were issued which stated that an event that terminates before identification,

should still be classified and reported, but not declared to implement the E-Plan. They

9

Enclosure

provided further guidance concerning a short spike where conditions rapidly recovered

above the EAL threshold. The appropriate action implied by the briefing, was the event

should have been classified after-the-fact, but not declared.

Based on information provided by the NRC, the licensee issued a revised version of the

root cause report and entered this issue into their corrective action process.

Analysis: A performance deficiency occurred in which AmerGens staff did not properly

determine the amount of time the plant was in an Alert condition as part of a root cause

analysis. Not determining all the significant facts, did not meet the intent of Procedure

LS-AA-125-1001, Root Cause Analysis Manual. The performance deficiency was that

the licensee inaccurately determined the duration that Alert conditions existed during the

August 6, 2005, event, and influenced some of the corrective actions that were

developed to prevent recurrence. The finding was more than minor because if left

uncorrected, it could have resulted in a more significant safety concern. Specifically,

failure to accurately identify information pertaining to operating events can lead to

deficiencies in corrective actions. Specifically, AmerGen initiated some of their

immediate corrective actions and their analysis of the significance of this event based on

the Alert lasting for a short duration. The inspectors also determined that this finding

was indicative of a cross-cutting weakness in the area of problem identification and

resolution.

This finding is not suitable for significance determination process evaluation, but has

been reviewed by NRC management and is determined to be a finding of very low

safety significance (Green). There was no direct impact on human performance and

equipment reliability, and the NRC intervened so that appropriate corrective actions

could be performed. This issue was entered into the licensees corrective action

program as IR No. 00384615. Because this finding does not involve a violation of

regulatory requirements and has very low safety significance, it is identified as FIN

05000219/2005011-04, Inadequate Root Cause Analysis.

Enforcement: Enforcement action does not apply because the performance deficiency

did not involve an explicit violation of a requirement.

5.0

Licensee-Identified Violations

The following finding of very low significance was identified by AmerGen and is a

violation of NRC requirements which meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600 for being dispositioned as a non-cited violation.

In accordance with 10 CFR 50.47(b)(2), adequate staffing must be provided for

initial facility accident response and maintained at all times. Contrary to the

above, during the August 6, 2005, event, both the STA and on-shift

communicator did not perform their emergency response duties in a timely

manner. This was identified in a root cause analysis report and documented in

the licensees corrective action program as IR 360630. This finding was

considered not more than Green significance because it did not constitute a

failure to meet a risk significant planning standard. The inspectors determined

10

Enclosure

that this finding was indicative of a cross-cutting weakness in the area of human

performance (personnel).

6.0

Meetings, including Exit

On September 23, 2005, the inspector presented the inspection results to Mr. B.

Swenson and other AmerGen staff. The inspector confirmed that no proprietary

information was provided or examined during the inspection.

A-1

Attachment

ATTACHMENT A

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Kandasamy, Manager, Regulatory Assurance and Licensing

J. Karkoska, Exelon, MAROG EP Manager

K. Poletti, Site EP Manager

R. Detwiler, Plant Operations Manager

J. Freeman, Plant Operations Superintendent

J. Hackenberg, Training Manager

P. Cervenka, Root Cause Team Leader

R. Brown, Prompt Investigation Team Leader

New Jersey State Department of Environmental Protections

R. Russell, Nuclear Engineer, Bureau of Nuclear Engineering (BNE)

D. Zannoni, Supervisor, Nuclear Engineering, BNE

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000219/2005011-02

AV

EAL Matrix Not Reviewed For Declaring an Alert

(Section 3.1)

Opened and Closed

05000219/2005011-01

NCV

Failure to Follow Procedures

(Section 2.1)05000219/2005011-03

NCV

Untimely State/Local Notification of UE

(Section 3.1)05000219/2005011-04

FIN

Inadequate Root Cause Analysis

(Section 4.1)

