L-88-166, Forwards mgt-on-shift Weekly Summary Repts,Per 871019 NRC Order

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Forwards mgt-on-shift Weekly Summary Repts,Per 871019 NRC Order
ML17347A726
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/06/1988
From: Conway W
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-88-166, NUDOCS 8804200005
Download: ML17347A726 (62)


Text

ACCELERATED DIS%1BUTION DEMONSTRO'ION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:0804200005 DOC.DATE: 88/04/06 NOTARIZED: NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit. 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATXON CONWAY,W.F.

Florida Power

& Light Co.

RECIP.NAME RECIPIENT AFFXLIATION GRACE,J.N.

Region 2, Ofc of the Director DOCKET 05000250 05000251

SUBJECT:

Forwards mgt-on-shift weekly summary repts,per 871019 NRC ox'dex' DISTRIBUTION CODE:

D036D COPIES RECEIVED:LTR C ENCL /

SIZE: + Q TITLE: Turkey Point Management Onshift Program NOTES RECXPIENT ID CODE/NAME DRP/ADR-2 PD2-2 PD COPIES LTTR ENCL 1

1 1

1.

RECIPIENT ID CODE/NAME NRR/DRP-1/2 EDISON,G COPIES LTTR ENCL 1

1 2

2 Sj A

INTERNAL: AEOD NRR DEPY NRR MORISSEAU,D NRR/ADT 12-G-18 NRR/DOEA DIR 11 NRR/PMAS/ILRB12 OGC 15-B-18 RGN2 FILE EXTERNAL: LPDR NSIC 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 DEDRO NRR DIR NRR/ADP 12-G-18 NRR/DLPQ/PEB NRR/DRIS DIR 9A 0

,XEBE N,J LE 01 NRC PDR 1

1 1,1 1

1 1

1 1

1 1

1 1

1

'A TOTAL NUMBER OF COPXES REQUIRED:

LTTR 23 ENCL 23

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P. O.

14000, JUNO BEACH, FL 33408 0420 gz4ki>>

APRIL' 6

1988 L-88-166 Dr. J. Nelson Grace Regional Administrator, Region II U.S. Nuclear Regulatory Commission 101 Marietta Street, N. W., Suite 2900 Atlanta, Georgia 30323 Re:

Turkey Point Units 3 and 4

Docket Nos.

50-250 and 50-251 Mana ement-on-Shift Weekl Re ort

Dear Dr. Grace:

Pursuant to the Nuclear Regulatory Commission Order dated October 19,

1987, the attached summary of Management-on-Shift (MOS) reports is submitted.

Should there be any questions on this information, please contact us.

Very truly yours, W. F.

Conway Acting Group Vice President Nuclear Energy Department WFC/SDF/gp Attachment cc:

J.

Lieberman, Director, Office of Enforcement, USNRC Dr.

G. E. Edison, Project Manager,

NRR, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant R. E. Talion, President, FPL 8804200005 880406 PDR ADOCK 05000250 R

PDR an FPL Group company

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MANAMENT ON SHIFT (IOTAS)

WEEKLY

SUMMARY

REPORT STARTING.

3/28/88 PAGE I

OF 1

Four MOS Observers were on shift; Daniel H.

West, St.

Lucie Nuclear Plant STA Supervisor (03/28-04/03/88 days),

Peter L.

Walker, Westinghouse Electric Corporation (03/28-04/04/88, nights),

D.

W.

Haase, Turkey Point Nuclear Plant Safety Engineering Group Chairman (03/28-30/88, nights),

and Daryle L.

Osborn, Turkey Point Nuclear Plant Configuration Manager (03/31-04/04/88, nights).

During the reporting period, Unit 4 operated at 100% power.

Unit 3 xeturned to 100% power on March 31, 1988 after the repair of a Unit 3 Condenser Tube leak.

No immediate safety problems were identified during the reporting period.

One questionable work practice was identified concerning a misaligned valve in the Auxiliary Feedwater Nitrogen Backup System for Unit 3.

The misaligned valve did not affect the operability of the system.

During the reporting

period, the MOS Observers noted eleven recommendations or areas for improvements.

These comments and suggestions included:

Three comments were made concerning administrative items associated with control of operational procedures in the PSN files, proper inventory control of spare paxts and I

& C testing of components prior to release to operations.

