JAFP-85-0952, Monthly Operating Rept for Nov 1985

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Monthly Operating Rept for Nov 1985
ML20137U471
Person / Time
Site: FitzPatrick 
Issue date: 11/30/1985
From: Radford Converse, Jackie Cook
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
JAFP-85-0952, JAFP-85-952, NUDOCS 8512090322
Download: ML20137U471 (11)


Text

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V DOCKET NO.

50-333 UNIT NAME FITZPATRICK-DATE DEC 1985 COMPLETED BY JOHN COOK-TELEPHONE (315)342-3840 a

0PERATING STATUS:

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1.f UNIT ' NAME: -

FITZPATRICK.

2. REPORTING PERIOD:

851101-851130 3.-LICENSED THERMAL POWER (MWT):

2436 4.; NAMEPLATE RATING ~(GROSS-MWE):

883

5.' DESIGN, ELECTRICAL RATING (NET MWE):

821 6.-MAXIMUM DEPENDABLE CAPACITY (GROSS MWE):

830

7. MAXIMUM DEPENDABLE CAPACITY (NET =MWE):

810

8.' IF. CHANGES' OCCUR IN CAPACITY RATINGS'(ITEMS 3 - 7) SINCE LAST REPORT, GIVE REASONS

R, J NONE.

4

9. POWER' LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE):

NONE f10.> : REASONS FOR~ RESTRICTIONS.' IF ANY:

THIS MONTH YR-TO-DATE

,. CUMULATIVE E 11.' : ' HOURS IN REPORTING. PERIOD:

720-8016

-90697

?l2.

= NUMBER OF HOURS': REACTOR'WAS CRITICAL:

674.6 5055.6 64671.6

<13.-

. REACTOR-RESERVE' SHUTDOWN HOURS:

-0 0

0 14.--

HOURS GENERATOR ON-LINE
'

648.7 4834.8 62782.1

15.

UNIT RESERVE' SHUTDOWN HOURS:

-0 0

-0 J16.

CROSS THERMAL ENERGY GENERATED (MWH):

1392504 10968360 133904314 17.-

' GROSS-ELECTRICAL ENERGY GENERATED (MWH):

469290 3693210 45973490 l18.)~NETELECTRICAL.ENERGYGENERATED(MWH):

452965 3568510 43966570

' :19.

. UNIT-SERVICE. FACTOR:

90.1 60.3-69.2

~

12 0.

. UNIT' AVAILABILITY FACTOR:

90.1 60.3 69.2 121s;. UNIT CAPACITY-FACTOR (USING MDC NET):

77.7 55.0 62.8

.22 1 UNIT CAPACITY FACTOR (USING DER-NET):

76.6 54.2 59.0:

.23.-

' UNIT FORCED OUTAGE RATE:

9.8 11.7

-13.4-24.;

SHUTDOWNS' SCHEDULED 0VER'NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):

Planned maintenance outage March 10, 1986 to last approximately 2 weeks 3 25.

(IF SHUT DOWN AT END OF' REPORT PERIOD,- ESTIMATED DATE OF STARTUP:

l i

26 > iUNITS IN TEST SIATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED-INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION n..

U 8512090322 851130 PDR ADOCK 05000333 R

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E DOCKET NO.

50-333 UNIT FITZPATRICK-DATE DECEMBER COMPLETED BY JOHN COOK TELEPHONE (315)342-3E40 zMONTH

-NOVEMBER'1985 s

DAY

~ AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL'

1 205 17 805

-2 462 18 805

-3 464:

19 805

-4.

'-466 20 806 5'

484-21 807 6

536 22 769 7-762 23 393 8-

-788 24 0

9 798 25 0

I10' 801 26' 164 11 803 27 595 12:

806 28 737 13:

806-29 789 14

--805 30 803 215 802 31 16-805

SUMMARY

The FitzPatrick plant started up and operated at near full thermal power.for the.first' twenty two days of the reporting period. On day twenty three the

--unit was taken off line to repair a Main Steam Isolation valve hydraulic cylinder and returned to service on day twenty six.