Discussed

None

A-2

Attachment

LIST OF DOCUMENTS REVIEWED

Procedures

Exelon Standardized Emergency Plan

Oyster Creek Radiological Emergency Plan

Oyster Creek Emergency Plan Implementing Procedures

OP-OC-100, Oyster Creek Conduct of Operations, Revision 4

EPIP-OC-.01, Classification of Emergency Conditions, Revision 14

EP-OC-114-100, State/Local Notifications, Revision 0

EP-OC-112-100, Control Room Operations, Revision 2

OP-AA-106-101-1001, Event Response Guidelines

LS-AA-125-1001, Root Cause Analysis Guidelines

Corrective Action Reports

IR No. 00360630, UE Declared on August 6, 2005 Due to Low Intake Level

IR No. 00360632, Heavy Grassing at Intake Collapses 3 North Intake Grates

IR No. 00360667, Intake Trash Rake Cable Damaged During Grating Collapse

IR No. 00360670, State/Local Phones Found Inoperable in Intake Level Event

IR No. 00360716, Opportunity To Capture Key Decisions in Operator Logs Missed

IR No. 00360956, Returned to Full Power 4.5 Hrs. Prior Than Shown

IR No. 00361537, Suggested Intake Improvements

IR No. 00362061, Problems at Intake Leading to Alert Declaration on 8/6/2005

IR No. 00362269, OCC Critique for Aug 6th Intake Grassing Event

IR No. 00362338, Revised EP-OC-114-100 Attachment 1

IR No. 00362472, Issues w/OC EAL Matrix

IR No. 00362554, Data Supports an Earlier LCO Entry Time for 8/6/5 ESW LCO

IR No. 00362628, Prompt Investigation Not Commenced in a Timely Manner

IR No. 00365568, NOS Identifies Inadequate ABN-32 Procedure Guidance

IR No. 00366205, Latest OC NLO Class did not Receive Shift Comm. DLA

IR No. 00371847, NOS ID Error Likely Situation During OC EAL Change

IR No. 00384615, Root Cause Report Missing Data Point

CAP No. 02003-2361, Plant Required Rapid Reduction in Power Due to Debris

CAP No. 02004-0165, Unexpected Low Intake Level Event on January 16, 2004

CAP No. 02004-0123, UE Declared on January 16, 2004 Due to Low Intake Level

Miscellaneous

Root Cause Analysis, IR Number 360630, dated September 13, 2005, Revision 0

Oyster Creek Prompt Investigation Report

Independent Review Team Assessment, dated August 15, 2005, Rev. 0

State/Local Notification Form for the UE

State/Local Notification Form for Termination of the Event

Memorandum from State of New Jersey, dated August 10, 2005, Oyster Creek Event

Reactor Plant Event Notification Worksheet No. 41899

Event Summary Report

E-Plan EAL Event Termination and Shift Communicator Expectations White Paper

Operations Standing Order Nos. 69 and 70

LS-AA-125-1001, Root Cause Investigation, dated January, 22, 2004, Low Intake Events

A-3

Attachment

LIST OF ACRONYMS

ABN

Abnormal Operating Procedure

AV

Apparent Violation

CAP

Corrective Action Process

EAL

Emergency Action Level

E-Plan

Emergency Plan

EP

Emergency Preparedness

ERO

Emergency Response Organization

ESW

Emergency Service Water

IMC

Inspection Manual Chapter

IR

Issue Report

LCO

Limiting Condition for Operation

NCV

Non-Cited Violation

NRC

Nuclear Regulatory Commission

PARS

Publicly Available Records

Psig

Pounds per Square Inch Gauge

RO

Response Organization

RSPS

Risk Significant Planning Standard

SDP

Significant Determination Process

SM

Shift Manager

STA

Shift Technical Advisor

UE

Unusual Event

B-1

Attachment

ATTACHMENT B

SEQUENCE OF EVENTS

Entries that appear in italics are notes or observations made by the NRC inspection team.

Times that appear in italics are due to approximations. All entries were obtained from control

room logs, interviews conducted by both the licensee and the NRC, and event notification

forms.

Initial Plant Conditions (Pre-Event) - 100% Reactor Power

Time

Event

[August 5, 2005]

23:00

Higher than normal levels of grass at intake structure reported to control room.

Plant personnel performed backwashing, raking and screen cleaning in attempts

to keep flow through the intake screens.

[August 6, 2005]

01:57

Received alarm k-5-e Intake Screen P Hi into the control room. This was due

to high traveling water screen differential pressure. Alarm cleared within a few

minutes. This was the operators first indication the grass was impeding water

flow.

02:05

On-shift communicator reports to intake structure from rad waste building

(normal duty station) to assist in removing debris.

02:35

Received alarm k-5-e Intake Screen P Hi for second time. Entered Abnormal

Procedure ABN-32, Abnormal Intake Level. Intake level pressure indicator is

less than 1.4 psig or -2.0 ft mean sea level. ABN-32 requires monitoring the

water level at 15 minute intervals. No monitoring schedule was established. No

review of EAL matrix was performed. (UE threshold is <0.94 psig and Alert

threshold is <0.5 psig.)