Two comments were made concerning priority of maintenance work associated with the Nitrogen Backup System to the Main Steam Isolation Valves and Intake Cooling Water System strainer cleaning.

Two comments were made concerning housekeeping practices associated with sandblasting and cleanliness near the Unit 3

steam jet Air, Ejector.

Four miscellaneous comments were made associated with the tightness of the Unit 3 6A and 6B Feedwater Heater anchor bolts, strainer cleaning procedures, two missing tags on the Backup Nitrogen System for the Auxiliary Feedwater System flow contxol valves and precautions associated with placing a

steam jet air ejector in service.

ATTACHMENT:

MOS DAlLY REPORTS

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0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

From:

D. H. West M

bserver)

W Shift:

Qx Day Night Plant evolutions observed

'Unit 4, Steady State full power operation Unit 3, Heat Up from 250 F to 350 F Shift turnovers Plan of day meetings B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement No comment Professionalism, Summary of Shift, Comments Observed shift operations and professionalism to be satisfactory F.

Recommendations None Completed By:

M bserver Date:

Reviewed By:

0 erations Superintendent-Nuclear Management g),

Review By:

PM N AM(N.Ialia7lw

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~VP ate Date 03/28/88

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0-ADM-019 M

agement on Shift (MOS)

MOS DAILYREI'ORT Page To:

Operations Superintendent - Nuclear Date.

03/28-29/88 From:

P. L. Walker (M

bseruer Shift:

Q Day Qx Night Plans evolutions observed Unit 3:

1.

Heatup from 365 to 460 P, recovering from Condenser tube leak outage.

Actions are underway to get conductivity back within limits.

All Emergency Core Cooling Systems (including Accumulators) have been placed in operable status.

2.

Independent verification procedure 3-OSP-075.5 was performed on March 28, 1988 between 1930 and 2105 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.009525e-4 months <br />.

Valve 3-40-1617 (Train I) was found to be in a noncomplying position and immediately reported to the FSN.

The valve's position was subsequently determined to be inappropriate, and was repositioned by a Turbine Operator and a licensed Senior Reactor Operator.

The valve is currently properly

aligned, and system operability was never compromised.

The valve's position was previously checked on day shift on Friday, March 25,

1988, when 3-OP-65.2 was performed on Train 1 of Nitrogen Backup System to Auxiliary Peedwater System.

Unit 4:

Steady State 10000 power B.

Immediate safety problems None C.

Questionable work practices During performance of 3-OP-65.2 (Train 1), valve 1-3-40-1617 was improperly signed off as being in the proper position.

An investigation as to the cause of this nonconformance is currently underway.

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0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Puge Area(s) for improvement None Professionalism, Summary of Shift, Comments The nonconformance was handled

properly, as was another potential problem (loss of all cooling fans on the Startup Transformer).

Operability of the transformer is not compromised by having fans shut off. During my next shift, I willlook into why the fans were off.

Recommendations None Completed By:

P. L. Walker M

bserver Date:

03/28-29/88 Reviewed By:

Operations Superi ntendent-Nuclear Management g ~

Review By:

7 ate 03/28-29/88

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agemeat on Shift (MOS)

MOS DAILYREI'ORT Pose To:

Operations Superintendent-Nuclear Date.

03 28-29 88 From:

(M server)

Shift:

Q Day Qx Night Plant evolutions observed Unit 4, Steady State operation at 100fo power Unit 3, Heatup from 370 to 460'F Observed portions of 3-OP-074, Condensate System Alignment, being performed Investigated previous activities associated with Unit 3 Auxiliary Feedwater Backup Nitrogen System B.

C.

Immediate safety problems None observed Questionable work practices During the performance of 3-OSP-075.5, Auxiliary Feedwater System Flowpath Verification, valve 3-40-1617 on Train 1 of the Auxiliary Feedwater Backup Nitrogen System was found to be in the open position rather than closed.

Train 1 of the system had been aligned in accordance with 3-OP-065.2 on March Z5, 1988.

An investigation needs to be done to determine the cause of the valve being in the incorrect position.

This will be followed up on my next shift.

D.

Area(s) for improvement Completed copies of portions of selected operating procedures are required to be retained in the PSN's file until the next performance of that proceduie.

However, when the file was accessed to obtain a copy of 3-OP-065.2 which was performed for Train 1 on March 25, 1988, all that was found was a copy of 3-OSP-065.2 performed on March 28, 1988 for Train 2.