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' JAMES AL FITZPATRICK t'UCLEAR POWER PLANT

. UNIT' SHUTDOWNS AND POWER-REDUCTIONS-

+

DOCKET NO.

50-3334

UNIT NAME.

FITZPATRICK'-

DATE' DEC. 1985 REPORT. MONTH NOVEMBER-1985

COMPLETED'BY-JOHN COOK-TELEPHONE' (315)342-3840 i.

D C

UH R

METHOD S

-O, R0 E

0F YC M C.

CAUSE AND CORRECTIVE ACTION

' A. U A'

SHUTTING LICENSEE

'S0 PO-TO i.

NO.

DATE TYPE-

'T R-

S-DOWN-EVENT TD 0D PREVENT RECURRENCE-I'S O

THE1 REPORT-E E' NE O '-

N REACTOR' M-E

.N' N

T 012 851031 F.

9.8 H

3 85-026 FK N/A Reactor Scram'on load-reject ~due to equipment ~ failure'at.the.EDIC substation.

(Cumulative hours 24.4)'-

13 851123 F

61.5 A

1 SB ISV-Reactor shut down to repair Main

. Steam Isolation Valve hydraulic l

cylinder. Cylinder was rebuilt and the gaskets were upgraded. The cause of the bolt failure is under investigation at this time.

CNOTE Event # on October: Report :Lncorrect.

4 4

1 2

3' 4

F: FORCED REASON:

METHOD:

EXHIBIT G.- INSTRUCTIONS-4 j

S: SCHEDULED

'A. EQUIPMENT FAILURE (EXPLAIN).'

1-MANUAL FOR PREPARATION OF DATA B. MAINTENANCE OF TEST 2-MANUAL SCRAM

. ENTRY SHEETS'FOR LICENSEE-a C. REFUELING 3-AUTOMATIC SCRAM EVENT REPORT (LER) FILE D.. REGULATORY. RESTRICTION'

'4-0THER'(EXPLAIN)

.(NUREG-0161)

'E. OPERATOR TRAINING.AND LICENSE EXAMINATION'

.F. ADMINISTRATIVE G. OPERATIONAL ERROR (EXPLAIN)

H. OTHER (EXPLAIN) 4

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~

NARRATIVE SUMMAFY OF OPERATING EXPERIENCE

'r November-1985 The FitzPatrick plant returned to service on November 1, 1985

. following the' October 31 shutdown.; The~.u t then.operatedLat:-

near full, thermal power until November 23 w en'the' plant was

~

-shutdown to repair a Main Steam Isolation valve. Investigation

. revealed-the hydraulic cylinder;on the valve had ruptured preventing proper-valve operation. :The cause of,the cylinder

- rupture was failure of,the end' bolts. ~The bolts are being.sent

.z out-for-analysis'at this time. The cylinder was rebuilt and the

- gaskets were. replaced with spares made of an' upgraded material.

' The plant'was returned-to'. service on November 26.

- At-the;end'of the r'eportingLperiod the FitzPatrick plant is operating:at approximately 803 mw.,

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..NEW YORK POWER AUTHORITY-V 2 JAMES A.'.FITZPATRICK NUCLEAR POWER, PLANT

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' MAINTENANCE'

SUMMARY

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. NOVEMBER 1985 l

. ACTION TAKEN-REPAIR.

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W iWORKiREQUEST NO.

HOW-

.CAUSE OF

. RESULTS'0F

'TO PRECLUDE' TIME.

^

DATEl SYSTEM COMPONENT NO.