02:54

STA leaves control room and reports to the intake structure as field supervisor.

03:00

North side #1 traveling screen grate collapsed, traveling screen pin #1 shear pin

had broken.

03:05

Control room receives report that all three traveling screens had broken shear

pins. Screen damage confirmed. Performed rapid power reduction to 75%

power by reducing reactor recirculation flow. Control room informed that the

intake level instrument for the north side indicated 0 psig on the bubble gage.

Plant conditions for the Alert were reached at this time. Since level was not

monitored it is unknown at what time conditions crossed the threshold for a UE.

B-2

Attachment

03:10

No.1-1 main circulator pump removed from service. This was due to the loss of

all north intake traveling screens. No. 2 NRW SW pump was started and #1

pump was secured.

03:10

Water level is noted to have recovered to 0.5 psig and slowly rising. This was

not reported back to the control room.

0313

No. 1-1 service water pump removed from service. This was due to loss of all

north intake traveling screens.

03:15

A-Reactor Water Cleanup removed from service. This was due to partial loss of

cooling to reactor building closed cooling water system.

03:30

Entered: LCO 3.4.C.3. Unplanned. Risk = Yellow action statement; the reactor

may remain in operation for a period not to exceed 7 days provided remaining

containment spray system loop and its associated emergency service water

system loop each have no inoperable components and are verified daily to be

operable. Emergency service water system no.1 and its associated containment

spray system loop is declared inoperable due to loss of the north side screens.

03:34

STA returned to control room, reviewed plant conditions and EAL matrix.

03:35

STA requested another reading of the water level which is reported at 0 psig.

STA made recommendation to declare an Alert. This was the first time the EAL

matrix was reviewed. Although the level initially recovered at 03:10 hours, it

appears the level continued to fluctuate.

03:40

Power is reduced to 44% to remove loads from north side of intake structure.

03:40

Shift Manager reviewed EAL basis document for clarification on the Alert

classification.

03:45

No.1-2 Main circulation water pump removed from service. All north side intake

loads were transferred to the south side intake structure or removed from

service.

03:50

Control room received report that the lower trash grate at No.1-2 traveling screen

had collapsed - intake structure trash rake was stuck where the grating was

damaged.

03:50

Control room is informed that the intake pressure gauge indicated 2.7 psig and

steady. This indicated that the plant was no longer in a Alert condition.

03:55

Communicator returned to rad waste building to take required 04:00 surveillance

readings.

04:00

No. 1-3 traveling screen returned to service.

B-3

Attachment

04:03

SM assumed the duty of Emergency Director and declared a UE. Shift manager

log stated, The north intake water level had been at EAL for an Alert but had

recovered to level for EAL for a UE. The 15-minute notification clock begins.

04:05

Control Room informs the communicator that he is needed in the control room.

04:08

Station alarm sounded and an announcement was made that a UE was

declared.

04:10

No. 1-2 Traveling screen returned to service.

04:11

Communicator entered control room. Shift manager informed communicator that

plant was at an Alert and de-escalated to a UE.

04:15

Communicator attempted to make the offsite notifications using the automatic

ring-down phones. Phone was out of service. This was due to a storm from the

previous evening had tripped a circuit breaker.

04:20

Communicator manually dialed telephone number. This is the backup method to

the ring-down phone.

04:26

Notification completed.

04:30

Intake trash rake returned to service for screens 4, 5, 6 only. Upper grate on No.

1 bay and middle grates on No. 2 and No. 3 bays had collapsed.

04:43

NRC notified of event.

04:50

No. 1 screen returned to service. All north screens were in service. No. 1 and

No. 2 high pressure and No. 4 low-pressure screen wash pumps were in service.

04:55

No. 1 service water pump returned to service.

0755

UE Terminated.

08:11

Exited procedure ABN-32. This was due to satisfactory intake levels above the

requirements to enter ABN-32.

09:08

Exited LCO: 3.4.C.3. Risk is Yellow. This is due to emergency service water

system No. 1 and its associated containment spray system loop was declared

operable after starting each emergency service water pump in system No. 1 and

verifying pumps responded appropriately to a start and 5 minute run. There was

no indication of any air binding. Discharge pressures, system flows and pump

amps all were normal. The north intake was functionally available but degraded,

and as such pant risk remained at yellow until both the north side intake

collapsed racks were replaced and the plant returned to full power.