Thus, if only a portion of a procedure is done on a given date, it is likely that the "old" procedure in the file will be discarded.

The practice of filing the procedure for reference needs to be improved so that the most recent status of all portions of the procedure are available.

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Q-ADM-Q19 Management on Shift (MOS)

MOS DAILYREI'ORT Puge Professionalism, Summary of Shift, Comments Upon discovery of the valve misalignment described in Section C, appropriate corrective action was taken to return the valve to the required position and document same.

Recommendations Review the practice of returning completed procedures and take necessary action to ensure that the most recent status of all portions of a system's procedures are retained in the file. (See Section D)

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Completed By:

D, V. HaaseI server Date:

03/28-29/88 Reviewed By:

Management Review By:

  • M(N.Iulna u perations Superintendent-Nuclear i

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03/28-29/88

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0-ADM-019 nagement on Shift (MOS)

MOS DAIIY REPORT Page TQ Operations Superintendent

- Nuclear Date:

03/29/88 From:

D. H. West M

bserver)

Shift:

Qx Day Q Night Plant evolutions observed

.Unit 4, Steady State full power operation Unit 3, Heat Up to normal operating temperature B.

Immediate safety problems None observed C.

Ouestionable work practices None observed Area(s) for improvement No comment B.

Professionalism, Summary of Shift, Comments No comment Recommendations None Completed By:

D. H. West M

bserver Date:

03/29/88 Reviewed By:

Management Review By:

PM

/g3o gs Operations Superintendent-Nuclear D~te: 8 3o /I

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03/29/88

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,0-ADM-019 M

agement on Shift (MOS)

MOS DAILYREPORT To:

Operations Superintendent-Nuclear Date:

03 29-30 88 From:

Peter Walker (M

bserver)

Shift:

Q Day Qx Night Plant evolutions observed Unit 3 1.

Confirmation of proper Condensate lineup 2.

6B Peedwater Relief Valve lifted when Main Peedpump was started-reseated when a

lower pressure (standby) pump was restarted-A Peedwater System realignment to allow more blowdown/feed corrected the problem.

3.

A smooth, successful startup was conducted after proper secondary water chemistry results were reported.

4.

Turbine was rolled to synchronous speed and brought on line.

Unit 3 at 60 MWB when I left.

Unit 4 continues to run steady state at 100~o power Station experienced grid fluctuations from lightning strikes up north

- dramatic, but created no problems.

B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement None

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0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Pug'.

Professionalism, Summary of Shift, Comments 2.

3.

Much was accomplished

tonight, in an efficient, professional manner.

A lot of valuable training for license candidates was conducted.

The Control Room was crowded at times, but was orderly and well-controlled.

Last night, I promised to investigate the root causes of the nonconforming Nitrogen Header Pressure Indicator Root Valve, and the lack of cooling fans for Unit 3's Startup Transformer.

I got assurance that R. Mende was investigating the nonconformance issue.

I was told that operation/maintenance of the fans falls in to the Transmission and Distribution Group.

The breaker for the fans was reset and reclosed, but the Transmission and Distribution Group is not going to pursue it any further.

No one in Operations takes logs or ensures fan operation, and no one could tell how long the fans had been out of service.

Recommendations 1,

During an alignment check on the Auxiliary Peedwater and Main Steam Isolation Valve Backup Nitrogen Gas Supply System using 3-OP-065.2, two valve identifying tags (3-40-1673 and 3-40-1674) were observed to be destroyed (melted) and should be replaced.

This is a sensitive system and operator confusion factors should be kept to a minimum.

2.

During alignment of the Condenser Air Ejector for operation, a large column of hot water was ejected from the exhaust

stack, forcing the Turbine Operators to scramble out of the way. I am told that this happens frequently, and it looked to me to be something of a safety hazard.

Perhaps a better way of placing the Ejector in service could be found, or a method of draining the water slug away prior to establishing full steam flow.