DETECTED:

MALFUNCTIONi MALFUNCTION RECURRENCE:

HOURS '

851031 01-125 L032742 I&C BAD. DIAPHRAGM'-

STDBY GAS "A" REPLACED DSPI-1A AND-

' 18 --

2 DPIS-1A' PREFILTER D/P SW.

PERFORMED ISP-84 851115l

'02-3 038923 OPS TRANSMITTER

'IND.. LOWER THAN ADJUSTED

~ 10 -

-LI-85A,85B DRIFT

. CORRESPOND;: INST

~

851106 02 038507.

I&C FAULTY TRIP UNIT' REPLACED XMITTER-

.20

.MTU-218B XMITTER INDICATES

-DOWNSCALE 851105 02 032702 I&C.

VARIOUS VARIOUS. PROBLEMS.

VARIOUS CIRCUIT 42.5

.3 SPARE ATTS~

FOUND IN PRE-OP BOARD REPAIRS' 851101 07 037425 OPS SWITCH S1.

RECORDER WON'T REPOSITION CABLES, 32-NM-131-4C SELECTOR ~

TRACE FOR-REPLACE SWITCH, SWITCH MACH. C CLEANED 851114 07 038508

-OPS

-AGE /USE

. BAD PEN MOTION-REALICNED X, 16-t NM-131 IN X DIRECTION-LUBRICATED, CLEANED 851030 07 034121 I&C-UNKNOWN

. READS 15 NO PROBLEM FOUND 7

LPRM-44-13 WITH REACTOR CHECKED SHUTDOWN-L i-

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.. NEW YORK' POWER' AUTHORITY?

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.' JAMES-A.'FITZPATRICK NUCLEAR; POWER. PLANT

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' MAINTENANCE

SUMMARY

. NOVEMBER 1985,

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~*- ACTION TAKEN-REPAIR'-

}.

WORK REQUEST NO.

HOW~

CAUSE.OF-

'RESULTS OF

-TO~ PRECLUDE.

TTME :.. 7 DATE SYSTEM COMPONENT NO.

DETECTED-MALTUNCTICN MALFUNCTION.

RECURRENCE HOURS +

851105 07 037561-

. OPS CONNECTOR CHART. ADVANCES RESOLDERED CONNECTOR

'4:

PR-46A LOOSE TOO SLOWLY IO SWITCH' B51113 07 038522 OPS ZENER DIODE VR3 READ WRONG,-

REPLACED DIODE-11 4 "

TIP D' WON'T SLOW-

'AT INDXR 851126 07 038586 OPS BROKEN HV.

INDICATOR NOT:

REPLACED CONNECTOR'.

-6 IRM C-CONNECTOR-TRACKING POWER' 851114 10 -

035310 OPS N/A-PERFORM LEAK PERFORMED LEAK RATE 10

'FT-134-RATE :. TEST.

IEST :

851030 13 032806' I&C1 AMPHENOL CONN.,

ERRATIC CONTROL-REPLACED CdNNECTORS, 14 i

RCIC CTRL' RING TERMINALS-TRIPPED TURBINE RING TERMINALS r

B51108 13 023185 I&C BAD STARTING REPAIR SPARE' DRDERED AND REPLACED.

26 N/A CAPACITOR TOPAZ C11

CAPACITOR I

~

851112 16 038459 OPS LOOSE PRINT RECORDER. PEN NOT-IIGHTENED, CLEANED 10 DPR-200 ASSEMBLY PRINTING ASSEMBLY, SHAFTS-

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,i JAMES'A.:FITZPATRICK NUCLEAR: POWER PLANT

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MAINTENANCE'

SUMMARY

NOVEMBER.1985

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. ACTION TAKEN-REPAIR:

WORK REQUEST NO.

"HOW CAUSE,OF.

RESULTS OF.!

TO PRECLUDE TIME DATE

< SYSTEM-COMPONENT NO..

DETECTED-MALFUNCTION MALFUNCTION-

' RECURRENCE 1 HOURS 2

' FAILED TRANSISTOR HV INOP. TRIP REPLACED Q17; TRANSISTOR 24 851031

~ 17 "

038740

-I&C RM-251A' DIDN'T-FUNCTION ~

~

851119 17 038481 OPS-N/A SOURCE DRIVE.

PERFORMED CHECKS-NO:

4)

~

RIS-458A-MECH. NOT-PROBLEM FOUND-WORKING.

851121 27

.038726 JIC' FAILED SAMPLE

- UNRELIABLE REPLACED PUMP,, SENSOR, 148~

PCX-101B PUMP AND' SENSOR OXYGEN DAC BOARD READINGS

- 851115 70 038455' OPS' HOLD' TAG'ON' ALARM COMES IN N/A 18 I

'AHU-3A' POWER TO SUPPLY WITH UNIT.

FAN.

RUNNING 851112

-72 '

037532 OPS OUT OF^

LO FLOW-ON~

CALIBRATED PER 6

DPS-104 CALIBRATION RETURN AIR, ISP-87 ALARM IN-851024 76 037634 OPS HEAD PRESSURE START PRESSURE CALIBRATED / CORRECTED 21 i

PS-102 IS TOO LOW SETPOINT-l l

851030 76.

023052 I&C UNKNOWN SWITCH WOULDN'T ~

INSTALLED NEW SWITCH-25-i PS-H/L-10

- RESET TO VALUE CALIBRATED SET f

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.IAMES A. FlTZPATRICK NUCLEAR POWER PIANT.

SAFEIY REIA1ED E[ECIRICAL & MECHANICAL MAINIENANCE SittiARY:

9 NOVEMBER 1985 '

4 MPEAIF, -

WRK REQUEST f TIE

- DATE SYSTDi C WPCNENT

~HOW DEIECIED CAUSE OF MAIRNCTION '

ACTION TAIGN 'IO PRECLUDE RECURRENCE : H0lRS 11/12 03 38408 OPS.

Worn Parts-Rebuilt pm p.

'250

P-16B

---_-----__------------___--_----_-_-_--_..__-_-_-----------------_-----------_-_-_-----_---_y 8736 OPS Motor Failure Replaced motor..

8' 3,,A" %

11/8 27


===_=___=_==------------------------------------<

21/14 13 30712 PMs Corrosion

. Replaced gear housing cmponents-18'-

FDV-131

- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - _ = _ _ _ _ _ = - - - - - - - - - - - - - - - - - - - - _ = = _ _ _ _ _ - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - <

J1/26 29 38566

-OPS

. Cylinder bolt failure Rebuilt seal' cartridge and replaced 56' A0V-86B bolts!


9 11/26 29 23895 OPS Air Leak Changed solenoid valve 4

AOV-86C

____--------------------s


=____===_==-----------------------------------------------===-

11/26 29 33582 -

OPS

. Foreign object on Replaced solenoid valve.

14 A0V-869 valve seat

__-------------_-__------------__---------------_---__--==______-------_--_-----__--_-_-_-_ -----------_---.-----.-------_---

11/26 13 38570 l OPS Motor shorted Replaced notor 23' NOV-15


==___==== -----------------------------....--<

11/25 12 38575 OPS Body to bonnet leak Retorqued bonnet bolts 6

MDV-15

_------------=_______--------------------<

____ =.----------------------------------------------------_._===__


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Jomo A. Fit Preri;k Nuclear Power Plant P.O. Onx 41 -

Lycomgr:g. N(w York 13093 315 342.3840 -

Radford J. Converse -

  1. > NewYorkPbwer 4# Authority December 4, 19f,5 JAFP 85-0952 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION:

DOCUMENT CONTROL DESK

REFERENCE:

D_0CKET NO. 50-333

Dear Sir:

Enclosed please find the J. A..FitzPatrick Operating Status Report for the month of November, 1985.

Refueling information remains the same as previously submitted.

If there are any questions concerning this report, please contact John Cook at (315) 342-3840, Ext. 439.

)

FORD J. C.

SE RJC:JPC:mac Enclosures cc: Distribution 4

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