Completed By:

6server Dt:~

Reviewed By:

I I

perations uperi ntendent-Nuclear Date: 0 G

Management Review By:

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  • MNi.I Ulna( m at i~S8 ate ate 03/29-30/88

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0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent-Nuclear Date:

03/29-30/88 From:

D. W. Haase seruer Shift:

Q Day Qx Night Plant evolutions observed Unit 4, Steady State operation at 100% power

,Unit 3, Startup from Mode 3 to Mode 1, 25% power Tour of portions of Unit 3

and Unit 4 Intake Cooling Water (ICW)

Component Cooling Water (CCW) Systems in the Auxiliary Building B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement PWO Tag No. 400878 was written on 3/24/88 for the cleaning of the 3A ICW strainer to the CCW Heat Exchanger in accordance with procedural requirements for failing to meet the differential pressure acceptance criteria following backwashing.

A Bl priority was established which iS less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to initiate the work.

As of the peak shift, 3/29/88, the strainer has not yet been cleaned nor has the high differential pressure (DP) been eliminated.

(It' probable that the DP indicator is reading high, because the DP on the 3B ICW strainer is about one psi lower).

Since strainer cleanliness can affect operability of the ICW system, the priority established by operations is appropriate and the FWO should have been worked or the high DP issue resolved within the required time period,

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Q-ADM-Q19 Management on Shift (MOS)

MOS DAILYREPORT Puge B.

Professionalism, Summary of Shift, Comments The evolutions required to take Unit 3 critical and place it on the line were observed.

Reactor operator trainees were used at each position during these efforts; each backed up and instructed by an experienced Reactor Operator or Senior Reactor Operator.

For both of of these major evolutions, a

professional atmosphere was maintained.

Recommendations (Reference item D)

Assure that work required by PWO's that have identified operability concerns (thus assigned a high priority) be initiated within the required time period, or that dispositioning of the issue that caused the PWO be initiated within the same time period.

Completed By:

D. W. Haase 6server Date:

03 29-30 88 Reviewed By:

Management Review By:

perations uperi ntendent-Nuclear (qgo g Date: 8 80 at ae ate 03/29-30/88

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~ '-ADM-019 1+nagement on Shift (MOS)0 MOS DAILYREPORT To:

Operations Superintendent - Nuclear Date:

03/30/88 From:

D. H. West M S bserver)

Shift:

Qx Day

'ight Plant evolutions observed

'Unit 4, Pull power operation Unit 3, Power escalation B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement No comment B.

Professionalism, summary of Shift, Comments No comment Recommendations None Completed By; D

H West bserver Dt:~

Reviewed By:

perations Superintendent-Nuclear Management Review By:

PM a M(lt;I olio7iaa at

/>SIN Date VP Date 03/30/88

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0-ADM-019 Management on Shift (MOS)

MOS 1)AILYREPORT

'I'o.

Operations Superintendent

- Nuclear Date:

03 30-31 38 From:

(M bseroer)

Shift:

p Day px Night Plant evolutions observed Unit 3, Power escalation, 40',b - 70~io at 3% per hour Unit 4, 100'/o Steady State B.

C.

D.

Immediate safety problems None Questionable work practices None Area(s) for improvement None Professionalism, Summary of Shift, Comments 1.

Smooth, relatively uneventful shift 2.

Over the past few days, I have noticed that extraneous noises over the plant page system are increasing in frequency compared to the past few months.

The PSN mentioned it during his shift briefings, and it helped to reduce the noises.

Recommendations IUhile looking over the secondary plant, I noticed that Unit 3's Air Ejector area was

messy, relative to the rest of the plant.

Unit 4's Air Ejector area is being cleaned, so it may be that the Maintenance Department is just getting around to cleaning unit 3's Air Ejector area.

Specifically, I observed four valve wrenches hung on valves, a broom and dust pan lying around, loose brackets on wire conduit, rust on one of the 50 gallon drums and air lines loose and dirty.

Radiation monitor RM-15 is non functional following the release of water from the air ejector last night.

Completed By:

Peter L. IValker M

bserver Date:

03/30-31/88 Reviewed By:

Operations Superintendent-Nuclear Date:

9/

Management Review By:

  • woe,> o>anne PM-Date P~

D 03/30-31/88

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9-'ADM-019 MINagement on Shift (MOS) ~

MOS DAILYREPORT To:

Operations Superintendent-Nuclear Date:

03/30-31/88 From:

D. W. Haa e (M

bserver Shift:

Q Day Qx Night Plant evolutions observed Unit 4, Steady state operation at 100o/o power Unit 3, increasing load at 3% per hour from 280 to 520 MWe Observed manual cleaning of the "3B" Intake Cooling Water strainer to the Component Cooling Water (CCW) Heat Exchanger Observed release of the clearance for the above strainer cleaning Followup of some labeling discrepancies identified on the previous shift Observed the post maintenance tests of a preventative maintenance procedure performed of the "4B2" travelling screen Toured portions of the Secondary System B.

C.

D.

Immediate safety problems None observed Questionable work practices None observed Area(s) for improvement 1.

When the Unit 4

condenser outlet water boxes were sandblasted for

painting, enclosures were not used.

Thus grit from this operation was observed in various areas containing equipment such as the Seal Oil Pumps and Motors, the Main and Auxiliary Transformer, the voltage regulator cabinets, the Iso-phase Cooling System and the "4A" Motor Control Center.

More care should be used to prevent the sandblasting grit from getting into such areas.

2.

When the ICW strainer to the CCW Heat Exchangers is placed back in service following

cleaning, it may improve the entire cleaning effectiveness to perform a backwash operation prior to placing in service.

This could be accomplished by simply changing the valving sequence when releasing.

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0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments The peak-to-mid shift turnover for the IGC Maintenance Department was very professional with good verbal communication on work in progress and jobs required for the shift. The Plan of the Day was used during the turnover.

The 'peak-to-mid shift turnover for the Mechanical Maintenance Department was observed with the following items of strength noted:

Plans for work to be executed by the mid shift had been prepared and approved by the peak shift personnel.

Five jobs were planned for four workers on the midnight shift.and prioritized in accordance with the Plan-of-the-Day.

The work on the cleaning of the "3B" ICW strairter was well coordinated resulting in minimum time in an LCO condition.

Workers used safe work practices in performing the cleaning and in removing the rigging from the overhead following the cleaning.

The area was cleaned of all tools and equipment, and ladders were stowed in their proper place following the work.

Recommendations (From D-1)

Any sand blasting that is to be performed should be evaluated for the effect on the surrounding equipment and appropriate measures taken to prevent spread of sand blasting grit to this equipment.

2.

(From D-2)

Evaluate the current procedures for strainer cleaning to assure that the maximum benefit from the cleaning is obtained.

Completed By:

D. W. Haase server Date:

03/30 31/88 Reviewed By:

perations Superintendent-Nuclear Date:

Management Review By:

  • M(ib.I u In'

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at VP Il 03/30-31/88

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0-ADM-019 nagement on Shift (MOS)

MOS DAII.YREPORT Page To:

Operations Superintendent

- Nuclear Date:

03 31 88 From:

D. H. liest (M

bseruer)

Shift:

px Day Night Plant evolutions observed B.

C.

D.

Unit 4, 100o,'0 power Unit 3, 80lvo power (holding for Chemistry)

Immediate safety problems None observed Ouestionable work practices None observed Area(s) for improvement No comment Professionalism, Summary of Shift, Comments No comment Recommendations None Completed By:

D. H. )Uest M

bseroer Date:

Reviewed By:

perations Superintendent-Nuclear Date:

Management Review By:

AM(Li,lOl 07155

/9 (SR Dke vp Date 03/31/88

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0-ADM-019 Management on Shift (MOB)

MOS 1)AILYREPORT Pttge

'I'o:

Operations Superintendent-Nuclear Date:

03/31-04/01/88 From:

P. L. IUalker (M

6ser ver)

Shift:

Q Day px Night A.

Plant evolutions observed Unit 3, Power escalation:

850'0 to 100% and stabilize Unit 4, Steady State 100'>b power B.

C.

Immediate safety problems None Questionable work practices None D.

Area(s) for improvement None Professionalism, Summary of Shift, Comments Smooth, quiet shift, It was nice to see that the Nitrogen Backup to Auxiliary Peed System pressure monitoring has been vastly simplified.

I observed the Thermography instrument in operation - a great diagnostic tool!

Recommendations None Completed By:

Peter L. IUalker M

bserver Date:

03/31-04/01/88 Reviewed By:

perations Superintendent-Nuc1ear Date: +~ I Management 0 y PM N Date AhtOS:t Ulte7/80 ili8 D te VP Date 03/31-04/01/88

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0-ADM-019 Management on Shift (MOS)

MOS DAlLYREPORT Puge To:

Operations Superintendent-Nuclear Date:

03/31-04/01/88 From:

Dar le Osborn (MO bser Uer)

Shift:

p Day px Night Plan( evolutions observed Unit 4, 1000/0 power Unit 3, 85% to 100'/0 power Plant tour Sh ift turno ver meetings C.

Immediate safety problems None Ouestionable work practices D.

None Area(s) for improvement Unit 3, "6A" 6 "6B" Feedwater Heaters anchor bolts are not secure Professionalism, Summary of Shift, Comments Operations Support conducted training at shift turnover on the revised Auxiliary Feedwater Nitrogen Backup System valve lineup.

The trainer presented the information in a clear, and concise manner followed by a good exchange of questions and answers involving Maintenance, Turbine

Operator, and the Operations Support Trainer; indicating the new valve lineup was well understood.

Recommendations None Completed By:

bseroer Date:

Reviewed By:

perations Superintendent-Nuclear Management Review By:

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Dt VP Date 03/31-04/01/88

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0-ADM-019 anagement on Shift (MOS)

MOS DAII.YREPORT Page TQ:

Operations Superintendent - Nuclear Date:

04 01 88 From:

D. H. iVest M

bserver)

Shift:

Qx Day g Night Plant evolutions observed Both units in full power Steady State operation B.

Immediate safety problems None observed C.

Ouestionable work practices None observed D.

Area(s) for improvement No comment Professionalism, Summary of Shift, Comments No comment Recommendations None Completed By:

D. H. iVest M

bserver Date:

04/01/88 Reviewed By:

Management Review By:

Operations Superintendent-Nuclear PM Date:

0 M(XKI el aj7/68 ae P

Date 04/01/88

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0-ADM-019 agement on Shift (MOS)

MOS DAILYREI'ORT To:

Operations Superintendent-Nuclear Date:

04/01-02/88 From:

P. L. Walker (M

bseruer)

Shift:

Q Day E Night Plant evolutions observed Unit 3, 100",o Steady State power operation Observed an aborted attempt to cure nitrogen leaks in the backup supply to the 3B Main Steam Isolation Valve Unit 4, 1000'a Steady State power operation B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement Proper logging of spares usage is needed.

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0-ADM-oi9 Management on Shift (MOS)

MOB DAILY,REPORT Puge E.

Professionalism, Summary of Shift, Comments The handling of repair attempt on the leaky nitrogen backup supply for the 3B Main Steam Line Isolation Valve had its good and bad points.

It was improperly scheduled for peak shift on Good Friday evening - a better time would have been a fully augmented day shift for work on a system as sensitive as this.

The PSN conducted a prudent, conservative and thorough evaluation of the problem.

Prior to authorizing the work, it was assured that all required tools and materials were available to complete the job.

The decision was made to wait.

Unfortunately, the leak appeared to be increasing, and the decision was reversed.

EUhile the work was underway, more problems than had been anticipated arose, almost requiring unit shutdown as the four hour grace period was elapsing.

A refurbished valve had to be used because spares listed on the computer were unavailable.

Fortunately, Maintenance was able to reassemble the nitrogen supply

lines, but they still leak.

Several hours of discussion with many people occurred.

Four hours of maintenance time elapsed and the problem is still unresolved.

F.

Recommendations I.

Schedule sensitive maintenance on fully augmented dayshifts..

2.

Ensure that all tools, parts and material to accomplish the repair are in hand prior to starting the work.

Completed By:

M 6server Date:

Reviewed By:

Management Review By Operations Superintendent-Nuclear P

t i/P H ate iM(Li.I elh)V'bh 04/01-02/88

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. 0-ADM-019 M nagement on Shift (MOS)

MOS DAILYREPORT To:

Operations Superintendent-Nuclear Date:

04/01-02/88 From:

Daryle L. Osborn W

bseruer Shift:

Q Day gx Night Plant evolutions observed Both units, 100% power Shift turnover meeting Procedure 3-OSP-72.2, MSIV Nitrogen Backup Periodic Test B.

Immediate safety problems None C.

Questionable work practices None

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0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Pose D.

Area(s) for improvement Valve 3-5243 was replaced due to nitrogen leakage at the Swaglock fitting.

The store's computer inventory system showed one 3/8" Whitey valve (MGS

¹570-39779-2) in-stock and a minimum/maximum inventory criteria of 15/20.

When. I/C went to obtain a 3/8" Whitey valve, none were in-stock.

This occurrence identifies two areas for further investigation:

1.

Computer inventory showed one and none were in stock.

2.

The minimum quantity

~ is 15 and the actual inventory was down to l.

In researching the above item ¹I; a requisition-on-stores (ROS) withdrew the last 3/8" Whitey valve on peak shift, 3/31/88.

In discussions with stores personnel, the earliest a revised status would show up on the computer would be 4/2/88, With verification that the ROS information was imputted into the computer, this concern is resolved.

No research concerning the above item ¹2 was performed to determine the root cause of the anomaly between a MGS minimum of 15 and only one 3/8" Whitey valve being in stock, Further action is required to (I) expedite the purchase of 3/8" Whitey valves "and (2) determine how the inventory got to zero without the reordered shipment arriving on site.

Professionalism, Summary of Shift, Comments No comment Recommendations No comment Completed By:

M bserver Date:

1-02 88 Reviewed By:

Management Review By:

Operations Superintendent-Nuclear I'f ~M Date:

0 M(N,I ulhli'M Dt ae ate 04/01-02/88

+v A

0 V

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page To Operations Superintendent

- Nuclear Date:

04 02 88 From:

D. H. iUest M

bserver)

Shift:

Qx Day Night Plant evolutions observed Both units at full power Steady State operation C.

D.

Immediate safety problems None observed Questionable work practices None observed Area(s) for improvement No comment Professionalism, summary of Shift, Comments No comment Recommendations None Completed By:

D. H. iVest M

bserver Date:

4 Reviewed By:

Operations Superintendent-Nuclear Management Q

Review By:

PM~

AM(N:Ial,a7es ate V

Da e i ~/e Da e 04/02/88

r I7 C'

~

v

<<+

W 0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page

'I'o:

Operations Superintendent-Nuclear Date:

04/02-03/88 From:

F. L. Walker (M

bserver)

Shift:

Q Day Qx Night Plant evolutions observed Both units, 100% power Steady State Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvements None Professionalism, Summary of Shift, Comments 1.

Professionalism is highly acceptable 2.

Shift activities normal 3.

No comments Recommendations None Completed By:

M bserver Date:

Reviewed By:

Operations Superintendent-Nuclear Date:

Management Review By:

PM N AM&i.Illltll7/Sb D

e ae Date 04/02-03/88

f~

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Psge Io'perations Superintendent

- Nuclear Date:

'4/02-03/88 From:

Dar le L. Osborn (M

bseruer)

Shift:

Q Day Qx Night Plant. evolutions observed Unit 3, 1009b Steady State Unit 4, 100",o Steady State Shift turnover meetings B.

Immediate safety problems None C.

Questionable work practices None Area(s) for improvement None B.

Professionalism, Summary of Shift, Comments No comments Recommendations No comments Completed By:

M bserver Date:

Reviewed By:

Operations uperi ntendent-Nuclear Management Review By:

PMN iMOS: I 0 IlilV/t+

//yq Dt i 7itLt!

P'b'e Da e Da e 04/03/88

ty

(

k

e, 0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Puge To'perations Superintendent-Nuclear Date:

04 03-04 88 From:

(M bserver)

Shift p

Day Qx Night Plant evolutions observed Both units, 100% Steady State power Toured Auxiliary Building B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement None Professionalism, Summary of Shift, Comments No comment.'

good, productive shift.

Recommendations None Completed By:

P. L. Walker M

bserver Date.

04/03-04/88 Reviewed By:

perations Superintendent-Nuclear Management Review By:

P N

  • MOB;I eluflluu te Dt ate 04/03-04/88

t 4

lg

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page

'I'o:

Operations Superintendent

- Nuclear Date:

04/03-04/88 From:

Dar le Osborn (M

bserver)

Shift:

p Day Qx Night Plant evolutions observed Unit 3, 100oo Steady State Unit 4, 100% Steady State Shift turnover meetings B.

Immediate safety problems None C.

Questionable work practices None Area(s) for improvement None Professionalism, Summary of Shift, Comments No comment Recommendations No comment Completed By:

M bserver Date:

Reviewed By:

perations Superintendent-Nuclear o.~: 4 Management Review By:

PM N

  • MOB.I Oli07ey Dt ae D te 04/03-04/88

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